IR 05000424/1988055

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Insp Repts 50-424/88-55 & 50-425/88-71 on 881212-16 & 890103-06.No Violations or Deviations Noted.Major Areas Inspected:Liquid & Gaseous Radwaste Treatment Sys & Effluent Monitoring Sampling Sys & Environ Radiological Monitoring
ML20235K644
Person / Time
Site: Vogtle  Southern Nuclear icon.png
Issue date: 02/02/1989
From: Kahle J, Stoddart P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20235K628 List:
References
50-424-88-55, 50-425-88-71, NUDOCS 8902270192
Download: ML20235K644 (12)


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UNITED STATES

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NUCLEAR REGULATORY COMMISSION.

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ATI.ANTA. GEORGIA 30323 LReportNos.:

50-424/88-55 and 50-425/88-71

o Licensee:. Georgia Power Company.

P. 0. Box 1295

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LBirmingham, AL 35201 Docket Nos.1 50-424 and 50-425 License Nos.:.NPF-68 and CPPR-109

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Facility'Name:

Vogtle 1 and 2 23'

. Inspection Cond ct d:.D mber 12 - 16, 1988 and January 3 - 6, 1989

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Inspector:

P. G. Stoddart Date Signed Accompanying e onnel:

J. B. Kahle, (January 3 - 6, 1989)

Approved.b :Vf/

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. Kahle, Chief.

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Date' Signed-R iological Effluents and Chemistry Section mergency Preparedness and Radiological Protection

' Branch Division of Radiation Safety and Safeguards SUMMARY

' Scope: This routine, announced inspection was conducted in the areas of liquid and gaseous radwaste treatment systems, liquid and gaseous effluent monitoring and sampling systems, plant water chemistry and plant equipment affecting water chemistry, and environmental ' radiological monitoring.

Emphasis was on preoperational testing of Unit 2 systems in the areas noted above.

Results: All preoperational tests of systems in the inspector's assigned review areas and required for Unit 2 fuel load had been completed. While most of the systems not needed for Unit 2 fuel load had been tested, not all of the preoperational tests of systems in any one review area had been completed.

Three HEPA filter and charcoal adsorber trains in the Unit 2 portion of the Auxiliary Building HVAC system had not been tested (Paragraph 4).

The waste gas processing system tests had been delayed by ) overheating of a recombiner heater, requiring heater replacement (Paragraph 5.

Only 13 out of 22 process and-effluent radiological monitors (PERMSS) assigned for review had been tested

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and only 6 out of 22 had been calibrated (Paragraph 6). Tests of floor drains in the Unit 2 -containment building and the Unit 2 portion of the Auxiliary Building had not been completed (Paragraph 3).

Plant water chemistry and plant systems affecting plant water chemistry were common-to both Units 1 and 2 and had beta extensively reviewed during Unit i startup and operation.

Preoperational aspects of the water chemistry program

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appeared to have been satisfactorily addressed (Paragraph 7).

The inspector considered the water chemistry program to be a licensee strength.

The inspector's review of the plant liquid radwaste system and of its management and operation indicated this area to be another licensee strength.

A radiological environmental monitoring program was initiated prior to startup of Unit 1 and was fully applicable to Unit 2 (Paragraph 8).

No violations or deviations were identified.

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'4 ll REPORT DETAILS 1.

Persons Contacted Licensee Employees

  • R. Bellamy, Plant Manager M. Biron, PERMS System Supervisor P. Burwinkel, HVAC Supervisor
  • C. Eckert, Manager,. Health Physics and Chemistry

-*G. Frederick, QA Site Manager, Operations

  • W. Gabbard, Senior Regulatory Specialist
  • C. Garrett, Operations Engineering D. Hallman, Chemistry Supervisor R. Legrande, Operations Supervisor
  • R. Pinson, Vice President, Construction, Georgia Power
  • J. Swartzwelder, Manager, NSAC Other licensee employees contacted during. this inspection included engineers, operators,. technicians, and administrative personnel.

Other Organizations R. Cislo

. PERMS Preoperational Testing Supervisor (Bartlett Corp)

J. Guimbellot, HVAC Preoperational Testing Supervisor (Bechtel)

I. Jamieson, Liquid and Gaseous Radwaste System'Preoperational Testing Supervisor (Bechtel)

Nuclear Regulatory Commission

  • J. Rogge, Senior Resident Inspector
  • Attended exit interview 2.

Licensee Action on Previous Enforcement Matters This subject was not addressed in the inspection.

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Liquid Radwaste Processing System (84523)

The inspector selectively reviewed 28 procedures either wholly or partially concerned with liquid radwaste processing for Unit 2.

All procedures appeared to be sufficiently detailed to facilitate radwaste operations and had been reviewed and approved by appropriate licensee staff in accordance with the provisions of the Technical Specifications.

The inspector and licensee personnel discussed licensee operating experience of the liquid radwaste system, which was to be shared between Units 1 and 2.

The radwaste system appeared to have the capability of

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1 handling the anticipated combined inputs from both units and to meet the system design objectives without exceeding the criteria of 10 CFR 50, Appendix 1.

The radwaste processing system had been in operation since shortly after startup of Unit 1 in 1987, and had been operated satis-factorily since that time.

As discussed in Paragraph 8 of Inspection Report Nos. 50-424/88-54 and 50-425/88-70 (November 14 - 18, 1988), the i

licensee had initiated improvements in pre-filtration for the liquid radwaste processing system which appeared to have the potential to improve both the decontamination efficiency and volumetric throughput of the system.

The inspector considered the management and operating staff of the liquid radwaste system to be a licensee strength.

As of the end date of this inspection, the Unit 2 connection to the shared liquid radwaste processing system had not been completed.

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drains in Unit 2 had not been preoperationally tested; these were in the

Unit 2 containment building and in the Unit 2 side of the Auxiliary Building.

None of the preoperational tests above were required to be completed prior to the fuel load date; however, the anticipated date for completion of the tests was the week of January 16, 1989.

The preoperational testing supervisor indicated that the equipment appeared to be satisfactory but that scheduling of test personnel had been the principal cause of delay in completing the required tests.

No violations or deviations were identified.

4.

High Efficiency Particulate Air (HEPA) Filter and Charcoal Adsorber Ventilation Treatment Systems (84524)

Preoperational testing of the Unit 2 HEPA filter and charcoal adsorber ventilation treatment systems, with the exception of the three trains servicing the Unit 2 portion of the Auxiliary Building, had been completed as of the end date of this inspection.

A licensee representative stated that it was anticipated that the preoperational tests of the remaining three trains would be completed during the week of January 16, 1989.

No violations or deviations were identified.

5.

Waste Gas Processing System (84524)

Preoperational testing of the waste gas processing system had not been completed as of the end date of this inspection.

A licensee representative indicated that four out of eight sections of the preoperational tests had been completed.

During the week of December 26, 1988, a recombiner preheater had been damaged by overheating during a

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test.

Replacement of the heater delayed test completion and required repeating of a portion of a prior test.

Full completion of the waste gas process system tests was anticipated to be accomplished during the week of January 24, 1989.

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No violations or deviations were identified.

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Process'and Effluent Radiological Monitoring and Sampling System (PERMSS)

(84523,84524)

Twenty-two. PERMSS monitors.or. samplers.were in the inspector's review area. Preoperational tests had been completed on 13 of the 22 monitors or samplers as of the end date of this inspection, leaving an additional nine tests;to be completed.. A licensee representative stated that the remaining tests were scheduled for completion prior to or during the week of January 19, 1989.

Calibration of the PERMSS monitors or samplers was being performed separately from the preoperational tests and it was required that each monitor be " turned over" to'the operating group by the preoperational test group before calibration could be performed.

As of the end date of this inspection, only six out of 22 calibrations had been performed.

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calibrations were scheduled for completion prior to February 9,1989.

l The. inspector's review of the 13 PERMSS monitor or sampler preoperational tests which had been completed showed that the tests appeared to have been conducted properly and that.the monitors or samplers were ready for operation, subject to calibration. The inspector's review of three of the six calibrations completed to date indicated that calibration had been performed in accordance with procedures and appeared to be satisfactory.

No violations or deviations were identified.

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7.

Plant Chemistry, Plant Water Chemistry, and Plant Systems Affecting Plant Water Chemistry (79501, 79502)

At Plant Vogtle, plant systems affecting plant water chemistry, procedures for the measurement and control of plant water chemistry, plant facilities for analyses of plant water chemistry, and the plant staff committed to plant water chemistry were common to both units and were shared by both units.

The procedures and criteria for plant water chemistry were essentially established and were in-place prior to the startup of Unit 1, with the

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exception of such changes as were made based on Steam Generator Owner; Group (SG0G) guidelines and on operational experience.

Plant chemistry was reviewed indepth in

Inspection Report

Nos. 50-424/88-46 and 50-425/88-61 (October 17 - 21, 1988), 50-424/87-29

(April 23 - 24,1987), 50-424/86-108 (October 27 - November 4,1986),

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50-424/86-92 (September 29 - October 3,

1986), 50-424/86-32 (April 15

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- 18, 1986), and in "NRC Review of Vogtle Readiness Review Module 9B,

Chemistry" (November 13,1986).

During the current inspection, the inspector reviewed portions of selected

plant chemistry laboratory procedures, discussed the plaat chemistry

program with plant chemistry staff representatives, and inspected the

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plant primary coolant and secondary 'mlant laboratories and the plant

water treatment (potable and makeup, % r systems) facilities,

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Based on the results of the current inspection and on the results of the

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inspections cited above, the inspector concluded that the licensee

appeared to have established an effective documented program for the

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control of water quality for the plant primary and secondary water

systems.

The plant had committed to the guidance set forth in the SG0G

guidelines and supported the Electric Power Research Institute (EPRI)

recommendations on plant water chemistry.

As of December 7,1988, the licensee's chemistry laboratory procedures

consisted of some 260 reviewed and approved procedures, approximately 120

of which pertained directly to the primary and secondary reactor water

systems.

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The licensee made extensive use of on-line instrumented monitoring of

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plant water chemistry, which enabled plant operators to maintain an

essentially instantaneous profile of plant chemistry conditions in the

primary and secondary water systems.

The on-line monitoring systems were

backed-up by periodic sampling and analy_.is of the principal points of the

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online monitored systems.

The sampling system also provided additional

sampling points for portions of the system which were not continuously

monitored.

A quality assurance program for chemistry of the primary and secondary

water systems was in place and functional.

Some 23 chemistry procedures

addressed quality control and calibration. Frequent use was made of

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" blind" samples and of control or reference standards.

Laboratory

analytical equipment, during periods of active use, was calibrated at

least daily against reference standards.

As of January 1989, the licensee had 42 analytical chemists assigned to

the primary and secondary water chemistry laboratories.

Of this number,

31 were Georgia Power Company employees and 11 were contractor employees.

Of those employed by Georgia Power Company,19 were considered to be

qualified under ANSI 3.1 criteria and 12 were in training to become

ANSI-qualified.

Of the 11 contractor employees, all were ANSI-qualified.

At the time of this inspection, the licensee had no INP0-qualified

analytical chemists on the staff.

However, the licensee's stated

objectives for the chemistry program were to minimize or eliminate

reliance on contractor chemists and to have all analytical chemists fully

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INPO-qualified.

The licensee had initiated an extensive training program

for all analytical chemists and projected that all experienced analytical

chemists currently on the plant staff would be INP0-qualified by

approximately April 1990.

At the time of this inspection, 20 licensee

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analytical chemists had completed the basic INP0 training program and 11

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were participating in the INP0 basic training program.

It was

acknowledged, however, that as a result of inevitable staff attrition, and

since it was difficult to recruit INP0-qualified analysts, there would be

periods of time when trainee analysts without full INP0-qualifications or

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INP0-qualified contractor analysts might be employed to meet operational

needs.

The inspector observed that housekeeping in the licensee's water chemistry-

laboratories was good, that radiation control areas had been established

in an appropriate manner, and that analytical chemists appeared to be

conducting their work in accordance with procedures and in a professional

manner.

.The licensee had an active program in-place at Unit 1 for the minimization

of in-leakage of air and' circulating cooling water into the condenser and

condenser hotwell.

This program was to be extended to Unit 2 upon-

startup.

The licensee's experience with'_ Unit 1 indicated good control of

the chemical quality of the secondary coolant water and of the primary

coolant water, as evidenced by. minimum fuel degradation and minimal

deterioration of steam generator tubes during the Unit 1 initial fuel

cycle.

The secondary coolant condensate cleanup system for. Unit I had been

successful in maintaining acceptable water purity in accordance with SG0G

guidelines during the initial fuel cycle.

Since tSe Unit 2 system and

operating procedures were essentially identical to those of Unit 1, the

licensee staff stated that they expected that a similar degree of water

chemistry performance would be attained for Unit 2.

Based on the above discussion and on results of previous inspections of

the chemistry and water chemistry programs at Plant Vogtle,-Units 1 and 2,

the inspector considered the plant chemistry and water chemistry programs-

to be licensee strengths and considered those programs to be adequate.

No violations or deviations were identified.

8.

Radiological Environmental Monitoring (80521)

The Vogtle, Unit 1

" Annual Radiological Environmental Surveillance

Report" for calendar year 1987 was issued April 29, 1988.

The Unit 1,

" Operating License Stage Environmental Report (0LSER)," covering the

periods 1981 through 1984, was issued May 23, 1988.

The 1987

environmental report covered the requirements of Unit 1 Technical

Specification Section 3/4.1.2, while the preoperational environmental

monitoring phase, which was equally applicable to Vogtle Unit 2 was

provided in Section 6.15 of the OLSER.

The transition between the OLSER

and the 1987 environmental report occurred March 9,1987, concurrent with

the initial criticality of Unit 1.

The inspector reviewed the licensee's annual radiological environmental

monitoring report for 1987, and discussed the contents and the licensee's

environmental monitoring program with licensee representatives.

The

environmental monitoring program for Vogtle, Units 1 and 2, was operated

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by the corporate environmental center at Marietta, Georgia.

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The annual environmental report provided an adequate overview of the

licensee's environmental monitoring program.

Based on a review of the

contents of the environmental report, the reporting requirements of the

plant Technical Specifications and the guidance of NRC Regulatory

Guide 4.2,

Preparation of Environmental Reports for Nuclear Power

Stations, Revision 1, January 1975, appeared to have been met.

The preoperational phase of environmental monitoring was conducted under

contract by the Center for Applied Studies at the Vriiversity of Georgia,

at Athens, Georgia.

The Center for Applied Studies also provided most of

the laboratory analyses performed during the preoperational phase.

Laboratory analyses of all 1987, and subsequent environmental samples were

performed by Georgia Power Company's Central Laboratory, at Smyrna,

Georgia.

Thermoluminescent dosimetry (TLD) service, and reading of TLDs, was

provided by Teledyne Isotopes Midwest Laboratory at Northbrook, Illinois.

Direct radiation was measured at 38 monitoring locations, each with two or

more TLDs. TLDs were collected and analyzed quarterly.

Airborne radioiodine and radioactive particulate were sampled at seven

locations.

Five of these locations were close to the plant but in

different sectors. One was located at'the nearest community having the

highest annual ground level D/Q, and one was at a " control location" 10 to

20 miles distant, in the least prevalent wind direction from the plant.

Surface water samples were collected from the Savannah River from one

point upriver and from two sample points downriver from the plant water

ir';t and discharge area. Each sample was a one-month composite.

? king water samples were collected at the two nearest water treatment

l'".ts downsteam from the plant discharge area. Control samples were also

cc3iected.

Provision was made in procedures for collecting composite

samples for I-131 analysis on two-week cycles when projected dose,

calculated from release sample analysis data, was greater than 1 mrem / year

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for water consumption.

Otherwise, samples were to be collected as monthly

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composites.

Analyses were for gross beta activity and gamma isotopic

content for monthly composites and additionally for I-131 for two-week

composites. Tritium was analyzed using quarterly composites prepared from

monthly composite samples.

Sediments from the shoreline of the Savannah River were collected

semi-annually from upriver and downriver areas with existing or potential

recreational value.

The potential for radiation dose from ingestion of food products was

monitored by analysis of samples of milk, fish, and leafy vegetation. Two

milk samples were collected bi-weekly from milking animals at control

locations approximately ten or more miles from the plant in wind

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directions of low prevalence.

No milk animals were identified in the

plant vicinity.

At least one fish specimen of any commercial or recreationally important

species was collected semi-annually in the vicinity of the plant discharge

area on the Savannah River.

At least one control sample of any species

was collected in an area of the river not influenced by plant discharge.

At least one sample of any anadromous fish species was collected in the

vicinity of the plant discharge during the spring spawning season.

One sample of grass or leafy vegetation was collected monthly from each of

two onsite locations near the site boundary, but in different downwind

sectors.

One sample was to be collected monthly from a location (if any)

that had a calculated dose commitment (based on plant gaseous releases)

20% greater than that calculated for any site boundary location.

One

sample was also co17,ected monthly from a control location at least

15 miles distant.

Environmental radioactivity analyses of all 1987 samples were less than

the Lower Limits of Detection (LLD) with the following exceptions:

(1)

Fish.

Cs-137 activity ranging from 228 to 446 pCi/kg (wet) was

detected in two out of three samples from the plant discharge area

(LLD: 150 pCi/kg).

Controls were LLD to 178 pCi/kg of Cs-137 in

three out of three samples.

The Vogtle, Unit 1, Semi Annual Radioactive Effluent Release Reports

for January - June,1987 and July - December 1987, showed that the

plant did not release detectable quantities or concentrations of

Cs-137 during or prior to CY 1987.

It appeared likely that the

amounts of Cs-137 found in fish samples were attributable to

operation of the Savannah River Plant (SRP), rather than to operation

of Plant Vogtle.

(2) Tritium was detected in finished drinking water at the Port Westworth

water treatment plant located some 122 miles downstream of the site.

Concentrations of up to 3,920 pCi/l were found in eight out of eight

samples, with a LLD of 2,000 pCi/1.

As in the case of Cs-137, above,

the concentrations of tritium detected were not consistent with the

limited discharges of tritium-contaminated water from Plant Vogtle in

1987.

In 1987, approximately 270 curies of tritium was released from

Plant Vogtle in liquid effluents at concentrations, prior to dilution

in the cooling tower blowdown and in the Savannah River, of

approximately 7E-05 uCi/ml or 70,000 pCi/1; however, diffusion and

dilution would rapidly reduce tritium from Plant Vogtle effluents to

nondetectable levels.

A possible source of the detected tritium was

the SRP, which also discharges plant waste water into the Savannah

River in the same general area as Plant Vogtle.

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The following releases of radioactive materials were known to have occurred

from the SRP in CY-1987:

(1) Tritium on July 31, 1987 (quantity not specified).

(2) Cs-137 in the third or fourth week (s) of November.

Plant Vogtle air

samples from November 24 and December 1,1987, contained high gross

beta activity and Cs-137 in areas downwind of SRP.

TLD results from all stations were within anticipated ranges for naturally

occurring radioactivity.

The Georgia Power Company's Central Laboratory, located at Smyrna,

Georgia, participated in the Environmental Protection Agency's (EPA's)

cross-check program for environmental radioactivity measurements.

The

cross-check program was operated by the EPA's Environmental Monitoring and

Support Laboratory at Las Vegas, Nevada. A review of cross-check results

indicated acceptable analytical performance.

The irspector's review of the licensee's report of environmental

monitoring activities for the preoperational period of 1981 - 1984 and for

calendar year 1987, concluded that the program met the guidance of NRC

Regulatory Guide 4.1, " Measuring and Reporting of Radioactivity in the

Environs of Nuclear Power Plants" (Revision 0, January 18,1973).

Based on the above discussion, the inspector concluded that the licensee

had provided an adequate radiological environmental monitoring program.

No violations or deviations were identified.

9.

NUREG-0737 and Regulatory Guide 1.97 Items

NUREG-0737.

Item II.B.3 Post-Accident Sampling and Regulatory

Guide 1.97, Table 3, Type E, Accident Sampling Capability (Analysis

Capability Onsite).

The licensee provided a Post Accident Sampling System (PASS) with the

design capability to meet the guidelines and requirements cited above for

containment air and for primary coolant and containment sump liquid

samples.

Unit 2 PASS preoperational testing was discussed in a previous

inspection report (See Inspection Report Nos. 50-424/88-54 and

50-425/88-70, November 14 - 18, 1988, Paragraph 5.) The next test of the

PASS to be observed by NRC will be the scheduled evaluation to be

performed after Unit 2 has completed at least 30 days of sustained full

power operation (IFI 50-425/88-70-01).

NUREG-0737, Item II.F.I, Attachments 1 and 2 (noble

monitor and sampling and analysis of plant effluents) gas effluent

and Regulatory

Guide 1.97, Table 3, Type C, Effluent Radioactivity and Type E,

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The licensee provided monitoring systems meeting the guidelines and

requirements cited above as part of the plant's PERMSS. Monitored release

points included the main plant vent and the condenser air ejector vent.

Monitor designs for the identified release points appeared to have the

requisite range capacity to meet the criteria specified above. As of the

end date of this inspection, the subject monitors had been

preoperationally tested and calibrated.

The inspector reviewed the

preoperational tests of the monitors and concluded that the preoperational

tests appeared to be adequate and that the results were acceptable. The

inspector will review these monitors again at a later date during full

power operation.

No violations or deviations were identified.

10. Exit Interview

The inspection scope and findings were summarized on January 6,1989, with

those persons indicated in Paragraph 1, above.

The inspector described

the areas inspected and discussed in detail the inspection findings listed

below. No dissenting comments were received from the licensee.

The inspection was principally concerned with review of preoperational

testing of plant systems in the areas of liquid and gaseous radwaste

systems, liquid and gaseous effluent monitoring and sampling systems,

plant water chemistry, plant equipment affecting water chemistry, and

environmental radiological monitoring.

All preoperational testing of systems which were within the inspector's

scope of review and which were required for fuel load had been completed.

Most of the preoperational testing had been completed for other systems

not required for fuel loading but needed for criticality, ascent to power,

and full power.

However, one or more items in each review area remained

to be tested.

Three HEPA filter and charcoal absorber trains in the Unit 2 Auxiliary

Building HVAC system had not been tested (Paragraph 4).

The waste gas

processing system tests had been delayed by overheating of a recombiner

heater, requiring heater replacement (Paragraph 5).

Thirteen out of

22 process and effluent radiological monitors assigned for review had been

tested and six out of 22 had been calibrated (Paragraph 6).

Tests of

floor drains in the Unit 2 containment building and the Unit 2 portion of

the Auxiliary Building had not been completed (Paragraph 3).

Plant water chemistry and plant systems affecting plant water chemistry

were common to both Units 1 and 2 and had been extensively reviewed during

Unit 1 startup and operation; preoperational aspects of the water

chemistry program appeared to have been satisfactorily addressed

(Paragraph 7).

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An adequate. radiological. environmental monitoring program had been

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initiated prior to startup of Unit 1 and was fully applicable to Unit 2

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(Paragraph 8).

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