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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M6631999-10-19019 October 1999 Forwards Insp Rept 50-277/99-07 & 50-278/99-07 on 990920.No Violations Noted ML20217K9241999-10-14014 October 1999 Forwards Amend 234 to License DPR-56 & Se.Amend Consists of Changes to TS in Response to Application & Suppls ,1001 & 06,which Will Support PBAPS Mod P00507,which Will Install Digital Pr Neutron Mining Sys ML20217F7391999-10-14014 October 1999 Requests Addl Info Re Peach Bottom Atomic Power Station Units 2 & 3 Appendix R Exemption Requests ML20217F6841999-10-13013 October 1999 Forwards Senior Reactor Operator Initial Exam Repts 50-277/99-302(OL) & 50-278/99-302(OL) Conducted on 990913- 16.All Applicants Passed All Portions of Exam ML20217F3021999-10-12012 October 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at PBAPS Have Been Completed.Ltr Also Confirms Completion of Actions Required by Confirmatory Order Modifying Licenses, ML20217E7451999-10-0808 October 1999 Forwards Response to NRC 990820 RAI Concerning Proposed Alternatives Associated with Third ten-yr Interval ISI Program for Pbaps,Units 2 & 3 ML20217B7701999-10-0606 October 1999 Submits Corrected Info to NRC 980528 RAI Re Util Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions ML20217B9151999-10-0606 October 1999 Provides Clarifying Info to Enable NRC to Complete Review of License Change Request ECR 98-01802,re Changes Necessary to Support Installation of Digital Pr Neutron Monitoring & Incorporate long-term T/H Stability Solution Hardware ML20217C4141999-10-0606 October 1999 Forwards Response to NRC 981109 RAI Re Resolution of USI A-46 for Pbaps.Proprietary Excerpts from GIP-2,Ref 25 Results of BWR Trial Plant Review Section 8 Also Encl. Proprietary Excerpts Withheld ML20217B3181999-10-0505 October 1999 Advises That Info Submitted in 990712 Application,Which Contained Attachment Entitled, Addl Info Re Cycle Spec SLMCPR for Peach Bottom 3 Cycle 13,dtd 990609, with Affidavit,Will Be Withheld from Public Disclosure ML20217B4051999-10-0505 October 1999 Forwards Amend 233 to License DPR-56 & Safety Evaluation. Amend Changes Minimum Critical Power Ratio Safety Limit & Approved Methodologies Referenced in Core Operating Limits Report 05000278/LER-1999-004, Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv)1999-10-0101 October 1999 Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv) ML20217B8891999-10-0101 October 1999 Forwards Response to RAI Re Request to Install Digital Power Range Neutron Monitoring Sys & Incorporate long-term,thermal-hydraulic Stability Solution Hardware. Revised TS Table 3.3.2.1-1 Encl ML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20212J6851999-09-29029 September 1999 Informs of Completion of mid-cycle PPR of Peach Bottom Atomic Power Station on 990913.No Areas Identified in Which Licensee Performance Warranted Addl New Insps Beyond Core Insp Program.Historical Listing of Plant Issues Encl ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212J5751999-09-28028 September 1999 Informs of Individual Exam Results for Applicants on Initial Exam Conducted on 990913-16 at Licensee Facility.Without Encls ML20216J0191999-09-27027 September 1999 Forwards Request for Addl Info Re Util 990301 Request to Support Installation of Digital Power Range Neutron Monitoring Sys & Incorporation of long-term thermal- Hydraulic Stability Solution Hardware,For Plant ML20212H6171999-09-24024 September 1999 Forwards Rev 2 to COLR for Pbaps,Unit 2,Reload 12,Cycle 13, IAW TS Section 5.6.5.d.Rept Incorporates Revised Single Loop Operation MAPLHGR Flow Multiplier ML20216H6451999-09-24024 September 1999 Forwards Notice of Withdrawal of Util 990806 Application for Amends to Fols DPR-44 & DPR-56.Proposed Change Would Have Involved Temporary Change to Increase Limit for Average Water Temp of Normal Heat Sink ML20212H5431999-09-24024 September 1999 Informs of Decision to Inspect H-3 & H-4 Shroud Welds During Upcoming 3R12 Outage Scheduled to Begin Late Sept 1999 ML20216H6751999-09-24024 September 1999 Forwards Amends 229 & 232 to Licenses DPR-44 & DPR-56, Respectively & Ser.Amends Will Delete SR Associated Only with Refueling Platform Fuel Grapple Fully Retracted Position Interlock Input,Currently Required by SR 3.9.1.1 ML20216F8811999-09-23023 September 1999 Withdraws 990806 Exigent License Change Application.Tech Spec Change to Allow Continued Power Operation with Elevated Cooling Water Temps During Potentially Extreme Weather Conditions No Longer Needed Due to Favorable Weather ML20212E8661999-09-22022 September 1999 Discusses GL 98-01 Y2K Readiness of Computer Sys at NPPs & Supplement 1 & PECO Response for PBAPS Dtd 990630. Understands That at Least One Sys or Component Listed May Have Potential to Cause Transient During Y2K Transition ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212D1191999-09-17017 September 1999 Forwards SE Re Proposed Alternatives to ASME Section XI Requirements for Containment Inservice Insp Program at Plant,Units 2 & 3 ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment ML20211P2961999-09-0707 September 1999 Provides Authorization to Administer NRC Approved Initial Written Exams to Listed Applicants on 990913 at Peach Bottom Npp,Delta,Pennsylvania ML20211K7031999-08-30030 August 1999 Forwards Response to NRC 990826 RAI Re License Change Application ECR 99-01255,revising TSs 2.1.1.2 & 5.6.5 ML20211E6941999-08-26026 August 1999 Forwards Request for Addl Info Re Min Critical Power Ratio. Response Should Be Submitted within 30 Days of Ltr Receipt ML20211Q4491999-08-25025 August 1999 Responds to Re Changes to PBAPS Physical Security Plan,Safeguards Contingency Plan & Guard Training & Qualification Plan Identified as Revs 13,11 & 9, Respectively.No NRC Approval Is Required,Per 10CFR50.54(p) ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211D5421999-08-23023 August 1999 Forwards Amends 228 & 231 to Licenses DPR-44 & DPR-56, Respectively & Se.Amends Revise TSs to Correct Typographical & Editorial Errors Introduced in TSs by Previous Amends ML20211A9721999-08-20020 August 1999 Forwards Request for Addl Info Re Third 10-year Interval Inservice (ISI) Insp Program Plan for Plant,Units 2 & 3 ML20210T5451999-08-12012 August 1999 Forwards Copy of Environ Assessment & Findings of No Significant Impact Re Licensee Request for Amends to Plant. Amends Consist of Changes to TS to Correct Typos & Editorial Errors Introduced in TS by Previous Amends ML20210P8321999-08-11011 August 1999 Responds to NRC 990715 Telcon Re Util 990217 Submittal of Proposed Alternatives to Requirements of 10CFR50.55a(g)(6)(ii)(B)(1) Re Containment Inservice Insp Program ML20210P8151999-08-11011 August 1999 Forwards Final Pages for Pbaps,Unit 2 & 3 OLs Re License Change Application ECR 99-01497,which Reflects Change in Corporate Structure at Pse&G ML20211B6521999-08-10010 August 1999 Informs That Dp Lewis,License SOP-11247,has Been Permanently Reassigned & No Longer Requires License,Per 10CFR50.74.Util Requests That Subject Individual Be Removed from List of License Holders ML20210P1561999-08-10010 August 1999 Submits Response to Requests for Addl Info Re GL 92-01,rev 1,Suppl 1, Rv Structural Integrity, for Pbap,Units 1 & 2. NRC Will Assume That Data Entered Into Rvid Are Acceptable for Plants,If Staff Does Not Receive Comments by 990901 ML20211B7881999-08-10010 August 1999 Transmits Summary of Two Meetings with Risk-Informed TS Task Force in Rockville,Md on 990514 & 0714 ML20210N7831999-08-0909 August 1999 Forwards Copy of Notice of Consideration of Issuance of Amends to Fols,Proposed NSHC Determination & Opportunity for Hearing, Re 990806 Request for License Amends.Amends Incorporate Note Into PBAPS TS to Permit One Time Exemption ML20210P0801999-08-0404 August 1999 Forwards Initial Exam Repts 50-277/99-301 & 50-278/99-301 on 990702-14 (Administration) & 990715-22 (Grading).Six of Limited SRO Applicants Passed All Portion of Exam ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response NUREG-1092, Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls1999-08-0303 August 1999 Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls ML20210J0161999-07-30030 July 1999 Forwards Copy of Notice of Consideration of Approval of Transfer of FOL & Issuance of Conforming Amends Re 990723 Application ML20210H5341999-07-27027 July 1999 Forwards Insp Repts 50-277/99-05 & 50-278/99-05 on 990518- 0628.NRC Determined That Two Severity Level IV Violations of NRC Requirements Occurred & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20210F3731999-07-23023 July 1999 Submits Confirmation That,Iaw 10CFR50.80,PSE&G Is Requesting NRC Approval of Transfer of Ownership Interests in PBAPS, Units to New Affiliated Nuclear Generating Company,Pseg Nuclear LLC ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20210E5811999-07-21021 July 1999 Forwards Final Tech Specs Pages for License Change Application.Proposed Change Will Revise Tech Specs to Delete Requirement for Refuel Platform Fuel Grapple Fully Retracted Position Interlock Currently Required by TS ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217F3021999-10-12012 October 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at PBAPS Have Been Completed.Ltr Also Confirms Completion of Actions Required by Confirmatory Order Modifying Licenses, ML20217E7451999-10-0808 October 1999 Forwards Response to NRC 990820 RAI Concerning Proposed Alternatives Associated with Third ten-yr Interval ISI Program for Pbaps,Units 2 & 3 ML20217C4141999-10-0606 October 1999 Forwards Response to NRC 981109 RAI Re Resolution of USI A-46 for Pbaps.Proprietary Excerpts from GIP-2,Ref 25 Results of BWR Trial Plant Review Section 8 Also Encl. Proprietary Excerpts Withheld ML20217B9151999-10-0606 October 1999 Provides Clarifying Info to Enable NRC to Complete Review of License Change Request ECR 98-01802,re Changes Necessary to Support Installation of Digital Pr Neutron Monitoring & Incorporate long-term T/H Stability Solution Hardware ML20217B7701999-10-0606 October 1999 Submits Corrected Info to NRC 980528 RAI Re Util Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions ML20217B8891999-10-0101 October 1999 Forwards Response to RAI Re Request to Install Digital Power Range Neutron Monitoring Sys & Incorporate long-term,thermal-hydraulic Stability Solution Hardware. Revised TS Table 3.3.2.1-1 Encl 05000278/LER-1999-004, Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv)1999-10-0101 October 1999 Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv) ML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212H6171999-09-24024 September 1999 Forwards Rev 2 to COLR for Pbaps,Unit 2,Reload 12,Cycle 13, IAW TS Section 5.6.5.d.Rept Incorporates Revised Single Loop Operation MAPLHGR Flow Multiplier ML20212H5431999-09-24024 September 1999 Informs of Decision to Inspect H-3 & H-4 Shroud Welds During Upcoming 3R12 Outage Scheduled to Begin Late Sept 1999 ML20216F8811999-09-23023 September 1999 Withdraws 990806 Exigent License Change Application.Tech Spec Change to Allow Continued Power Operation with Elevated Cooling Water Temps During Potentially Extreme Weather Conditions No Longer Needed Due to Favorable Weather ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment ML20211K7031999-08-30030 August 1999 Forwards Response to NRC 990826 RAI Re License Change Application ECR 99-01255,revising TSs 2.1.1.2 & 5.6.5 ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20210P8321999-08-11011 August 1999 Responds to NRC 990715 Telcon Re Util 990217 Submittal of Proposed Alternatives to Requirements of 10CFR50.55a(g)(6)(ii)(B)(1) Re Containment Inservice Insp Program ML20210P8151999-08-11011 August 1999 Forwards Final Pages for Pbaps,Unit 2 & 3 OLs Re License Change Application ECR 99-01497,which Reflects Change in Corporate Structure at Pse&G ML20211B6521999-08-10010 August 1999 Informs That Dp Lewis,License SOP-11247,has Been Permanently Reassigned & No Longer Requires License,Per 10CFR50.74.Util Requests That Subject Individual Be Removed from List of License Holders ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML20210F3731999-07-23023 July 1999 Submits Confirmation That,Iaw 10CFR50.80,PSE&G Is Requesting NRC Approval of Transfer of Ownership Interests in PBAPS, Units to New Affiliated Nuclear Generating Company,Pseg Nuclear LLC ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20210E5811999-07-21021 July 1999 Forwards Final Tech Specs Pages for License Change Application.Proposed Change Will Revise Tech Specs to Delete Requirement for Refuel Platform Fuel Grapple Fully Retracted Position Interlock Currently Required by TS ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 05000278/LER-1999-002, Forwards LER 99-002-01 to Correct Title Contained in Box (4) of LER Coversheet Form.Rev Does Not Change Reportability Requirements or Any Other Info Contained in Original Submittal of LER1999-07-12012 July 1999 Forwards LER 99-002-01 to Correct Title Contained in Box (4) of LER Coversheet Form.Rev Does Not Change Reportability Requirements or Any Other Info Contained in Original Submittal of LER ML20209G9121999-07-0909 July 1999 Informs That Ja Hutton Has Been Appointed Director,Licensing for PECO Nuclear,Effective 990715.Previous Correspondence Addressed to Gd Edwards Should Now Be Sent to Ja Hutton ML20209D9781999-07-0808 July 1999 Forwards Addl Info to Support EA of Proposed 990212 License Application ECR 98-01675,correcting Minor Administrative Errors in TS Figure Showing Site & Exclusion Areas Boundaries & Two TS SRs ML20209D8821999-07-0707 July 1999 Submits Estimate of Number of Licensing Actions Expected to Be Submitted in Years 2000 & 2001,as Requested by Administrative Ltr 99-02.Renewal Applications for PBAPS, Units 2 & 3,will Be Submitted in Second Half of 2001 ML20209D2671999-07-0202 July 1999 Responds to NRC 990322 & 0420 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20209E1131999-06-30030 June 1999 Forwards Proprietary NRC Form 398, Personal Qualification Statement-Licensee, for Renewal of RO Licenses for EP Angle,Md Lebrun,Jh Seitz & Zi Varga,Licenses OP-10646-1, OP-11081,OP-11082 & OP-11085,respectively.Encls Withheld ML20209B7001999-06-30030 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20209C1201999-06-30030 June 1999 Informs of Util Intent to Request Renewed License for PBAPS, Units 2 & 3,IAW 10CFR54.Licensee Anticipates That License Renewal Application Will Be Submitted in Second Half of 2001 05000277/LER-1999-004, Forwards LER 99-004-00 Re Unplanned ESF Actuations During Planned Electrical Bus Restoration Following Maint Activities1999-06-20020 June 1999 Forwards LER 99-004-00 Re Unplanned ESF Actuations During Planned Electrical Bus Restoration Following Maint Activities ML20196A5291999-06-14014 June 1999 Forwards Final Pbaps,Unit 3 TS Pages for License Change Request ECR 98-01802 Re Installation of Digital Power Range Neutron Monitoring (Prnm) Sys & Incorporation of long-term thermal-hydraulic Stability Solution Hardware ML20195E6051999-05-27027 May 1999 Requests Exemption from Requirements of 10CFR72.44(d)(3) Re Submittal Date for Annual Rept of Principal Radionuclides Released to Environ.Exemption from 10CFR72.72(d) Re Storage of Spent Fuel Records,Additionally Requested ML20195B8171999-05-25025 May 1999 Forwards Final TS Pages for License Change Application ECR 96-01511 Re Rev to Loss of Power Setpoints for 4 Kv Emergency Buses ML20195B6191999-05-19019 May 1999 Forwards PBAPS Units 2 & 3 Annual Radiological Environ Operating Rept 56 for 980101-1231, Per Section 6.9.2 of Ol. Trace Concentrations of Cs-137 Were Found in Sediment Consistent with Levels Observed in Previous Years ML20206P9171999-05-10010 May 1999 Updates Some of Transmitted Data Points Provided in Data Point Library ERDS for Pbaps,Units 2 & 3.Data Point Info Format Consistent with Guidance Specified in NUREG-1394 ML20206K6581999-05-0404 May 1999 Forwards PBAPS Bases Changes Through Unit 2 Bases Rev 25 & Units 3 Bases Rev 25.Bases Reflect Change Through Apr 1999, Thereby Satisfying Frequency Requirements of 10CFR50.71 ML20206D4651999-04-29029 April 1999 Forwards Rev 16 to UFSAR & Rev 11 to Fire Protection Program (Fpp), for Pbaps,Units 2 & 3.Page Replacement Instructions for Incorporating Rev 16 to UFSAR & Rev 11 to Fpp,Encl ML20207B8431999-04-23023 April 1999 Forwards Final Rept for 981117,plume Exposure Pathway Exercise of Offsite Radiological Emergency Response Plans site-specific for Peach Bottom Atomic Power Station.One Deficiency & 27 Areas Requiring C/A Identified ML20206C5461999-04-20020 April 1999 Forwards Radioactive Effluent Release Rept 41 for Jan-Dec 1998 for Pbaps,Units 1 & 2. Revs Made to ODCM & Station Process Control Program (PCP) During Rept Period,Encl 05000277/LER-1999-003, Forwards LER 99-003-00 Re 990318 Failure to Maintain Provisions of Fire Protection Program to Properly Address Effects of Flooding1999-04-16016 April 1999 Forwards LER 99-003-00 Re 990318 Failure to Maintain Provisions of Fire Protection Program to Properly Address Effects of Flooding ML20205K4541999-04-0808 April 1999 Forwards Revised Info Re 990330 NRC Nuclear Power Reactor Licensee Financial Qualifications & Decommissioning Funding Assurance Status Rept 05000278/LER-1999-001, Forwards LER 99-001-00 Re 990312 ESF Actuation of Rcics Due to High Steam Flow Signal During Sys Restoration.Rept Submitted Per 10CFR50.73(a)(2)(iv)1999-04-0808 April 1999 Forwards LER 99-001-00 Re 990312 ESF Actuation of Rcics Due to High Steam Flow Signal During Sys Restoration.Rept Submitted Per 10CFR50.73(a)(2)(iv) ML18106B1431999-03-31031 March 1999 Forwards Pse&G Rept on Financial Min Assurance for Period Ending 981231 for Hope Creek,Salem,Units 1 & 2 & Pbaps,Units 2 & 3,IAW 10CFR50.75 ML20205F8981999-03-31031 March 1999 Provides Info Re Status of Decommissioning Funding for LGS, Units 1 & 2,PBAPS,Units 1,2 & 3 & Sgs,Units 1 & 2,per Requirements of 10CFR50.75(f)(1) ML18106B1411999-03-30030 March 1999 Forwards Decommissioning Info on Behalf of Conectiv Nuclear Facility License Subsidiaries,Atlantic City Electric Co & Delmarva Power & Light Co,For Listed Nuclear Facilities ML20205J0831999-03-26026 March 1999 Requests Enforcement Discretion from Requirements of PBAPS, Units 2 & 3 Ts.Enforcement Discretion Pursued to Avoid Unneccessary Plant Transient Which Would Result from Compliance with TS ML20205B6421999-03-24024 March 1999 Submits 1998 Annual Decommission Rept for Pbaps,Unit 1. There Were No Reportable Events Involving Unit 1 for 1998 1999-09-09
[Table view] Category:UTILITY TO NRC
MONTHYEARML20064A7171990-09-18018 September 1990 Comments on SALP Board Repts 50-277/89-99 & 50-278/89-99. Author Pledges Continued Mgt Support of & Attention to Rate of Improvement,Achievement of Goals & Performance of Routine Activities ML20065D4421990-09-14014 September 1990 Responds to Generic Ltr 90-07, Operator Licensing Natl Exam Schedule. Proposed Schedules for Operator Licensing Exams, Requalification Exams & Generic Fundamental Exams Encl ML20064A7751990-09-13013 September 1990 Advises That Ba Stambauth No Longer Maintains Need to Hold Senior Operator License ML20065D3741990-09-11011 September 1990 Forwards Rev to Relief Request 10-VRR-2 Re RHR stay-fill Supply Check Valves,Per ML20059F0541990-08-31031 August 1990 Responds to NRC Re Violations Noted in Safety Insp Repts 50-277/90-13 & 50-278/90-13.Corrective Actions: Training Will Be Provided for Personnel Re Requirements of Drawing E1317 & Administrative Procedures A-2 & A-6 ML20028G8181990-08-27027 August 1990 Forwards Peach Bottom Atomic Power Station Semiannual Effluent Release Rept,Jan-June 1990. No Revs Made to ODCM During Rept Period ML20059A6461990-08-15015 August 1990 Responds to Violation Noted in Insp Repts 50-277/90-200, 50-278/90-200,50-277/90-06 & 50-278/90-06 & Payment of Civil Penalty in Amount of $75,000.Corrective Actions:Emergency Svc Water Sys Restored to Operable Status ML20058N1991990-08-0909 August 1990 Advises of Change of Address for Correspondence Re Util Operations.All Incoming Correspondence Must Be Directed to One of Listed Addresses ML20058Q4051990-08-0606 August 1990 Forwards Public Version of Revised Emergency Response Procedures,Including Rev 12 to ERP-140,App 2,Rev 13 to ERP-140,App 3,Rev 4 to ERP-230,Rev 3 to ERP-305 & Rev 3 to ERP-660 ML20058M6631990-08-0303 August 1990 Responds to NRC 890406 Integrated Assessment Team Insp Repts 50-277/89-81 & 50-278/89-81.Based on Encl Schedule,Overall Projected Implementation Date Will Be 901119 ML20056A9611990-08-0303 August 1990 Notifies That Be Saxman Terminated Employment & Operating Responsibilities W/Util on 900706 ML20081E1581990-07-30030 July 1990 Forwards List of 1990 QA Program Changes for Plant.List Identifies Page & Paragraph Number,Brief Description & Type of Change ML20056A0421990-07-27027 July 1990 Forwards Updated Human Resource Status Rept for Jan-Jul 1990 for Areas Identified in Integrated Assessment Team Insp Repts 50-277/89-81 & 50-278/89-81 ML18095A3761990-07-26026 July 1990 Forwards Decommissioning Repts & Certification of Financial Assurance for Plants ML18095A3661990-07-26026 July 1990 Forwards Decommissioning Repts for Hope Creek,Peach Bottom & Salem Nuclear Generating Stations ML18095A3721990-07-24024 July 1990 Forwards Rept & Certification of Financial Assurance for Decommissioning for Plants,Per 10CFR50.75 ML20055H8331990-07-20020 July 1990 Submits Change of Addresses for Correspondence Re Util Nuclear Operations ML20044B2621990-07-12012 July 1990 Forwards Annual Progress Rept on Implementation of Control Room Enhancements,Per NUREG-0737.Corrective Actions for All Priority 1 Human Engineering Discrepancies Completed for Unit.Remaining Priority 2 Discrepancies Under Reevaluation ML20055G5481990-07-11011 July 1990 Forwards Public Version of Revised Epips,Including Rev 12 to ERP-140,App 3 & Revs 3 to ERP-310 & ERP-317 ML20043H7041990-06-21021 June 1990 Forwards Endorsements 143-146 to Nelia Policy NF-140 & Endorsements 93-96 to Maelu Policy MF-67 ML20044A2961990-06-21021 June 1990 Submits Revised Response to NRC Bulletin 89-002 Re safety- Related Swing Check Valves to Be Installed on Emergency Diesel Generator.Bolts Will Not Be Replaced Because Valves W/Original Internal Bolts Meet Requirements of Bulletin ML20043H6081990-06-19019 June 1990 Corrects 900427 Response to Generic Ltr 87-07, Info Transmittal of Final Rulemaking for Revs to Operator Licensing - 10CFR55 & Conforming Amends. ML20055C7621990-06-18018 June 1990 Informs NRC of Plans Re Licensing of Senior Reactor Operators (Sros) Limited to Fuel Handling at Plants.Util in Process of Implementing New Program for Establishment & Maint of Licensed SROs Limited to Fuel Handling at Plants ML20043G8131990-06-13013 June 1990 Responds to NRC 900515 Ltr Re Violations Noted in Insp Repts 50-277/90-06 & 50-278/90-06.Corrective Actions:Surveillance Test 6.16, Motor Driven Fire Pump Operability Test, Will Be Revised ML20043H0111990-06-12012 June 1990 Advises That AR Wargo Reassigned from Operating Shift Responsibilities & Will Be Resigning License,Effective on 900514 ML20055D1141990-06-0808 June 1990 Forwards Public Version of Revs to Emergency Response Procedures,Including Rev 9 to ERP-140 & Rev 3 to ERP-315 ML20043D7351990-06-0404 June 1990 Responds to NRC 900504 Ltr Re Violations Noted in Insp Repts 50-277/90-04 & 50-278/90-04.Corrective Actions:Procedural Controls Strengthened to Preclude Licensed Operators from Performing Licensed Duties W/O Successfully Passing Exams ML20043E9261990-06-0404 June 1990 Forwards Response to 900327 Request for Addl Info Re Generic Ltr 88-01, NRC Position on IGSCC in BWR Austenitic Stainless Steel Piping. ML20043D2681990-05-31031 May 1990 Forwards Response to NRC Requests Re PECo-FMS-0006, Methods for Performing BWR Reload Safety Evaluations. Util Core Monitoring Activities Routinely Access Accuracy of steady-state Physics Models Used in Evaluation of Parameter ML20043D6451990-05-30030 May 1990 Responds to NRC 900503 Ltr Re Violations Noted in Insp Repts 50-277/90-08 & 50-278/90-08.Corrective Actions:Glaucoma Testing Program Initiated for Security Personnel & Necessary Equipment to Perform Glaucoma Testing Onsite Obtained ML20055C5491990-05-18018 May 1990 Forwards Response to Request for Addl Info on 900412 Tech Spec Change Request 89-20 Re Postponement of Next Snubber Visual Insp,Due 900526,until Scheduled mid-cycle Outage in Fourth Quarter 1990 ML20055C5121990-05-18018 May 1990 Provides Info Inadvertently Omitted in Re Property Insurance Coverage for Plants.Limerick Generating Station Unit 2 Should Have Been Ref as Being Included Under Insurance Coverage ML20055C4851990-05-15015 May 1990 Forwards Annual Financial Repts for 1989 for Philadelphia Electric Co,Pse&G,Atlantic Energy,Inc & Delmarva Power & Light Co ML20043A3341990-05-14014 May 1990 Advises of Util Proposal to Provide Response to NRC Request for Schedule for Compliance W/Reg Guide 1.97 Re Neutron Monitoring Instrumentation 3 Months After NRC Concurrence W/Bwr Owners Group Design Criteria ML20042E7651990-04-27027 April 1990 Informs That Mod 2285 Completed on Unit 3,but That Mod 2285 Will Not Be Completed on Unit 2 During 8th Refueling Outage ML20042E8931990-04-27027 April 1990 Responds to Violation Noted in Insp Rept 50-278/90-01. Corrective Actions:Automatic Depressurization Sys Logic Sys Functional Tests Will Be Revised to Include Guidance in Unique Application of Test Lights ML20042F3241990-04-27027 April 1990 Advises That Organizational Changes Made in Advance of Approval of Tech Spec Change Request 88-06.Changes Do Not Present Unreviewed Safety Question ML20042E8741990-04-27027 April 1990 Responds to Generic Ltr 87-07, Info Transmittal of Final Rulemaking for Revs to Operator Licensing. Certifies That Limerick Operator Requalification Training Program Renewed on 900125 & Peach Bottom Subj Program Renewed on 890622 ML20012F4801990-04-0202 April 1990 Forwards Errata to Unit Shutdowns and Power Reductions Monthly Operating Rept for Feb 1990 ML20012F0971990-03-22022 March 1990 Forwards Summary of ASME Repairs & Replacement Completed, Per Facility Second 10-yr Interval Inservice Insps Completed During 900331-891111 Extended Refueling Outage ML20012E2151990-03-20020 March 1990 Responds to Generic Ltr 89-19, Request for Action Re Resolution of USI A-47, 'Safety Implication of Control Sys in LWR Nuclear Power Plants,' for Peach Bottom.Response for Limerick Generating Station Will Be Provided by 900504 ML20012C2931990-03-12012 March 1990 Responds to Generic Ltr 90-01, Request for Voluntary Participation in NRC Regulatory Impact Survey, Per 900118 Request ML20012B6211990-03-0808 March 1990 Provides Actions Taken to Ensure & Verify Sys Design Basis Performance,Per 900205 SSFI at Facility ML20012B9011990-03-0606 March 1990 Forwards 870331-891111 Inservice Insp Program Final Rept for Peach Bottom Atomic Power Station Unit 3 1987-1989 Extended Refuel Outage. Several Indications Identified ML20012A2661990-02-26026 February 1990 Forwards Application for Amends to Licenses DPR-44 & DPR-56, Consisting of Tech Spec Change Requests 89-13 & 89-14, Revising Nuclear Review Board Membership & Meeting Frequency & Adding Independent Safety Engineering Group Requirements ML20011F2541990-02-23023 February 1990 Forwards Revs to Physical Security Plan.Encls Withheld (Ref 10CFR73.21 & 2.790) ML20011F3791990-02-21021 February 1990 Provides Revised Schedule for Installation of Hardened Wetwell Vent,Per Generic Ltr 89-16 & Explanation Why Jan 1993 Completion Date Cannot Be Met Due to Unavailability of Matls.Intallation Scheduled for Cycle 9 Outage ML20006F5491990-02-16016 February 1990 Certifies That 891122 Tech Spec Change Request (Tscr) 89-15, 891228 Tscr 88-18 & 900214 Tscr 90-04 Mailed to Commonwealth of Pa,Dept of Environ Resources ML20006F1621990-02-15015 February 1990 Forwards Progress Rept Re Implementation of Control Room Enhancements as of End of Seventh Refueling Outage,Per NUREG-0737.Rept Delayed to Allow for Independent Verification of Control Room Enhancement Status ML20012B1731990-02-15015 February 1990 Forwards Public Version of Revs to Epips,Including Rev 5 to ERP-101,App 1 to Rev 13 to ERP-110,App 2 to Rev 10 to ERP-110,App 1 to Rev 7 to ERP-140,App 2 to Rev 10 to ERP-140,App 3 to Rev 11 to ERP-140 1990-09-18
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. r-PHILADELPHIA ELECTRIC COMPANY 23O1 M ARKET STREET P.O. BOX 8699 PHILADELPHI A. PA.19101 SHIELDS L. D A LTROFF sttcta c PW D CION May 20, 1982 Docket Nos. 50-277 50-278 Mr. R. C. Haynes Administrator Region I U. S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA 19406
Dear Mr. Haynes:
Attached for your review is the detailed scepario for the Peach Bottom Atomic Power Station 1982 full sca16 emergency exercise on June 16, 1982. This detailed scenario supplements the scenario submitted to you on May 11, 1982.
To provide further scenario details and exercise
, information, a briefing will be held for NRC observers on June 15, 1982 at 9:00 a.m. at the Peach Bottom Atomic Power Station President's Utility Building (PUB).
To ensure access by NRC observers to various plant locations, the observers must be properly badged. Please provide a list of NRC observers, their probable observation locations, and their PBAPS badge status to facilitate the badging process.
This list will be used to arrange processing for NRC observers requiring authorized access to PBAPS protected area.
Dye to the length of the exercise, the post-exercise critique has been scheduled for June 17, 1982 at 2:00 p.m. at the PBAPS PUB. The FEMA /NRC post-exercise public critique is scheduled for June 18, 1982 at 10:00 a.m. at the PECo. Muddy Run News Center.
8206220272 820520 PDR ADOCK 05000277 F PDR
/E3f
Mr. R. C. Haynes Page 2 Please forward the requested list of observers to R. A.
Kankus. Should you have any questions concerning the planned exercise or the scenario, please contact R. A. Kankus (215) 841-5465 or W. J. Knapp (215) 841-5164.
Very truly yours,
/ /
cc. c.s.c-gu1
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. .. - - m e e e e e e - e e e e e e-1
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PEACH BOTTOM ATOMIC POWER STATION NRC/ FEMA OBSERVED EMERGENCY EXERCISE June 16, 1982 Detailed Scenario Initial Conditions Both units are operating at continuous full power. Unit 2 is approaching a refueling outage while Unit 3 has recently completed its refueling outage.
Unit 3 core spray pump "B" has excessive seal leakage and a maintenance crew is repairing it. On Unit 2, safety relief valve (SRV) "C" is leaking and heating the torus water at the rate of I degree F per day. Torus water temperature is 90 degrees F. All other power generation and safety system equipment is operable.
The following information relates to events occurring on Unit 2.
Initial control rod positions are all fully extracted except that rods 22-31 and 38-31 are at position 24 and 30-23 and 30-39 are at position 28.
Meteorological conditions are representative of Stability Class II and the average wind velocity is 10 mph from the west (270 degrees).
CLOCK ! SCENA RIO TIME TIME 0615 0 hr. O min. Core plate differential pressure is 18 paid and air ejector off-gas monitor reading is 45 mr/hr.
0630 0 hr. 15 min. Differential pressure reading on recirculation jet pump #6 flow indicator falls to zero.
Air ejector monitor reading has increased to 300 mr/hr.
0645 0 hr. 30 min. Core plate differential pressure has
. risen to 20 psid.
Total core flow has decreased by 10%.
Reactor power and main steam flow have also decreased 10%.
APRM's indicate 2% power decrease.
Main steam line monitor reading has increased 10%.
Air ejector off-gas monitor now reading 700 mr/hr.
l i
00* UNUSUAL EVENT Should be declared. **
Air ejector off-gas monitor readings increased more than 500 mr/hr in 30 minutes.
0700 0 hr. 45 min. Reports from local jet pump instruments in cable spreading room are that:
l l
l l
_ W
CLOCK I SCENARIO TIME TIME
- 6 jet pump reading zero
- 7 and #8 jet pump reading 60% normal
- 13 and #14 jet pump reading 130% normal
- 15 jet pump reading 160% normal All other jet pumps reading 100% normal.
. 0715 1 hr. 30 min. Main steam line flow and reactor power j have declined to 75% of full power 1 values.
Reactor vessel head temperature constant
.at 550 degrees F.
Reactor vessel bottom he.:o drain temperature has dropped from 520 degrees F to 510 degrees F.
Air ejector off-gas monitor now reading 1200 mr/hr.
Main steam line radiation monitors reading 40% above normal full power.
Core plate P has risen to 21 psid.
0745 1 hr. 30 min. Operators continue power reduction to 50% power but main steam line radiation
, level reaches 3 times normal full power l reading and reactor scrams.
Air ejector off-gas monitor now reading 9000 mr/hr.
l Recirculation pumps trip.
Group I, II, and III containment isolation occurs.
All neutron detectors confirm that reactor is subcritical.
1 Reactor water level shrinks rapidly to
-10 inches.
I
ULOCK SCENARIO TIME TIME Reactor pressure rises immediately to 1100 psig and safety relief valves
( SRVs ) open to control pressure.
0746 1 hr. 31 min. Three control rods (10-19, 22-59, 38-23) did not insert at all on scram.
Seventeen rods are inserting slowly.
0747 1 hr. 32 min. , Eleven of the slow rods have completely inserted, but:
control rod 02-31 is stuck at notch 38 14-43 " 17 22-07 26 38-51 " " " "
14 50-19 " " " "
23 54-39 32 0750 1 hr. 35 min. Operators take manual control of HPCI after HPCI initiated to maintain reactor level between +15 and +30 inches.
Packing leak on MOV 23-15 in drywell.
Operators open isolation valves on nitrogen supply lines to instrument nitrogen system to re-establish manual control of SRVs.
Torus water temperature has increased to 95 degrees F and two RHR pumps are put into torus cooling mode.
0815 2 hrs. O min. Torus water temperature has leveled off at 110 degrees F.
Reactor pressure has dropped of f to 1030 psig but SRV-C remains open despite efforts to close it.
GLOCK; SCENA RIO TIME TIME Reactor vessel head temperature has increased to 560 degrees F.
Reactor vessel bottom head drain temperature has dropped t.o 500 degrees F.
Core plate differential pressure is 2 psig.
0845 2 hrs. 30 min. Control rods 14-43, 38-51, and 50-19
.have been fully inserted and work
. continues on the other three.
Alarm is received indicating containment pressure has increased to 1.5 psig.
Drywell temperature is 135 degrees F.
Core plate differential pressure has risen to 4 psid.
Reactor pressure has fallen to 950 psig.
Reactor vessel head temperature has riser. to 580 degrees F.
SBLC i.ni tia ted .
I i
0900 2 hrs. 45 min. Reactor pressure has fallen to 850 psig and SRV C is successfully closed.
Reactor vessel head temperature is 590 degrees F.
Reactor vessel bottom head drain temperature has dropped to 490 degrees l
F.
( 0915 3 hrs. O min. Reactor pressure has leveled off at 950 l psig.
1
_mm-____ _, __ _ _. __
CLOCK SCENARIO TIME TIME
. Containment pressure reaches 2 psig.
Drywell radiation level starts increasing rapidly and presently reads 50 R/hr on the containment hi-range area monitors.
Core plate differential pressure is 6 psid.
Drywell temperature has started increasing at the rate of 10 degrees F per hour.
. Reactor vessel head temperature is 600 degrees F.
Reactor vessel bottom head drain temperature is 480 degrees F.
Emergency Diesels start, E3 diesel shuts down due to fuel line clogged. E32 bus failure due to phase-to-phase ground problem.
0930 3 hrs. 15 min. Containment radiation level is 500 R/hr.
0945 3 hrs. 30 min. Containment radiation level is 6000 R/ hr .
Operators decide to reduce reactor pressure by using SRVs (A&B) in order to minimize leakage to drywell and place condensate pumps in service.
Reactor level is maintained at +30 inches.
Torus water temperature is down to 105 degrees P.
Drywell temperature is 140 degrees F.
Drywell pressure is 2.5 psig.
CLOCK SCENARIO TIME TIME 1000 3 hrs. 45 min. Containment radiation level is 10,000 R/hr.
Reactor pressure is 700 psig.
coe ALE RT Should be declared. ***
EP-101 Item 4.b.3.
Containment high range area monitor readings greater than 10,0(i0 R/hr.
1015 4 hrs. 0 min. Reactor pressure is 600 ps: g.
One of the remaining 3 stuck control rods (54-39), is fully inserted. The other 2 remain frozen in their partially inserted position. Three control rods (10-19, 22-59, 38-23) are still fully extracted.
1030 4 hrs. 15 min. Core plate differential pressure is 9 psid.
Reactor pressure remains 600 psig.
Reactor vessel head temperature pegged at 600 degrees F (Temperature reading is 630 degrees F) .
Reactor vessel bottom head drain temperature is 460 degrees F.
1045 4 hrs. 30 min. Message received that someone claiming to be a television newsreporter attempts to gain entrance. She says she has an appointment with Mr. Conley, the
ug-- = -- m
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CLOCK SCENA RIO TIME TIME director of the Emergency Support Center.
Containment radiation level is 25,000 R/hr .
Core plate differential pressure is 12 psid.
1105 4 hrs. 50 min. Medical emergency for supervisory personnel.
1115 5 hrs. 0 min. Core plate differential pressure is 13 psid.
Torus temperature is 100 degrees F.
Drywell temperature is 155 degrees F.
Drywell pressure is 3 psig.
Reactor vessel head temperature >600 degrees F (640 degrees F is me'asured with potentiometer).
Reactor vessel bottom head drain temperature is 430 degrees F.
Reactor pressure is 450 degrees psig.
Core Spray B and D loop injection valve (MOV 14-12B) fails to open.
" A" Core Spray pump breaker trips.
Breaker racked out and racking mechanism fails.
Fire in the 2A Instrument nitrogen compressor motor which requires about 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> to repair.
CLOCK SCENARIO TIME TIME 1215 6 hrs. O min. Reactor pressure is 425 psig, level is
+30 inches.
Containment radiation level is 40,000 R/hr.
Core plate differential pressure is 14 psid.
Reactor vessel head temperature - 660 degrees F (reads > 600).
l Reactor vessel bottom head drain temperature is 420 degrees F.
1 Drywell temperature is 165 degrees F. I l
Drywell pressure is 4 psig.
Torus temperature is 100 degrees F.
Reactor building general area 50 mr/hr.
1245 6 hrs. 30 min. Core plate differential pressure is 16 psid.
Containment radiation level is 50,000 R/hr .
Drywell temperature is 170 degrees F.
Drywell pressure is 4.5 psig.
Reactor vessel head temperature is 670 degrees F.
Reactor vessel bottom drain temperature is 400 degrees F.
Reactor building general area 100 mr/hr.
, 1300 6 hrs. 45 min. Waste collector surge tank low level alarm received. Investigation reveals that the tank is draining through a
dLOCK'. SCENARIO TIME TIME broken feed line. HP reports rising airborne radiation levels and recommend evacuation. Site evacuation should be called since two buildings are inaccessible. Airborne levels in the Radwaste building are IN7 at the 91'6" elevation. Radwaste building general area is 100 mr/hr.
1315 7 hrs. O min. Reactor core plate differential pressure is 19 psid.
Reactor vessel head temperature' is 680 degrees F.
Reactor vessel bottom head drain temperature is 380 degrees F.
Containment radiation level is 75,000 R/hr .
Drywell temperature is 175 degrees F.
Drywell pressure has leveled off at 4.5 psig.
Status lights indicate nitrogen purge isolation outboard valve is not fully closed.
Main stack effluent releases have risen to 0.1 Ci/sec of noble gases.
1325 7 hrs. 10 min. SAR team finds one missing man contaminated and injured.
1345 7 hrs. 30 min. Drywell temperature remains at 175 I
degrees F and pressure is constant at 4.5 psig.
l
[ LOC K '- SCENARIO TIME TIME Reactor building airborne activity is negligible.
Containment radiation level is 110,000 R/hr.
- SITE EMERGENCY Should be declared.
EP-101 Item 4.c.3 Containment high range area monitor
. readings greater than 100,000 R/hr.
1400 7 hrs 45 min. Core plate differential pressure is 23 psid.
Reactor vessel head temeprature is 700 degrees F.
Reactor vessel bottom head drain temperature is 350 degrees F.
1415 8 hrs. O min. Report from personnel checking nitrogen purge isolation valves is that the inboard valve is fully closed, but leaking. Outward valve is partially open. They estimate six hours to repair.
1430 8 hrs. 15 min. Instrument nitrogen compressor 2A is returned to service.
High pressure service water pump "A" trips out. In a short time, a hi-radiation alarm is received from the corresponding service water effluent monitor. Monitor reads 100,000 cpm for
1 [ LOCKI SCENARIO TIME TIME several minutes before the situation is corrected.
1500 8 hr. 45 min. Reactor pressure is 450 psig, core spray pumps B and D start. Core plate dif ferential pressure starts falling.
1515 9 hrs. O min. Reactor pressure is 350 psig.
Core plate differential pressure is 18 psid.
Drywell pressure has fallen to 4 psig.
Torus temperature is 110 degrees F.
Word is received of a potentially serious radiation exposure. A plant operator has fallen into very contaminated waste collector surge tank water at the 91'6" elevation. Radwaste building. External contamination of at least 250,000 cpm and internal contamination due to swallowing about one cup (250 ml) of water in the range of 1N3 to 1N4. Offsite medical and RMC assistance required.
1545 9 hrs. 30 min. Containment radiation level has increased to 500,000 R/hr.
Stack releases have increased to 2 Ci/sec. Analysis indicate about 300:1 noble gas to iodine ratio.
Reactor pressure is 270 psig.
Core plate differential is 14 psid.
Containment hydrogen level is 0.5%.
, CLOCK SCENARIO TIME TIME Reactor vessel head temperature is 590 degrees F.
Reactor vessel bottom head temperature is 360 degrees F.
A fire is discovered on a flat bed truck loaded with a radwaste shipment. At the time of ALERT declaration, the truck had been in the process of checkiug through security and it had been parked there ever since. Off-site assistance is required since it is a smoky fire in the cab and there is a danger of spreading to the trailer or the fuel tanks.
1615 10 hrs. O min. Containment radiation level has increased to 8 00,000 R/hr.
Containment hydrogen level.is 0.7%.
Reactor vessel head temperature is 560 degrees F.
Drywell temperature is 160 degrees F.
Torus temperature is 105 degrees F.
Drywell pressure is 4 psig.
Condensate and HPCI pumps have been secured.
1630 10 hrs. 15 min. containment radiation level has increased to 1,100,000 R/hr .
Stack releases now 250 Ci/sec (0.3%
iodine).
Torus temperature is 105 degrees F.
GL'OC K-SCENARIO TIME
- GENERAL EMERGENCY Should be declared.
EP-101 Item 4.d.3 ,
i containment high range area monitor readings greater than 1,000,000 R/hr.
1630 10 hrs. 15 min. Wind direction shif ts although wind speed and stability class remain the same. Wind direction is now from 315 degrees.
1700 10 hrs. 45 min. Reactor pressure is 270 psig.
Core plate differential pressure is 9 psid.
Containment hydrogen concentration is 1.5%.
Reactor vessel head temperature is 520 i
degrees F.
Drywell pressure is 4 psig.
! Reactor vessel bottom head drain temperature is 360 degrees F.
, 1730 11 hrs. 15 min. SGTS fan trips out on high differential pressure across filter "A". Filter "B" is placed in service and no differential pressure noted although flow is 110% of l rated.
Releases increases to 800 Ci/sec of which about 3% is iodine.
i
I .
l , -.
l CLOCII' SCENARIO TIME TIME 1800 11 hrs. 45 min. Word is received that a member of the team sent to investigate the problem
, with the SGTS filters was injured and contaminated. Off-site medical assistance is required.
Reactor vessel head temperature is 480 degrees F.
Reactor vessel level is +35 inches.
Reactor pressure is 260 psig.
Drywell pressure is 4 psig.
1900 12 hrs. 45 min. Reactor vessel head temperature is 400 degrees F.
Reactor vessel level is +60 inches.
Reactor pressure 'is 250 psig.
1 Torus temperature is 100 degrees F.
Drywell temperature is 140 degrees F.
Drywell pressure is 3.5 psig.
. Drywell radiation level is 2 x 10 R/hr .
1930 13 hrs. 15 min. Successful closure of nitrogen purge isolation valves terminates release.
- DE-ESCALATION TO SITE EMERGENCY POSSIBLE.
RECOVE RY PHASE DISCUSSION IS BEGUN.
2000 13 hrs. 45 min. Exercise is terminated.
-,-