ML20056G849

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Insp Repts 50-424/93-16 & 50-425/93-16 on Stated Date. Violations Noted.Major Areas Inspected:Plant Operations, Surveillance,Maint & Fire Protection
ML20056G849
Person / Time
Site: Vogtle  
Issue date: 08/23/1993
From: Balmain P, Brian Bonser, Skinner P, Starkey R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20056G847 List:
References
50-424-93-16, 50-425-93-16, NUDOCS 9309070236
Download: ML20056G849 (19)


See also: IR 05000424/1993016

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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REGION 11

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101 MARIETTA STREET, N.W., SUITE 2900

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ATLANTA, GEORGIA 30323-0199

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Report Nos.: 50-424/93-16 and 50-425/93-16

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Licensee: Georgia Power Company

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P. O. Box 1295

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Birmingham, AL. 35201

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Docket Nos.: .50-424 and 50-425

License Nos.: NPF-68 and NPF-81

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Facility Name: Vogtle 1 and 2

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Inspection Conducted: June 27, 1993 - July 31, 1993

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Inspector:

3. R. 3g Senior Resident Inspector

Date Signed

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. h R. 0" Star W esident Inspector

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p. A. Balm

Resident Inspector

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Approved by:

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P. Skinner, Chief'

Date Signed

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Reactor Projects Section 3B

Division of Reactor Projects

SUMMARY

Scope:

This routine inspection entailed inspection in the following

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areas: plant operations, surveillance, maintenance, fire

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protection and follow-up of open items.

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Results:

One violation and one non-cited violation (NCV) were identified.

The violation involved the inappropriate storage of

flammable / combustible materials within a safety related area of

the plant. A locker was identified in the Auxiliary building

containing these materials in quantities exceeding those allowed

and in a mix that was recognized as unsafe, and without any

evaluation by fire protection personnel (paragraph Sb).

The NCV involved a failure to follow procedure. During

restoration of the Unit 1 D-train battery following a cell

replacement, an operator incorrectly restored a battery charger to

service prior to closing the battery breaker. This error in the

9309070236 930823

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equipment restoration sequence resulted in losing power to a vital

instrument panel which tripped all the bistables on channel IV of

the Solid State Protection System (paragraph 2f).

An Unresolved Item (URI) was opened to complete a review of the

causes of a Unit 1 reactor trip on July 28. The trip occurred on

pressurizer low pressure while technicians were valving in a

pressurizer pressure transmitter following its replacement

(paragraph 2e).

The inspectors found that the licensee's root cause determination

and evaluation of Emergency Core Cooling System (ECCS) venting

deficiencies was effective in determining the cause of recurrent

gas accumulation while performing ECCS flowpath verification

surveillance tests (paragraph 3b).

The inspectors reviewed the licensee's use of a temporary reverse

osmosis system to process Unit 1 Recycle Holdup Tank waste water.

The system was of particular interest because it is similar to a

previous issue on the use of temporary radwaste processing systems

at Vogtle. The inspectors found that the licensee had adequately

addressed the concerns that may be associated with this system

(paragraph 2g).

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REPORT DETAILS

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Persons Contacted

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Licensee Employees

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  • J. Beasley, General Manager, Plant Vogtle

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S. Bradley, Reactor Engineering Supervisor

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W. Burmeister, Manager Engineering Support

  • S. Chesnut, Manager Engineering Technical Support
  • C. Christiansen, SAER Supervisor

C. Coursey, Maintenance Superintendent

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G. Frederick, Manager Maintenance

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  • W. Gabbard, Nuclear Specialist, Technical Support

M. Griffis, Manager Plant Modifications

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M. Hobbs, I&C Superintendent

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K. Holmes, Manager Operations

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  • D. Huyck, Nuclear Security Manager

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  • W. Kitchens, Assistant General Manager Plant Support

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  • I. Kochery, Health Physics Superintendent

R. LeGrand, Manager Health Physics and Chemistry

G. McCarley, ISEG Supervisor

R.--Moye, Plant Engineering Supervf " r

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M. Sheibani, Nuclear Safety and C W

Supervisor

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C. Stinespring, Manager Administration

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  • J. Swartzwelder, Manager Outage and Planning

C. Tynan, Nuclear Procedures Supervisor

  • J. Williams, Operations Superintendent

Other licensee employees contacted included technicians, supervisors,

engineers, operators, maintenance personnel, quality control inspectors,

and office personnel.

Oglethorpe Power Company Representative

T. Mozingo

NRC Resident Inspectors

  • B. Bonser
  • D. Starkey
  • P. Balmain
  • Attended Exit Interview

An alphabetical list of abbreviations is located in the last paragraph

of the inspection report.

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Plant Operations - (71707)

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a.

General

The inspection staff reviewed plant operations throughout the

reporting period to verify conformance with regulatory

requirements, TSs, and administrative controls. Control logs,

shift supervisors' logs, shift relief records, LC0 status logs,

night orders, standing orders, and clearance logs were routinely

reviewed. Discussions were conducted with plant operations,

maintenance, chemistry, health physics, engineering support and

technical support personnel. Daily plant status meetings were

routinely attended.

Activities within the control room were monitored during shifts

and shift changes. Actions observed were conducted as required by

the . licensee's procedures. The- complement of licensed personnel

on each shift met or exceeded the minimum required by TS. Direct

observations were conducted of control room panels,

instrumentation and recorder traces important to safety.

Operating parameters were verified to be within TS limits. The

inspectors also reviewed DCs to determine whether the licensee was

appropriately documenting problems and implementing corrective

actions.

Plant tours were taken during the reporting period on a routine

basis. They included, but were not limited to the turbine

building, the auxiliary building, electrical equipment rooms,

cable spreading rooms, NSCW towers, DG buildings, AFW buildings,

and the low voltage switchyard.

During plant tours, housekeeping, security, equipment status and

radiation control practices were observed.

The inspectors verified that the licensee's health physics

policies / procedures were followed. This it.:1uded observation of

HP practices and review of area surveys, radiation work permits,

postings, and instrument calibration.

The inspectors verified that the security organization was

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properly manned and security personnel were capable of performing

their assigned functions.

Inspectors observed that persons and

packages were checked prior to entry into the PA; vehicles were

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properly authorized, searched, and escorted within the PA; persons

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within the PA displayed photo identification badges; and personnel

in vital areas were authorized.

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b.

Unit 1 Summary

The unit began the period operating at 100% peer and operated at

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' full power until July 28. On this date an automatic reactor trip

occurred because a low pressurizer pressure signal was generated

when maintenance technicians incorrectly valved in a pressurizer

pressure-transmitter. The unit returned to power operation on

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July 29. At the close of the inspection period the unit was

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operating at 80% power.

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Unit 2 Summary

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The unit began the period operating at full power. On June 28,

the unit was manually tripped due to decreasing SG 2 narrow range

level caused by SG 2 MFRV failing closed. The unit returned to

power operation on June 29, reached full power on June 30, and

remained at full power through tha end of the inspection period.

d.

Unit 2 Manual Reactor Trip

On June 28, Unit 2 was manually tripped from full power (99%

power)'because of indications of loss of feedwater flow to SG 2,

and because narrow range level for SG 2 was at approximately 45%

(trip _setpoint) and decreasing. The event occurred due to MFRV 2

failing closed.

Follcwing the event all systems functioned

normally with the exception of source range nuclear instrument,

2NI-32, which did not indicate onscale when the source range

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instruments were energized.

The licensee's investigation of the MFRV failure determined that

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the valve closed due to a tracking / driver card failure in the 7300

process control system. The circuit board was replaced and the

MFRV was returned to service. The licensee initiated a failure

analysis of the defective card. A similar tracking / driver card

failed on September 14, 1992, resulting in the loss of speed

cont:ol to the Unit IA MFP causing pump speed to decrease to

minimum and the initiation of a manual trip due to decreasing SG

levels.

While the unit was shutdown the inspectors reviewed two recent NRC

generic issues with the licensee that could have required action

prior to startup. These issues concerned NRC GL 93-04:

Rod

Control System Failure and Withdrawal of Rod Control Cluster

Assemblies, and NRC Bulletin 93-02: Debris Plugging of ECCS

Suction Strainers. The inspectors verified that the licensee

completed actions 1, 2, and 4 of Westinghouse Nuclear Safety

Advisory Letter 93-007, which addressed the rod control system

concerns. The licensee had already completed the actions required

by Bulletin 93-02. A review of these actions was documented in

NRC IR 50-424,425/93-14.

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The-inspectors observed the reactor startup on June 29, and noted

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that there were no significant problems.

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Prior to the reactor startup, the inspectors reviewed results of

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NI-32 troubleshooting documented in MWO 29302223, which determined

that a pulse driver card had failed. The inspectors verified from

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the work description documentation that the card was replaced in

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accordance with procedure 22408-C, Circuit Board Removal and

Reinstallation. The inspectors noted no calibration or

adjustments were required for this card and procedure 24696-2, NIS

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Source Range Channel 2N32 Channel Calibration, sections 4.2.3 and

4.2.4 were performed to verify the NIs operation. Following the

reactor start up the inspectors observed that the licensee

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declared 2NI-32 inoperable again because it was indicating onscale

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at 30-40 cps with the source range instruments deenergized. The

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inspectors reviewed this problem with I&C supervision and the

maintenance manager and verified that the false indication was

unrelated to the pulse card failure and does not impact operation

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of the instrument when it is energized.

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e.

Unit 1 Reactor-Trip

At 11:50 pm on July 28, 1993, Vogtle Unit I tripped from 100%

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power on pressurizer low pressure. At 10:14 pm I&C technicians

entered the Unit I containment building to replace pressurizer

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pressure transmitter IPT-457. The transmitter was successfully

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replaced and calibrated without incident. However, while valving

in the transmitter to return it to service a reactor trip occurred

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on two out of four pressurizer low pressure logic.

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transmitter IPT-457 shares a common sensing line with pressurizer

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pressure transmitter IPT-458 and two pressurizer level

instruments. When IPT-457 was valved in it dropped pressure in

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the sensing line causing two of the four pressurizer pressure

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instruments to read low pressure. Although procedure 24527-1,

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Rev.13, Pressurizer Pressure Protection Channel III IP-457 Analog

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Channel Operational Test and Channel Calibration', contains

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cautions on valving in this instrument since the pressure in this

sensing loop can affect other pressure and level transmitters,

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there were indications that an error was made while valving in

IPT-457.

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All safety systems functioned as expected following the trip. A

problem occurred, however, on digital rod position indication.

Rod M-14 on control bank D indicated full- out on one DRPI channel

and full in on the other channel. There were no other indications

that the rod was stuck and the licensee promptly completed n

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shutdown margin calculation to verify a safe shutdown. Since

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there was a pre-existing DRPI problem on another control rod,

repairing the rod position indication was a start-up restraint.

Following repair of DRPI the plant commenced a reactor startup on

July 29 at 2:53 pm and was critical at 4:07 pm. The Unit was

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subsequently synchronized to the grid and power was increased. On

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the morning of July 30, with reactor power at about 50%, a QPTR

calculation identified that the measured QPTR exceeded the TS

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3.2.4 limit of 1.02.

This placed the Unit in the QPTR LC0 action

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statement. Reactor power was reduced to less than 50 percent to

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investigate the power tilt. This phenomenon was significant

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because it was unexpected and could not be explained. The

licensee suspected a xenon transient in the core caused the power

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tilt and anticipated that it would burn away with continued

operation. This was partially confirmed several hours later when

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the QPTR had lowered to less than 1.02.

Due to this core anomaly

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the licensee approached full power invoking the TS Special Test

Exceptions'normally reserved for core physics tests. The

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inspectors reviewed the licensee's actions to reach full power

with the special test exceptions invoked, and concluded that their

use was appropriate.

In this case, as with a core following a

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refueling, fundamental nuclear characteristics of the reactor core

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and related instrumentation were measured. The licensee is

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continuing to investigate the cause of the power tilt.

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At the close of the inspection period the inspectors had not fully

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reviewed and assessed the cause of the trip.

Pending completion

of this review this issue is identified as an Unresolved Item

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(URI) 50-424/93-16-01: Review Causas of Pressurizer Low Pressure

Reactor Trip.

f.

Inadvertent Tripping of Unit 1 SSPS Channel IV Bistables

On July 22, the licensee entered the 2-hour action statement of TS

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3.8.2.1, DC Sources, when float voltage on cell #26 of the D-train

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battery, IDDIB, was measured below the allowable voltage during

the routine weekly surveillance.

Prior to the cell replacement,

Operations personnel had deenergized one of the two battery

chargers which normally supply power to the 125 VDC switchgear

1D01, as required by procedure 13405-1, 125 VDC IE electrical

Distribution System. The battery breaker at IDDI was also opened

by Operations as directed by procedure 13405-1. Once the

defective battery cell was replaced, Operations attempted to

restore the deenergized battery charger and the battery to

service.

During the restoration process the operators incorrectly

reenergized the second D train battery charger (IDDICA) prior to

closing the battery breaker-to IDDI. This error in sequencing the

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equipment caused a voltage swing on the bus. This resulted in the

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redundant battery charger IDDICB tripping (charger IDDICA remained

on-line); a blown fuse in, and tripping of, inverter IDDlI4; and

the resultant loss of power to 120 VAC vital instrument panel

IDYlB, powered from the inverter. Numerous control room

annunciators were illuminated and all the Channel IV SSPS

bistables were tripped.

Panel IDY1B remained deenergized for 27

minutes until its alternate power supply, a regulated transformer,

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was energized. During the 27 minutes, Channel IV of SSPS remained

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in a tripped condition.

If another bistable of either of the

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remaining three channels of SSPS had been tripped prior to or

during this event, the reactor would have automatically tripped.

The licensee subsequent;y restored inverter IDDlI4 and the D-train

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battery prior to the expiration of the LCO action statement time

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limits.

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The inspector discussed this event with several of the licensee

personnel involved, reviewed procedure 13405-1, and toured the

plant areas where the breaker manipulations occurred.

Two

deficiencies were noted which contributed to the event.

First,

the operator, when restoring battery charger IDDICA to service,

failed to follow the procedural limitation of step 2.2.5 of

procedure 13405-1 which states that without the battery breaker

c?osed in, only one charger should be energized to supply the bus.

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The operator stated that even though he understood the correct

sequence and had performed the evolution numerous times he became

confused during this particular evolution and mistakenly closed

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the wrong breaker. He also failed to communicate with the control

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room prior to beginning the restoration process. The second

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contributing factor was the lack of a specific " Caution" in

procedure section 4.1.3, Place a 125 VDC Bus Battery Charger In

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Service. Although a " Limitation" was stated at the beginning of

the procedure, the inspector concluded that a " Caution"

appropriately placed in section 4.1.3 regarding the use of two

chargers without the battery breaker closed may have prevented

this event.

This event was significant because one channel of SSPS remained in

a tripped condition for 27 minutes during which time the margin to

a RPS and/or ESFAS was significantly reduced.

The licensee took

prompt corrective action in identifying the cause of the error and

restoring the SSPS channel to service and has initiated a human

factors evaluation to review procedure 13405-1. The details of

this event were discussed with shift personnel during subsequent

Operations shift turnover meetings. This event was caused by both

a failure to follow a procedure and the inadequacy of the same

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procedure. This violation will not be subject to enforc2 ment

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action because the licensee's efforts in identifying and

correcting the violation meet the criteria specified in Section

VII. B of the Enforcement Policy.

This non-cited violation is

identified as NCV 50-424/93-16-02, Failure to Follow Procedure and

Inadequate Procedure Results in Inadvertent Tripping of SSPS

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Channel IV.

g.

Recycle Hold-Up Tank Waste Water Processing

On July 2 the licensee notified the inspectors that they intanded

to use a temporary reverse osmosis system to process about 90,000

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gallons of mixed (radioactive and chemical) waste water stored in

the Recycle Holdup Tank in the auxiliary building. The reverse

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osmosis system is a portable skid mounted unit which will be

operated in the ARB. The licensee stated that the waste is

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composed of relatively high concentrations of nitrates and is

radiologically contaminated requiring processing prior to

discharge to the environment. The reverse osmosis system will

concentrate the mixed waste for later disposal. This system was

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selected instead of processing the waste water through the

normally used ion exchangers because nitrates readily exchange

with the resins currently in use in~the ARB and would cause

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premature exhaustion.

Large amounts of exhausted resin would

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create a larger volume of solid radioactive waste.

This system was of particular . interest to the inspectors because

it is similar to a previous issue, that was reviewed and closed,

on the use of temporary radwaste processing systems that do not

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meet RG 1.143_(see NRC Inspection Reports 50-424,425/90-19

Supplement I and 50-424,425/92-20). The inspectors reviewed the

safety evaluation, and the set-up of the reverse osmosis system in

the ARB while considering the concerns identified with the

previous system. The licensee's previous calculation package and

safety analysis bounds this clean-up activity. The licensee has

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also implemented controls to ensure the reverse osmosis skid is

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monitored at all times. The inspectors verified it was attended

while in operation. The inspectors concluded that the licensee

had adequately addressed the concerns associated with this

temporary system. The inspectors will continue to monitor the

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system while it is in operation.

One non-cited violation was identified.

3.

Surveillance Observation (61726)

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a.

General

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Surveillance tests were reviewed by the inspectors to verify

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procedural and performance adequacy. The completed tests reviewed

were examined for necessary test prerequisites, instructions,

acceptance criteria, technical content, data collection,

independent verification where required, handling of deficiencies

noted, and review of completed work. The tests witnessed, in

whole or in part, were inspected to determine that approved

procedures were available, equipment was calibrated, prerequisites

were met, tests were conducted according to procedure, test

results were acceptable and systems restoration was completed.

SURVEILLANCE NO.

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14705-1

Boron Injection Flow Path Verification

14980-2

Diesel Generatu 2A Operability Test

14986-301

Security Diesel Generator Operability Test

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SURVEILLANCE NO.

TITLE

14952-C

Fire Suppression System Annual Pump Test

14423-2

Source Range NIS ACOT

14980-1

D/G 1A Semi-Annual Operability Test

b.

Review of ECCS Venting Deficiencies

During the previous inspection period on June 23, the licensee

identified a large volume of gas vented from valve 2-1204-X4-451,

RWST Return Line Vent. This discovery was made during the weekly

venting performed in accordance with operations standing order

C-93-007, which was initiated to determine the cause of the gas

accumulation. Gas was vented from this point on two previous

occasions in April 1993 and October 1992, during monthly ECCS

venting _ required by TS (see NRC irs 50-424,425/93-07 and 92-23).

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Following the identification of_ the gas on June 23, the licensee

reviewed all activities that occurred since the last venting, as

documented in operations logs, that could have potentially caused

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the gas accumulation. On June 26, the licensee reperformed these

activities with venting both before and after to determine the

source of accumulation.

Following the draining of a safety

injection accumulator, a large volume of gas which was determined

by chemistry to be nitrogen, was vented from the 451 valve. The

licensee concluded that the pressure drop from accumulator

pressure of approximately 600 psi to 30 psi at the SI test header

caused nitrogen to come out of solution and collect in the RWST

common miniflow return line.

The inspector reviewed the results of a corporate engineering

evaluation of the effects of gas accumulation in the miniflow

line. This evaluation determined, based on the maximum volume of

nitrogen accumulation that there would be no inipact on the

performance of the ECCS subsystem during miniflow operation of the

CCPs and/or SIPS since any trapped nitrogen would be swept toward

the RWST. Based on review of the piping configuration the

licensee's evaluation concluded that there is no potential for

water hammer in the miniflow line.

The evaluation also considered the possibility of gas migrating

upstream to the CCPs or SIPS which was a greater concern for ECCS

operability. The licensee's review of drawings showed that the

CCP alternate miniflow line contains a closed relief valve and the

SIP miniflow lines each contain a check valve which would prevent

backflow. The evaluation also determined that gas would not be

able to migrate towards the SIPS assuming the check valves leak

based on the piping configuration.

The licensee is considering a change to operations procedures for

both units to require venting of the RWST return line whenever any

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of the SI accumulators are drained to minimize the amount of time

that any gas remains in the line.

The inspector considered the licensee's root cause determination

and evaluation of the ECCS venting deficiencies effective in

determining the cause of recurrent gas accumulation. The

inspector concluded based on this review that the nitrogen

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accumulation in the RWST return line does not impact the ECCS

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subsystems.

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c.

Inadequate Post Testing Verification of Containment Spray

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Actuation Circuitry

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On July 8, following a review of NRC Information Notice 93-38,

Inadequate Testing of Engineered Safety Features Actuation

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Systems, the licensee determined that the configuration for CS

ESFAS actuation circuitry was not verified following TS

surveillance testing. The CS actuation circuitry contains

normally closed relay contacts which are opened during

surveillance testing. These contacts are restored to the closed

position following the surveillances and were not verified closed

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during the restoration.

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The licensee developed a test to measure the electrical resistance

of the affected CS loops to determine that the contacts were

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closed. The inspector observed this testing on July 14, for each

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CS loop on both units and verified that all measured resistances

were within the required limits specified in MW0s 19302540 and

29302445. The licensee will revise TS surveillance procedures to

incorporate this resistance check following CS surveillance

testing'to verify continuity of the actuation circuitry.

Based on this review the inspector concluded that the licensee

responded appropriately to IN 93-38 and is taking adequate

corrective action to ensure the configuration of CS actuation

circuitry following.

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No violations or deviations were identified.

4.

Maintenance Observation (62703)

a.

General

The inspectors observed maintenance activities, interviewed

personnel, and reviewed records to verify that work was conducted

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in accordance with approved procedures, TSs, and applicable

industry codes and standards. The inspectors also verified that

redundant components were operable, administrative controls were

followed, clearances were adequate, personnel were qualified,

correct replacement parts were used, radiological controls were

proper, fire protection was adequate, adequate post-maintenance

testing was performeo, and independent verification requirements

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were implemented. The inspectors independently verified that

selected equipment was properly returned to service.

Outstanding work requests were reviewed to_ ensure that the

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licensee gave priority to safety-related maintenance activities.

The inspectors witnessed or. revieved the following maintenance

activities:

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MWO NOS.

WORK DESCRIPTION

29302270

Tighten Bonnet Capstrews on MFIV 2HV-5230

29302278

Disassemble and Inspect Failed 4-Way Valve From

MFIV 2HV-5228

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C9300061

- Adjust Governor on Diesel Fire Pump #1

29302293

Investigate Cause of Invalid Count Rate on

Source Range N32

.29202339

Repair Control Building Safety Feature

Electrical Fan Inboard Bearing Pedestal Support

19302614

Replace Cell #26 on Train D Battery

19302540,

Take Resistance Readings for Loops IP-

29302445

934,935,936 and 937 (Unit 1) and Loops 2P-

934,935,936,and 937 (Unit 2)

29302223

CPS Meter Not Indicating on N32

19302644

NSCW Pump #3. Discharge Valve Failed to Shut When

Pump Stopped

b.

Non-Class IE 4160/480 Volt Load Center Transformer Failures

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On' July 7 and again on July 20 the licensee experienced failures

of non-1E 4160/480 volt transformers. The two failures occurred

on transformers located in the maintenance building (transformers

ANB-09X and ANB-10X} and were similar to past failures of these

type GE transformers. These failures were the twelfth and

thirteenth failures since the first failure occurred in April,

1988. These two transformers were shared by both units, and were

similar in age to the Unit I transformers that failed. The

history of 4160/480 volt non-lE transformer failures at Vogtle has

been documented in several NRC inspection reports and was most

recently documented by the EDSFI team inspection in NRC IR 50-

424,425/93-11, dated July 23, 1993. The inspectors will continue

to monitor any further corrective action by the licensee.

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c.

Moisture Controller Calibration Frequencies On Safety Related

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Ventilation Systems

As a followup to a weakness identified with the PM calibration

intervals established for pressure switches in the EHC system and

MFPT thrust bearing wear detectors (see NRC Inspection Report 50-

424,425/93-13) the inspectors reviewed other instrument

calibration intervals. A review of moisture controllers on the

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safety related piping penetration and CREFS HVAC systems found

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that the calibration frequency of these controllers was 600

months. These controllers assist in the function of the HVAC

system by modulating electric heaters to maintain the relative

humidity of the air passing through the system filters. Two

controllers on Unit I had not been calibrated since January, 1987.

The inspectors found that these controllers have no TS or FSAR

required or vendor recommended calibration interval. The

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inspectors were concerned, however, that with a 600 month

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calibration interval these instruments may not receive any

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calibrations after their initial set up.

After reviewing this issue with the licensee, the inspectors found

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that the licensee had recently recognized that the 600 month

calibration interval on these controllers appeared excessive and

was in the process of revising the interval to 60 months. The

inspectors also learned that the PM program is periodically

reviewed and FM intervals are frequently revised based on work

history, system reliability, and system engineer input. The

inspectors were satisfied that the licensee's present PM program

was adequate to recognize and act upon issues as identified in

this case. The inspector also concluded that there were no

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immediate system operability concerns since TS required

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surveillance tests are performed which test most of the moisture

controller loop.

No violations or deviations were identified.

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5.

Fire Protection Program (64704)

a.

Diesel Driven Fire Pump No.1 Fails Surveillance

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On July 7, diesel driven fire pump No.1 failed to meet the

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acceptance cr.teria of procedure 14952-C, Fire Suppression System

- Annual System Pump Test, when it did not achieve the required

calculated net pump pressure (discharge pressure minus suction

pressure) of at least 123 psi. The actual recorded net pressure

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was 117 psi which was subsequently confirmed using temporary M&TE

equipment.

The inspector observed vendor recommended governor adjustments as

they were made by licensee mair,tenance personnel and observed the

maintenance run of the diesel fire pump following those

adjustments. The inspector was satisfied that appropriate

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procedures were followed and that the diesel fire pump

subsequently achieved the required acceptance criteria.

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b.

Improper Storage of Flammable / Combustible Liquids

On July 15, during a routine walkdown of the Unit 2 Auxiliary

Building, the inspector opened a flammable storage cabinet in room

144 to inspect the contents of the cabinet. The cabinet contained

numerous flammable / combustible items. The inspector did not take

a complete inventory of the cabinet but did note the following

items: 1) five 5-gallon cans of diesel fuel, each full of diesel;

2) two 1-gallon cans of isopropanol; 3) one gallon of ethyl

alcohol; 4) one aerosol can of magnaflux cleaner / remover; 5) one

aerosol can of enamel paint; 6) approximately 20 plastic l-gallon

containers of various lubricating oils,10 of which were

completely full; 7) a 1-gallon container of isopropyl alcohol

labeled as " Internally Contaminated" and 8) various other

lubricants and unidentifiable substances.

The inspector was concerned that a potential fire hazard existed

because the cabinet was unorganized and in crowded condition.

Some of the containers were turned on their side and were resting

atop other upright containers apparently because the cabinet was

too crowded to place them in an upright position. The inspector

searched the area for a transient combustibles permit but could

not find one which evaluated the contents of the cabinet. The

inspector informed the SS of the condition of the cabinet and

questioned the lack of a posted permit.

Afterwards, the inspector reviewed procedure 92015-C, Use, Control

and Storage of Flammable / Combustible Materials, and discussed it

with the engineering supervisor responsible for the fire

protection program. The procedure states that

flammable / combustible liquids with a permit may be temporarily

placed in flammable storage cabinets in safety related structures

provided the liquids are used on a periodic basis.

This

particular cabinet did not contain a permit, and based on the

crowded condition of the cabinet, it was apparent that none of the

liquid been used recently enough to be reasonably considered

periodic usage. Step 4.3.3.16 of the procedure states that

aerosols shall not be stored with other flammable / combustible

materials in flammable storage cabinets. As discussed earlier,

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two aerosol can were found in the cabinet.

Table 8 of procedure

92015-C lists the amount of combustible materials allowed within

an area without a permit being required. The quantity of

materials stored in the cabinet far exceeded the allowable amount

stated in Table 8.

Step 4.2.8 states that materials not

specifically listed in Table 8 require a permit before transport

or use. The diesel fuel stored in the cabinet is not listed in

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Table 8 and should have had a permit.

Step 4.3.4.3 requires that

each flammable or combustible container shall be conspicuously

labeled per procedure 00262-C, Control of Chemicals / Fluids, to

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indicate the contents of the container. Contrary to that

requirement, the cabinet contained a 1 gallon can of isopropyl

alcohol with the contents of the can written in pencil on the side

of the can.

Finally, step 4.3.3.12 of the procedure states that

transient flammable / combustible liquids left unattended in safety

related areas without a permit are considered inappropriately

stored.

In addition to the cabinet described above, an adjacent locked

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cabinet within the same room contained a 55-gallon drum used to

temporarily store used lube oil.

Step 4.3.3.3 ::f procedure 92015-

C states that drum storage of Class IB liquids, which includes

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lube oil, is allowed only in non-safety related plant buildings.

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The licensee took prompt corrective action by cleaning out both

the cabinets and leaving only those items which will be used on a

periodic basis. A Transient Combustible Permit listing the

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contents of the cabinet was affixed to the front of the cabinet.

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This inappropriate storage of flammable / combustible liquids within

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a safety related area is a violation of procedure 92015-C and is

identified as VIO 50-424,425/93-16-03, Failure to Follow Procedure

Involving Indoor Storage of Flammable / Combustible Liquids.

One violation was identified.

6.

Follow-up (90712) (92700) (92701) (92702)

The Licensee Event Reports and follow-up items listed below were

reviewed to determine if the information provided met NRC requirements.

The determination included:

adequacy of description, verification of TS

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compliance and regulatory requirements, corrective action taken,

existence of potential generic problems, reporting requirements

satisfied, and relative safety significance of each event.

a.

(Closed) LER 50-424/92-010, Technical Specification Surveillance

Not Performed When Diesel Generator Inoperable.

The cause of DG 1A start failures was a vendor fabrication error

in an air distributor housing sleeve which prevented proper

venting of the pilot air from an air start valve. This resulted

in continuous starting air admission to a cylinder, impeding the

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starting roll and subsequent start. The details of these DG start

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failures and the immediate corrective actions taken by the

licensee were documented in NRC IR 50-424,425/92-30. This

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inspection report documents that the inspector personaliy observed

or verified the replacement of the right bank air distributor and

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the replacement of several leaking air start valves.

Report 92-30

also documents that the licensee tested the remaining DGs and no

similar discrepancies were found. Additionally, Shift

Superintendents were advised by Standing Order C-92-08 to alert

upper management whenever unexpected events occur during DG runs

or surveillances.

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Because the licensee identified that there were four leaking air

start valves on DG 1A (each valve was subsequently replaced), a

request was made of the DG vendor, Cooper Energy Services, to

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evaluate the maximum acceptable leakage of these air start valves.

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The evaluation results were issued in Cooper Engineering Report

  1. SA-01-1993, dated May 13, 1993. The vendor conducted both an

analytical investigation and an actual field test on a DG similar

to those at Vogtle. The results of those tests demonstrated that

even when accounting for the accumulation of all possible worst

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case conditions, it is unlikely that starting air valve leakage

could prevent an engine from starting. The inspector reviewed the

vendor evaluation and test methodology and ad no concerns with

the conclusions of that evaluation.

Based upon the inspector's review of the licensee's corrective

actions and the documentation of the DG 1A failure event as

described in IR 92-30, this LER is considered closed.

b.

(Closed) LER 50-425/92-012, Quarterly Valve Stroke Time Testing

Performed Late - Missed TS Surveillance.

The cause of this event was a procedure inadequacy. Procedure

00404-C, Surveillance Test Program, was revised on August 31,

1992, to require the surveillance task sheet to be dated when the

)

first independent task for any surveillance is completed and then

signed-off when all tasks on that task sheet are completed.

The

date for completion of the first independent task will key the

next due date for proper scheduling of the surveillance.

This event was documented in NRC IR 50-424,425/92-18 and

identified as a NCV. Furthermore, the inspector verified that

procedure 00404-C has been appropriately revised to preclude

recurrence of this event. This LER is considered closed.

c.

(Closed) LER 50-425/92-13, Control Room Controls Area Inadequately

Attended - Violation of Administrative Controls

The cause of the event was personnel error. The B0P operator

forgot that he had relieved the operator at the controls, and left

the Unit 2 "at the controls area." This event was documented in

NRC 1R 50-424,425/93-13 as two violations.

The inspector verified by reviewing commitment tracking system

printouts, a shift briefing book event summary, and an August 26,

1993 memo from the operations unit superintendent to the Manager,

Operations that the BOP operator vas counseled, shift briefings

were held for control room personnel, and the event was discussed

individually with each licensed operator. The briefings and

discussions emphasized the safety significance of the event;

procedural requirements concerning the "at the controls"

responsibility; how the responsibility is turned over; and log

keeping requirements for this turnover.

Based on this review, this item is closed.

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d.

(Closed) VIO 50-424,425/92-18-01, Failure To follow Procedure; and

LER 50-425/92-08, Improper Calibration of Instrument Loop Results

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in Condition Prohibited By Technical Specifications

The licensee responded to this violation in correspondence dated

October 14, 1992. This violation involved three examples of a

failure to follow procedure.

One example involved a failure to

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ensure a radiation monitor was returned to service. The licensee

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promptly counseled the USS on procedural compliance and placed a

synopsis of this event in the required reading for licensed

operators. The licensee also conducted a review of procedures

requiring personnel to " block" radiation monitor actuations. The

licensee revised procedures for the fuel handling building

effluent monitors and for the control room air intake gas monitors

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to include a sign-off step in the " Restore To Service" section for

Operations to place the "Bloct" switch in the desired position and

independently verify. The inspector reviewed the current

revisions of these procedures to confirm the licensee's corrective

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actions.

The second example involved a valve misalignment and overflow of

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waste water from an oily waste separator. The licensee counseled

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the individual, and discussed this event and the importance of

self-verification at shift briefings. Training was also given to

licensed and non-licensed operators during requalification

training on operation of the oily waste separator.

The third example in this violation involved an incorrect I&C

surveillance procedure and a failure by the I&C technician to

follow the procedure which would have led to a detection of the

procedural error. The technicians responsible for the error were

counseled and a meeting was held with other I&C personnel to

discuss the importance of performing accurate calibrations. The

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procedures which had incorrect data sheets were corrected. Other

procedures were reviewed for errors and none were identified.

Based on this review of the licensee's corrective actions the

violation and the LER covering the third example of the violation

are closed.

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No violations or deviations were identified.

7.

Exit Meeting

The inspection scope and findings were summarized on August 2, 1993,

with those persons indicated in paragraph 1.

The inspector described

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the areas inspected and discussed in detail the inspection findings

listed below. No dissenting comments were received from the licensee.

The licensee did not identify as proprietary any of the material

provided to or reviewed by the inspectors during the inspection.

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Item No.

Description and Reference

URI 50-424/93-16-01

Review Causes of Pressurizer low Pressure

Reactor Trip (paragraph 2e)

NCV 50-424/93-16-02

Failure to Follow Procedure and Inadequate

Procedure Result in Inadvertent Tripping

of SSPS Channel IV (paragraph 2f)

VIO 50-424,425/93-16-03

Failure to Follow Procedure Involving

Indoor Storage of Flammable / Combustible

Liquids (paragraph Sb)

8.

Abbreviations

ACOT

- Analog Channel Operational Test

AFW

- Auxiliary Feedwater System

ARB

- Alternate Radioactive Waste Building

B0P

- Balance of Plant Operator

CCP

- Centrifugal Charging Pump

CFR

- Code of Federal Regulations

cps

- counts per second

CREFS

- Control Room Emergency Filtrations System

CS

- Containment Spray System

CVI

- Containment Ventilation Isolation

DC

- Deficiency Card

DC

- Direct Current

DG

- Diesel Generator

DRPI

- Digital Rod Position Indication System

ECCS

- Emergency Core Cooling System

EDSFI

- Electrical Distribution System Functional Inspection

EHC

- Electro-Hydraulic Control System

ESFAS

- Engineered Safety Feature Actuation System

FSAR

- Final Safety Analysis Report

GL

- Generic Letter

3

HP

- Health Physics

HVAC

- Heating, Ventilation, and Air Conditioning

I&C

- Instruments and Controls

IR

- Inspection Report

ISEG

- Independent Safety Engineering Group

LCO

- Limiting Condition for Operation

LER

- Licensee Event Report

M&TE

- Measuring and Test Equipment

MFIV

- Main Feedwater Isolation Valve

MFP

- Main Feed Pump

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MFPT

- Main Feedwater Pump Turbine

MFRV

- Main Feedwater Regulating Valve

MWO

- Maintenance Work Order

NCV

- Non-Cited Violation

NI

- Nuclear Instrumentation

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NIS

- Nuclear Instrumentation System

NPF

- Nuclear Power Facility

NRC

- Nuclear Regulatory Commission

NSCW

- Nuclear Service Cooling Water System

PA

- Protected Area

PM

- Preventive Maintenance

psi

- pounds per square inch

QPTR

- Quadrant Power Tilt Ratio

RCS

- Reactor Coolant System

RG

- Regulatory Guide

RPS

- Reactor Protection Syatem

RWST

- Refueling Water Storage Tank

SAER

- Safety Audit And Engineering Review

SI

- Safety Injection

SIP

- Safety Injection Pump

SG

- Steam Generator

SS

- Shift Superintendent

SSPS

- Solid State Protection System

TS

- Technical Specifications

URI

- Unresolved Item

USS

- Unit Shift Supervisor

VAC

- Volts Alternating Current

VDC

- Volts Direct Current

VIO

- Violation