ML20210S060

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Insp Repts 50-424/97-07 & 50-425/97-07 on 970706-0802. Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support
ML20210S060
Person / Time
Site: Vogtle  Southern Nuclear icon.png
Issue date: 08/28/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20210S052 List:
References
50-424-97-07, 50-424-97-7, 50-425-97-07, 50-425-97-7, NUDOCS 9709040377
Download: ML20210S060 (26)


See also: IR 05000424/1997007

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U. S. NUCLEAR REGULATORY COMMISSION (NRC)

REGION 11

1

Docket Nos. 50-424 and 50-425

License Nos. NPF-68 and NPF-81

Report No:

50-424/97-07, 50-425/97-07

Licensee:

Southern Nuclear Operating Company, Inc.

Facility:

Vogtle Electric Generating Plant (VEGP) Units 1 and 2

Location:

7821 River Road

"

Waynesboro, GA 30830

Dates:

July 6 through August 2. 1997

Inspectors:

C. Ogle, Senior Resident Inspector

M. Widmann. Resident Inspector

K. O'Donohue. Resident Inspector (in training)

P. Harmon. License Examiner (05.1 - 05.3)

G. Kuzo. Health Protection Inspector (R1.1 - R8.1)

L. Stratton Safeguards Inspector (Section S2.1)

Approved by:

P. Skinner. Chief

Reactor Projects Branch 2

Division of Reactor Projects

Enclosure 2

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9709040377 970828

PDR

ADOCK 05000424

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PDR

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EXECUTIVE SUMMARY

Vogtle Electric Generating Plant Units 1 and 2

NRC Inspection Report 50-424/97-07, 50-425/97-07

This integrated inspection included aspects of licensee operations,

engineering, maintenance, and plant support.

The report covers a four-week

period of resident inspection.

It also includes the results of announced

inspections by a regional operator license examiner, health physics inspector,

and a safeguards inspector.

Operations

In general, the conduct of operations was professional and

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safety-conscious (Section 01.1).

A violation was identified for entry into the incorrect action condition

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during maintenance on the Unit 1 airlock (Section 02.2).

A poor practice was identified for attempting to start the auxiliary

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building supply fan number 1 with limited troubleshooting guidance

(Section 03.2).

The Requalification Program was adequate to ensure that licensed

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operators are trained to operate the facility safely (Section 05.1).

A program weakness was identified in the documentation of individual

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performance during simulator operating examinations (Section 05.2).

The Written Examination was considered discriminating and valid, and

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closely followed the examination plan (Section 05.3).

The Operating Examination was considered to be marginally adequate due

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to a low discrimination level in the dynamic simulator scenarios and in

Job Performance Measures (Section 05.3).

Plant Review Board (PRB) discussions were thorough and appropriately

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focused on safety (Section 07.1).

Maintenance

Maintenance and surveillance activities were generally completed

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thoroughly and professionally (Section M1.1 and M1.2).

Enaineerina

A non-cited violation was identified for the improper storage of a

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monorail beam immediately adjacent to centrifugal charging pump 2A

(Section E8.2).

Enclosure 2

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Plant Support

Radiation and contamination controls for radwaste processing and storage

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areas, and chemistry laboratory operations were appropriate and in

accordance with TS and 10 CFR Part 20 requirements (Paragraph R1.1).

Doses to workers resulting from contamination events were evaluated

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properly, and were within limits and recorded in accordance with

10 CFR Part 20 requirements (Section R1.2).

Licensee guidance and training incorporated recently revised

49 CFR Parts 100-179 and 10 CFR Part 71 regul6tions (Section R1.3).

A non-cited violation was identified for failure to meet 49 CFR 172.200

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shipping paper documentation details in accordance with 10 CFR 71.5

requirements (Section R1.3).

The primary and secondary coolant chemistry programs were managed and

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implemented effer.tively (Section R1.4).

Chemistry and HP self-assessments were performance based with no

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programmatic issues identified.

Identified issues were tracked by

licensee representatives and resolved appropriately. (Section R1.4).

In general, licensee OC primary and secondary OC activities verified

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accuracy of analytical measurements (Section R7.2).

One Inspector Followup Item was identified to review licensee actions to

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improve chemistry QC data trending and Anomaly Report issuance

(Section R7.2).

A non-cited violation was identified for failure to conduct Containment

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High Range Monitor calibrations in accordance with NUREG 0737 Table

II.F.1-3 as specified in Final Safety Analysis Report Section 7 (Section

R8.1).

A violation was identified for failure to take proper compensatory

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action in response to a degraded vital area barrier (Section S2.1).

Enclosure 2

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Reoort Details

Summary of Plant Status

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Unit 1

The unit began the inspection period at 100% power.

On July 7. power was

reduced to supprt condenser water box maintenance.

On July 8. power was

stabilized at 80% power. At the completion of maintenance activities, on

July-8. 100% reactor power was achieved.

The unit operated at full power for

the remainder of the inspection period.

Unit-2

The unit operated at full power throughout the inspection period.

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OoeratioDS

01

Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707. the inspectors conducted frequent

reviews of ongoing plant operations.

In general, the reviews indicated

that the conduct of operations was professional and safety conscious.

02

Operational Status of Facilities and Equipment

02.1 Safety-Related Walkdowns

a.

Insoection Scooe (7170]l

The inspectors walked down Diesel Generator ESF Heating Ventilation and

Air Conditioning (HVAC) systems for Units 1 and 2 as part of the routine

inspection effort to verify availability and overall condition of the

systems,

b'.

Observations and findinas

The ins)ectors verified proper system configurations both electrically

and mec1anically for the above ESF systems through accessible portions

in the plant, a walk down of main control room boards, and a review of

system drawings and plant lineup procedures.

The inspectors also

observed overall material condition of system components during the walk

downs.

Enclosure 2

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c.

Conclusions

The inspectors concluded that the systems reviewed were available to

aerform their design function and that systems were properly aligned.

io discrepancies were noted during these inspections.

02.2 Documentation Associated With Att ock Maintenance

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a.

Insoection Scooe (71707F

The ins)ectors reviewed the licensee's actions associated with repairs

to the Jnit 1 containment airlock on July 8.1997. The inspectors

reviewed Technical Saecification (TS) 3.6.2. Containment Airlocks:

precedure 24905-C. "3ersonnel Air Lock Leak Rate Test." Revision 12:

procedure 25236-C. " Personnel Airlock Maintenance," Revision 10:

3rocedure 10008-C. " Recording Limiting Conditions for Operations."

Revision 19: the Unit Shift Supervisor (USS) Log: and Limiting Condition

for Operation / Technical Recuirements (LC0/TR) Status Sheets.

The-

inspectors also interviewec selected operations personnel regarding this

issue.

b,

Observations and Findings

=On July 8. 1997. maintenance personnel had disassembled and reassembled-

the shaft seal assembly on the inner airlock bulkhead, associated with

the inner door operating mechanism.

Log entries indicated that the

repairs started at approximately 1:40 p.m.-and had finished for the day

at 3:25 o.m,

lhe ;nspectors were informed that the shaft seal assembly

leakage h3d not been determined following the reassembly. The licensee--

also indicated that additional repairs to this seal were planned _for

July 9.=1997.

Procedure 10008-C requires documentation of entry into an LC0 acticq

statement which will continue past a shift turnover.

After shift

turnover. the inspectors noted that the licensee had documented entry

into Action Condition "A" of TS LC0 3.6.2 as opposed to Action Condition

"C."

Action Condition "A" provides required actions in the event that

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an air lock door is rendered inoperable. Action Condition."C" applies

when an airlock is rendered inoperable for reasons other than Condition

A or 8 [ interlock mechanism).

The inspectors determined that since the

repairs were not made to the inner door, entry into Action Condition "C"

was more appropriate.

Following discussions with the Operations Manager and Shift

Superintendent, the licensee commenced repairs to the shaft seal that

evening.

During additional reviews, the inspectors determined that-the

airlock was restored to service on July 9.1997, prior to the expiration

of the Action Statement "C" time limits. At approximately 5:00 a.m. on

July 9.1997, the licensee also documented entry into Action Statement

"C" retroactive to the start of the initial shaft seal' maintenance.

Enclosure 2

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c.

Conclusion

The initial failure to document entry into nction Condition "C" was

contrary to the requirements of procedure 10008-C.

This is identified

as Violation (VIO) 50-424/97-07-01. Failure To Document Entry Into

Proper Action Condition Following Airlock Maintenance.

02.3 Containment Penetrat)ons Walkdown

a.

Inspection Scone (71707)

The inspectors walked down accessible portions of the following

containment penetrations to verify proper valve lineups:

Penetratign

Unit

Title

32

1.2

Boron Injection Line to Cold Leg

56

1.2

Residual Heat Removal (RHR) Pump Discharge

to Hot Leg

b.

Observations and Findinas

Proper valve lineups were observed for all penetrations,

c.

Conclusion

No discrepancies were identified.

03

Operations Procedures and Documentation

03.1 Walkdown of C harances (71707)

During the inspection period, the inspectors walked down the following

clearances:

19700542

Control room HVAC filter units - planned outage

19700554

Diesel oil storage tank pump #2

b.

Observations and Findinos

The inspectors did not identify any problems during these walkdowns.

Enclosure 2

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.03.2 Slave State protection System Slave Relav K614

a.

Insnection Scone (71707)

The inspectors reviewed a performance anomaly (slower than expected

operation) of the auxiliary building supply fan number 1 during the

3erformance of procedure 14655-2. " Solid State Protection System Slave

Relay K614 Train B Containment Ventilation Isolation." Revision 4 on

July 14. 1997. The inspectors reviewed maintenance work order 2971673:

electrical drawing 1-1551-A7-001-M01, elementary diagram auxiliary

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building outside air supply and normal HVAC system: deficiency card (DC)

2-97-195: the Unit 2 Control Room Reactor Operator and Shift Supervisor

log entries; and Institute of Electrical and Electronics Engineers.-Inc.

(IEEE) Std 383-1977 " Standard Criteria for Periodic Testing."

Operations and maintenance personnel were also interviewed.

b.

Observations and Findinas

On July 14. 1997. operations personnel performed arocedure 14655-2.

This procedure tests safety related slave relay

(614. to satisfy

portions of the surveillances in TS 3.3.2. 3.3.6 and 3.7.13.

Both

safety related and non-safety related components of the auxiliary

building normal ventilation and piping penetration ventilation area

filtration and exhaust systems are actuated during this surveillance.

During the performance of the test, an operator noted that auxiliary

building supply fan number 1. a non-safety related component, did not

immediately trip as expected.

Instead, the fan tripped approximately

three minutes after the relay actuation. The licensee stated that all

other components repositioned as expected.

During troubleshooting efforts, after reviewing the fan control circuit,

the control room operators attempted to restart the auxiliary building

supply fan number 1 with the K614 relay still energized.

The fan did

not start and an amber trouble-light was received at the control

handswitch for the fan.

The inspectors were informed that this activity

was accomplished to determine the state of the K614 relay contact in the

fan control circuit.

The initial surveillance was signed and logged as completed satisfactory

with comments about the fan stopping after approximately 3 minutes.

0)erations aersonnel then performed procedure 14655-2 a second time.

T11s time t1e auxiliary building supply fan number 1 tripped

immediately, as expected.

The surveillance was again signed off as

completed satisfactorily. The surveillance traveler, used to document

accomplishment of the surveillance for TS tracking, was also signed.

A

DC 2-97-195 was written addressing the failure of auxiliary building

supply fan number 1 to stop immediately during the first performance of

procedure 14655-2. in addition, a work order was written.

Enclosure 2

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The inspectors discussed with licensee management that the inspectors'

review identified that no procedure or other written instruction existed

directing the attempted restart of the auxiliary building supply fan

number 1.

Another point was that the failure of the fan to restart

during this troubleshooting effort provided limited information (i.e. ,

the existing state of the K614 contact in the fan control circuit: it

did not provide any information on why the 3-minute delay in fan

operation occurred).

Management was aggressivt in their efforts regarding this issue the

follcwing day. Additional extensive troubleshooting was performed but

failed to reveal the cause of the delayed operation. The licensee

indicated that they are currently enhancing their procedures regarding

troubleshooting,

c.

Conclusions

Attempting to start the auxiliary building supply fan number 1 with

limited troubleshooting guidance was identified as a poor practice.

05

Operator Training and Qualification (71001)

The inspectors assessed the licensee's Requalification Program using NRC

Inspection Procedure 71001, " Licensed Operator Requalification Program."

The inspectors visited the facility during the week of July 14-18, and

on July 29 and 30. 1997, to further evaluate this aspect of the program.

During the second visit to the facility, the inspectors determined that

operating tests were documented in an adequate manner, but identified a

program weakness in this area (Saction 05.2). A second Exit Interview

was conducted on July 30 with members of licensee management.

05.1 Review of Facility Operating History

a.

Insoection Scoce

The inspectors reviewed the licensee's operating history using Licensee

Event Re) orts (LERs), NRC' inspection reports, and the Plant Integration

Matrix (31M).

The inspectors also reviewed the licensee's feedback

mechanisms to determine whether deficiencies below the threshold for

generation of an LER or a Notice of Violation were adequately addressed

by the training program,

b.

Qb.servations and Findinos

The plant's operating history did not indicate that operator training

was a factor in identified performance issues. A concern involving

operator performance has been the continued mispositioning of valves and

incorrect equipment operation.

Root cause analysis )erformed by the

licensee concluded that training deficiencies or wea(nesses were not

involved in this area.

Enclosure 2

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The inspectors reviewed lesson plans derived from two LER-identified

performance issues.

The inspectors determined that minor deficiencies

received adequate notice and response by the training program.

Specifically. Management Observation forms, particularly from the

0)eration Department, provided direct feedback to the training program.

T1e inspectors: reviewed lesson plans developed and presented to the

operations personnel to address specific deficiencies identified by this

method.

Independent assessment of the Requalification Training Program was

provided-by the licensee's Quality Assurance Program. Audits conducted

in August 1996, and July 1997 concluded that the program was adecuately.

implemented.

Minor deficiencies identified in the 1996 audit hac been

addressed and corrected.

c.

Conclusions

The requalification program provided a mechanism for identifying areas

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of operator performance problems. The identified deficiencies were

addressed by appropriate changes in the training curriculum.

05.2 Simulator Evaluation

a.

Insoection Scong

The inspector reviewed the licensee's-evaluation for the dynamic

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simulator examinations on July 15 and July 29.

The crew consisted of

five licensed operators in the

Balance of Plant Operator (RO). position of Reactor Operator' (RO).

Extra or Common Operator (RO). Shift

Supervisor (SRO) and Unit Shift Supervisor (SRO).

The licensee

evaluators consisted of three training staff and one management

-representative.

b.

Observations and Findinas

Dynamic simulator evaluations were conducted in accordance with plant

procedure 60007-C. " Licensed Operator Requalification Examination

Guidelines." Revision 3.

This procedure re

(section 6.4), and Individual evaluations (quired Crew evaluations

section 6.5) during the-

operating test. The licensee recorded only the results of Crew

competencies unless performance deficiencies were noted.

Data sheet 7.

" Team Evaluation Summary." was the. record for performance and documented

grades as (Satisfactory / Unsatisfactory) for six separate crew

competencies matrixed by individuals.

Comments or observations

concerning.an individual were not recorded except for those operators

identified as having deficiencies.

The individual evaluations recorded

performance in eight competencies or categories.

Enclosure 2

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During the week of July 14. the inspectors observed two dynamic

simulator exercises administered to a single crew, and attended the

post-examination critique (debrief) presented to the crew by the

evaluators. The inspector observed several instances of communications

by the individual operators which did not meet the requirements of the

licensee's communications standard, procedure number 00004-C. " Plant

Communications." The standard required the use of repeat backs and

verification that the message was 3roperly received (three-part

communications).

The inspectors oaserved that each of the operators

exhit'ited several deficiencies in performing communications in

accordance with the established site standards.

However, since there

were no instances where communications caused a crew critical task to be

missed, the licensee evaluators marked all operators as " Satisfactory"

for the Communications competency. A satisfactory mark with no comments

implied that there were no deficiencies.

Therefore, there were no

requirements to document comments or observations in the evaluation

records.

The licensee's evaluators * critique did not develop the

specific instances of improper or incom)lete communications, but

generalized that communications should ae improved.

The simulator

examination documentation evaluations did not address improper

communications. The lack of individual evaluations failed to provide

direct. objective feedback to the concerned operators.

The evaluation

process took approximately 15 minutes followed by a debrief of the

crew, which lasted approximately 10 minutes.

The inspectors noted marked improvement in communications by crew

members during the scenarios performed on July 29.

The evaluation

process for the crew evaluated the morning of July 29 took.approximately

1-3/4 hours. The evaluators explained that this evaluation took longer

than the previous evaluations due to an observed deficiency which

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required further analysis and discussion by the evaluators.

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During the scenario a crew critical task, emergency borating in excess

of 30 gpm, was not performed satisfactorily.

The operator had allowed

the flow rate to drift slightly below 30 gpm to approximately 28 gpm for

several minutes.

The evaluators discussed whether the 30 g)m minimum

limit constituted a true limit below which the task should )e considered

as failed. After deciding to mark the operator competency

" Unsatisfactory" in the area of system response, the evaluators agreed

to evaluate the task further.

The inspectors found that the scenarios were not designed to ensure that

neither the Common R0 nor the Shift Suaervisor were sufficiently

challenged in all competency areas. T1ese individuals provided

oversight or supported the three individuals directly concerned with

shift duties and, as a result, there was little opportunity to evaluate

those individuals.

The licensee stated that these individuals are

rotated to one of the more actively involved positions on one of the two

scenarios, allowing ample opportunity for evaluation.

Enclosure 2

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The simulator scenarios were written to test crew competency.

There was

no systematic process to construct the scenarios to ensure that each of

the crew positions could be evaluated to demonstrate competency in each

evaluation category.

This could result in an individual receiving an

incomplete evaluation.

c.

Conclusions

The Requalification Program adequately evaluated licensed crews and

operators during the dynamic simulator portion of the operating tests.

However, the program only required individual evaluation comments and

observations to be recorded in instances where deficiencies were

associated with a crew critical task. This process discriminates

against recording (and tracking and trending) individual performance

deficiencies below the level which would cause an " Unsatisfactory"

competency rating.

The process of evaluating and documenting competencies was not effective

in identifying deficiencies below the threshold which causes a critical

crew task to be missed. When individual mistakes were identified,

developed, and presented at the criticues, documentation of those

deficiencies were not developed to aic in trending.

This precluded

identification of weaknesses or inadequacies until a critical failure

occurred.

The combination of crew-oriented simulator scenarios and

weaknesses in evaluation and documentation could result in an individual

not being thoroughly and objectively evaluated, and does-not provide the

feedback to properly implement the Systems Approach To Training (SAT).

A program weakness was identified in the documentation of individual

performance during simulator operating examinations.

Documentation-did

not include specifics of. minor-deficiencies, nor details that ensured

that all relevant competencies are evaluated for each individual.

05.3 Examination Develcoment

a.

Insoection Scope

The ins)ector reviewed the written examination administered to two R0s

and eig1t SR0s on June 12, 1997.

The examinations consisted of-25.

. questions, and administered with plant reference materials available.

-.The inspectors audited two dynamic simulator (DS) scenarios (2Z and 3Y),

administered to two R0s and two SR0s in one crew on July 15. 1997.

The

inspectors also witnessed DS 11 and DS 33 administered July 29.

On July 16. the inspector accompanied the licensee evaluator who

administered three simulator and four in-plant Job Performance Measures

(JPMs) to a single SRO.

The seven JPMs constituted a single " set."

Enclosure 2

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The inspector did not attend any sessions involving static simulator

evaluations.

b.

Observations and Findinas

The written examinations were satisfactory and tested on the appropriate

level of comprehension and analysis.

The examination items closely

followed the sample plan. There were no instances of " direct look-up"

identified.

All failed individuals were remediated.

The JPM set contained two JPMs which were not complex enough to

demonstrate an understanding of the operation being performed due to

their simplistic nature. JPM RQ-JP-23101-002-01. " Place Control Room

HVAC in Smoke Purae Mode." only required locating the appropriate

control room Janel, and aligning two switches identified in the

)rocedure.

J)M RQ-JP-60322-001-01. " Establish SFP Feed Path Following

_oss of CCW." only required the operator to locate and manipulate two

valves.

The remaining JPMs were appropriately discriminating, and

constituted a minimally adequate examination tool.

One individual

failed a JPM set.

The failed individual was remediated.

The simulator scenarios met the minimum standards for demonstrating

operator competency.

Scenario DS #13Y contained only two events that

effectively challenged the crew: " Charging Flow Control valve FV 121

Fails Closed", and a " Steam Generator Tube Rupture" complicated by a

loss of a single Auxiliary Feedwater (AFW) pump. The scenario's single

required instrument failure. " Turbine : Impulse Channel Failure." did not

initiate a transient requiring action by an operator.

In effect, the

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failure only disabled the Steam Dumfs arming circuit.

This only

required that the operator select tle Steam Dump Control to " Steam

Pressure-Mode" to allow the system to respond to any future load

reduction transients. Another scenario event. " Failure of the Safety

' Injection System to Automatically Actuate." was addressed by activating

a manual actuation switch. This problem involved fairly simple

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recognition and response. Another weakness in the developed scenario

involved the lack of a challenging malfunction after entering the E0P.

There was a malfunction. but the malfunction did not create a condition

which influenced the operators' choice of mitigation strategy.

An E0P

transition was not required.

In effect, the exercise did not provide an

opportunity to evaluate the crew's ability to determine which mitigation

strategy should be used, which E0P should be used, or to transition

between E0Ps.

Since the dynamic simulator evaluation was biased toward crew

evaluations, scenarios were not developed with a full consideration of

ensuring that the Shift Supervisor and Common RO receive challenges

which were adequate to fully evaluate them while in that position.

This

required careful consideration in rotating assignments and full

documentation of how those competencies are observed.

The inspectors

considered the dynamic simulator scenarios deve'oped as part of the

Enclosure 2

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operating examination to be minimally adequate.

No crew critical tasks

were failed,

Four R0, three shift SRO, and 2 Staff SR0 individual

failures were identified and remediated.

c.

Cta.clusions

The written portion of the Requalification examination was considered

discriminating and valid.

The JPH set observed by the inspector contained examples of JPMs that

were not sufficiently discriminating to ensure that individuals with

performance deficiencies could be identified.

The JPM portion of the

examination was considered minimally adequate, but did not contain a

high level of difficulty or discrimination.

The simulator scenarios were considered minimally adequate, but did not

contain a high level of difficulty or discrimination.

Each scenario was

not fully developed to adequately evaluate each crew member's

competency, but together they were adequate as long as rotation of

assignments between scenarios was carefully controlled.

07

Quality Assurance in Operations

07.1 Plant Review Board (PRB) Meetinas (40500)

The inspectors attended PRB meetings on July 8 and 11, 1997.

The

meeting on July 8 was a normally scheduled PRB and the majority of the

items discussed were routine in nature,

included in the July 8 PRB

meeting was a review of an NRC question regarding lowering the

pressurizer safety valve setooint and the resultant effect on the plant

analysis concerning bulk boiling.

The meeting of July 8 also discussed

the licensee's proposed response to inspection report violations 50-424,

425/97-05-01 and 50-424, 425/97-05-02, concerning the unexpected

behavior of the Unit 2 containment sump level transmitter and the

appropriate LCO entered by the USS.

The-PRB discussions were thorough and appropriately focused on safety.

In particular, ine inspectors noted that questions raised by the PRB

enhanced the quality of the reviews.

Enclosure 2

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II.

Maintenance

M1

Conduct of Maintenance

M1.1 Maintenance Work Order Observations

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a.

Insoection Scoce (62707)

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The. inspectors observed portions of maintenance activities involving the

following work orders:

196015B6

Heater contact cutoff switch verification of proper

installation on control room heating, ventilating and

air conditioning (HVAC) filter unit

19602419

Inspect / lube air filter air handling unit

11531N7001M01

19702189

Spent fuel pool skimmer pump replacement

29502715

Auxiliary feedwater heat trace troubleshoot

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29701262

Motor driven auxiliary feedwater (MDAFW) discharge to

steam generator number 2

29701673

Auxiliary building sup)ly fan

29701735

Replace handswitch on )oron thermal regenerative

system

29701802

Changeout power supply on 2RE12444: plant vent

radiation monitor

b,

Observations and Findinas

The observed maintenance activities were satisfactorily performed.

M1.2 Surveillance Observation

a.

Insnection Scone (61726)

The inspectors observed the performance or reviewed the following

surveillances and plant procedures:

14415-C

Fuel handling building post accident ventilation

actuation logic test

14546-2

Turbine driven auxiliary feedwater pump operability

test

14805-1

Residual heat removal inservice test (IST) and

response time test

14809-2

Engineered safety feature chill water pump IST

b.

Observations and Findinas

The observed surveillance activities were satisfactorily performed.

Enclosure 2

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III.

Enaineerina

E3

Engineering Procedures and Documentation (37551)

E3.1 h stina of Containment Soray (CS) Pumo Loaic

The inspectors reviewed the licensee's disposition of Deficiency Card

(DC) 1-97-311.

This DC was generated to address potential shortcomings

in the surveillance testing of the CS Jumps identified during the

licensee's review pursuant to Generic _etter (GL) 96-01. " Testing of

Safety-Related Logic Circuits." dated January 10, 1996.

The DC

documented several sequencer contacts in the CS pump control circuit

e

which were not tested by the licensee,

These contacts represented

supplemental starting times after the first sequencer starting time for

the pumps,

The inspectors reviewed documentation provided by the licensee which

documented that these contacts were not required and that there was no

'

impact in terms of the licensee's accident analysis.

No additional

followup is planned,

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E8

Miscellaneous Engineering Issues (37551)

'

E8.1

(Closed) Unresolved Item (URI) 50-424/95 27-02: Adequacy of Nuclear

Service Cooling Water (NSCW) Valve as Closed System Isolation Valve

Following additional review of this issue in response to Task Interface

Agreement (TIA) 96-05, this item is closed.

E8.2 (Closed) URI 50-425/97-06-01:

Monorail Beam Stored On 2A Centrifugal

.

Charging Pump (CCP)-Bedplate,

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a.

Insoection Scoce

This item documented inspectors' concerns associated with the July 3,

1997, identification of a portion of the overhead monorail beam placed

4

,

in close proximity to the CCP 2A motor.

The inspectors reviewed

procedure 00352-C " Control of In-Process Materials " Revision 6. the

resulting DC, and an engineering evaluation of the as found condition,

b. 10bservations and Findinos

The beam was documented as being returned to its storage location

shortly after the inspectors * observation.

Tha inspectors independently

confirmed that the beam was removed from the motor area during a later

tour of the auxiliary building. The licensee's review of the event

failed to conclusively determine how the beam came to be placed by the

motor.

Enclosure 2

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The engineering evaluation concluded that the CCP remained operable with

the beam in its as-found condition.

The inspectors reviewed the b sis

-for this-conclusion and found it to be adequate.

Procedure 00352-C required actions-to protect against damage to safety-

related equipment during seismic events.

The procedure requires an

engineering evaluation or restraint / separation of equipment stored

adjacent to safety-related equipment.

The licensee was unable to

provide documentation that the observed beam location was previously

. evaluated.

Likewise, the separation of the beam did not meet the

restraint / separation requirements of procedure 00352 C.

c.

Conclusion

Storage of the monorail beam in close proximity to CCP 2A was contrary

to the requirements of procedure 00352-C.

However, consistent with

Section IV of the NRC Enforcement Policy this was identified as Non-

Cited Violation (NCV) 50-425/97-07-02, Improper Storage of Monorail Beam

Adjacent to CCP 2A Motor. Based on this action, URI 50-425/97-06-01 is

closed,

E8.3 (Closed) URI 50-424. 425/97-06 02: Testing of Parallel Circuits For Main

Steam isolation Valves (MSIVs)

This issue documented a potential-deficiency in the testing of MSIV

circuits identified during a review conducted pursuant to GL 96-01.

Based on a review of the MSIV electrical circuit design, the ins

determined that each valve handswitch (1/2-3007-A and 1/2-30078)pectors

contains two redundant parallel control circuits that close four MSIVs

(a total of eight valves per unit).

However, a review of system design

requirements indicated no requirement to have redundant circuits for

closure of the MSIVs. Technical Specifications (TSs) required that the

MSIVs close within a specified time and do not consider the method by

which they close.

However, as a result of this issue the licensee plans

to revise procedure 14240-1, " Manual Trip Actuation Device Operability

Test (TAD 0T)." Revision 1 and procedure 14240-2, " Manual Steamline

'

Isolation," Revision 2.

Based on this review, the inspectors concluded that the licensee's

actions are appropriate, This item is closed.

E8.4 Unclanned/Unmonitored Release from Unit 1 Eauioment Buildina

On July 28. 1997, an unplanned /unmonitored release from the Unit 1

equiament building occurred.

The release was due to an opening in the

fan 3elt housing of the containment mini-purge exhaust system.

Due to

sampling being performed on the volume control tank, elevated levels of

Enclosure 2

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activity were present in the plant ventilation ductwork.

The mini-purge

system exhausts to the plant ventilation.

However, due to system

operation with positive pressure and a resultant back flow through the

plant ductwork, the activity was released at the mini-purge fan opening.

This-release was recognized by thz licensee as a result of an alarm on a

portable monitor located inside the equipment building. A release

permit was subsequently generated as a result of this event.

This issue is identified as inspection Followu) Item (IFI) 50-424/97-07-

03. Unplanned /Unmonitored Release from Unit 1 Equipment Building.

IV.

Plant Suppott

R1

Radiological Protection and Chemistry Controls

R1.1 Radioloqical Controls

a.

Insoection Scone (83750. 84750. 86750)

Radiological controls associated with radwaste processing and storage

areas, and primary chemistry laboratory facilities were reviewed and

evaluated by the inspectors.

The reviewed controls included area

)ostings, radioactive waste (radwaste) and material container labels.

ligh and locked-high radiation area controls and procedural guidance.

Established guidance and physical controls were compared against Final

Safety Analysis Report (FSAR) Section (S) 12 details and documented

recairements in applicable sections of Technical Specifications (TSs)

anc 10 CFR Part 20.

The inspectors made tours of the radiologically controlled areas (RCAs)

associated with radwaste processing and storage facilities.

Procedural

guidance for on-going activities and associated survey records also were

reviewed and discussed with responsible Health Physics (HP) staff. The

inspectors directly observed technician Jerformance and discussed

radiation and contamination controls witlin the primary chemistry

laboratory,

b.

Observations and Findinas

Physical controls associated with radwaste storage areas were in

accordance with TS requirements. Area postings were proper and in

accordance with TS or 10 CFR 20 Subpart J requirements.

Containers

holding radwaste contaminated materials and equipment were labeled in

accordance with 10 CFR 20.1904 requirements.

Pro)er contamination and

radiation control practices were observed for teclnicians conducting

analyses within the priwy chemistry laboratory.

Enclosure 2

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c.

Conclusions

Radiation and contamination controls for radwaste processing and storage

areas and primary chemistry laboratory operations were appropriate and

in accordance with TS and 10 CFR Part 20 requirements.

R1.2 Dose Assessments

a.

Insnection Scooe (83740)

Licensee assessments and assignment of whole body or extremity shallow

dose equivalent (SDE) associated with selected contamination events from

January 1. 1996 through July 25. 1997, were reviewed and discussed.

Applicable records of exposure assumptions. radionuclide gamma

spectroscopy data and com)leted euluations fw the five maximum SDEs

assigned to workers for t1e reviewed period were evaluated and discussed

with cognizant licensee representatives.

In addition, dose records for

individuals involved in the reviewed contamination events were evaluated

for completeness and accuracy.

Licensee actions, assigned SDEs and records were compared against

established procedural guid6nce and 10 CFR-Part 20 dose limits and

reporting requirements.

~

b.

Observations and Findinas

The SDE assessments were conducted in accordance with procedure 44019 C.

" Dose Assessment Font F 9tamination and Immersion in Noble Gas."

Revision 10. dated l'ay 44, 1997.

Licensee assumptions regarding

location of radioactivt contamination or particles. shielding. exposure

times and radioisotope mixtures were appropriate.

Assigned doses for

the five maximum calculated SDEs were with 10 CFR Part 20 limits and

ranged from 2451 to 24.098 millirem (mrem).

The maximum doses were

associated with outage work conducted during the fall of 1996.

The

inspectors verified that the individuals' assigned SDEs were included in-

the appropriate NRC Form 5 records.

c.

Conclusions

The SDEs to workers from contamination events were evaluated properly,

were within 10 CFR Part 20,1201 limits and were recorded in accordance

with 10 CFR 20.2106. requirements.

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Enclosure 2

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R1,3 Radioactive Waste and Material Transnortation Activities

a.

Insnection Stone (86750. T12515/133)

The inspectors evaluated and discussed the licensee's current guidance

for radioactive material and waste packaging and transportation

arogram

activities.

Selected procedures and records associated with paccaging

and shipping of radioactive material and waste to either vendor

processing facilities or directly to a licensed burial facility were

reviewed and evaluated against recently revised 10 CFR Part 20,

49 CFR Parts 100 179 and 10 CFR Part 71 regulations.

Copies of shipping

records for the following transportation activities were reviewed in

detail.

Radwaste Shipment (RWS) Number (No) 97 001. Reportable Quantity

.

(RO) Radioactive Material, Low Specific Activity (LSA). n.o.s 7

UN-2912, Fissile Excepted, containing dewatered Ion Exchange Resin

(Bead) from Plant Demineralizer System, shipped July 14, 1997.

Radwaste Volume Reduction Shipment (RWVS) No.97-007. Radioactive

.

Material. Low Specific Activity. n.o.s.

7. UN 2912, 14 Drums of

High Rad trash, paper cloth, metal and filter media in a Type A

Package, shipped February 7, 1997.

RWVS No.97-015. Radioactive Material. LSA, n.o.s 7: UN-2912. Non-

.

compacted trash: shipped June 13, 1997.

Radioactive material shipment 97-01 002. Radioactive material.

.

Surface contaminated object, n.o.s. 7: UN-2913: Reactor coolant

pump, shipped January 10. 1997.

Radioactive material shi) ment 97-06-004. Radioactive material.

.

SCO 2, n.o.s 7. UN2913:

RCP Box: shipped June 19, 1997

Radioactive material shi > ment 97-07-002. Radioactive material.

.

SCO 2 n.o.s 7 UN2913: _ong-handled tools: shipped July 8. 1997.

The inspectors noted that for five of the six shipments reviewed,

licensee documentation did not meet the detailed shipping paper

requirements as specified in 49 CFR 172.200,

Identified documentation

errors included an example of failure to consecutively number shi) ping

pages; inconsistencies in shipment volume and in listed isotopes Jetween

separate pages of a shipping document: incorrectly including "LSA-2" and

"SCO 2" as part of the proper shipping names contrary to 49 CFR 172.101,

and failing to document LSA-Il for one shipment.

The inspectors

verified that for all shipments with documentation errors. the proper

isotopes and their quantities, material volumes, and radiation and

contamination surveys were used in determining transportation

categories, shipping containers and waste classifications, as

applicable.

From review of procedures and discussion of training with

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Enclosure 2

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responsible licensee representatives, the inspectors determined the

recent revisions to 49 CFR Department of Transportation (DOT)

regulations were incorporated appropriately into the transportation

program activities and that the identified issues resulted from

personnel errors in updating licensee computerized database spreadsheet

programs.

The inspectors identified the failure to complete shipping

paper documentation in accordance with-49 CFR 172.200 as a violation of

10 CFR 71.5 requirements. However, the inspectors noted that these

failures constituted a violation of minor safety significance and

consistent with Section IV of the NRC Enforcement-Policy are being

identified as NCV 50 424.425/97 07 04. Failure To Meet 49 CFR 172.200

Shipping Paper Documentation Details in Accordance with 10 CFR 71.5

Requirements.

Licensee representatives reviewed additional shipments made since

January 1997 and found no significant document errors affecting

transportation or wast classification,

in addition, the licensee was

implementing use of an approved vendor computerized system to generate

radioactive material / waste ship)ing documents and burial manifest

records.

Initial training on t1e system was scheduled for August 7.

1997.

In addition, the licensee stated that the accuracy of shipment

records would be double verified for all shipments until the

computerized system is fully implemented.

c.

Conclusions

Licensee guidance and training incorporated recently revised

49 CFR Parts 100-179 and 10 CFR Part 71 regulations.

NCV 50 424.425/97-07-04 taas identified for failure to meet

49 CFR 172.200 shipping paper documentation details in accordance with

10 CFR 71.5 requirements.

R1.4 Primary and Secondary Coolant System Cold Chemistry

a.

Insnection Scone (84750)

Licensee activities for monitoring and managing primary and secondary

coolant cold chemistry parameters were reviewed and discussed.

The

inspectors toured primary and secondary chemistry laboratories,

secondary chemical addition room, and directly observed technicians

completing selected chemical analyses.

In addition, selected January 1.

1997 through July 25, 1997, primary and secondary cold chemistry data

trends were reviewed and discussed.

Parameters reviewed included Unit 1

(U1) and Unit 2 (U2) reactor coolant system (RCS) dissolved hydrogen.

lithium, dissolved oxygen, feedwater hydrazine. and steam generator

sodium and sulfate concentrations.

Licensee program activities and results were reviewed against applicable

TS. procedural requirements and industry standards.

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b.

Observations and Findinas

Housekeeping and cleanliness of the primary and secondary chemistry

laboratories and within the secondary chemical addition room were

adequate.

As required, secondary system on line analytical chemistry

instrumentation was verified to be operable.

Technicians in both the

primary and secondary chemistry laboratories were knowledgeable of

procedures and demonstrated proficiency in completing the selected

chemical analyses observed,

in general, the inspectors verified that primary and secondary coolant

analysis results were reviewed by technicians and management with

appropriate actions taken to maintain the chemical concentrations within

established limits.

Licensee representatives discussed chemistry

program initiatives and presented chemistry trend data demonstrating

improvements for steam generator sodium to chloride molar ratio control,

and reductions in potassium, sodium and iron transport,

c.

Conclusions

The primary and secondary coolant chemistry program was managed

appropriately and activities were implemented effectively.

R7

Quality Assurance in Radiation Protection and Chemistry Activities

R7,1 Audits and Self assessments

a,

Irdoection Stone (83750. 84750)

The inspectors reviewed and discussed results of health physics and

chemistry program assessments conducted since January 1, 1997.

The

inspectors evaluated the scope, thoroughness and status of corrective

actions for selected issues identified.

Health Physics (HP) and

Chemistry self-assessments. HP weekly area status checklists; chemistry

internal assessments, and performance monitoring reports were revieu d,

In particular, the inspectors reviewed and discussed the HP Department

February 3-7, 1997 Self-assessment and followup actions,

b,

Observations and rind _i_0_qi

The assessments consisted of interviews, record review and direct

observations by qualified personnel.

In particular, the inspectore

noted that the HP self-assessment team consisted of qualified site and

outside personnel, and involved review of separate HP program areas

including ALARA, contamination control, external radiation, personnel

dosimetry, Radiation Work Permit, Posting, labelling, solid radioactive

waste, and surveys and documentation.

The assessment was performance

based and the contents were appropriate sam)les of the program

attributes.

The inspectors verified that t1e findings were

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Enclosure 2_

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characterized appropriately % the report and were being tracked to

closure.

The inspectors noted that no programmatic issues were

identified within either the HP or chemistry self assessment activities,

c. -Conclusions

Chemistry and HP self assessments were performance based with no

programmatic issues identified.

Identified issues were tracked by

licensee representatives and resolved appropriately.

R7.2 Primary and Secondary Chemistry 00ality Control Activities

a.

Insoection Scone (84750)

The inspectors reviewed selected calibration and January 1. through

July 25. 1997, quality control (0C) data records associated with primary

and in-line secondary system chemistry measurements.

Program

implementation and adecuacy of results were compared against

specifications detailec in approved procedures and schedules,

b.

Observations and Findinas

in general, licensee activities to verify analytical instrument accuracy

were conducted in accordance with approved schedules and procedures

31001-C. " Chemistry Control Charts.

Revision 5. 34000-C. "0)eration and

Calibration of Process Monitors." Revision 8, and 31010-C. ")rocess

Analyzer Calibration Scheduling Program." Revision 12.

Completion of

acceptable calibrations of selected analytical instruments used for

oxygen, hydrazine and sodium analyses were verified.

To demonstrate in-

line instrument accuracy comparisons of in-line monitors with grab

sample bench-top analysis results were conducted at the required

frequencies or subsequent to instrument recalibration.

However, during

review of QC trend data records for the primary chemistry and laboratory

counting room, the inspectors noted that OC trending and anomaly reports

were inconsistently implemented by the technician staff.

For example,

in use boron analyses control charts were missing data and selected

gamma-spectroscopy systems QC trend data which trended above the

established mean did not result in Anomaly Reports being issued on a

consistent basis.

From review of selected data and discussions with

technicians and supervisors. the inspectors verified that the required

OC analyses and re analyses were Jerformed and met estchlished

procedural acceptance criteria,

lowever, the inspectors identified the

lack of consistently implementing all details of the QC program as an

area for improvement.

The inspectors informed licensee representatives

that OC program implementation would be considered an IFl 50 424.425/97-

07-05. Review Licensee Actions to Improve Implementation of Chemistry QC

Program Details.

Enclosure 2

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c.

Conclusions

in general, licensee OC primary and secondary OC activities verified

accuracy of analytical measurements.

One IFl was identified to review

implementation of chemistry QC data trending and Anomaly Report

issuance.

R8

Hiscellaneous Radiation Protection and Chemistry Issues (84750)

R8.1

(Closed) URI 50-424.425/97-02-03: evaluate commitments and radiation

monitor sensitivity to meet NUREG 0737 Table ll.F.1-3 Containment High

Range Monitor Requirements.

Licensee audit findings documented in Safety Audit Engineer Review

(SAER) audit report VSAER 97-016, dated February 7, 1997, documented

that electronic calibrations of the containment high range monitors were

not conducted for all range decades above 10 Roentgens per hour (R/hr)

as specified in NUREG 0737, Table ll.F.31.

Subsequent reviews also

identified that the strength of the in situ calibration source exceeded

the specified range of 1 -10 R/hr, and the inspectors cuestioned whether

the monitors met the required sensitivity, (i.e.,1 rac per hour,

s )eci fied. ) The inspectors noted that FSAR Section 7,5,4-2 specified

t1at containment area radiation monitors were in conformance with

NUREG-0737, ll.F,1, Attachment 3.

From review and discussion of

applicable vendor documents, the inspectors verified that the

containment high range monitor sensitivity met NUREG 0737 Table ll.F.1-3

requirements and the calibration source was in accordance with vendor

specifications. Although, documentation errors in electronic signal

limits were noted, data for completion of electronic signal calibration

testing were accurate and testing was completed successfully in February

1997 for both units.

Current revisiens to surveillance procedures

24625-1, " Containment High Range Area Monitor 1RX-005 Analog 0)erational

Test and Channel Calibration." and 24625 2. " Containment High

Range Area

Monitor 2RX-005 Analog Operational Test and Channel Calibration,"

'

specify the appropriate electronic calibration limit values.

The

licensee initiated licensing Document Change Request FS97-047. which

would update FSAR Table 7,5,4-2 to allow source calibration of the CHRMs

in accordance with the vendor recommendations.

Consistent with Section

IV of the Enforcement Policy and based on corrective actions taken prior

to the end of the inspection, the identified issues regarding the

containment high range monitor calibration was identified as a non-cited

violation (NCV) 50-424.425/97-07 06. Failure to Meet NUREG-0737

Requirements for Containment High Range Monitors.

Enclosure 2

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S2

Status of Security Facilities and Equipment

S2.1 Vital Area Barriers

a.

Insoection Scone (81700) (71750)

The inspector evaluated the licensee's com)ensatory actions for a

degraded vital area barrier at the Unit 1 Jiesel Generator (DG)

Building.

The inspector reviewed the Physical Security Plan (PSP).

specific building drawings, and security procedures associated with the

DG building.

b.

Observations and Findinas

On July 7, 1997, maintenarce activities on the DG controls inadvertently

caLsed a fuel oil spill to occur.

Maintenance Work Order 19702156 was

generated on July 8, 1997, to request support and equipment to clean up_

the fuel oil outside DG 18 and from inside the IB day tank vent room.

The licensee's PSP, Amendment 34, dated April 28, 1997, Table 4 1,

designates the Unit 1 and 2 DG buildings and their controls as vital

areas.

Licensee Drawing AX1002FA06, Revision 0, dated 1988, designates

the outermost boundary of the Unit 1 and 2 OG buildings as a vital

barrier.

Licensee procedt're 90106-C. Revision 22. dated August 6,1996,

Section 4.7 states in part, that decreased effectiveness of physical

barriers shall be compensated for by posting armed nuclear security

officers.

On July 8, a vital area barrier to the IB day tank vent room was removed

to allow efficient cleanup of the fuel oil in this area.

The barrier

consisted of steel louvers and rebar,

The inspector determined that on

July 8. prior to removing the day tank vent room vital area barrier,

security pre posted the area with an armed officer. However,

approximately 15 minutes later, upon inspection by the licensee, it was

determined that "no unauthorized entry could be gained to the components

of the building," The compensatory post was released upon this

determination.

However, increased surveillance checks were initiated on

the building.

Subsequently, the licensee failed to compensate for a

decrease in effectiveness of a vital area barrier for approximately 19

hours with an armed security officer.

On July 24 the inspector performed a walkdown of the Unit 1 DG building

and verified there were no openings in the IB day tank vent room greater

than allowed by the PSP.

The inspector noted that the area was secured

and all barriers were in place.

The licensee initiated a Request for Engineering Review (97-0264) dated

July 16.-1997. to determine whether all protected and vital area

barriers currently in place were required by security commitments in

addition to ensuring appropriate plant drawings reflect actual barrier

locations.

Enclosure 2

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c.

Conclusion

Through observation. discussion with licensee representatives, and

document review the inspector identified a violation for failure to

compensate for a decrease in effectiveness of the IB day tank vent room

barrier.

This is identified as VIO 50 424/97-07-07. Failure To Take

Compensatory Actions For A Decrease in Effectiveness Of A Vital Area

Barrier.

Y. Manacement Meetinas and Other Areas

X

Review of Updated Final Safety Analysis Report (UFSAR)

A recent discovery of a licensee o)erating its facility in a manner

contrary to the UFSAR description lighlighted the need for a special

focused review that compares plant practices, procedures and/or

parameters to the UFSAR descriptions. While performing the inspections

discussed in this re) ort. the inspectors reviewed the applicable

portions of the UFSAR that related to the areas inspected.

The

inspectors verifled that the UFSAR wording was consistent with the

observed plant practices, procedures and/or parameters.

X1

Exit Meeting Summary

The inspectors ) resented the inspection results to members of licensee

management at t1e conclusion of the inspection on August 7.1997.

The

licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during

the inspection should be considered proprietary. No proprietary

information was identified.

X2

Other NRC Personnel On Site

On July 16 and 17. Mr. L. Wheeler and Mr. H. Berkow of NRR. met with the

licensee to discuss various topics.

X3

NRC Interface Meeting with Southern Nuclear

On July 31. 1997, the NRC met with representatives of Southern Nuclear

Company (SNC) management in Birmingham. Alabama, to discuss the plant

status and major issues for the three nuclear power plants: Farley.

Hatch, and Vogtle.

In addition.

Mr. L. Reyes, presentations by the NRC Regional Administrator.

and the Director of Reactor Projects. Mr. J. Johnson, were

made.

Enclosure 2

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X4

Local Public Document (PDR) Review

On July 9, 1997, the inspectors visited the Vogtle PDR located at the

Burke County Public Library in Waynesboro, Georgia.

During the visit,

the inspectors reviewed the status of the collection and discussed the

operation of the PDR with the local custodian.

Using available indexes in the PDR, the inspectors retrieved several

randomly selected documents,

The microfiche printer was in good working

order and produced legible copies. The inspectors noted that there were

five unopened envelopes from the NRC on the shelves of the collection.

The oldest envelope was postmarked June 27, 1997.

The inspectors also

noted ten unfiled NRC weekly accession lists. The custodian indicated

that she files NRC documents as time permits and that there was no other

unopened mail.

She also indicated that visitors to the PDR are rare and

are usually NRC personnel.

The custodian indicated that she contacts

NRC headquarters personnel responsible for the PDR when questions arise.

-The custodian demonstrated the library's internet link to the NRC home

page.

PARTIAL LIST OF PERSONS CONTACTED

Licensee

J. Beasley. Nuclear Plant General Manager

J. Gasser, Plant Operations Assistant General Manager

S. Chestnut, Operations Marager

W. Burmeister, Manager Engineering Support

K. Holmes, Manager Maintenance

1. Kochery, Health Physics Superintendent

A. Parton, Chemistry Superintendent

K. Duquette, Plant Health Physicist

M. Sheibani, Supervisor, Nuclear Safety and Compliance

C. Stinespring Manager Plant Administration

M. Griffis, Manager P1 ant Modifications and Maintenance

C. Tippins, Jr., Nuclear Specialist 1

INSPECTION PROCEDURES USED

IP 37551:

Onsite Engineering

IP 40500:

Effectiveness of Licensee Controls In Identifying,

Resolving, and Preventing Problems

'

IP 61726:

Surveillance Observation

IP 62707:

Maintenance Observation

IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

IP 81700:

Physical Security Program For Power Reactors

IP 83750:

Occupational Radiation Exposure

Enclosure 2

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IP 84750:

Radioactive Waste Treatment, and Effluent and Environmental

Monitoring

IP 86750:

Solid Radioactive Waste Management and Transportation of

Radioactive Materials

Tl 2515/133:

Implementation of Revised 49 CFR Parts 100-170 and

10 CFR Part 71

ITEMS OPENED AND CLOSED

Onened

50-424/97-07-01

VIO

Failure to Document Entry into Proper Action Condition

following Airlock Maintenance (Section 02.2).

50 425/97-07-02

NCV

Improper Storage of Monorail Beam Adjacent to CCP 2A

Motor (Section E8.2).

50 424/97-07 03

IFl

Unplanned /Unmonitored Release From Unit 1 Equipment

Building (Section E8.4).

50 424, 425/

NCV

Failure To Meet 49 CFR 172.200 Shipping Paper

97-07 04

Documentation Details in Accordance With 10 CFR 71.5

Requirements (Section Rl.3).

50 424. 425/

IFl

Review Licensee Actions To im

Chemistry QC Program-Details prove implementation Of

97 07 05

(Section-R7.2).

50-424, 425/

NCV

Failure To Meet NUREG 0737 Requirements For

97-07 06

Containment High Range Monitors (Section R8.1).

50-424/97 07-07

V10

Failure to Take Compensatory Actions For A Decrease In

Effectiveness of A Vital Area Barrier (Section S2,1).

Closed-

50-424/95-27-02

URI .

Adequacy of Nuclear. Service Cooling Water Valve as

Closed System Isolation Valve (Section E8.1).

50-425/97 06-01

URI

Monorail Beam Stored On-2A Centrifugal Charging Pump-

(CCP) Bedplate (Section E8.2).

50-425/97-07-02

NCV

Improper Storage of Monorail Beam Adjacent to CCP 2A

Motor (Section E8.2).

50-424. 425/

URI

Testing-of Parallel Circuits For MSIVs (Section E8.3).

97-06 02

50-424. 425/

NCV

Failure To Meet 49 CFi,172.200 Shipping Paper

97-07-04-

Documentation Details In Accordance-With 10 CFR 71.5

Requirements (Section R1.3).

Enclosure 2

. _ _ _ .

.

..

..

..

.

.

.

4

4

l

25.

50-424. 425/

URI

Evaluate Licensee Commitments And Monitor

97 02 03

Sensitivity To Meet NUREG 0737 Table II.F.3-1

Containment High Range Monitor Requirements

(Section R8.1).

50 424. 425/

NCV

Failure To Meet NUREG 0737 Requirements For

97-07-06

Containment High Range Monitors (Section R8.1).

_

_

_

Enclosure 2

_ _ _

. _ _ _ _ .

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_

.

.