ML20245F423

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Insp Repts 50-424/89-14 & 50-425/89-15 on 890318-0505. Violations Noted.Major Areas Inspected:Plant Operations, Radiological Controls/Chemistry,Maint,Surveillance & Security & Administrative Controls Affecting Quality
ML20245F423
Person / Time
Site: Vogtle  Southern Nuclear icon.png
Issue date: 06/15/1989
From: Aiello R, Patterson C, Rogge J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20245F400 List:
References
50-424-89-14, 50-425-89-15, NUDOCS 8906280135
Download: ML20245F423 (37)


See also: IR 05000424/1989014

Text

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d 1 UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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o REGION 11

"g 101 MARIETTA ST., N.W. .

.'..,, ATLANTA, GEORGIA 30323

Report Nos.:- . 50-424/89-14 and 50-425/89-15

Licensee:. Georgia Power Company

P.O. Box 1295

Birmingham, AL 35201

Docket Nos.: 50-424 and 50-425 License Nos.: NPF-68 and NPF-81

Facility Name: Vogtle 1 and 2

Inspection Conducted: March 18 - May 5, 1989

Inspectors: ,

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J. Edogge Senior Resident Inspector Date Signed

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R. K Aiello, Resident Inspector

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C.-AT Patterson, Project Ehgineer (April 3-6) Date Signed

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J. ,ErMenning, Hatch Sent'or Resident (April 1-2)

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Date Signed

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R.-t'. Prevatte, Summer Senior Resident (April 1-2)

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Date Signed

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PT C At5pkins, Summer Resident <1 April 1-2) Date Signed

Accompanied By: Rick Mc hort r (March 27-30) i

Approved By: [ <<LIuAn-

M. V,'/Sinkule, Secti6n Chief

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Date Signed

Divistion of Reactor Projects

SUMMARY )

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Scope:

This routine inspection entailed resident inspection in the following areas: a

plant operations, radiological controls / chemistry, maintenance, surveillance,

security, startup testing (Unit 2), engineering technical support, and quality

programs and ada.L istrative controls affecting quality.

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Results:

In. the areas inspected, fourteen violations were identified. Of these, one

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violation was cited, and thirteen violations were non-cited pursuant to the

discretionary provisions of the NRC Enforcement Policy. The cited violation

was identified in the area of operations, and it involved six examples of

failure to establish or implement procedures. One of the six examples

pertained to Unit 1 only (paragraph 5.f), three pertained to Unit 2 only

(paragraphs 4.b(3)(q), 4.b(3)(r), and 4.b(3)(s)), and two pertain to both

units (paragraphs 2.b(1) and 3). Of the thirteen non-cited violations, five

pertained to Unit 1: one in the area of radiological controls / chemistry

(paragraph 4.b(2)(d)), two in the area of surveillance (paragraphs 4.b(2)(a)

and 4.b(2)(b)), and two in the area of emergency technical support (para-

graphs 4.b(2)(c) and 4.b(3)(h)). The remaining eight non-cited violations

pertainer! to Unit 2. Three were identified in the area of plant operations

(paragraphs 4.b(2)(f), 4.b(3)(m), and 4.b(3)(p)), three were identified in the

area of radiological controls / chemistry (paragraphs 4.b(2)(h), 4.b(2)(i), and

4.b(2)(j)), one was identified in the area of maintenance (paragraph 4.b(2)

(k)), and one was identified in the area of engineering technical support

(paragraph 4.b(2)(e)).

Two inspector followup items were also identified involving the adjustment of

the P-9 setpoint when steam dumps are removed from service (paragraph 3) and

the resolution of restoring the safety system monitor panel to a condition to

correctly indicate the operability status (paragraph 5.d).

Two strengths and one weakness was noted within the report. The areas of

maintenance and startup testing (Unit 2) were noted as strengths with the area

of operations noted as a weakness.

- Maintenance (paragraph 2.b(7)) was considered a strength primarily due to

the planning and execution of the work schedule. Short system outages on

Unit 1 and short plant outages on Unit 2 were effectively conducted. Most

noteworthy was the elimination of a 10-day scheduled outage during the

Unit 2 test program due to this proficiency.

- Startup Testing on Unit 2 (paragraph 3) was a second strength even though

one procedure error resulted in a preventable transient. The transient

was preventable because the identical error was identified during Unit I

test program. More significant was the proficient and efficient conduct

of the Remote Shutdown Test and the Loss of Offsite Power Test.

- Operations evidenced weakness in the area of procedure establishment and

implementation of the basic operating procedure 12004-C " Power Operation."

Examples included in the cited violation are failure to open bypass ,

isolation valves (paragraph 3), to secure from long-cycle cleanup  !

(paragraphs 3 and 4.b(3)(s)), and to perform the transfer from auxiliary

Other operations errors were noted in

to

themain

LERsfeedwater

(paragraphs(parag(raph

4.b 2) and 3).

4.b(3)). This concern has been verbally

expressed to licenset management.

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. REPORT DETAILS

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1. . Persons Contacted

Licensee Employees

  • G. Bockhold, Jr., General Manager Nuclear Plant .
  • A. L. Mosbaugh, Plant Support Manager
  • R. M. Odom, Nuclear Safety & Compliance Manager / Plant Engineering

Supervisor

  • J. E. Swartzwel_ der, Manager Operations

W. F. Kitchens, Assistant General Manager Plant Operations

R. L. Legrand, Manager Chemistry and Health Physics

.

  • H. M. Handfinger, Manager Maintenance

G. A. McCarley,-ISEG Supervisor

  • G. R. Frederick, SAER Supervisor

W. E. Mundy, Quality Assurance Audit Supervisor

C. L._Coursey, Maintenance Superintendent

Other licensee employees . contacted - included craftsmen, technicians,-

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supervision, engineers, operations, maintenance, chemistry,- quality

control inspectors, and office personnel.

  • Attended Exit Interview

An alphabetical list of acronyms and initialisms used throughout this -

report are listed in the last paragraph.

2 .- Operational' Safety Verification - (71707)(93702)(71715)

Unit 1 operated this inspection period _ in _ Power Operations (Mode 1) at

100% reactor power.

Unit 2 began this inspection period in Mode ^ 4 (Hot shutdown). On-

March 18, 1989, Unit 2 entered into Mode 3 (Hot Standby). Later that'same

day.(night shift), Unit 2 experienced an inadvertent SI due to personnel

error followed by an. NUE declaration. On March 19, following the SI,

Unit 2 experienced a CVI due to 2RE-2565 radiation monitor. Additionally,

on March 19, (night shift), Unit 2 expei enced a FWI due to P-14 on SG #4

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caused by personnel error. On March 28, , nit 2 entered Mode 2 (Startup),.

went critical, and commenced low power r'aysics testing. On April 5, MFP

"A" tripped .resulting in a MDAFW pump actuation. On April 7, Unit 2

entered Mode 1. Later that same day, a FWI occurred as a result of a Hi Hi

SG 1evel. The unit later entered Mode 2. The unit reentered Mode 1 on

= April 8. On April 9, MFP "A" tripped resulting in a MDAFW pump actuation

and subsequent Mode 2 entry. The unit reentered Mode 1 on April 10. The

-main turbine was tied to the grid on April 11. Later that same day, the

reactor was tripped from the remote shutdown panel and placed in Mode 3 as

part of a required test. While recovering, the unit received an AFW

actuation during transfer of controls from remote shutdown panel with both

MFW pumps tripped. On April 12, the unit entered Mode 2 and went critical

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with subsequent entry into Mode 1. On April 14, the unit conducted a LOSP

test with subsequent entry.into Mode 3. Following the LOSP test, the. unit

went into a three day maintenance outage. On April 15, the unit entered

Mode 2, went critical, and entered Mode 1. On April 16, the unit was tied

to the grid. On April 18, the main turbine was removed from the grid and-

tripped to conduct secondary system repairs. On April 19, the main

turbine was returned to service and tied to the grid. On April 22, a unit

turbine trip occurred due to a loss of stator cooling. This was followed

by a FWI on SG #3 Hi Hi level and subsequent AFW start. The unit then

entered Mode 2. Later the same day, the unit reentered Mode 1. On

April 23, the main generator was tied to the grid. On April 24 with all

of the 30% plateau testing complete, the unit commenced power ascension to

50% for 50% power plateau testing. On May 2, the unit was increasing

power to 75%. for 75% power plateau testing when a reactor trip occurred

with the plant at 63% from a turbine trip following a test of the

electrical overspeed trip circuit. On May 3, the unit reentered Mode 2

achieved Mode 1, and was operating at 75% at the end of the inspection

period.

a. Control Room Activities

Control Room tours and observations were performed to verify that

facility operations were being safely conducted within regulatory

requirements. These inspections consisted of one or more of the

following attributes as appropriate at the time of the inspection.

- Proper Control Room staffing

- Control Room access and operator behavior

- Adherence to approved procedures for activities in progress

- Adherence to technical specification limiting conditions for

operation

- Observance of instruments and recorder traces of safety-related

and important-to-safety systems for abnormalities

- Review of annunciators alarmed and action in progress to correct

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Control Board walkdowns

- Safety parameter display and the plant safety monitoring system

operability status

- Discussions and interviews with the On-Shift Operations

Supervisor, Shift Supervisor, Reactor Operators, and the Shift

Technical Advisor (when stationed) to determine the plant

status, plans, and to assess operator knowledge

- Review of the operator logs, unit logs and shift turnover sheets

No violations or deviations were identified.

b. Facility Activities

facility tours and observations were performed to assess the

effectiveness of the administrative controls established by direct

observation of plant activities, interviews and discussions with

licensee personnel, independent verification of safety system status

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and LCOs, licensee meetings and facility records. During these

inspections, the following abjectives were achieved:

~(1) Safety System Status (71710) - Confirmation of system

operability was -obtained by verification that flowpath valve

alignment, control and power supply alignments, component j

conditions, and support systems for the accessible portions of

the ESF trains were proper. The inaccessible portions are

confirmed as availability permits. An additional indepth

inspection of the Unit 1 SI system was performed to review the

system lineup- procedure with the plant drawings and as-built

configurations and to compare valve remote and local

indications. Walkdowns were expanded to include hangers and

supports and electrical equipment interiors. The inspector

observed that the lineup was not in accordance with license

requirements in that the SI RCDT pump discharge to RWST

isolation (1-1204-U4-002), SI RWST INL FI-0928A and FI-0928B

isolation valves were found open. DCs were properly issued by

the SS to correct these deficiencies. These valve misalignments

did not render the SI system inoperable. Several valves were

noted to have missing label plates. Rooms A9 and A10 need a

great deal of attention from a Health Physics and cleanliness

point of view.

The licensee's program for maintaining control room drawings was

reviewed. On April 28 and May 4,1989, the unit control rooms

and TSC drawings were inspected. This inspection included a

detailed walkdown of the SI system (discussed above) and a

review Of the following drawings to determine legibility,

current revision verification and verification that procedure

valve lineups were appropriate:

1X4DB119 Rev 20 1X4DB130 Rev 22 1X4DB129 Rev 23

1X4DB133-1 Rev 23 1X4DB136 Rev 22 1X4DB161-1 Rev 22

1X4DB170-1 Rev 23 1X4DB120 Rev 14 1X4DB138-2 Rev 15

1X4DB136 Rev 22 1X4DB121 Rev 24 1X4DB131 Rev 19

1X4DB139 Rev 18 IX4DB138-1 Rev 16 1X4DB122 Rev 26

1X4DB132 Rev 14 1X4DB133-2 Rev 26 IX4DB135-1 Rev 21

1X4DB137 Rev 15 IX4DB161-2 Rev 22 IX4DB161-3 Rev 20

1X4DB170-2 Rev 22 1X4DB116-2 Rev 15 1X4DB117 Rev 18

IX4DB118 Rev 20 CX40B173-557 Rev 1 CX4DB173-558 Rev 1

CX4DB173-553 Rev 1 i

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The inspector determined that the procedures for controlling the

distribution of drawings were satisfactory. The drawings

adequately represent the plar,t's current configuration. Three

drawings IX4DB133-1 Rev 23, 1X4DB122 Rev 24, and IX4DB122

Rev. 26, (NSCW, SI, and RHR respectively) are too congested and

therefore, difficult to read. It was also determined that most

of the safety-related drawing ABNs were not legible. Three in

particular which are examples of the worst case are 1X4DB161

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t Rev. 22,1X40B121 Rev. 24, and 1X4DB122 Rev. 26 (AFW, SI, and

RHR respectively). Administrative procedure 00101-C, " Drawing

Control," Step 3.4.4, requires that drawing legibility be

ensured prior to distribution and engineering procedure 50009-C,

"As-Built Notices," Step 4.6.3, requires ABNs to be legible and

-reproducible. This constitutes a violation of administrative

procedure 00101-C and engineering procedure 50009-C.

This violation is one example of violation 50-424/89-1a-01 and

50-425/89-15-01, " Failure To Implement Procedures 00101-C and

50009-C Resulting In TS 6.7.1.a Violation."

(2) Plant Housekeeping Conditions - Storage of material and

components and cleanliness conditions of various areas

throughout the facility were observed to determine whether

safety and/or fire hazards existed.

(3) Fire Protection - Fire protection activities, staffing, and

equipment were observed to verify that fire brigade staffing wa.c

appropriate and that fire alarms, extinguishing equipment,

actuating controls, fire t ihting equipment, emergency

equipment, and fire barriers were operable.

(4) Radiation Frotection - Radiation protection activities,

staffing, and equipment were observed to verify proper program

implementation. The inspection included review of the plant

program effectiveness. Radiation work permits and personnel

compliance were reviewed during the daily plant tours.

Radiation Control Areas were observed to verify proper

identification and implementation.

(5) Security - Security controls were observed to verify that

security barriers were intact, guard forces were on duty, and

access to the Protected Area was controlled in accordance with

the facility security plan. Personnel were observed to verify

proper display of badges and that personnel requiring escort

were properly escorted. Personnel within Vital Areas were

observed to ensure proper authorization for the area. Equipment

operability or proper compensatory activities were verified on a

periodic basis.

(6) Surveillance (61726)(61700) - Surveillance tes#s were observed

to verify that approved procedures were being ; sed, qualified

personnel were conducting the tests, tests were adequate to

verify equipment operability, calibrated equipment was utilized,

and TS requirements were followed. The inspectors observed

portions of the following surveillance and reviewed completed

data against acceptance criteria:

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Surveillance No. Title

14000-1 Rev. 17 Operations Shift And Daily Surveillance.

Logs

14000-2 Rev. 2 Operations Shift And Daily Surveillance

Logs

14220-1 Rev. 3 Main Turbine Valves Weekly Stroke Test

14228-: Rev. 1 Operations Monthly Surveillance Logs

14230-1 Rev. 4 Weekly Train A & B Verification Offsite

To Onsite Class 1E A.C. Distribution

System Circuit Breaker Alignments While

In Modes 1-4

14235-2 Rev. 1 Onsite Power Distribution Operability

Verification

14450-2 Rev. 1 RCS Pressure Isolation Valve Leakage

Test

14495-1 Rev. 3 TDAFW System Flow Path Verification

14551-2 Rev. 1 CCW Flow Path Verification

14808-2 Rev. 2 CCP And Check Valve Inservice Test

14825-2 Rev. 1 RCS Quarterly Inservice Valve Test

14905-1 Rev. 21 RCS Leakage Calculation

Surveillance procedure 14825-2 was conducted during the night

shift on March 22, 1989. The resident inspector conducted a

review of the data on the following morning. It was noted that

data sheet 1 (test section 5.3.1) requiring independent

verification was not documented for PORV block valves 2-HV-8000A

and B. The inspector promptly brought this to the attention of

the Operations Superintendent, OSOS, and unit SS. The SS took

the necessary corrective action to complete these steps of the

procedure on the following shift. It is apparent that an

inadequate operator and supervisory review was conducted on the

previous shift.

(7) Maintenance Activities (62703) - The inspector observed  ;

maintenance activities to verify that correct equipment i

clearances were in effect; work requests and fire prevention I

work permits, as required, were issued and being followed;

quality control personnel were available for inspection

activities as required; retesting and return of systems to

service was prompt and correct; and TS requirements were being

followed. Maintenance Work Order backlog was reviewed.

Maintenance was observed and work packages were reviewed for the

following maintenance activities: ,

MWO No. Work Description

18901524 Replace NSCW Torque Switch Limiter Plate Due

To Valve 1HV-1668A Not Stroking Properly

28902508 Stroke Steam Dump Valves

28902598 Main Feed Isolation Valve Repair

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28902715 investigate / Rework / Replace Cards As Required

To Restore MFP Slave Relay K-620 To Proper

Operation

28903135 Reset Power Range Detector Current Per Start

Up Test Procedure 2-6SE-01 & 03

During this inspection, the inspectors noted that maintenance

planning and execution was effectively conducted during short

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system outages (Unit 1) and plant outages (Unit 2). Most

noteworthy was the elimination of a 10-day scheduled outage

during the Unit 2 test program due to this proficiency.

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One example of one violation was identified (paragraph 2.b(1)).

3. Startup Test Program Implementation / Verification -

Unit 2

(72302)(724008)(71715)

The inspector reviewed the present implementation of the Startup Test

Program. Inspected Test Program attributes including review of

administrative requirements, document control, documentation of major test

events and deviations to procedures, operating practices, instrumentation

calibrations, and correction of problems revealed by testing.

Periodic facility tours were made to observe Startup Test activities in

progress. The inspector verified that procedural prerequisites and

initial conditions were mat. Verification was performed by the

inspector's review of records (valve lineup sheets, test equipment

calibration status, system status checklists, or appropriate sign-offs

listed in procedure were maintained current) or by direct observation

(monitoring instrumentation indications, valve positions, equipment

position switches, or personnel actions). Discussions were held with

responsible personnel, as they were available, to determine their

knowledge of the Startup Test Program. Schedules for Startup Test Program

completion and progress reports were routinely monitored. Specific

inspections conducted are listed below:

Initial Criticality and Low Power Test Sequence

The initial criticality and low power test sequence directing the test

activities as contained in procedure 2-600-04 was reviewed during testing.

The following specific tests were partially witnessed:

(a) Step 6.2, Initial Criticality per Procedure 2-600-02

(b) Step 6.3, Determination of Low Power Physics Testing Power Range

(c) Step 6.4. Boron Endpoint, Isothermal Temperature Coefficient  ;

Measurement i

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(d) Step 6.4.11, Flux Map 2-6SE-02

(e) Step 6.11, Control Bank A Worth

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Power Ascension Test Sequence (72509)(72582)(72583) l

The power ascension test secuence directing the test activities as ,

contained in procedure 2-600-13 was reviewed during testing. The  ;

following specific tests were partially witnessed.

(a) Step 6.1.1, Adjustment of Nuclear Instruments to 50% Trip Level

(b) Step 6.1.7, Main Feedpump Operation per 12004-C

(c) Step 6.1.8, Perform 12004-C

(d) Step 6.1.10, 2-6AB-01, Dynamic Auto Steam Dump Control

(e) Step 6.1.11, 2-6AE-01, Automatic Steam Generator Level Control

Position Indication Test

(f) Step 6.1.20, 2-600-08, Remote Shutdown Test

(g) Step 6.1.23, 2-600-09, Loss of Offsite Power Test

(h) Step 6.4.5, 2-6SE-02, Flux Map At 30" Power

(i) Step 6.4.7, 2-6SE-03, Operational Alignment Of The Nuclear

Instruments

(j) Step 6.5.3.1, 2-6SC-02 Load Swing Test

(k) Step 6.10.2, 2-6AE-01, Automatic Steam Generator Level Control

(1) 2-600-06, MFW Dynamic Response Test

On April 2, 1989, during performance of Step 6.1.8 which directed

operation of the plant to proceed per procedure 12004-C, the inspector

observed the unit perform the transfer from auxiliary feedwater to main

feedwater for the #3 Steam Generator. Procedure 12004-C, Step 4.1.4,

specifies that the transfer is to be completed as follows:

4.1.4 TRANSFER Auxiliary Feedwater to Main Feedwater one Steam

Generator at a time by performing the following:

a. STABILIZE the SG NR level between 45% and 55%,

b. Slowly CLOSE the Auxiliary Feedwater Supply Valve and

OPEN the BFRV while maintaining SG level in program

band,

c. When the Auxiliary Feedwater Supply Valve is fully

closed, Stabilize SG level and then PLACE the BFRV in

automatic,

d. Repeat valve transfer for remaining Steam Generators.

Prior to the start of the transfer, the inspector noted that the

Balance-of-Plant Operator discussed the transfer with the operator

controlling Steam Generator level. The operators decided that the best

way to make the transfer was for the B0P operator to close the Auxiliary

Feedwater Supply Valve and the other operator would " punch" the BFRV into

automatic. The operators then commenced the transfer without discussion

with the Shift Supervisor. The B0P operator did however involve the shift

supervisor in the transfer by directing him to display narrow range and

wide range computer trends of #3 Steam Generator on the ERF computer.

Upon closing the Auxiliary Feedwater Supply Valve, the SG Water level

initially lowered. The second operator placed the BFRV into Automatic as

previously planned. The BFRV automatic control began to slowly open in

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order to restore steam generator levels. The response time necessary for

. the controller and~ valve were slow. and resulted in eventual' overshoot of.

SG 1evel to approximately 64%. The ERF computer displays were valuable in

monitoring the. inventory of water in the steam generator during- the

transient'. A'second effect was observed in the #1 SG involving lowering

. level. The. #1 SG had been transferred to its BFRV on the prior shift.

The B0P operator directed a plant equipment operator to. fail the feedpump

miniflow valve open. The inspector questioned the Operations Manager on

why the procedure had not been followed for the . transfer and why the

miniflow-valve had to be failed open. The inspector also noted that the

prior Step 4.1.3g had been signed off complete when in fact, only the #1'

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and'#3 BFIVs were open. Procedure 12004-C. Step 4.1.3.g, states: _

4.1.3.g OPEN the Bypass Feed Isolation Valve an'd VERIFY the

Feedwater Isolation Valve is closed for each SG.

The Operation Manager counseled the operators on not going in automatic

control too soon. The .failing of the miniflow valve was~ explained as a-

necessary evolution in that the flow from one feedpump feeding two steam

generators is at the point when the miniflow valve closes (500 gpm) which

affects 'the output pressure of the feedpump and hence flow to the steam

generators. By failing the miniflow valve open the feedpump performs in a

smoother manner. Later, the inspector learned that had all four BFIVs

been open, that normal leakage through.the BFRVs would account for.about

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500 gpm and the miniflow valve would have closed prior to or during the

swapover on the first steam generator.

The fact- that procedure 12004-C was not followed in Steps 4.1.3.g and

4.1.4 constitutes a violation of TS 6.1.7 requirements and is one example

of violation 50-424/89-14-01 and 50-425/89-15-01, " Failure to Implement

Procedure 12004-C, Steps 4.1.3.g and 4.1.4, For Performing Transfer From

Auxiliary Feedwater To Main Feedwater."

The inspector observed the subsequent transfer to the #4 Steam Generator

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computer. When the Shift Supervisor called up the display, he obtained

the #1 SG trend instead of the #4 SG. The transfer had already commenced'

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and'was essentially complete by the time the proper display was achieved.

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The following of procedure 12004-C, Step 4.1.4, by the operators resulted

in a smooth transfer. '

On April 3, 1989, during the performance of 2-6AB-01, " Dynamic Auto Steam

Dump Control," the plant experienced a SG level transient when a test

signal specified by procedure was incorrect. Procedure 2-6AB-01,

Step 6.3.3, directed that a test signal be- inserted equivalent to the

signal generated at a T-ref of 553 F by using Attachment 10.5.

Attachment 10.5 called for connection of a Ronan calibrator Model X85

(2.3 volt signal) (pins 26- and 27+). The reversal in polarity resulted

in the steam dumps being commanded to full open when the controller was

placed in the T-avg control mode per Procedure Step 6.3.5. At the time of

the transient, six of the twelve dumps were isolated. The resultant swell l

in SG 1evels resulted in a feedwater isolation. Further details of the

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event ; isi contained in LER _50-425/89-15. This same error ~ occurred on .

R Unit i during- the startup program; however, an LER did.not result. Unit 2

procedure development did not incorporate the Unit' 1 procedure change.

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Failure to establish an appropriate procedure is an example _of a violation:

of 10 CFR Part_50,' Appendix B, Criterion-V, and of TS 6.7.1'.a.

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l; This item .is one of the examples of violation 50-424/89-14-01 - and

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50-425/89-15-01, " Failure To -Establish An Adequate Procedure For Thel

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Testing Of Steam Dumps." (Refer to the discussion'on LER 50-425/89-14'in.

paragraph 4.b(3)(r) for additional information.-)

The inspector questioned why the identical error on Unit I did not result.

l in a more severe transient. While no specific answers are known,.

speculation was made regarding the number of steam dumps that are-

inservice. On Unit 2 six of the twelve were inservice, .and the test

procedure called for verification that three valves be unisolated and

ready for testing (PV-507A, B, and C). If Unit 1 bac' only three

unisolated dumps, then the transient would not have resulted in es severe

l a level-swell. A review by the inspector on procedure 12004-C noted that

no guidance or control regarding steam dumps existed. Inspection of Unit

I revealed that one steam dump was not inservice.

The above events regarding establishment and adherence to procedures was

discussed :with the General Manager on April 6,1989. The._ inspector

addressed observations regarding:

- failures to follow procedure 12004-C,

- failure of the Shift Supervisor to closely control the operator

actions,

- failure to have appropriate procedures in place for control of

steam dumps and feedwater pump miniflow valves,

- excessive eating of food in the' control room, and

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telephone distractions to the operators.

In response to the above, the General Manager took action to address these

concerns by having by operations manager review and discuss these events 1

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with operators and supervisors.

On April 7, 1989, a feedwater isolation occurred which illustrated another .

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failure of the operators to implement procedure 12004-C. On April 6, with

the unit in Mode 3 on long-cycle cleanup, the shift f.upervisor directed

that in order to support another surveillance that long .;ycle cleanup be

secured from the control room. Following the surveillance, the cleanup j

was not restored. The following shift decided to replace the existing

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copy of 12004-C due to the number of items which had been signed off and

however no longer represented the plant configuration. Since the action i

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to secure long-cycle cleanup had been accomplished in the control room,

the shift supervisor assumed that all of Step 4.1.3 directing the stopping

of feedwater recirculation in long-cycle cleanup were not applicable.

This error resulted in the failure of the plant to close six manual

isolation valves and produced a situation wherein all four steam

generators were cross connected. On April 7, with reactor power at

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approximately 7%, operators noticed that the #1 SG BFRV was at 60% demand,

  1. 2 and #3 SGs were at 30% demand, and #4 SG was at 0% demand. Even though

two steam generators gave the indication that only one- BFRV was

maintaining level, the operators notified I&C to investigate the

' indication problem. Since SGs 1 and 4 are on the same side of

containment, the physical piping layout results in these two SGs_ being

related. While resolving the problem, the operators decided to stroke the

  1. 2 MFIV as part of a maintenance functional test. As soon as the MFIV was

opened, flow from the other SGs was diverted to the #2 SG until a

feedwater isolation occurred due to Hi Hi #2 SG water level. The root

cause is related to the first shift supervisor failing to implement

procedure 12004-C, Step 4.1.3, in securing from long-cycle recirculation.

This item is an additional example of violation 50-424/89-14-01 ' and

50-425/89-15-01, " Failure To Implement Procedure 12004-C To' Secure From

Long-Cycle Recirculation." (Refer to the discussion of LER 50-425/89-15

in paragraph 4.b(3)(s) for additional information.) l

The proper control of the steam dumps was addressed by the inspector as a

concern in that the basis for the P-9 reactor protection interlock assumes

that all dumps are available with normal pressurizer pressure control.

TS 2.2.1, Table 2.2-1, item 18.3, specifies a trip setpoint of ,,50% where

the reactor trip on turbine trip can be blocked. The inspector asked for

a review by the licensee to determine if the actual setpoint should be

adjusted downward when ' dumps were not available. Followup of this item

will be tracked as IFI 50-424/89-14-02 and 50-425/89-15-02, " Review

Licensee Evaluation Regarding Adjustment Of The F-9 Setpoint When Steam

Dumps Are Removed From Service."

The above sections represent a weakness in the area of operations to

implement and adhere to the basic " Power Operation" procedure 12004-C. It

becomes apparent when combined with other operations procedure /imple-

mentation as documented in LERs 50-424/89-07, 50-425/89-02,.50-425/89-03,

50-425/89-04, 50-425/89-06, 50-425/89-08, 50-425/89-11, and 50-425/89-16

(see paragraph 4) that additional management attention and oversight are

needed. Response by licensee management has been noted; however,

effectiveness of this effort will require more time to evaluate.

The startup test program has been relatively successful with only one

noted failure discussed above regarding the steam dump testing. More  ;

noteworthy was the proficient and efficient conduct of the Remote Shutdown l

Test and the Loss of Offsite Power Test. Key in the successful

accomplishment was the decision by management to perform the test only

during the day shif t at specific times. This decision affected the

appropriate personnel the ability to be well rested and prepared for the

tes ting.

Three examples of one violation and one inspection followup item were

identified.

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4.'-Review'ofLicensee' Reports (90712)(90713)(92700)

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a. In-Office Review of Periodic and Special Reports

This . inspection consisted of reviewing the below listed ' reports to_-

determine whether the.. information reported by the licensee was

technically adequate and consistent with the inspector. knowledge of-

n the material contained within the report. Selected material-within-

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the report was questioned randomly to verify accuracy and to provide.

a reasonable assurance that other NRC personnel have an appropriate

document: for their activities.

Monthly Operating- Report:- The inspector reviewed the Unit 1 and 2'

monthly operating reports dated March 15, 1989. This review included

the data revision for an earlier Unit I report. The inspector had no

comments.

No violations or deviations were ideritified.

b. Licensee Event Reports and Deficiency Cards

Licensee' Event Reports and Deficiency Cards were reviewed for

potential generic impact, to detect trends, and to determine whether

corrective actions appeared appropriate. Events which were reported

pursuant to 10 CFR 50.72,-were reviewed as they occurred to determine

if the technical specifications and other regulatory requirements

were satisfied. In-office review of LERs may result in further.

followup to verify ' that the stated corrective actions have been -

completed or to identify violations in addition to those described in

the-LER. Each LER is reviewed for enforcement action-in accordance

with 10 CFR Part 2, Appendix C, and if the violation is not being

cited the' criteria specified in Section V.G of the Enforcement

Pclicy was satisfied. Review of DCs was performed.to maintain a

realtime status of deficiencies,. determine . regulatory compliance,

follow the licensee corrective actions, and assist as a basis for

closure of the.LER when reviewed. Due to the numerous DCs processed

only those DCs which resuh in enforcement action or further

inspector followup with the licensee at the end of the inspection are

listed below. The LERs and DCs denoted with an asterisk indicates

that reactive inspection occurred at the time of the event prior to

receipt of the written report.

(1) Deficiency Card Review

(a) DC 1-89-831, " Inadvertent Addition Of Radioactive Gas To

Decay Tank Number 10."

On April 18, 1989, the licensee discovered that radioactive

gas was apparently added to waste gas decay tank number 10

without the lab being notified for determining the quantity

of gas contained in the tank. This deficiency will be

followed up on when submitted as an LER.

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(b) *DC12-89-985, " Unit 2 Turbine Trin Following Standby Stator

Cooling-Pump Trip."

On April.22, 1989', a-turbine trip. occurred.as'a result of a

loss of stator; cooling during a routine swapping of' stator

cooling . pumps. When~ the standby. pump.was started, both -

pumps tripped, causing. the turbine. to . trip. While

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attempting to stabilize- the plant, 'a feedwater isolation

Loccurred due to Hi-Hi SG 1evel on SG:#3, leading to an AFW -

actuation. when the running MFP tripped. The reactor was

stabilized at 2% with the SG being fed from AFW. This

deficiency will be followed up.when submitted as an LER.

(c) DC 2-89-1027' " Reactor Trip From 60% Power On A Turbine

Trip."

On May 2',.1989, the unit received a reactor vip from 60%

power on a turbine trip.: AFW' actuated on Lo.Lo SG 1evel

following the trip. All systems functioned -as required.

~The turbine trip' occurred while Engineering and a GE. Vendor-

representative were investigating a test malfunction alarm

which'was received during the weekly turbine trip device

operability test. The' cause of the turbine trip is still

under' investigation. This deficiency will be followed up

when submitted as an LER.

(2) .The following LERs were reviewed and. are ready for closure

pending verification that the licensee's stated corrective

actions have been completed.

(a) 50-424/89-06, Rev. O, " Inadequate Functional Test Leads To

Improper Termination Of Limiting Condition For Operation."

On January 30, 1989, the Gaseous Waste Processing System's

Outlet Analyzer,1 ARC-1119, failed to pass the surveillance

requirements of Technical Specification 4.3.3.10. The TS-

1- required grab samples to be taken and analyzed at least

once per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. A micro fuel' cell in the analyzer was

replaced and tested on February 7,1989. On February 23,

1989, a review of the work order discovered that the

equipment was placed in service, even though a complete

surveillance test of the analyzer had not been performed to

verify that the surveillance requirements were met. The

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surveillance test was then performed satisfactorily. This

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event was caused by personnel error. Procedural

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inadequacies contributed to this event. The appropriate

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procedure was revised. The appropriate personnel have been

counsels Proper checks now exist to ensure all required

testing is performed prior to exiting a LCO. This item

represents a violation of NRC requirements which meets the

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criteria for non-citation. . In order to track this item,

the following licensee-identified item is established.

NCV 60-424/89-14-03, " Failure To Perform Required Testing 3

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Per Surveillance Requirements Results In TS 4.3.3.10

, Violations - LER 50-424/89-06."

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(b) 50-424/89-07, Rev. O, " Failure To Take Required

Temperatures Results In Inadequately Performed

Surveillance."

On February 16, 1989, while performing Procedure 14001-1,

" Shift Area Temperature Log," the plant operator noted that

there was no entry for Fuel Handling Building Room B008 for

the two previous shifts. The Shift Supervisor was notified

of the missed readings, which are required per Technical

Specification 3.7.10. The current temperature was taken

for Room B008 (76 F), and as it was well within the normal

maximum technical specification limit (104 F), no

compensatory action was required. The cause of this event

was personnel error. Two plant operators failed to take

the required reading and their respective shift supervisors

failed to note the missing temperatures when the data

sheets were reviewed. Corrective actions included

counseling of the operators and shift supervisors on the

importance of ensuring that all required technical

specification surveillance temperatures are obtained and

data sheets thorcaghly reviewed. This item represents a

violation of NRC requirements which meets the criteria for

non-citation. In order to track this item, the following

licensee-identified item is established.

NCV 50-424/89-14-04, " Failure To Take Required Temperatures

Results In Inadequately Performed Surveillance Resulting In

A TS Violation - LER 50-424/89-07."

(c) 50-424/89-08, Rev. O, " Inadequate Review Of Drawing Change

Results In Use Of Improper Breakers."

On February 23, 1989, it was discovered that 125V DC

breakers for motor-operated valves in the Turbine Driven

Auxiliary Feedwater pump system were not the proper size.

The breakers, as installed and as shown on design

drawings, were 15 amp thermal magnetic but should have been

sized as 30 amp themol magnetic per the design criteria.

Therefore, the plant has operated in a condition prohibited

by Technical Specifications. Technical Specifica-

tion 3.7.1.2 requires at least three independent steam

generator auxiliary feedwater pumps and flowpaths to be

operable. The undersized breakers were discovered as a

result of an investigation of the same problem in Unit 2.

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LCO L1-89-121 was entered. The breakers' were replaced..

successfully tested, and the LC0 was exited. The cause of-

this event was due to inadequate review by the responsible-

c engineer whenia drawing change notice corrected the M0V

horsepower rating form 0.66 hp' to 1.0 hp.- Corrective

actions . included a- review of all 125V -DC MOV- breaker.

protection. This review indicated-this incident to be an.:

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isolated . case. This' item represents a violation 'off NRC

requirements which meets the criteria for non-citation. In

order to track this item, the following licensee-identified

item is established.

NCV 50-424/89-14-05 . " Failure .To Coriduct An. Ade' quate -

Engineering Review Of The AFW Electrical System Which Led

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To AFW Inoperability Resulting In a TS 3.7.1.2. Violation -

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LER 50-424/89-08."

(d) . 50-424/89-10, Rev. 0, . " Valved Out Radiation Monitor Leads

< To_Unmonitored Liquid Waste Release."

On March 14,1989, a plant operator was preparing to

perform a liquid waste release per. procedure 13216-1,

" Liquid -Waste Release." The operator verified - that

radiation monitor 1-RE-0018 was registering normal'

background levels and that isolation release . valve

1-RE-0018 would close on a high radiation signal. ' The

release began and the operator checked the signal from

1-RE-0018 and found it was not registering above background

levels. A brief search found that the inlet valve to

1-RE-0018 was closed. This valve, 1-1901-X4-144, was -

opened; 1-RE-0018 registered the proper activity level; and

the liquid waste release continued. The release was

completed and the closure of the inlet valve resulted in

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liquid waste being released unmonitored which is a

condition prohibited by Technical Specification 3.3.3.9.

The operator omitted the performance of a pre-release line

flush which would have ensured that the inlet valve was

opened. Corrective actions included counseling the

operator and changing procedure 13216-1 to require

independent verification of the inlet valve being open.

This item represents a violation of NRC requirements which

meets the criteria for non-citation. In order to track

this item, the following licensee-identified item is

established.

NCV 50-424/89-14-06, " Failure To Follow Procedures While

Conducting A Liquid Waste Release Resulting In A TS 3.3.3.9

Violation - LER 50-424/89-10."

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l(e) 50-425/89-05,.Rev. 0, " Inadequate Review Of A Modification

' Results In A Technical Specification Violation."'

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0n. March 17, 1989, while1 investigating a proble'm'with the-

AutomaticL Surveillance Technical system, field' voltage

measurements - were taken 'that . revealed an ' electrical short

on valve 2HV-19051, the Reactor Coolant Pump #1 thermal-

. barrier isolation valve. The valve was required.to bei

operable upon entry into Mode 4, which ~ had occurred on

March.4. A Surveillance had been performed on February.4,

1989, to prove operability of 2HV-19051; however, a change

to the ASTEC system wiring. on February 10 resulted in valve

2HV-19051 being inoperable. The cause of this event was;

the issuance of an incorrect. As-Built Notice. Corrective

actions included counseling the appropriate engineering

. personnel-involved, training for all engineering personnel'

recently transferred from the Unit' 2 test organization on

use of the ABN, and issuing a second ABN to restore-the.

system to its . original configuration. This item represents-

a violation of NRC requirements which meets the criteria.

for non-citation. In order to track this item, the

following licensee-identified-item'is established.

NCV 50-425/89-15-04. " Failure To Meet A Mode Change

,

Prerequisite Resulting In A TS 3.7.12 Violation Requiring

Valve 2HV-19051 To Be Operable Prior To Entering Mode 4 -

LER 50-425/89-05."

(f) *50-425/89-06, Rev. O, " Operation Of Incorrect Handswitch

Results In Safety Injection."

On March 18, 1989, while warming main steam' lines as part

of procedure 12002-2, " Unit Heatup To Normal Operating.

Temperature And Pressure," automatic Engineered Safety

Features actuation. A- step of the procedure . called for

handswitches HS 40047/48 to be operated to reset the main

steam isolation signal. However, handswitches HS 40068/69

were operated. These switches reset the low steamline

pressure safety injection and steamline isolation logic,

removing the blocking signal. Since the main steam line

pressure was below the safety injection setpoint pressure,

the SI occurred. Appropriate ECCS pumps and valves

actucted resulting in approximately 2900 gallons being

injected into the Reactor Coolant System. The SI was

manually reset and injection into the RCS was terminated.

.The cause of this event was personnel error. The operator

failed to ensure that the proper switch was being operated.

Corrective actions will include counseling the operator on

the importance of verifying that the proper device is being

operated, changing the color of SI handswitches, adding

cautions to the handswitches, and incorporating details of

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this event into . training. This item was ? formally ,

" ' discussed following the' Enforcement-Conference on March 22,.

K .1989. ,This itcm represents a violation'of NRC requirements

which meets the criteria- for' non-citation. In-order to'

~ track this item, the following licensee-identified item is

. established,

u- .NCV 50-425/89-15-05, " Failure- To Follow Procedures -

~Resulting In Inadvertent SI Actuation - LER 50 425/89-06."

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(g) 50-425/89-07, 'Rev. 0, " Lockup Of: A Computer. Communications-

Device Results In Containment Ventilation Isolation."

On March 19,1989, 'while restoring the Plant Effluent.

Radiation Monitoring ' System to service ' the plant

experienced 'an automatic Engineered Safety Features

actuation which resulted in a ' Containment Ventilation

Isolation. Appropriate valves and dampers actuated to.

isolate containment ventilation. _ Control room operators

verified that no abnormal radiological' conditions existed

using'2RE-0002/0003. The monitor that actuated the CVI,

2RE-2565, was placed in bypass. The CVI was. reset and

equipment that actuated was returned to normal _ operating

position. Due to an earlier SI,. power was-lost to most of

the. PERMS system. On ' restoration of power, the compute _r

parameter files are initialized with a -9.99E-20 value.

The_ computer replaces this value with pa* 1 meters received

from each monitor. Due to a communication failure of a

multiplexer, communication with the monitors was lost and

no value was received for 2RE-2565. When the mutiplexer

was reset the computer detected the original power failure

, for 2RE-2565. On a power failure, the computer gives'the

monitor the current" parameter on file and assigned the

monitor -9.99E-20 value. This resulted in 'a high alarm,

causing the CVI actuation. Corrective action is a

procedure revision to require 2RE-2565 to be placed in

bypass when the computer is initialized to receive

parameters.

(h) 50-425/89-09, Rev. O, " Procedure Misinterpretation Leads

To Late Surveillance Testing." ,

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On March 20, 1989, a diesel fuel oil shipment arrived l

onsite for offloading into the Diesel Fuel Oil Storage

tanks. A technician obtained and analyzed a sample. The

technician and his foreman interpreted a note in the

analyses scheduling procedure to mean that the

neutralization number and mercaptan were not required to be j

performed. In fact, only the mercaptan was exempt from the  !

analysis and neutralization number was required to be

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performed. After the analysis found the other fuel ,

properties to be satisfactory, the shipment was unloaded l

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into the DF0S tanks. Meanwhile, a second diesel fuel oil

shipment arrived onsite, a sample was'obtained and analyzed

as before and unloading into the DF05. tanks began. A-

laboratory supervisor reviewed the data sheets and question

the omission of the neutralization number from the data

sheets. After the requirement was clarified, - the

technician obtained the original samples from each shipment

and determined that the neutralization number of each was

within technical specification requirements. The cause of

this event was the misleading nature of the procedure note.

The procedure note was rewritten and clarified. This item

represents a violation of NRC requirements which meets the

criteria for non-citation. In order to track this item,

the following licensee-identified item is established.

NCV 50-425/89-15-06, " Failure To Establish An Adequate

Sampling Procedure For Diesel Fuel Oil Per is 6.7.1.a - LER

50-425/89-09."

(i) 50-425/89-10, Rev. O, " Radioactive Discharge Without Permit

Leads To Technical Specification Violation."

Technical Specification 3/4.11.1 requires that releases of

radioactive materials to unrestricted areas be sampled and

analyzed for appropriate alpha, beta, and gamma emitters.

On March 8, 1989, the contents of the Unit 2 Turbine

building drain tank, 2-2412-T4-002, were sampled for gamma

emitters to determine if a release permit was required. On

March 9, a plant operator released the tank contents to the

Unit 2 Waste Water Retention Basin without a permit. On

March 14, during a review of releases, it was found that no

permit had been issued for the March 9, release. The

permit ensures that required samples have been taken,

analyzed and are within allowable limits for releases.

Procedure 13211-2, " Turbine Building Drain System,"

required that sample analysis be used to determine how

drain tank contents are to be processed but did not specify

that a release permit may be required. The cause of this

event was that the operator did not obtain a radioactive

release permit prior to releasing. Procedure 13211-2 has

been revised to provi-de specific instructions that a

radioactive release permit may be required for releasing  ;

the contents of a turbine building drain tank. Also, at  ;

shift briefings, operators were reminda.d that waste permits

are required prior to release of radioactively contaminated

tank contents. This item represents a violation of NRC

requirements which meets the criteria for non-citation. I r.

order to track this item, the following licensee-identified

item is established.

NCV 50-425/89-15-07, " Failure To Obtain A Radioactive

Release Permit Prior To Releasing Radioactive Materials To

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LER 50-425/89-10."

(j) 50-425/89-12, Rev. O "Oper' ting Incorrect Switch Results

In Inoperable Monitor Requi >.ng Entry Into TS 3.0.3."

On March 30, 1989, while performing maintenance on

2RE-2562A, an Instrument and Controls Technical

inadvertently placed' 2RE-2562A and 2RE-2562C in purge

instead of activating the paper drive on 2RE-2562A. This

caused 2RE-2562C to be -inoperable. Later the same day, a

chemistry foreman discovered 2RE-2562C to be inoperable and

notified the control room. .An entry into TS 3.0.3 was made

due to an existing limiting condition for operation.for the

Reactor Coolant System Leakage Detection System and

2RE-2562C being inoperable. With 2RE-2562C inoperable the-

LCO for Technical Specification 3.4.6.1 could not be met.

2RE-2562C was restored to service and TS 3.0.3 exited. The'

cause of this event was personnel error. The I&C

technician failed to pay attention to detail when

activating plant equipment. The purge switch was activated

instead of the paper drive. Corrective actions included

counseling the individual and issuing a memo to all I&C

personnel concerning attention to detail when performing .

maintenance / trouble shooting on plant equipment. This item

represents a violation of NRC requirements which meets the

criteria for non-citation. In order to track this item,

the following licensee-identified item is established.

NCV 50-425/89-15-08, " Failure To Follow Procedures While

Performing Maintenance On 2RE-2562A Resulting In The Plant

Operating In A Condition Prohibited By TS Thus Requiring

Entry Into TS 3.0.3 - LER 50-425/89-12."

(k) 50-425/89-13, Rev. O, " Flood Barrier Removal Leads To

Auxiliary Feedwater Inoperability."

Technical Specification 3.7.1.2 requires that three

independent steam generator AFW pumps and associated flow

paths be operable in Modes 1, 2, and 3. On March 30, 1989,

plant personnel were conducting a routine walkdown. They ,

found a flood protection barrier removed from the wall l

between che AFW discharge piping room (room 105) and the

Turbine Driven AFW pump room (room 106). The barrier was

replaced and the TS action statement was exited. The cause

of this event is an apparent personnel error by removing

the barrier without the proper review and approval. Work

had been performed on a check valve in room 105. When a

functional test was performed on March 23, the existence of

a flood barrier and precautions to be observed were not

addressed by those requesting the test or by those

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implementing'the. work order..-A sign will be installed near

the flood ~ barrier and information. will be added to the-

equipment file advising of the: flood barrier's existence.

This item represents a violation of NRC requirements which

meets' the criteria'.for non-citation. . In order to' track

this- item, the following licensee-identified- item . is-

established.

. .NCV 50-425/89-15-09, " Failure To Maintain The Auxiliary

Feedwater System Operable Resulting. In A Condition

Prohibited By TS 3.7.1.2. - LER 50-425/89-13."

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(1) *50-425/89-16, Rev. O, " Unplanned Auxiliary Feedwater

Actuation On Recovery From Remote Shutdown Test."

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On April 11, 1989, while recovering from a Remote Shutdown

Test, -an automatic Engineered Safety Features actuation

(auto start signal to motor. driven Auxiliary Feedwater

pumps) occurred. During the Remote Shutdown test, both-

Main Feedwater Pumps were manually tripped and AFW was in-

service. With both .MFPs tripped an AFW actuation signal

was generated; however, .while control- was at the Remote

Shutdown Panel, the signal is interrupted. . - When control

was returned to the control room, the signal was

reinstated. As the AFW pumps were already in operation,

the AFW actuation signal caused the discharge. valves of the

L Train. A to stroke full open. Control room operators

immediately throttled AFW flow to-_ prevent overfilling of

the steam generators. MFP "A" was reset to allow return of

the remaining trains to the control room. All AFW systems

were' restored to readiness. The cause of this event was a

situation that was not anticipated by the procedure.

Procedure 18038-2, " Operation From Remote Shutdown Panels,"

will be revised to caution. operators of a possible

actuation of transfer of control to the control room.

(3) .The following LERs were reviewed and closed.

(a) 50-424/87-81, Rev. 0, " Excessive Valve Weight Could Have

Prevented Fulfillment Of Safety System Function."

On May 5,1987, two valves supplied by Anchor Jarling Valve

on the sludge mixing recirculation line of the Refueling

Water Storage Tank were found to weigh significantly more

than shown on the A/DV drawings. The initial analysis from

an employee of Bechtel Power Corporation indicated that the

valves weighed in excess of the seismic design capacity of

their associated pipe supports and that if a line failure

had occurred in the non-safety related portion of the

sludge mixing line during a seismic event, the valves could

have been closed and allowed the RWST water volume to be

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available for plant shutdown. On March 6, -1989, the

Project Field Engineering-0ffice advised plant personnel

that there was an error in the application af potential

failure point and that the potential failure point was

actually between the valves and the RWST. Thus, if a

seismic event caused a line failure to occur, the broken

line could have potentially drained the RWST to a level

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below minimum requirements for plant shutdown. The cause

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of this condition was determined to be the failure of A/DV

to advise Bechtel of a change in valve weights from those

originally shown on the valve drawings and an error by a

Bechtel Power employee in the initial review of this

condition. Corrective actions included adding an

additional pipe support and reviewing other safety related

valves for weight discrepancies. The-inspector has no

further questions.

(b)*50-424/88-16, Rev. O, " Water Leakage Into Control

Room / Potential Exists For A Safety System Failure."

On June 3, 1988, smoke from an electric duct heater

actuated smoke detection alarms. Although sprini cr heads

did not actuate, water from the preaction valve leakoff

lines ran into the upper cable spreading room and seeped

into the control room from the ceiling. Water entered some

process panels and led to spurious equipment actuations in

the Reactor Coolant System which were promptly addressed

and corrected by control room personnel. On June 5, 1988,

it was concluded that a condition existed which alone could

have prevented the fulfillment of the safety function of a

systera needed to mitigate the consequences of an accident.

The cause of this event is an inadequate design of the

control room ceiling penetrations which are supposed to be

watertight. Corrective actions were verified complete.

This item resulted in a NRC violation 50-424/88-24-01.

(c) 50-424/88-19, Rev. O, " Inadequate Installation Leads To

Containment Ventilation Isolations."

On June 10, 1988, a CVI occurred due to an apparent power

supply failure in radiation monitor 1RE-2565C. The

appropriate dampers and valves actuated as designed.

Control room personnel verified that no abnormal condition

existed. 1RE-2565C was bypassed and the CVI signal was

reset. Later, the same day, another CVI occurred, when

plant personnel removed 1RE-2565C from bypass in order to

reenter monitor setpoints. Again the proper dampers and

valves actuated and control room personnel verified that no

abnormal radiation condition existed. 1RE-2565C was again

placed in bypass and the CVI signal was reset. An

investigation demonstrated that the cause of the CVI was an

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inadequate installation . which left ' a flow' transmitter

. shield wire _ exposed that electrically grounded, simulating.

a loss of. power. Corrective action included _ insulating the

shield wire ~and new default values were installed.

1 (d) 50-424/88-20..Rev' 1, " Inadequate Breaker Leads.:To

Condition Prohibited By Technical Specification."

On June 29, 1988, it was determined that. ten containment

penetrations may not have adequate redundant overload

protection, as. required by Regulatory Guide 1.63. The

redundant protection was not provided because-in each of

the~ ten penetration circuits one of the two breakers use_dL

was magnetic-only, which did not provide adequate overload

. protection for the penetration. The other. breaker pro ~ided-

v

was a ' thermal-magnetic and provided adequate ' overload

protection for the penetration. Since the magnetic-only

breakers did not provide the redundant overload protection,

the requirements of . Technical Specification 3.8.4.1 for

operability was not satisfied. When it was determined that.

redundant overload protection may not have been adequate

over the entire range, the identified containment

penetrations were declared inoperable and the requirements

of Technical Specification 3.8.4.1 were satisfied while the

breakers were being replaced. Prior' to. the operation of

Vogtle Unit 1, a construction test was performed for each

breaker to verify its tripping function. All tests were

performed satisfactorily and the breakers declared

operable. The inspector has reviewed documentation which

indicated that the- corrective action was complete. The

magnetic-only breakers were replaced with thermal-magnetic

breakers.

1

(e) *50-424/88-22, Rev.1, " Failed Potential Transformer i.eads

To Turbine / Reactor Trip."

On July 14, 1988, a generator / turbine / reactor trip occurred

as a result of an overexcitation condition on the generator

.

field. Control rods inserted. The Main Feedwater system

l

isolated and the Auxiliary Feedwater system actuated.

Control room operators responded . properly to assist in

plant stabilization. An investigation revealed that the

failure of a potential transformer caused the primary fuse

to blow. The resultant transient caused the GENERREX

voltage regulator to malfunction, increasing generator

voltage to the Volts / Hertz relay setpoint, which

subsequently initiated a generator / turbine / reactor trip.

Corrective action includes replacing all primary PT fuses,

PT 2A, and the malfunctioning circuit boards in the

GENERREX system. The GENERREX system's operational history

has been evaluated and additional adjustments are not

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considered necessary at. this time. Engineering review of

design enhancements to .the present GENERREX system will i

continue to be performed as part of the Trip Reduction i

Program. The failed PT was analyzed and a winding failure

was identified. Improved test methods to detect this-type

of PT failure were evaluated. However, a more appropriate

'

test method has not been identified. This LER was closed

in report 50-424/88-37.

(f) 50-424/88-23, Rev. O, " Inadequate Design Leads To Condition

Prohibited By Technical Specification."

On July 29, 1988, LER 50-424/88-20 was issued, identifying-

that several electrical penetrations may not have been

provided with adequate redundant overload protection. As a

result of the interpretation for deportability of that

event, two previously identified deficiencies have been

re-evaluated for deportability. As a result of the

re-evaluation, an event that was discovered on August 14,

1987, was determined to be reportable on July 28, 1988.

The other event was discovered on July 7,1987, and

determined to be reportable on August 11, 1988. It was

determined that for each event, redundant overload

protection may not have been adequate for the entire range

of protection . as required by Regulatory Guide 1.63.

Technical Specification 3.8.4.1 required that electrical

penetration overload protection may not have been provided

for several penetrations, Unit 1 may have been operating in

a condition prohibited by TS until the event was

discovered. For each event the limiting condition for

operation action statement for TS 3.8.4.1 was implemented

on the event discovery dates of July 7,1987, and

August 14, 1987. The event on August 14, 1987, involved

electrical penetrations No.12 and No. 69, concerning the

  1. 12 and #14 size conductors. The other event on July 7,

1987 involved penetration No. 03, 14, 34, 41, 60, and 61,

concerning #10 size conductors. The inadequate overload

protection was discovered during a broadness review for

Unit 2 by the designer, Bechtel Power Corporation. The

inspector verified the work complete by reviewing the

closed MW0s.

(g) 50-424/88-26, Rev. O, "Use Of Improper Tools Leads To

Containment Ventilation Isolation."

On September 7, 1988, an electrician was in the process of

installing shorting bars into fuse holders following the

completion of an electrical switch replacement. The y

electrician unintentionally created a short between two 120  ?

volts AC circuits. Various alarms and indicators actuated,

including those for a CVI. The appropriate CVI valves and

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dam;:ers ' actuated. Control room personnel verified that no

abnormal radiation condition existed by observing redundant ~

-monitors. The control room personnel and the electrician

immediately confirmed that the electrical short had

'

initiated the "JT . The cause of this event was the use of

an improper toct -y the electrician. Fuse pullers provided

to the electrician would not fit between the inserted

shorting bars, so he used needle-nose pliers to perform the

insertions. These pliers made the electrical short by

simultaneously contacting two shorting bars following one-

shorting bar's insertion. Appropriate personnel were

advised to avoid the use of needle-nose pliers or makeshift

tools for installation of fuses or shorting bars. The

proper size fuse-pullers were made available.

(h) 50-424/88-30, Rev. 0, " Surveillance Missed Due To

Inoperable Rod Position Deviation Monitor."

On October 27, 1988, while preparing a licensing document

change, it was discovered that a plant computer design-

feature _ for monitoring deviations between Digital Rod

Position Indication System and Domand Position Indication-

System had not been implemented within the plant computer

software as intended. The absence of this feature means

the Rod Position Deviation Monitor is operable for this

function and that surveillance 4.1.3.2 has not been met,

when required, since issuance of the Unit I license. The

surveillance required operability determination of the

digital rod position indicators. For this determination,

the DPIS must be verified to be with + or - 12 steps of the

DRPIS every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />, except when the RPDM is inoperable,

then the requirement is at least once per 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. As the

plant staff were unaware of the software omission, they did

not take the required action to manually make the

comparisons every 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> as required. The cause of this

event was the omission of appropriate rod supervision.

programs in the original vendor supplied computer software

specifications. Corrective actions include increased

frequency of the surveillance and an evaluatica to

determine if either changes to W computer software are

feasible or changes to licensing documents are required.

The inspector reviewed documentation which indicated that

the corrective action was complete. This item represents a

violation of NRC requirements which meets the criteria for

non-citation. In order to track this item, the following

licensee-identified item is established.

NCV 50-424/89-14-07, " Failure To Conduct Surveillance

Resulting In A Violation Of TS 4.1.3.2 - LER 50-424/88-30."

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(i)-*50-424/88-41, Rev. O and 1, " Containment Purge Supply

Isolation Valve Inoperable Due To Failure To Fully Close."

On December 13, 1988, while. performing 'a revised Type C

Local Leak Rate Test- for. surveillance of the containment

purge supply isolation valves in Penetration 83, it was.

discovered that the 24-inch containment purge supply

isolation valve 1-HV-2626A was not fully seated.

'

This

condition is prohibited by Technical Specification 3.6.1.7

which requires that this valve be closed and sealed closed.  ;

LC0 1-88-922 was entered for 1-HV-2626A failing the leak

'

. ate test. This event occurred because the valve did not

fully close, even though the limit switch indicated that

the valve was closed. Corrective actions included issuing

LC0 1-88-922,1mmediate manual seating of the valve and

successfully repeating the LLRT, and . establishing

conservative administrative controls to ensure that each

24-inch purge isolation valve, if cycled, will be either

manually seated or have an LLRT performed, as appropriate.

Procedures 13125-1, Rev. 8, and 13125-2, Rev. 2, were

verified by the inspector to have been revised.

(j) *50-424/89-05, Rev. O, " Trip Of Main Feed Pump On High  !

Vibration Resulting In Manual Reactor Shutdown."

l

On February 10, 1989, Control Room operators received Main

Feedwster Pump Turbine "A" high vibration alarms. A check

of the vibration monitor system showed a vibration of only

1.2 mils. (The vibration system alarms at 3 mils and trips ,

at 5 mils). Shortly thereafter, MFP " A ". tripped. t

Steam /feedwater flow mismatch alarms were received on all >

four steam generators. Turbine load was manually reduced l

to approximately 700 MWe and control rods placed in Auto to  ;

'

follow load. Steam dump valve controllers were manually

operated to attempt to match steam / feed flow. SG #4

reached 20% level and the Shift Supervisor directed the  !

reactor to be manually tripped. Feedwater isolation and 1

start of Auxiliary Feedwater pumps occurred as expected.

However, the Turbine Driven AFW pump tripped on overspeed  ;

after startit:g. The cause of the MFP high vibration trip l

was not positively identified. The cause of the TDAFW pump

overspeed trip, although not positively identified, may l

have been caused by particulate contamination of the lube  :

oil, which serves as the control system hydraulic fluid.  !

Corrective actions included temporarily installing l

vibration instrumentation to collect MFP vibration data.  !

Additional surveillance were also performed on the TDAFW

pump to ensure operability.

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(k) 50-424/89-09, Rev. 0, " False Radiation Monitor Signal

Caused Containment Ventilation Isolation And TS 3.0.3

Entry."

On March 13, 1989, radiation monitor 1RE'-0003 spiked high

causing a Containment Ventilation Isolation. Appropriate

valves and dampers actuated from the CVI signal to isolate

containment ventilation. LC0 1-89-155 was entered for

1RE-0003. Radiation monitor 1RE-0002 was out of service

for a surveillarice and 1RE-2565 was not operable because of

reliability concerns. Technical Specification 3.3.2,

Table 3.3-2, requires a minimum of two of the three channel

be operable, but there is a provision for operation with

only one channel in operation. An entry was made into TS 3.0.3 since all three channels were inoperable. Control

room operators verified that no abnormal radiological

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conditions existed using IRE-0002, which was functional but

not operable. Later that same day, 1RE-0002 was declared

operable, the high alarm on.1RE-0003 was cleared, the

monitor placed in. bypass, and the CVI signal was reset.

The cause of this event was the failure of the detector

tube. The tube was replaced; however, the replacement tube

did not function properly and required replacement due to

degradation of the voltage plateau. The replacement tube

was monitored and the monitor was declared operable.

(1) 50-425/89-01, Rev. O, " Spurious. Signal Resulting From

Circuit Board Causes Control Room Isolation."

On February 14, 1989, a Control Room Isolation occurred due

to a spurious signal from radiation monitor channel

2RE-12116. Prior to this actuation, the Safety Parameters

Display Console had received intermittent trouble light

indications from the channel. Control room operators

verified no high radiation condition existed. The

monitor's output was blocked, a LC0 was entered, the CRI

signal was reset, and normal ventilation was established.

Radiation monitor channel 2RE-12116 was returned to service

and the LCO exited on February 18. The event was caused by

a random failure detected on the Central Processing Unit

board in the Digital Processing Module. This random event

caused the internal timer to lock up and initiate a system

reset signal. During a system reset, the monitor's fail

safe function initiates a high alarm signal which caused

the CRI actuation. Corrective actions included initiation

of a LC0 for the monitor, replacement of the defective

circuit board, observation of the monitor for proper

operation and return of the monitor to service.

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L (m)'*50-425/89-02 Rev.0- " Opening Discharge Valves Causes Plant

Operation'0utside Of Technical Specifications."

Technical Specification .Se'ction. 3.4.1.4.2 _ states,"

... Reactor Makeup Water Storage Tank discharge ' valves

- (1208-U4-175, 1208-U4-176, 1208-U4-177, and 1208-U4-183)

.shall be closed and secured in position (in) Mode 5 with

reactor coolant loops not filled.". On February 19, 1989,

the unit made its initial entry into Mode 5. - valves

2-1208-U4-175 and 2-1208-U4-177 were opened. After shift

change, new shift personnel realized that the; reactor

o . coolant system loops were not filled and that the two open-

discharge valves were required to be closed. -A LCO was

initiated, the valves were closed and locked, and the LC0

was terminated. Plant personne1' believed that filling .the -

RCS above the loops to L the reactor vessel flange leve11

constituted a " loops filled" condition, after which opening

the discharge' valves would have been; permissible. With the

-discharge. valves open, an inadvertent dilution event of the-

RCS could have been initiated. A TS interpretation of what.

constitutes " loops filled" has been.added to the Operations

Required Reading Boolg The personnel involved were

counseled regarding the' importance of complying with TS.

Inspector. followup determined that prior to the Mode 5

entry, the.SS had been asked to open these same valves to

allow chemistry to add primary chemicals. At that time,

the SS was : aware that TS 3.9.1 required the valves to be

maintained shut in Mode 6 and thought that the change to

Mode 5 would allow the evolution. TS 3.4.1.4.2 however,

also controls these valves when the RCS loops are not

filled. Operations procedure 12006-C established positive

control of these valves by tagging them closed. These

valves are untagged by operations procedure -13000-2 upon

filling and completing air sweeping of the RCS. The.

removal of the RMWST valves to the CVCS was a discussion

item at the shift turnover, however, neither SS recognized

the consequences. Later in the shift, the deficiency was

identified and corrected. This item was formally discussed

' following the enforcement conference on March 22, 1989.

This item represents a violation of NRC requirements which

meets the criteria for non-citation. In order to track

this item, the following licensee-identified item is

established.  !

NCV 50-425/89-15-10 " Failure To Maintain RMWST, Discharge

Valves Shut Closed And Secured In Position While In Mode 5

Resulting In TS 3.4.1.4.2 Violation - LER 50-425/89-02."

(n) 50-425/89-03, Rev. O, "Depressurizing RHR System Leads To

Technical Specification 3.0.3 Entry."

On March 9,1989, with the unit having just entered mode 3

for the initial heatup, preparations were being made to

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perform the Pressure.1 solation Valve Leakage Test. In

order to ensure proper pressure across the valves :to be

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tested, the Shift Supervisor decided, without an approvedi

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procedure, to depressurize the Residual Heat Removal

system, using the RHR test return valves. The SS directed.

a momentary opening of these valves. This resulted in the

return .line valves being left open for approximately 14

hours, reducing the flow capacity of both RHR trains, and

leading to operation under Technical Specification 3.0.3

provisions. This event was caused by -(1) operations -

personnel attempting an evolution without approved

procedural guidance, (2) lack of closed loop communication.

and (3) inadequate system status sensitivhy by the

operations' shift team. Corrective actions include s(1)

counseling the Shift Supervisor and briefing of each

operating crew by th Plant General- manager on the

importance of conducting plant evolutions with approved

procedures, (2) changing the appropriate procedure, (3)

stressing precise control room . communications,. (4)

stressing sensitivity to system status in shift briefings

'and requalification training, and (5) improving the locked

valve program.. . This item was. cited as a NRC violation. in

report 50-425/89-12. ~ Remaining corrective actions will.be

verified in closecut of the violation. -

(o) *50-425/89-04, Rev. O, " Reactor Coolant System Leakage

During Check Valve Testing."

On March 9,1989, with Unit 2 in Mode 3, plant operations

personnel performed a pressure isolation valve leakage

test. The Primary Coolant Loop #3 Cold Leg Check Valve

(2-1204-U6-085) exhibited excessive leakage. A

Notification of Unusual Event was declared, because.the

Reactor Coolant System leakage - exceeded the technical

specification limit of 5 gpm specified in Section

3.4.6.2.f. On March 10, 1989, the plant entered Mode 5 and

the NUE was terminated. The event was caused by excessive

wear on internal check valve components. Wear was found

near the' pivot pin which allowed the disc to drop down and

not seat properly. The valve consists of a disc with two

arms which insert into a lock block. The pivot pin goes

into the lock block. The disc arms are notched out for

alignment with the pivot pin. Wear was found on both

notches in the arms which allowed the disc to drop.

' Corrective action included replacement of the internal

components in this valve and the three identical check

valves in the other three loops.

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(p)*50-425/89-08, Rev. O, " Improper Control Of Steam Generator

Water Level Leads To Feedwater Isolation."

On March 19, 1989, unit 2 heatup was in progress. The unit

Balance-of-Plant operator was manually controlling the

steam generators water levels when a technician requested

I his assistance in performing a surveillance test. The B0P

operator left the front panel to go to a back panel area.

When he returned several minutes later, he found that an

automatic feedwater isolation had occurred because SG #4

had exceeded the 78% (narrow range) high-high water level

setpoint. The operator stopped the feed to SG #4, returned

the flow to normal, and long cycle recirculation was

L re-established. The B0P operator intended to leave the

front panel for only a few moments and did not request

relief. This is the direct cause of this event.

Contributing to this event was the Shift Supervisor's

omission in assigning a dedicated Steam Generator Water

Level Controller which is the plant policy when manual SG

feeding it. in progress. The BOP operator was counseled

regarding the importance of maintaining a continuous watch

on operations in progress or else requesting relief if

needed. The SS was advised of the necessity to comply with

plant practice to have a dedicated SGWLC when manual SG

feeding is in progress. This item was formally discussed

following the enforcement conference on March 22, 1989.

This item represents a violation of NRC requirements which

meets the criteria for non-citation. In order to track

this item, the following licensee-identified item is

established'.

NCV 50-425/89-15-11 " Failure To Exercise The Duties And

Responsibilities Of The R0 And SS As Delineated In

Operations Procedure 10000-C - LER 50-425/89-08."

(q)*50-425/89-11, Rev. O, " Valve Closure Leads To

Non-Compliance With Technical Specifications."

Technical Specification 3/4.5.2 requires that the Safety

Injection Pump Cold Leg Injection valve 2-HV-8835 be open

while in Modes 1, 2, and 3. On March 19, 1989, the shift

operating crew closed the Safety Injection pump cold leg

injection valve to the Reactor Coolant System cold legs

(2HV-8835) while performing the system operating procedure

to fill SI accumulators at low RCS pressure in Mode 3.

Closure of this valve prevents both SI pumps from being

capable of providing automatic injection to the RCS cold

legs upon receipt of a SI actuation signal. On March 26,

while considering LER 2-89-003 (both trains of Residual

Heat Removal rendered inoperable due to common valve

manipulations) and similar situations for other

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safety-related. systems, a shift supervisor realized that

the system operating procedure for filling SI accumulators

at low RCS pressure requires closure of 2HV-8835 while in

,

Mode 3. Upon discovering this, a review of the Unit 1 and

Unit 2 accumulator fills was initiated. Nine separate

instances were identified for Unit I when 1-HV-8835 was

closed while in Mode 3, in addition to the single

occurrence on Unit 2, specified previously. The cause of

these events is inadequate procedures which did not prevent

closure 2HV-8835 during Mode 3 or require accumulator fill

prior to Mode 3 entry. The procedures are being changed to

correct these inadequacies. Future followup on this LER

corrective actions will be in closecut of the violation.

This event is one example of violation 50-424/89-14-01 and

50-425/89-15-01, " Failure To Establish An Appropriate

Procedure To Maintain SI Operable While Filling

Accumulators.

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(r) ~ *50-425/89-14, Rev. 0, "Feedwater Isolation Results From

Error In Startup Test Procedure."

On April 3, Unit 2 startup testing was in progress. A test

signal was incorrectly inputted into the steam dump control

circuit causing the steam dumps to fully open instead of

opening 10% to 15% as expected. This led to a steam

generator water level swell and a feedwater isolation due

to SG #4 reaching the high-high level. Main feedwater

isolation occurred as designed, and the safety grade

isolation valves closed, but main feed pump "A" did not

trip. As a result, the Auxiliary Feedwater system did not

automatically start, although it was already being used to

supply SG water. Manual control was taken of the Steam

Generator Feed and unit parameters were stabilized. The

test procedure, which called for an incorrect test signal,

was corrected and the remaining startup tests are being

reviewed to ensure that proper connections are specified.

Sliding links associated with MFP "A" circuits were found

open and are believed to be an oversight from the Unit 2

construction phase. Similar slidici links were inspected

to ensure closure.

This item is part of one ex%+ k of violation

50-424/89-14-01 and 50-425/89-15-01 discussed in paragraph

3.

(s) *50-425/89-15 Rev. O, " Faulty Circuit Cards Results In ESF

Actuations."

On April 5,1989, a spurious trip of Main Feedwater Pump

"A" generated a Feedwater Isolation signal and automatic

actuation of the Auxiliary Feedwater System. On April 7, a

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FWI and AFW actuation occurred when a steam generator

reached its high-high level setpoint during a test of a

Main Feedwater Isolation Valve. On April 9, a second

spurious trip of MFP "A" generated a FWI and subsequent AFW

actuation. The cause of the April 5 and April 9 events was

faulty circuit boards in the Solid State Protection System 1

'

logic circuits. The April 7 event, although not directly I

caused by a faulty circuit card, was a consequence of the

valve lineup used to functionally test repairs made

following the April 5 event. The lineup of long-cycle

recirculation was not properly restored prior to resumption

of startup testing. Corrective actions include replacing

the faulty- circuit boards and counseling . plant operators

regarding proper shift turnover of unusual plant

configurations and the need for procedural compliance.-

This event is part of one example of violation

50-424/89-14-01 and 50-425/89-15-01 discussed in paragraph

3.

One example of a cited violation and thirteen non-cited violations

were identified.

5. Actions on Previous Inspection Findings - (92701)(92702)

a. (Closed) Violation 50-424/87-30-03, " Failure To Properly Close

Valve."

The inspector reviewed the licensee respor e dated July 13, 1987.

Valve No. 1-1208-U4-348 has had the lock removed to preclude future

errors in positioning from the renote operator.

b. (Closed) Violation 50-424/88-05-02, " Lack Of Material Control."

The inspector reviewed the licensee response dated March 10, 1988.

The inspector noted that procedures exist to control the purchase and

receipt of weld rod.

c. (Closed) Violation 50-424/88-24-01, " Failure To Adequately Design

And Install Water Tight Penetration Seals And Perform An Analysis i

Which Evaluates Their Failure."

The inspector reviewed the licensee response dated September 15, 1988 i

and reviewed completed MW0s 18900130 and 18900180. During this

inspectica period, a similar actuation of the fire suppression system

occurred which challenged the seal configuration. Observation by the

NRC inspector at that time noted that no water penetrated into the

Control Room.

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d. (Closed)'IFI 50-424/88-43-01, " Verify Resolution Of Restoring The j

, SSMP To A Condition To Correctly Indicate The Operability Status." <

.The licensee corrected the condition by implementing a design change

which removed the Boric Acid Pump Motor handswitches as an input to

the SSMP. The inspector urified the change was implemented on

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Unit 1. Following the verification, the inspector noted that Unit 2

had- not implemented a similar change. The inspector was informed

that design change MDD 89-V2M035 was being developed for Unit 2. The

inspector considered the late implementation of a Unit 2 change to be

a weakness in the area of engineering support in maintaining the

designs both units identia , , as possible. This change involves the

lifting.of two leads in eatn train panel. To track the accomplishment

of Unit 2 change, the foi'owing inspector followup item is

identified.

IFI 50-425/89-15-03, " Verify Resolution Of Restoring The SSMP To A

Condition To Correctly Indicate The Operability Status."

e. (Closed) Violation 50-424/88-56-01, " Failure To Implement Operations

Procedure 14900-1, Containment Exit Inspection Required By TS 6.7.1."

The inspector reviewed the licensee response dated March 7,1989.

Corrective actions have been observed in'pri. tice by the inspector.

Procedure 43006-C was revised to include controls for health physics

responsibilities.

f. (Closed) Unresolved Item 50-424/88-56-02, " Review Licensee

Evaluation Of Compliance To 10 CFR 50.62."

This item concerned the sensitivity of unit personnel to the proper

operation and maintenance of AMSAC equipment. The licensee has

implemented quarterly and refueling surveillance procedure 54804-1,

revised response procedure 54804, and revised response procedure

17005-1. Unit operating procedures 12004-C has been revised to the

correctly indicate the power level where the equipment becomes i

operational. Failure to comply with 10 CFR 50.62 was the result of a

failure to establish adequate procedures. Failure to comply with 10

CFR 50.62 was the result of a failure to establish adequate

procedures.

This item is considered to be one of the examples of violation

50-424/89-14-01 and 50-425/89-15-01, " Failure to establish adequate

procedures to ensure AMSAC was available.

g. (Closed) Violation 50-424/88-61-01, " Failure To Implement Operations

Procedure 10001-C, Required By TS 6.7.la, To Annotate And Verify

Proper Operations Of Control Room Chart Recorders."

In the licensee response dated March 7,1989, to the Notice dated

January 20, 1989, the licensee committed to full compliance on

January 31, 1989, upv 'ssuance of standing order C-89-01. This

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standing order was reviewed by the resident inspector on March 24,

1989, and was found to be satisfactory.

One example of a cited violation and one inspector followup item were

identified.

6. Exit Interviews - (30703)

The inspection scope and findings were summarized on May 5,1989, with

these persons indicated in paragraph 1 above. The inspector described the.

areas inspected and discussed in detail the inspection results. No

dissenting comments were received from the licensee. The licensee did not

identify as proprietary any of the materials provided to or reviewed by

the inspector during this inspection. Region based NRC exit interviews

were attended during the inspection period by a resident inspector. This

inspection closed five violations (paragraph 5), one unresolved item

(paragraph 5), one inspector followup item (paragraph 5), and nineteen

Licensee Event Reports (paragraph 4.b(3)). The items identified during

this inspection were:

Violation 50-424/89-14-01 and 50-425/89-15-01 contains six examples where

procedures were not either established or implemented as follows:

- " Failure To Implement Procedures 00101-C and 50009-C Resulting In TS 6.7.1.a Violation" - paragraph 2.b(1)

- " Failure to Implement Procedure 12004-C Step 4.1.39 and 4.1.4 for

Performing Transfer From Auxiliary Feedwater to Main Feedwater" -

paragraph 3

- " Failure To Establish An Adequate Procedure For The Testing Of Steam

Dumps" - paragraphs 3 and 4.b(3)(r)

- " Failure To Implement Procedure 12004-C To Secure From Long-Cycle

Recirculation" - paragraphs 3 and 4.b(3)(s)

-

" Failure To Establish An Appropriate Procedure To Maintain SI .

Operable While Filling Accumulators" - paragraph 4.b(3)(q)  !

- " Failure to establish adequate procedures to ensure AMSAC was

available" - paragraph 5 f

IFI 50-424/89-14-02 and 50-425/89-15-02, " Review Licensee Evaluation

Regarding Adjustment Of The P-9 Setpoint When Steam Dumps Are Removed From

Service" - paragraph 3

IFI 50-425/89-15-03, " Verify Resolution Of Restoring The SSMP To A

Condition To Correctly Indicate The Operability Status" - paragraph 5.d .

I

NCV 50-424/89-14-03, " Failure To Perform Required Testing Per I

Surveillance Requirements Results In TS 4.3.3.10 Violations - LER

50-424/89-06" - paragraph 4.b(2)(a)

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NCV 50-424/89-14-04, " Failure To.Take Required Temperatures Results In

Inadequately Performed . Surveillance Resulting In A TS Violation - LER

50-424/89-07" - paragraph 4.b(2)(b)

NCV 50-424/89-14-05, " Failure To Conduct An Adequate Engineering' Review

Re

Of

TS The AFW

3.7.1.2 Electrical

Violation - LER System Which Led

50-424/89-08" To AFW Inoperability(c)sulting

- paragraph 4.b(2) In a

NCV 50-424/89-14-06 " Failure To Follow Procedures While Conducting A

Liquid Waste Release Resulting In A TS 3.3.3.9 Violation -

LER

50-424/89-10" - paragraph 4.b(2)(d)

NCV 50-424/89-14-07, " Failure To Conduct Surveillance Resulting In A

Violation Of TS 4.1.3.2 - LER 50-424/88-30" - paragraph 4.b(3)(h)

NCV 50-425/89-15-04, " Failure To Meet A Mode Change Prerequisite

Resulting In A TS 3.7.12. Violation Requiring Valve 2HV-19051 To Be

Operable Prior To Entering Mode 4 - LER 50-425/89-05" - paragraph

4.b(2)(e)

NCV 50-425/89-15-05, " Failure To Follow Procedures Resulting In

Inadvertent SI Actuation - LER 50-425/89-06" - paragraph 4.b(2)(f)

NCV 50-425/89-15-06, " Failure To Establish An Adequate Sampling Procedure

For Diesel Fuel Oil Per TS 6.7.1.a - LER 50-425/89-09" - paragraph

4.b(2)(h)

NCV 50-425/89-15-07, " Failure To Obtain A Radioactive Release Permit

Prior To Releasing Radioactive Materials To Unrestricted Areas Resulting

In A TS 3/4.11.1 Violation - LER 50-425/89-?0" - paragraph 4.b(2)(1)

'

NCV 50-425/89-15-08, " Failure To Follow Procedures While Performing

Maintenance On 2RE-2562A Resulting In The Plant Operating In A Condition

Prohibited By TS Thus Requiring Entry Into TS 3.0.3 - LER 50-425/89-12" -

paragraph 4.b(2)(j)

NCV 50-425/89-15-09, " Failure To Maintain The Auxiliary Feedwater System

Operable Resulting In A Condition Prohibited By TS 3.7.1.2. - LER

50-425/89-13" - paragraph 4.b(2)(k)

NCV 50-425/89-15-10 " Failure To Maintain RMWST, Discharge Valves Shut

Closed And Secured In Position While In Mode 5 Resulting In TS 3.4.1.4.2

Violation - LER 50-425/89-02" - paragraph 4.b(3)(m)

NCV 50-425/89-15-11 " Failure To Exercise The Duties And Responsibilities

Of The R0 And SS As Delineated In Operations Procedure 10000-C - LER

50-425/89-08" - paragraph 4.b(3)(p)

The strengths in the areas of maintenance (paragraph 2.b(7)) and startup

testing (paragraph 3) and the weakness in the area of operations

(paragraphs 3, 4.b(2), and 4.b(3)) were also discussed.

I

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7. Acronyms And Initialism l

!

ABN As-Built Notice

A/DV Anchor Darling Valve

AFW Auxiliary Feedwater System

AMSAC ATWAS Mitigating System Actuating Circuitry

ASTEC Automatic Surveillance Technical System

BFIV Bypass Feed Isolation Valve

BFRV Bypass Feed Regulation Valve

B0P Balance-of-Plant

CCP Centrifugal Charging Pump

CCW Component Cooling Water System

CFR Code.of Federal Regulations

CRI Control Room Isolation

CVCS Chemical & Volume Control System

CVI Containment Ventilation Isolation

DC Deficiency Cards

DF0S Diesel Fuel Oil Storage

DPIS Digital Position Indication System

DRPIS Digital Rod Position Indication System

ECCS Emergency Core Cooling System

ERF Emergency Response Facility

ESF Engineered Safety Feature

FI Flow Indicator

FWI Feedwater Isolation

GE General Electric ,

GPM Gallons Per Minute

HS Hand Switch

HV High Voltage

I&C Instrument and Control

IFI Inspector Followup Item

ISEG Independent Safety Engineering Group

LC0 Limiting Condition for Operation

LER Licensee Event Reports

LLRT Local Leak Rate Test

LOSP Loss of Offsite Power

MDAFW Motor Driven Auxiliary Feedwater System Pump

MDD Minor Departure from Design

MFIV Main Feedwater Isolation Valve

MFP Main Feed Pump

MFW Main Feedwater

M0V Motor Operatcc Valve

MWO Maintenance Work Order

NCV Non-cited Violation

NPF Nuclear Power Facility

, NR Narrow Range

NRC Nuclear Regulatory Commission i

NSCW Nuclear Service Cooling Water i

i NUE Notice of Unusual Event l

0S05 On-Shift Operation Supervisor

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35'

PERMS Plant Effluent Radiation Monitoring System

PORV Power Operated Relief Valve

PT Pressure Transmitter

PV Pressure Valve

.RCDT Reactor Coolant Drain Tank

RCS Reactor Coolant System

RHR Residual Heat Removal System

RMWST- Reactor Makeup Water Storage Tank

R0 Reactor Operator

RPDM . Rod Position Deviation Monitor

RWST Reactor Water Storage Tank

SAER Safety Audit and Engineering Review

SG Steam Generator

SGWLC Steam Generator Water Level Control

SI Safety Injection System

SS Shift Supervisor

SSMP Safety System Monitor Panel

TDAFW Turbine Driven Auxiliary Feedwater Pump

TS Technical Specification

TSC Technical Support Center

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