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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M6631999-10-19019 October 1999 Forwards Insp Rept 50-277/99-07 & 50-278/99-07 on 990920.No Violations Noted ML20217K9241999-10-14014 October 1999 Forwards Amend 234 to License DPR-56 & Se.Amend Consists of Changes to TS in Response to Application & Suppls ,1001 & 06,which Will Support PBAPS Mod P00507,which Will Install Digital Pr Neutron Mining Sys ML20217F7391999-10-14014 October 1999 Requests Addl Info Re Peach Bottom Atomic Power Station Units 2 & 3 Appendix R Exemption Requests ML20217F6841999-10-13013 October 1999 Forwards Senior Reactor Operator Initial Exam Repts 50-277/99-302(OL) & 50-278/99-302(OL) Conducted on 990913- 16.All Applicants Passed All Portions of Exam ML20217F3021999-10-12012 October 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at PBAPS Have Been Completed.Ltr Also Confirms Completion of Actions Required by Confirmatory Order Modifying Licenses, ML20217E7451999-10-0808 October 1999 Forwards Response to NRC 990820 RAI Concerning Proposed Alternatives Associated with Third ten-yr Interval ISI Program for Pbaps,Units 2 & 3 ML20217B7701999-10-0606 October 1999 Submits Corrected Info to NRC 980528 RAI Re Util Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions ML20217B9151999-10-0606 October 1999 Provides Clarifying Info to Enable NRC to Complete Review of License Change Request ECR 98-01802,re Changes Necessary to Support Installation of Digital Pr Neutron Monitoring & Incorporate long-term T/H Stability Solution Hardware ML20217C4141999-10-0606 October 1999 Forwards Response to NRC 981109 RAI Re Resolution of USI A-46 for Pbaps.Proprietary Excerpts from GIP-2,Ref 25 Results of BWR Trial Plant Review Section 8 Also Encl. Proprietary Excerpts Withheld ML20217B3181999-10-0505 October 1999 Advises That Info Submitted in 990712 Application,Which Contained Attachment Entitled, Addl Info Re Cycle Spec SLMCPR for Peach Bottom 3 Cycle 13,dtd 990609, with Affidavit,Will Be Withheld from Public Disclosure ML20217B4051999-10-0505 October 1999 Forwards Amend 233 to License DPR-56 & Safety Evaluation. Amend Changes Minimum Critical Power Ratio Safety Limit & Approved Methodologies Referenced in Core Operating Limits Report 05000278/LER-1999-004, Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv)1999-10-0101 October 1999 Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv) ML20217B8891999-10-0101 October 1999 Forwards Response to RAI Re Request to Install Digital Power Range Neutron Monitoring Sys & Incorporate long-term,thermal-hydraulic Stability Solution Hardware. Revised TS Table 3.3.2.1-1 Encl ML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20212J6851999-09-29029 September 1999 Informs of Completion of mid-cycle PPR of Peach Bottom Atomic Power Station on 990913.No Areas Identified in Which Licensee Performance Warranted Addl New Insps Beyond Core Insp Program.Historical Listing of Plant Issues Encl ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212J5751999-09-28028 September 1999 Informs of Individual Exam Results for Applicants on Initial Exam Conducted on 990913-16 at Licensee Facility.Without Encls ML20216J0191999-09-27027 September 1999 Forwards Request for Addl Info Re Util 990301 Request to Support Installation of Digital Power Range Neutron Monitoring Sys & Incorporation of long-term thermal- Hydraulic Stability Solution Hardware,For Plant ML20212H6171999-09-24024 September 1999 Forwards Rev 2 to COLR for Pbaps,Unit 2,Reload 12,Cycle 13, IAW TS Section 5.6.5.d.Rept Incorporates Revised Single Loop Operation MAPLHGR Flow Multiplier ML20216H6451999-09-24024 September 1999 Forwards Notice of Withdrawal of Util 990806 Application for Amends to Fols DPR-44 & DPR-56.Proposed Change Would Have Involved Temporary Change to Increase Limit for Average Water Temp of Normal Heat Sink ML20212H5431999-09-24024 September 1999 Informs of Decision to Inspect H-3 & H-4 Shroud Welds During Upcoming 3R12 Outage Scheduled to Begin Late Sept 1999 ML20216H6751999-09-24024 September 1999 Forwards Amends 229 & 232 to Licenses DPR-44 & DPR-56, Respectively & Ser.Amends Will Delete SR Associated Only with Refueling Platform Fuel Grapple Fully Retracted Position Interlock Input,Currently Required by SR 3.9.1.1 ML20216F8811999-09-23023 September 1999 Withdraws 990806 Exigent License Change Application.Tech Spec Change to Allow Continued Power Operation with Elevated Cooling Water Temps During Potentially Extreme Weather Conditions No Longer Needed Due to Favorable Weather ML20212E8661999-09-22022 September 1999 Discusses GL 98-01 Y2K Readiness of Computer Sys at NPPs & Supplement 1 & PECO Response for PBAPS Dtd 990630. Understands That at Least One Sys or Component Listed May Have Potential to Cause Transient During Y2K Transition ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212D1191999-09-17017 September 1999 Forwards SE Re Proposed Alternatives to ASME Section XI Requirements for Containment Inservice Insp Program at Plant,Units 2 & 3 ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment ML20211P2961999-09-0707 September 1999 Provides Authorization to Administer NRC Approved Initial Written Exams to Listed Applicants on 990913 at Peach Bottom Npp,Delta,Pennsylvania ML20211K7031999-08-30030 August 1999 Forwards Response to NRC 990826 RAI Re License Change Application ECR 99-01255,revising TSs 2.1.1.2 & 5.6.5 ML20211E6941999-08-26026 August 1999 Forwards Request for Addl Info Re Min Critical Power Ratio. Response Should Be Submitted within 30 Days of Ltr Receipt ML20211Q4491999-08-25025 August 1999 Responds to Re Changes to PBAPS Physical Security Plan,Safeguards Contingency Plan & Guard Training & Qualification Plan Identified as Revs 13,11 & 9, Respectively.No NRC Approval Is Required,Per 10CFR50.54(p) ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211D5421999-08-23023 August 1999 Forwards Amends 228 & 231 to Licenses DPR-44 & DPR-56, Respectively & Se.Amends Revise TSs to Correct Typographical & Editorial Errors Introduced in TSs by Previous Amends ML20211A9721999-08-20020 August 1999 Forwards Request for Addl Info Re Third 10-year Interval Inservice (ISI) Insp Program Plan for Plant,Units 2 & 3 ML20210T5451999-08-12012 August 1999 Forwards Copy of Environ Assessment & Findings of No Significant Impact Re Licensee Request for Amends to Plant. Amends Consist of Changes to TS to Correct Typos & Editorial Errors Introduced in TS by Previous Amends ML20210P8321999-08-11011 August 1999 Responds to NRC 990715 Telcon Re Util 990217 Submittal of Proposed Alternatives to Requirements of 10CFR50.55a(g)(6)(ii)(B)(1) Re Containment Inservice Insp Program ML20210P8151999-08-11011 August 1999 Forwards Final Pages for Pbaps,Unit 2 & 3 OLs Re License Change Application ECR 99-01497,which Reflects Change in Corporate Structure at Pse&G ML20211B6521999-08-10010 August 1999 Informs That Dp Lewis,License SOP-11247,has Been Permanently Reassigned & No Longer Requires License,Per 10CFR50.74.Util Requests That Subject Individual Be Removed from List of License Holders ML20210P1561999-08-10010 August 1999 Submits Response to Requests for Addl Info Re GL 92-01,rev 1,Suppl 1, Rv Structural Integrity, for Pbap,Units 1 & 2. NRC Will Assume That Data Entered Into Rvid Are Acceptable for Plants,If Staff Does Not Receive Comments by 990901 ML20211B7881999-08-10010 August 1999 Transmits Summary of Two Meetings with Risk-Informed TS Task Force in Rockville,Md on 990514 & 0714 ML20210N7831999-08-0909 August 1999 Forwards Copy of Notice of Consideration of Issuance of Amends to Fols,Proposed NSHC Determination & Opportunity for Hearing, Re 990806 Request for License Amends.Amends Incorporate Note Into PBAPS TS to Permit One Time Exemption ML20210P0801999-08-0404 August 1999 Forwards Initial Exam Repts 50-277/99-301 & 50-278/99-301 on 990702-14 (Administration) & 990715-22 (Grading).Six of Limited SRO Applicants Passed All Portion of Exam ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response NUREG-1092, Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls1999-08-0303 August 1999 Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls ML20210J0161999-07-30030 July 1999 Forwards Copy of Notice of Consideration of Approval of Transfer of FOL & Issuance of Conforming Amends Re 990723 Application ML20210H5341999-07-27027 July 1999 Forwards Insp Repts 50-277/99-05 & 50-278/99-05 on 990518- 0628.NRC Determined That Two Severity Level IV Violations of NRC Requirements Occurred & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20210F3731999-07-23023 July 1999 Submits Confirmation That,Iaw 10CFR50.80,PSE&G Is Requesting NRC Approval of Transfer of Ownership Interests in PBAPS, Units to New Affiliated Nuclear Generating Company,Pseg Nuclear LLC ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20210E5811999-07-21021 July 1999 Forwards Final Tech Specs Pages for License Change Application.Proposed Change Will Revise Tech Specs to Delete Requirement for Refuel Platform Fuel Grapple Fully Retracted Position Interlock Currently Required by TS ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217F3021999-10-12012 October 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at PBAPS Have Been Completed.Ltr Also Confirms Completion of Actions Required by Confirmatory Order Modifying Licenses, ML20217E7451999-10-0808 October 1999 Forwards Response to NRC 990820 RAI Concerning Proposed Alternatives Associated with Third ten-yr Interval ISI Program for Pbaps,Units 2 & 3 ML20217C4141999-10-0606 October 1999 Forwards Response to NRC 981109 RAI Re Resolution of USI A-46 for Pbaps.Proprietary Excerpts from GIP-2,Ref 25 Results of BWR Trial Plant Review Section 8 Also Encl. Proprietary Excerpts Withheld ML20217B9151999-10-0606 October 1999 Provides Clarifying Info to Enable NRC to Complete Review of License Change Request ECR 98-01802,re Changes Necessary to Support Installation of Digital Pr Neutron Monitoring & Incorporate long-term T/H Stability Solution Hardware ML20217B7701999-10-0606 October 1999 Submits Corrected Info to NRC 980528 RAI Re Util Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions ML20217B8891999-10-0101 October 1999 Forwards Response to RAI Re Request to Install Digital Power Range Neutron Monitoring Sys & Incorporate long-term,thermal-hydraulic Stability Solution Hardware. Revised TS Table 3.3.2.1-1 Encl 05000278/LER-1999-004, Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv)1999-10-0101 October 1999 Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv) ML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212H6171999-09-24024 September 1999 Forwards Rev 2 to COLR for Pbaps,Unit 2,Reload 12,Cycle 13, IAW TS Section 5.6.5.d.Rept Incorporates Revised Single Loop Operation MAPLHGR Flow Multiplier ML20212H5431999-09-24024 September 1999 Informs of Decision to Inspect H-3 & H-4 Shroud Welds During Upcoming 3R12 Outage Scheduled to Begin Late Sept 1999 ML20216F8811999-09-23023 September 1999 Withdraws 990806 Exigent License Change Application.Tech Spec Change to Allow Continued Power Operation with Elevated Cooling Water Temps During Potentially Extreme Weather Conditions No Longer Needed Due to Favorable Weather ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment ML20211K7031999-08-30030 August 1999 Forwards Response to NRC 990826 RAI Re License Change Application ECR 99-01255,revising TSs 2.1.1.2 & 5.6.5 ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20210P8321999-08-11011 August 1999 Responds to NRC 990715 Telcon Re Util 990217 Submittal of Proposed Alternatives to Requirements of 10CFR50.55a(g)(6)(ii)(B)(1) Re Containment Inservice Insp Program ML20210P8151999-08-11011 August 1999 Forwards Final Pages for Pbaps,Unit 2 & 3 OLs Re License Change Application ECR 99-01497,which Reflects Change in Corporate Structure at Pse&G ML20211B6521999-08-10010 August 1999 Informs That Dp Lewis,License SOP-11247,has Been Permanently Reassigned & No Longer Requires License,Per 10CFR50.74.Util Requests That Subject Individual Be Removed from List of License Holders ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML20210F3731999-07-23023 July 1999 Submits Confirmation That,Iaw 10CFR50.80,PSE&G Is Requesting NRC Approval of Transfer of Ownership Interests in PBAPS, Units to New Affiliated Nuclear Generating Company,Pseg Nuclear LLC ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20210E5811999-07-21021 July 1999 Forwards Final Tech Specs Pages for License Change Application.Proposed Change Will Revise Tech Specs to Delete Requirement for Refuel Platform Fuel Grapple Fully Retracted Position Interlock Currently Required by TS ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 05000278/LER-1999-002, Forwards LER 99-002-01 to Correct Title Contained in Box (4) of LER Coversheet Form.Rev Does Not Change Reportability Requirements or Any Other Info Contained in Original Submittal of LER1999-07-12012 July 1999 Forwards LER 99-002-01 to Correct Title Contained in Box (4) of LER Coversheet Form.Rev Does Not Change Reportability Requirements or Any Other Info Contained in Original Submittal of LER ML20209G9121999-07-0909 July 1999 Informs That Ja Hutton Has Been Appointed Director,Licensing for PECO Nuclear,Effective 990715.Previous Correspondence Addressed to Gd Edwards Should Now Be Sent to Ja Hutton ML20209D9781999-07-0808 July 1999 Forwards Addl Info to Support EA of Proposed 990212 License Application ECR 98-01675,correcting Minor Administrative Errors in TS Figure Showing Site & Exclusion Areas Boundaries & Two TS SRs ML20209D8821999-07-0707 July 1999 Submits Estimate of Number of Licensing Actions Expected to Be Submitted in Years 2000 & 2001,as Requested by Administrative Ltr 99-02.Renewal Applications for PBAPS, Units 2 & 3,will Be Submitted in Second Half of 2001 ML20209D2671999-07-0202 July 1999 Responds to NRC 990322 & 0420 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20209E1131999-06-30030 June 1999 Forwards Proprietary NRC Form 398, Personal Qualification Statement-Licensee, for Renewal of RO Licenses for EP Angle,Md Lebrun,Jh Seitz & Zi Varga,Licenses OP-10646-1, OP-11081,OP-11082 & OP-11085,respectively.Encls Withheld ML20209B7001999-06-30030 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20209C1201999-06-30030 June 1999 Informs of Util Intent to Request Renewed License for PBAPS, Units 2 & 3,IAW 10CFR54.Licensee Anticipates That License Renewal Application Will Be Submitted in Second Half of 2001 05000277/LER-1999-004, Forwards LER 99-004-00 Re Unplanned ESF Actuations During Planned Electrical Bus Restoration Following Maint Activities1999-06-20020 June 1999 Forwards LER 99-004-00 Re Unplanned ESF Actuations During Planned Electrical Bus Restoration Following Maint Activities ML20196A5291999-06-14014 June 1999 Forwards Final Pbaps,Unit 3 TS Pages for License Change Request ECR 98-01802 Re Installation of Digital Power Range Neutron Monitoring (Prnm) Sys & Incorporation of long-term thermal-hydraulic Stability Solution Hardware ML20195E6051999-05-27027 May 1999 Requests Exemption from Requirements of 10CFR72.44(d)(3) Re Submittal Date for Annual Rept of Principal Radionuclides Released to Environ.Exemption from 10CFR72.72(d) Re Storage of Spent Fuel Records,Additionally Requested ML20195B8171999-05-25025 May 1999 Forwards Final TS Pages for License Change Application ECR 96-01511 Re Rev to Loss of Power Setpoints for 4 Kv Emergency Buses ML20195B6191999-05-19019 May 1999 Forwards PBAPS Units 2 & 3 Annual Radiological Environ Operating Rept 56 for 980101-1231, Per Section 6.9.2 of Ol. Trace Concentrations of Cs-137 Were Found in Sediment Consistent with Levels Observed in Previous Years ML20206P9171999-05-10010 May 1999 Updates Some of Transmitted Data Points Provided in Data Point Library ERDS for Pbaps,Units 2 & 3.Data Point Info Format Consistent with Guidance Specified in NUREG-1394 ML20206K6581999-05-0404 May 1999 Forwards PBAPS Bases Changes Through Unit 2 Bases Rev 25 & Units 3 Bases Rev 25.Bases Reflect Change Through Apr 1999, Thereby Satisfying Frequency Requirements of 10CFR50.71 ML20206D4651999-04-29029 April 1999 Forwards Rev 16 to UFSAR & Rev 11 to Fire Protection Program (Fpp), for Pbaps,Units 2 & 3.Page Replacement Instructions for Incorporating Rev 16 to UFSAR & Rev 11 to Fpp,Encl ML20207B8431999-04-23023 April 1999 Forwards Final Rept for 981117,plume Exposure Pathway Exercise of Offsite Radiological Emergency Response Plans site-specific for Peach Bottom Atomic Power Station.One Deficiency & 27 Areas Requiring C/A Identified ML20206C5461999-04-20020 April 1999 Forwards Radioactive Effluent Release Rept 41 for Jan-Dec 1998 for Pbaps,Units 1 & 2. Revs Made to ODCM & Station Process Control Program (PCP) During Rept Period,Encl 05000277/LER-1999-003, Forwards LER 99-003-00 Re 990318 Failure to Maintain Provisions of Fire Protection Program to Properly Address Effects of Flooding1999-04-16016 April 1999 Forwards LER 99-003-00 Re 990318 Failure to Maintain Provisions of Fire Protection Program to Properly Address Effects of Flooding ML20205K4541999-04-0808 April 1999 Forwards Revised Info Re 990330 NRC Nuclear Power Reactor Licensee Financial Qualifications & Decommissioning Funding Assurance Status Rept 05000278/LER-1999-001, Forwards LER 99-001-00 Re 990312 ESF Actuation of Rcics Due to High Steam Flow Signal During Sys Restoration.Rept Submitted Per 10CFR50.73(a)(2)(iv)1999-04-0808 April 1999 Forwards LER 99-001-00 Re 990312 ESF Actuation of Rcics Due to High Steam Flow Signal During Sys Restoration.Rept Submitted Per 10CFR50.73(a)(2)(iv) ML18106B1431999-03-31031 March 1999 Forwards Pse&G Rept on Financial Min Assurance for Period Ending 981231 for Hope Creek,Salem,Units 1 & 2 & Pbaps,Units 2 & 3,IAW 10CFR50.75 ML20205F8981999-03-31031 March 1999 Provides Info Re Status of Decommissioning Funding for LGS, Units 1 & 2,PBAPS,Units 1,2 & 3 & Sgs,Units 1 & 2,per Requirements of 10CFR50.75(f)(1) ML18106B1411999-03-30030 March 1999 Forwards Decommissioning Info on Behalf of Conectiv Nuclear Facility License Subsidiaries,Atlantic City Electric Co & Delmarva Power & Light Co,For Listed Nuclear Facilities ML20205J0831999-03-26026 March 1999 Requests Enforcement Discretion from Requirements of PBAPS, Units 2 & 3 Ts.Enforcement Discretion Pursued to Avoid Unneccessary Plant Transient Which Would Result from Compliance with TS ML20205B6421999-03-24024 March 1999 Submits 1998 Annual Decommission Rept for Pbaps,Unit 1. There Were No Reportable Events Involving Unit 1 for 1998 1999-09-09
[Table view] Category:UTILITY TO NRC
MONTHYEARML20064A7171990-09-18018 September 1990 Comments on SALP Board Repts 50-277/89-99 & 50-278/89-99. Author Pledges Continued Mgt Support of & Attention to Rate of Improvement,Achievement of Goals & Performance of Routine Activities ML20065D4421990-09-14014 September 1990 Responds to Generic Ltr 90-07, Operator Licensing Natl Exam Schedule. Proposed Schedules for Operator Licensing Exams, Requalification Exams & Generic Fundamental Exams Encl ML20064A7751990-09-13013 September 1990 Advises That Ba Stambauth No Longer Maintains Need to Hold Senior Operator License ML20065D3741990-09-11011 September 1990 Forwards Rev to Relief Request 10-VRR-2 Re RHR stay-fill Supply Check Valves,Per ML20059F0541990-08-31031 August 1990 Responds to NRC Re Violations Noted in Safety Insp Repts 50-277/90-13 & 50-278/90-13.Corrective Actions: Training Will Be Provided for Personnel Re Requirements of Drawing E1317 & Administrative Procedures A-2 & A-6 ML20028G8181990-08-27027 August 1990 Forwards Peach Bottom Atomic Power Station Semiannual Effluent Release Rept,Jan-June 1990. No Revs Made to ODCM During Rept Period ML20059A6461990-08-15015 August 1990 Responds to Violation Noted in Insp Repts 50-277/90-200, 50-278/90-200,50-277/90-06 & 50-278/90-06 & Payment of Civil Penalty in Amount of $75,000.Corrective Actions:Emergency Svc Water Sys Restored to Operable Status ML20058N1991990-08-0909 August 1990 Advises of Change of Address for Correspondence Re Util Operations.All Incoming Correspondence Must Be Directed to One of Listed Addresses ML20058Q4051990-08-0606 August 1990 Forwards Public Version of Revised Emergency Response Procedures,Including Rev 12 to ERP-140,App 2,Rev 13 to ERP-140,App 3,Rev 4 to ERP-230,Rev 3 to ERP-305 & Rev 3 to ERP-660 ML20058M6631990-08-0303 August 1990 Responds to NRC 890406 Integrated Assessment Team Insp Repts 50-277/89-81 & 50-278/89-81.Based on Encl Schedule,Overall Projected Implementation Date Will Be 901119 ML20056A9611990-08-0303 August 1990 Notifies That Be Saxman Terminated Employment & Operating Responsibilities W/Util on 900706 ML20081E1581990-07-30030 July 1990 Forwards List of 1990 QA Program Changes for Plant.List Identifies Page & Paragraph Number,Brief Description & Type of Change ML20056A0421990-07-27027 July 1990 Forwards Updated Human Resource Status Rept for Jan-Jul 1990 for Areas Identified in Integrated Assessment Team Insp Repts 50-277/89-81 & 50-278/89-81 ML18095A3761990-07-26026 July 1990 Forwards Decommissioning Repts & Certification of Financial Assurance for Plants ML18095A3661990-07-26026 July 1990 Forwards Decommissioning Repts for Hope Creek,Peach Bottom & Salem Nuclear Generating Stations ML18095A3721990-07-24024 July 1990 Forwards Rept & Certification of Financial Assurance for Decommissioning for Plants,Per 10CFR50.75 ML20055H8331990-07-20020 July 1990 Submits Change of Addresses for Correspondence Re Util Nuclear Operations ML20044B2621990-07-12012 July 1990 Forwards Annual Progress Rept on Implementation of Control Room Enhancements,Per NUREG-0737.Corrective Actions for All Priority 1 Human Engineering Discrepancies Completed for Unit.Remaining Priority 2 Discrepancies Under Reevaluation ML20055G5481990-07-11011 July 1990 Forwards Public Version of Revised Epips,Including Rev 12 to ERP-140,App 3 & Revs 3 to ERP-310 & ERP-317 ML20043H7041990-06-21021 June 1990 Forwards Endorsements 143-146 to Nelia Policy NF-140 & Endorsements 93-96 to Maelu Policy MF-67 ML20044A2961990-06-21021 June 1990 Submits Revised Response to NRC Bulletin 89-002 Re safety- Related Swing Check Valves to Be Installed on Emergency Diesel Generator.Bolts Will Not Be Replaced Because Valves W/Original Internal Bolts Meet Requirements of Bulletin ML20043H6081990-06-19019 June 1990 Corrects 900427 Response to Generic Ltr 87-07, Info Transmittal of Final Rulemaking for Revs to Operator Licensing - 10CFR55 & Conforming Amends. ML20055C7621990-06-18018 June 1990 Informs NRC of Plans Re Licensing of Senior Reactor Operators (Sros) Limited to Fuel Handling at Plants.Util in Process of Implementing New Program for Establishment & Maint of Licensed SROs Limited to Fuel Handling at Plants ML20043G8131990-06-13013 June 1990 Responds to NRC 900515 Ltr Re Violations Noted in Insp Repts 50-277/90-06 & 50-278/90-06.Corrective Actions:Surveillance Test 6.16, Motor Driven Fire Pump Operability Test, Will Be Revised ML20043H0111990-06-12012 June 1990 Advises That AR Wargo Reassigned from Operating Shift Responsibilities & Will Be Resigning License,Effective on 900514 ML20055D1141990-06-0808 June 1990 Forwards Public Version of Revs to Emergency Response Procedures,Including Rev 9 to ERP-140 & Rev 3 to ERP-315 ML20043D7351990-06-0404 June 1990 Responds to NRC 900504 Ltr Re Violations Noted in Insp Repts 50-277/90-04 & 50-278/90-04.Corrective Actions:Procedural Controls Strengthened to Preclude Licensed Operators from Performing Licensed Duties W/O Successfully Passing Exams ML20043E9261990-06-0404 June 1990 Forwards Response to 900327 Request for Addl Info Re Generic Ltr 88-01, NRC Position on IGSCC in BWR Austenitic Stainless Steel Piping. ML20043D2681990-05-31031 May 1990 Forwards Response to NRC Requests Re PECo-FMS-0006, Methods for Performing BWR Reload Safety Evaluations. Util Core Monitoring Activities Routinely Access Accuracy of steady-state Physics Models Used in Evaluation of Parameter ML20043D6451990-05-30030 May 1990 Responds to NRC 900503 Ltr Re Violations Noted in Insp Repts 50-277/90-08 & 50-278/90-08.Corrective Actions:Glaucoma Testing Program Initiated for Security Personnel & Necessary Equipment to Perform Glaucoma Testing Onsite Obtained ML20055C5491990-05-18018 May 1990 Forwards Response to Request for Addl Info on 900412 Tech Spec Change Request 89-20 Re Postponement of Next Snubber Visual Insp,Due 900526,until Scheduled mid-cycle Outage in Fourth Quarter 1990 ML20055C5121990-05-18018 May 1990 Provides Info Inadvertently Omitted in Re Property Insurance Coverage for Plants.Limerick Generating Station Unit 2 Should Have Been Ref as Being Included Under Insurance Coverage ML20055C4851990-05-15015 May 1990 Forwards Annual Financial Repts for 1989 for Philadelphia Electric Co,Pse&G,Atlantic Energy,Inc & Delmarva Power & Light Co ML20043A3341990-05-14014 May 1990 Advises of Util Proposal to Provide Response to NRC Request for Schedule for Compliance W/Reg Guide 1.97 Re Neutron Monitoring Instrumentation 3 Months After NRC Concurrence W/Bwr Owners Group Design Criteria ML20042E7651990-04-27027 April 1990 Informs That Mod 2285 Completed on Unit 3,but That Mod 2285 Will Not Be Completed on Unit 2 During 8th Refueling Outage ML20042E8931990-04-27027 April 1990 Responds to Violation Noted in Insp Rept 50-278/90-01. Corrective Actions:Automatic Depressurization Sys Logic Sys Functional Tests Will Be Revised to Include Guidance in Unique Application of Test Lights ML20042F3241990-04-27027 April 1990 Advises That Organizational Changes Made in Advance of Approval of Tech Spec Change Request 88-06.Changes Do Not Present Unreviewed Safety Question ML20042E8741990-04-27027 April 1990 Responds to Generic Ltr 87-07, Info Transmittal of Final Rulemaking for Revs to Operator Licensing. Certifies That Limerick Operator Requalification Training Program Renewed on 900125 & Peach Bottom Subj Program Renewed on 890622 ML20012F4801990-04-0202 April 1990 Forwards Errata to Unit Shutdowns and Power Reductions Monthly Operating Rept for Feb 1990 ML20012F0971990-03-22022 March 1990 Forwards Summary of ASME Repairs & Replacement Completed, Per Facility Second 10-yr Interval Inservice Insps Completed During 900331-891111 Extended Refueling Outage ML20012E2151990-03-20020 March 1990 Responds to Generic Ltr 89-19, Request for Action Re Resolution of USI A-47, 'Safety Implication of Control Sys in LWR Nuclear Power Plants,' for Peach Bottom.Response for Limerick Generating Station Will Be Provided by 900504 ML20012C2931990-03-12012 March 1990 Responds to Generic Ltr 90-01, Request for Voluntary Participation in NRC Regulatory Impact Survey, Per 900118 Request ML20012B6211990-03-0808 March 1990 Provides Actions Taken to Ensure & Verify Sys Design Basis Performance,Per 900205 SSFI at Facility ML20012B9011990-03-0606 March 1990 Forwards 870331-891111 Inservice Insp Program Final Rept for Peach Bottom Atomic Power Station Unit 3 1987-1989 Extended Refuel Outage. Several Indications Identified ML20012A2661990-02-26026 February 1990 Forwards Application for Amends to Licenses DPR-44 & DPR-56, Consisting of Tech Spec Change Requests 89-13 & 89-14, Revising Nuclear Review Board Membership & Meeting Frequency & Adding Independent Safety Engineering Group Requirements ML20011F2541990-02-23023 February 1990 Forwards Revs to Physical Security Plan.Encls Withheld (Ref 10CFR73.21 & 2.790) ML20011F3791990-02-21021 February 1990 Provides Revised Schedule for Installation of Hardened Wetwell Vent,Per Generic Ltr 89-16 & Explanation Why Jan 1993 Completion Date Cannot Be Met Due to Unavailability of Matls.Intallation Scheduled for Cycle 9 Outage ML20006F5491990-02-16016 February 1990 Certifies That 891122 Tech Spec Change Request (Tscr) 89-15, 891228 Tscr 88-18 & 900214 Tscr 90-04 Mailed to Commonwealth of Pa,Dept of Environ Resources ML20006F1621990-02-15015 February 1990 Forwards Progress Rept Re Implementation of Control Room Enhancements as of End of Seventh Refueling Outage,Per NUREG-0737.Rept Delayed to Allow for Independent Verification of Control Room Enhancement Status ML20012B1731990-02-15015 February 1990 Forwards Public Version of Revs to Epips,Including Rev 5 to ERP-101,App 1 to Rev 13 to ERP-110,App 2 to Rev 10 to ERP-110,App 1 to Rev 7 to ERP-140,App 2 to Rev 10 to ERP-140,App 3 to Rev 11 to ERP-140 1990-09-18
[Table view] |
Text
10 CFR 2.201 10 CFR 2.205 I 4' .
PHILADELPHIA ELECTRIC COMPANY NUCLEAR GROUP HEADQUARTERS 955 65 CHESTERBROOK BLVD.
WAYNE,PA 19087 5691 I ' " I " " "
- o. w. suirs August 15. 1990
.2 mon vice pen iosur . nucLean Docket Nos. 50-277 50-278 )
License Nos. DPR-44 I
-DPR-56 <
l 1
Director Office of Enforcement U.S. Nuclear Regulatory Commission -
ATTN: Document Control Desk Washington, D.C. 20555 1
SUBJECT:
Peach Botton Atomic Power Station. Units 2 and 3 1
' Response to a Notice of Violation and Remittance of Civil Penalty - NRC Insper. tion Report Nos. "
50-277/90-200; 50-278/90-200 and 50-277/90-06; 50-278/90-06 ,
Dear Sir:
Attached is Philadelphia Electric Company's (PECo's) response to the July 16, 1990 NRC letter that transmitted the " Notice of Violation and Noposed '
y Imposition of Civil Penalty - $75.000 (NRC Inspection Report Nos. 50-277/O-200 50-278/90-200 and 50-277/90-06; 50-278/90-06)" for violations involving the emergency service water (ESW) system at Peach Botton Atomic Power Station (PBAPS) Units 2 and 3.
As a result of the' findings of the NRC Safety System Functional
- Inspection (SSFI) of the ESW system. PBAPS has conducted a Root Cause Analysis (RCA) of the identified ESW system problems. The results of the RCA have been used in determining the reasons for Violations A and C. The RCA also supported ,
evaluation of the effectiveness of previous corrective actions, and the development of corrective actions to prevent recurrence of these violations. ,
The attachment to this letter provides a restatement of the violations and the PECo response to each vinlation. A check in the amount of 1 seventy-five thousand dollars for payment of the civil penalty is also remitted i by this letter, and is enclosed. .
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Document Control Desk August 15, 1990 Page 2 The Notice of Violation stated the NRC staff is particularly concerned about the lack of aggressive management action to ensure the initiation of corrective actions to resolve the identified ESW system deficiencies in a timely manner. The actions we have taken to assure safety issues are identified and resolved in a timely manner are described in the response to Violation A. We believe the programs we currently have in place, as described in the response, are adequate to ensure that unresolved deficiencies will receive appropriate management action to initiate timely corrective actions, if you have any questions, or require additional information, please do not hesitate to contact us.
Very truly yours.
Enclosure 1 Attachment cc: T. T. Martin, Administrator, Region I, USNRC J. J. Lyash, USNRC Senior Resident Inspector i
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. . l COWebMWCALTH Of PENNSYLVANIA 3
- ss. 1 COUNTY Of CHESTER :
D. M. Smith, being first duly sworn, deposes and says:
' l That he is Senior Vice President of Philadelphia Electric Company; the Applicant herein; that he has read the response to the Notice of Violation and 1 Proposed luposition of Civil' Penalty - $75,000 (NRC Inspection Report Nos. 50-277/90-J 4
200;50-278/90-200and50-277/90-06;50-278/90-06), and knows the contents thereof; l and that the statements and matters set forth therein are true and correct to the best of his knowledges information and belief.
Senior Vice President l Subscribed and sworn to a
i beforamethis/6 day t
of d.w , 1990.
Ltin:
Dwh Notary Public I-
' NOTAPAL SEAL CATHERINE A MENDEZ Notary Pubuc
! Treevffnn Two., Chester county W Commission Exotres Sept 4.1993 _
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'. ,.., Attachment RESPONSE 10 A NOTICE OF VIOLATION 1
i Restatement of the Violations 1
- DuringaNRCsafetysystemfunctionalinspection(SSft)conductedbetween s I february 5 - March 2, 1990, as well as a routine resident inspection conducted I between February 20 - April.2, 1990, violations of NRC requirements were !
- identified. In accordance with the " General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2. Appendix C (1990), the Nuclear i
Regulatory Commission proposes to impose a civil penalty pursuant to Section 234 of the Atomic Energy Act of 1954, as amended ("Act"), 42 U.S.C. 2282, and 10 CFR 2.205. The particular violations and associated civil penalty are set forth ,
below:
A. 10 CFR Part 50 Appendix B Criterion XVI, requires, in part, that measures be established to assure that conditions adverse to quality, such as deficiencies, are promptly identified and corrected. i Technical Specifications Limiting Condition for Operation (LCO) 3.9.C.1 4
(Emergency Service Water) requires the ESW system to be operable at all times when reactor coolant. temperature is greater than 212 degrees fahrenheit.
Contrary to the above, measures were not established to assure that conditions adverse to quality in the plant emergency service water (ESW) system were promptly identified and corrected. Specifically ESW flow calculations perfomed in 1983 and 1984 indicated that system flow rates could be significantly lower than design flow rates such that the ESW system could not meet the original design flow requirements to the ECCS and RCIC room coolers; however, the licensee did not identify the safety l significance of this condition, nor did they initiate adequate corrective t
actions to correct this condition adverse to quality. As a result, for an indeterminate period prior to the shutdown of the unit on March 3, 1990 Unit 2operatedatupto100gpower(andwiththereactorcoolant temperature greater than 212 F) with the ESW system inoperable.
B. Technical Specifications Limiting Condition for Operation (LCO) 3.0.0 requires, in part, that when a system, subsystem, train, component or device is determined to be inoperable solely because its emergency power source is inoperable, it may be considered CPERABLE for the purpose of satisfying the requirements of the Limiting Condition for Operation.
I provided: (1) its corresponding normal power source is OPERABLE; and (2) all of its redundant systems, subsystems, trains, components and devices are OPERABLE. Unlessbothconditions(1)and(2)aresatisfied,theunit shall be placed in HOT SHUTDOWN within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in COLD SHUTDOWN within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.
Contrary to the above, the Unit 2 ESW system became inoperable when the emergency power source for ESW pump "A" was rendered inoperable at 11:55 p.m. on August 13, 1989, with the emergency cooling water pump already out of service, and the redundant "B" ESW subsystem isolated from Unit 2 due to the misalignment of two remote manual valves; however, ESW pump "A" was not declared inoperable, nor was the unit placed in HOT SHUTDOWN within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and COLD SHUTDOWN within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. Specifically Unit 2 power
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4 operations continued in this configuration until approximately 7:30 a.m. J l on August 15, 1989 (a period of approximately 32 hours3.703704e-4 days <br />0.00889 hours <br />5.291005e-5 weeks <br />1.2176e-5 months <br />.)
l C. 10 CFR 50.59(a)(1) permits the holder of a license to make changes in the facility as described in the safety analysis report, without prior l
Commission approval, unless the proposed change involves a change in the ;
technical specifications or an unreviewed safety question 10CFR50.59(b)(1) requires,inpart,thatrecordsofthesechangesbe I maintained, and these records shall include a written safety evaluation .
which provides the basis for the determination that the change does not involve an unreviewed safety question.
i Section 10.8.3 (Reactor Building Cooling Water System Description) of the 1 facility FSAR states that in the event of off-site power failure, the ;
emergency service water system can supply cooling water to the reactor ,
building cooling water system. Section 10.9.3 (Emergency Service Meter ;
System Descriptdon) of the FSAR states, in part, the emergency service !
i water system supply to the reactor building cooling water system heat.
exchangers is sufficient to maintain the cooling water system water design-temperature.
Section10.24.3(EmergencyHeatSinkDescription)oftheFSARalsor'ates. I in part, the emergency service water pumps take suction from the puny bays !
and supply water to standby diesel-generator coolers and the ECCS's pump I room air coolers. The return water from the coolers is boosted in ;
pressure by one of two emergency service water booster pumps and de'ivered !
to the emergency cooling tower.
Contrary to the above, changes were made to the facility ESW system as ;
described in the FSAR; however, adequate written safety evaluations were not prepared to provide'a basis for a determination that these changes did not involve an unreviewed safety question as evidenced by the following examples:
l 1. In 1979, the ESW system design was changed by isolating the reactor building closed cooling water system from the ESW system resulting in i
the reduction of ESW flow to the suction side of the ESW booster pumps; and
- 2. In 1989, plant procedures were revised such that the ESW booster pump-discharge valve was throttled resulting in reduced ESW flow to the l ECCS coolers when the emergency heat sink was placed in service.
These violations have been categorized in the aggregate as a Severity Level Ill problem. (Supplement 1) .
Civil Penalty - $75,000 l
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. Response to Violations Violation A Admission of Alleged Violation Philadelphia Electric Company acknowleoges the violation as stated.
Reason for the Violations ARootCauseAnalysis(RCA)wasconductedinresponsetothe-findingsofthe SSF1 and the following causes were identified to contribute to PECo's failure to promptly identify the safety significance and initiate adequate corrective actions to correct the conditions adverse.to the quality of the ESW system: 1) inadequate understanding of the ESW system design basis 2) poor communication between station and corporate engineering and during turnover of engineer responsibilities,and3)lackofanadequateprocessforidentifyingand correcting deficient conditions.
The inadequate understanding of the ESW system design basis and changing system design requirements led to the misinterpretation of the significance of the loss of instrument air. The original ESW system design did not include the. effects of a loss of station air on the ESW design flows. The diversion of flow from-the primary room coolers to both the primary and backup room coolers upon the loss of instrument air results in a reduction in ESW systes perfomance which would have been acceptable, based on a revised environmental qualification analysis, had the piping not degraded. The loss of instrument air, therefore, presented an ESW system performance challenge because the system piping had degraded and the flow t M become imbalanced in the system, i
The significance of the tsults of the 1984 Bechtel Network Analysis was not effectively communicates between corporate engineering and the station.. During the 1984/1985 period it was not recognized that the design basis needed to be changed, as the result of the Network Analysis, to consider the loss of instrument air. During subsequent test problems and modifications on the ESW system many communications between the station and engineering were infomal and some identified concerns were not tracked to closure by either group. Combined '
with inadequate turnover of responsibilities between engineers during-staffing changes. ESW system concerns existed without resolution for a number of years.
Corrective Steps Taken and Results Achieved The corrective actions taken to restore the ESW system to operable status during twoApril on unit power 12 andoperation have been previously provided during meetings with MRC June 1. 1990.
The corrective actions included extensive ESW system flow testing, inspection and maintenance, system configuration revision.
test procedure revisions, safety evaluations. and initiation of UFSAR changes.
Information developed during and since the SSFI has provided the foundation for an adequate understanding of the ESW design basis. !
This information was used to i revise test procedures and safety evaluations and update the UFSAR. A further i
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l enhancement to the design basis description information will be developed by our l Design Basis Document (D80) Program. The D80 Program, which is currently in the '
pilot program phase, will serve to increase our understanding of the design ;
basis for the ESW and other plant systems by providing information regarding the design, operation, and regulatory requirements of a plant system in one accessible document. The D80 will identify the specific functions to be i performed by a structure, system, or component and the specific values or ranges !
of values chosen for controlling parameters as reference bounds for design. The DBDs for the ESW and Emergency Cooling Water / Emergency Cooling Tower systems are 1
expected to be completed in March, 1992.
Forinal communication between the station and corporate engineering. Nuclear EngineeringDivision(NED)oftheNuclearEngineeringandServicesDepartment (NESD),wasenhancedwiththeinstitutionoftheEngineeringWorkRequest(EWR)-
) process in February, 1988. The EWR system requires timely response to and tracking of station requests by NESD. The P8APS Project Management Division of HESD has Project Managers to facilitate NESD responses to station requests and :
coordinate NESD support of modification designs. Engineering support of station )
activities is also a subject reviewed during Station Review and NESD staff ;
meetings. Station and NESD management have recognized improvement in NESD's support of the stations.
- l The process for identifying and correcting plant deficiencies was strengthened forNuclearGrouppersonndlinaNuclearGroupAdministrativeProcedure(NGAP)
NA-03N001, titled Control of Nonconfonnances in September,1989 The procedure
- addresses deficiencies generated as a result of plant work activities, '
modification activities, receipt inspection, or whenever equipment, .
l documentation, or methodologies appear to be deficient.. The NGAP provides a ,
uniform approach to identify, document. evaluate and resolve hardware and other !
deficiencies. Apparent hardware defic w ' 3re evaluated and resolved through the Monconformance Report (NCR) process. . . NCR disposition addresses the .
deficiency's effect on equipment operability. .apact on. design basis, the need 1 for a safety evaluation, reportability, and necessary document changes. The i NGAP directs non-hardware issues to be addressed through the Corrective Action Request (CAR) process which is implemented by the Nuclear Quality Assurance l l
(NQA) Department. The NQA Department monitors the NCR process and highlights- '
! outstanding items and trends for increased management attention. Since its i inception, the NCR process has effected many physical plant changes, procedure
- and program changes, and UFSAR changes to correct recognized deficiencies.
In addition, the process for determining reportable conditions was formalized in NGAP NA-02R001, titled Identification and Evaluation of Potentially Reportable Items and Events of Potential Public Interest, in March, 1990. This procedure requires any PECo employee or contractor who suspects or identifies a potentially reportable item to 1) immediately notify a Group i Evaluator /Reportability Coordinator of the item for review and processing, and l
- 2) initiate an appropriate corrective action process; e.g., an NCR.
l Corrective Steps Taken to Avoid Further Violation l The corrective actions currently being implemented, as described above, will serve to prevent recurrence of this violation. The effectiveness of these corrective actions will be monitored through existing self assessment activities.
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l The conduct of engineering responsibility turnover will be enhanced for station
, and NED engineering personnel, to minimize the loss of plant / system knowledge l
and experience during staffing changes, by December,1990.
In addition to the previously stated corrective actions, the 10 CFR 50.59 review process was strengthened through implementation of a NGAP and personnel training, in December, 1989. The training and procedure requirements have increased NESO and station personnel's sensitivity to plant / system changes which may adversely impact their required perfonnance.
i Date When Full Comp',iance,Will Be Achieved 1
The ESW syst a wr.s i n urned to operable status for two unit operation on April 14, 1990.
l Violation B l Admission Of The Alleged Violation Philadelphia Electric Company acknowledges the violation as stated.
l Reasons for the Violation The reasons for this violation are described below,
- a. The failure to open valves M0-2972 and M0-3972 during system restoration following maintenance prevented proper ESW design basis system alignment. This situation resulted from the lack of guidance provided in the use of the " tag-off" process where the blocking permit tag was removed without returning the valves from the blocked condition to their appropriate position. This process was frequently used curing outages where blocked valves or system components would be tagged off during permit removal and subsequently repositioned by the completion of appropriate check-off lists (COL) prior to restoring the system to operation. At the time of this event, Unit 2 was operating at 737. power and Unit 3 was in an extended outage. Although the blocking permit involved work being done on Unit 3 equipment, the permit blocked ESW equipment connon to both units. Operations personnel were using outage " tag-off" methodology, relying on a completed COL prior to declaration of U3 ESW system operability although Unit 2 was in operation. The repositioning of the valves and system restoration were dependent upon completion of the appropriate COL. This outage " mind-set" concerning the use of " tag-off" by operations personnel was further compounded by the lack of guidance on when it was appropriate to use " tag-off". The Unit 3 COL did not contain M0-2972, which was only contained in the Unit 2 COL. The velve position verification step of the Unit 3 COL for H0-3972 was not per.'ormed, and the COL was also not properly completed. Additionally, the p0sition of M0-3972 was incorrectly transcribed as in the open
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l position when data was transferred to a final COL. Also, an '
i independent verification of safety system alignment was not performed.
These factors contributed to the failure to reopen M0-2972 and MO-3972.
- b. 'The Chief Operator. Unit Reactor Operator, and Shift Technical Advisors are required to perfom control panel walkdowns as indicated on their respective shift turnover COL's shortly after assumi shift responsibilities. Part of this walkdown for the Unit Reactor rator-i is to compare nomal valve position indicated by color specific dots on the panel with valve position indicating lights. This comparison J indicates whether the valve is in the appropriate normal position or if the valve has been blocked or isolated. During the time of the event, however, the ESW panel with M0-2972 and M0-3972 was not-included on any of the shift turnover COL's to compare normal valve (
position versus present valve position. This oversight occurred
! during the development of the shift turnover COL's. These factors contributed to the delay in detecting the closed positions of MO-2972 I and M0-3972.
- c. The emergency cooling water (ECW)' pump was m ved from service August 13, 1989 for scheduled maintenance. At that time-the ECW pump was considered to be equivalent to an ESW pump. On the night of August j
13, 1989, the E2 emergency diesel generator (EDG) was removed from-service for an annual maintenance outage. The E2 EDG is the emergency a
power supply to the "A" ESW pump. The inoperable status.of this equipment and the mis-alignment of M0-2972 and M0-3972 altered the
! operability of the "A" and "B" ESW pumps resulting in non-compliance with Technical Specification (TS) 3.0.0. In this condition. TS 3.0.C-
! required the unit to be in Hot Shutdown within six hours and in Cold Shutdown within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. '
- l. d. The valve misalignment was discovered and corrected approximately 31.5 l hours after the E2 diesel was taken out of service. A critique was l conducted iimmediately following the discovery of the valve mispositioning. During the critique, the plant-staff incorrectly determined that ESW was still operable because either the M0-2972 or M0-3972 could be quickly operated from the Control Roon. thereby providing ESW flow to Unit 2. An Operations Incident Report was initiated to determine the details of the incident e d contributing factors. Follow-up discussions with the NRC and subseg ent .
i engineering analysis corrected misinterpretations of the' initial
! critique and disclosed the non-conformance with TS 3.0.D and 3.0.C as well as the failure to consider and properly address a potentially unanalyzed condition.
Corrective Steps Taken and Results Achieved
- The valve misalignment of M0-2972 and M0-3972 was identified and the valves were promptly returned to their normal open position. This resulted in the return of the ESW system to its proper design basis positioning. Operations management was notified and an investigation was initiated.
I Page 7 The use of " tag off" has been severely restricted for an operating unit. " Tag-off" may be used during an outage provided " Permit to be removed tag-off" is specified on the permit and the Operations Coordinator ensures appropriate S0/ COL (s) to restore the components are in the Outage Schedule. Specific guidance on proper component positioning during permit restoration was provided in a revision to the permit and blocking manual. Notification of this revision ,
- was also made to appropriate Operations personnel. I The procedure for control room panel walkdowns has been revised to provide ;
additional guidance on valve positioning comparison to the Shift Technical '
Advisor as well as the addition of ESW system panel to the Chief Operator shift i turnover COL.
A training letter on operability was distributed to licensed personnel that detailed this incident and included a discussion of adverse system aligtment.
Appropriate members of plant staff were issued the operability letter to ensure future issues are properly understood and evaluated.
l The corrective actions completed have improved procedural control and have heightened operations personnel awareness of the equipment restoration process, 1 Technical Specifications 3.0.0 and operability awareness. .
Corrective Steps That Will Be Taken To Avoid further Violation The training Department will formally train licensed operator personnel and plant staff on Technical Specification 3.0.0 using this incident and other industry events to reinforce Technical Specification compliance and operability deteminations. This training will be incorporated into licensed operator continuing training by December 1, 1990. t A procedure will be developed to formalize the pre-release review requirements and operability determination before removing a diesel generator from service for maintenance or testing. This procedure will be completed by December 31, 1990.
System COLs for common safety related systems will b. revised to ensure appropriate port ions cf the system affecting both units are properly incorporated into each unit's COL. All apprcpriate revisions will be completed by October 31 i
1990. >
lhe actioni described in the previous section will also prevent recurrence and will improve methods to avoid future violations.
Date When Full Compliance Was Achieved full compliance was achieved August 15, 1969 when M0-2972 and M0-3972 were '
returned to open positions, resalting in the design basis alignment for the ESW system.
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, Page 8 Violation C Admission of Alleged Violation Philadelphia Electric Cow any acknowledges the violation as stated.
Reasons for The Violation
- 1he reasons for the subject inadequate safety evaluations were 1) inadequate understanding of the impact of the change made in 1979 on the design basis and 2)thelackofunderstandingthatchangingapositionofavalvetothrottle flow needed to be evaluated against the design basis. 1 Corrective Steps Taken and Results Achieved The inneediate corrective actions taken to address the improper isolation of the RBCCW system from the ESW system were_ testing of the ESW system in the isolated t configuration, performance of a safety evaluation in accordance with 10 CFR 50.59, and initiation of a UFSAR change.
A 10 CFR 50.59 review performed to support modifications associated with the closed loop mode of ESW was updated to properly evaluate the potential effects of throttling system flow on the systems served by ESW and the throttled valves, in addition, the system operating procedure has been revised to. incorporate information on the throttling of the pump discharge valve.
The 10 CFR 50.59 review process was revised and formally implemented in the NGAP, NA-02R002, in December, 1989. The NGAP was developed as the result of recognized inconsistencies in complying with the intent and specific requirements of 10 CFR 50.59. The revised 50.59 Review is a two-step process consisting of a 50.59 Determination and a 50.59 Safety Evaluation and is based upon guidance in WSAC 125. " Guidelines for 10 CFR 50.59 Safety Evaluations."
The Determination is a screening step to decide whether or not 50.59 is applicable.
If 50.59 is applicable, a Safety Evaluation is required to be performed. A 50.59 Review is initiated for any proposed change to the facility or procedures and for any proposed new or altered test or experiment.
The two events in this violation involved safety evaluations performed in 1980 and April,1989, prior to tapheentation of the 10 CFR 50.59 Review NGAP. ,
The Independent Safety Engineering Group. Nuclear Review Board, NQA, and self-a:sessment activities have indicated significant improvement in the quality of 10 CFR 50.59 reviews since the implementation of the NGAP. ;
i Corrective Steps Taken to Avoid Further Violation i
The strengthening of the 50.59 review process through the implementation of the NGAP and personnel training in its use will prevent further violations concerning inadequate safety evaluation reviews.
, ; 7.- Page 9 The effectiveness of the implementation of the revised 10 CFR 50.59 review process, NGAP NA-02R002, will be monitored through existing self assessment activities. j Date When Full Compliance Was Achieved The revision of the safety evaluations and test procedures and initiation of the ;
UFSAR changes were completed on May 9, 1990. i
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