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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217L0421999-10-21021 October 1999 Forwards Insp Rept 50-382/99-20 on 990815-0925 & Notice of Violation.Two Severity Level IV Violations of NRC Requirements Identified & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20217N2111999-10-19019 October 1999 Forwards Insp Rept 50-382/99-14 on 990913-17 & 1004-08.No Violations Noted.Licensed Operator Requalification Program, Effective,Utilized Systems Approach to Training & Showed Continued Improvements Over Previous Insp Findings ML20217L0101999-10-18018 October 1999 Provides Update of Waterford 3 Effort for Review of Ufsar. Info Listed Includes Background Mgt Expectations,Review Status & Results,Clarifications Re Review & Conclusions ML20217L0141999-10-18018 October 1999 Submits Update to NRC Staff Re Circumstances & Plans for Submitting Certification Rept on Waterford 3 Plant Specific Simulator ML20217G7051999-10-14014 October 1999 Forwards Comments on Four of NRC RO Examination Questions for Exam Administered During Week of 991004 05000382/LER-1999-014, Forwards LER 99-014-00,providing Details of Reactor Shutdown Due to Loss of RCP Controlled bleed-off Flow.Attached Commitment Identification/Voluntary Enhancement Form Identifies All Commitments Contained in Submittal1999-10-12012 October 1999 Forwards LER 99-014-00,providing Details of Reactor Shutdown Due to Loss of RCP Controlled bleed-off Flow.Attached Commitment Identification/Voluntary Enhancement Form Identifies All Commitments Contained in Submittal ML20217D5151999-10-0707 October 1999 Forwards Application for Renewal of SRO License for C Fugate License SOP-43039-3,IAW 10CFR55.57.Without Encls ML20217C6251999-10-0505 October 1999 Informs That NRC Reviewed Util Ltr & Encl Exercise Scenario Package for Waterford 3 Emergency Plan Exercise Scheduled for 991013.Based on Review,Nrc Determined That Exercise Appropriate to Meet Objectives ML20212J6921999-09-29029 September 1999 Forwards Insp Rept 50-382/99-18 on 990830-0902.One Noncited Violation Identified Re Failure to Follow Procedural Instructions to Ensure That Members on Fire Brigade Shift Were Qualified ML20216G2441999-09-27027 September 1999 Forwards Insp Rept 50-382/99-19 on 990830-0903.No Violations Noted 05000382/LER-1999-013, Forwards LER 99-013-00,providing Details of Exceeding TS Limits for RCS Cooldown Rates.All Commitments Contained in Submittal Are Identified on Encl Commitment Identification/ Voluntary Enhancement Form1999-09-23023 September 1999 Forwards LER 99-013-00,providing Details of Exceeding TS Limits for RCS Cooldown Rates.All Commitments Contained in Submittal Are Identified on Encl Commitment Identification/ Voluntary Enhancement Form IR 05000382/19993011999-09-21021 September 1999 Informs That NRC License Exam Previously Associated with NRC Insp Rept 50-382/99-301 Will Be Incorporated Into NRC Insp Rept 50-382/99-14 ML20212D8761999-09-16016 September 1999 Informs That on 990818,NRC Staff Completed Midcycle PPR of Waterford 3.During Assessment Period,Number of Personnel Errors Occurred,Which Demonstrated Lack of Attention to Detail by Plant Personnel.Historical Listing of Issues,Encl ML20212C2471999-09-16016 September 1999 Forwards Five Final Applications for RO Licenses for G Esquival,Jm Hearn,Md Lawson,Re Simpson & PI Wood.Written Exam & Operating Test to Be Administered,Is Requested. Encls Withheld ML20212C2391999-09-16016 September 1999 Requests Cancellation of SRO Licenses for Bn Coble,License SOP-43835,due to Job Assignment Location & CA Rodgers, License SOP-43537-1,due to Resignation from Company, Effective 990901 ML20212C5881999-09-14014 September 1999 Forwards Insp Rept 50-382/99-15 on 990719-23 with Continuing in Ofc Insp Until 0819.No Violations Noted ML20211Q4421999-09-0909 September 1999 Forwards Insp Rept 50-382/99-07 on 990601-11.Three Violations Being Treated as Noncited Violations ML20211P4121999-09-0707 September 1999 Requests NRC Staff Review & Approval of Integrated Nuclear Security Plan (Insp) & Integrated Security Training & Qualification Plan (Ist&Q), for Use by All Entergy Operations,Inc.Encl Withheld,Per 10CFR2.790(d) ML20211M8391999-09-0303 September 1999 Forwards Revised Epips,Including Rev 25 to EP-001-020,rev 24 to EP-001-030,rev 25 to EP-001-040,rev 30 to EP-002-100,rev 22 to EP-001-010,rev 27 to EP-002-010,rev 26 to EP-002-102 & Rev 16 to EP-002-190.Listed Proprietary Revs to Epips,Encl ML20211L3681999-09-0202 September 1999 Forwards Five Preliminary Applications for Reactor Operator Licenses for Individuals Listed,Iaw 10CFR55.31.Encls Withheld ML20211K9741999-09-0101 September 1999 Forwards Insp Rept 50-382/99-16 on 990704-0814.Two Severity Level IV Violations Identified & Being Treated as Noncited Violations,Consistent with App C of Enforcement Policy 05000382/LER-1999-011, Forwards LER 99-011-00,providing Details of Reactor Shutdown Due to Loss of Controlled bleed-off Flow.All Commitments Contained in Submittal Identified on Attached Commitment Identification/Voluntary Enhancement Form1999-08-31031 August 1999 Forwards LER 99-011-00,providing Details of Reactor Shutdown Due to Loss of Controlled bleed-off Flow.All Commitments Contained in Submittal Identified on Attached Commitment Identification/Voluntary Enhancement Form ML20211M3641999-08-30030 August 1999 Forwards Written Examination,Operating Tests & Supporting Ref Matl Identified in Attachment 2 of ES-210,in Response to NRC .Encl Withheld ML20211G5751999-08-27027 August 1999 Forwards RAI Re IPEEE Submittal.Please Provide RAI within 60 Days of Receipt of Ltr,Per Util Response to GL 88-20,suppl 4 ML20211E3281999-08-26026 August 1999 Forwards fitness-for-duty Performance Data for Period of 990101-0630,IAW 10CFR26.71(d).Ltr Does Not Contain Commitments 05000382/LER-1999-009, Forwards LER 99-009-00 Re Discovery of Condition of Noncompliance with App R Involving Inadequate Separation of Essential Cables Routed in Fire Area RAB-30 in Rab. Compensatory Measures Were Established Immediately1999-08-26026 August 1999 Forwards LER 99-009-00 Re Discovery of Condition of Noncompliance with App R Involving Inadequate Separation of Essential Cables Routed in Fire Area RAB-30 in Rab. Compensatory Measures Were Established Immediately 05000382/LER-1999-010, Forwards LER 99-010-00,providing Details of Inadequate Pumping Capacity in Dry Cooling Tower Area.All Commitments Contained in Submittal Are Identified on Attached Commitment Identification Voluntary Enhancement Form1999-08-26026 August 1999 Forwards LER 99-010-00,providing Details of Inadequate Pumping Capacity in Dry Cooling Tower Area.All Commitments Contained in Submittal Are Identified on Attached Commitment Identification Voluntary Enhancement Form ML20211F5421999-08-24024 August 1999 Forwards Proposed marked-up TS Page Xviii, Index Administrative Controls, Correcting Page Number Re TS Change Request NPF-38-220.Editorial Changes for TS Change NPF-38-221 Discussed ML20211F3561999-08-24024 August 1999 Forwards CTS Pages & TS Proposed marked-up Pages for Insertion Into TS Change Request NPF-38-207 Re Efas, Originally Submitted on 980702.Original NSHC Determination Continues to Be Applicable ML20211F4611999-08-24024 August 1999 Informs That NRC Reviewed Ltr & Encl Objectives for Waterford 3 Emergency Plan Exercise Scheduled for 991013.Exercise Objectives Appropriate to Meet Emergency Plan Requirements ML20211G1731999-08-23023 August 1999 Informs That Info Submitted in ,B&W Rept 51-1234900-00,will Be Withheld from Public Disclosure,Per 10CFR2.790 ML20211C5101999-08-19019 August 1999 Forwards Certified Copies of Liability Insurance Policy Endorsements Issued in First Half of 1999 for Each Entergy Operations,Inc Nuclear Unit,Per 10CFR140.15 ML20210T9791999-08-18018 August 1999 Discusses Which Responded to Reconsideration of Violation Denial (EA 98-022) Enforcement Action Detailed in .Concludes That Violation Occurred as Stated ML20211A9501999-08-12012 August 1999 Discusses 990720-21 Workshop Conducted in Region IV Ofc,Re Exchange of Info in Area of Use of Risk Insights in Regulatory Activities.List of Attendees,Summary of Topic & Issues,Agenda & Copies of Handouts Encl ML20210S0561999-08-12012 August 1999 Submits Voluntary Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for NRC Fys 2000 & 2001 for Waterford 3 ML20210Q6161999-08-12012 August 1999 Forwards Corrected Copy of Monthly Operating Rept for July 1999 for Waterford 3.Original Rept,Submitted with ,Contained Typos ML20217F2661999-08-12012 August 1999 Forwards Copy of 1999 Waterford 3 Biennial Exercise Package to Be Performed Using Waterford 3 CR Simulator ML20210R9231999-08-11011 August 1999 Forwards Insp Rept 50-382/99-10 on 990719-23.Violations Noted.Nrc Has Determined That One Severity Level IV Violation of NRC Requirements Occurred ML20210L1461999-08-0303 August 1999 Informs That NRC Plans to Administer Gfes of Written Operator Licensing Exam on 991006.Requests Submittal of Ltr Identifying Individuals Taking Exam,Personnel Allowed Access to Exams & Mailing Address for Exams 05000382/LER-1999-008, Forwards LER 99-008-00,re Failure to Perform Testing of ESF Filtration Units Per TS Srs.Commitments Made by Util Also Encl1999-07-29029 July 1999 Forwards LER 99-008-00,re Failure to Perform Testing of ESF Filtration Units Per TS Srs.Commitments Made by Util Also Encl ML20210H4291999-07-29029 July 1999 Forwards Response to NRC Rai,Associated with TS Change Request NPF-38-208,proposing to Replace Ref to Supplement 1 with Ref to Supplement 2 of Calculative Methods for CE Small Break LOCA Evaluation Model, in ACs Section of TSs ML20210F9451999-07-27027 July 1999 Forwards Proprietary & non-proprietary Version of Rev 29 to EPIP EP-002-100, Technical Support Ctr Activation,Operation & Deactivation. Proprietary Info Withheld,Per 10CFR2.790 ML20210D3171999-07-23023 July 1999 Submits Proposal for Final Resolution of Reracking Spent Fuel Pool at Plant,Per License Amend 144,issued by NRC in .No New Commitments Are Contained in Ltr 05000382/LER-1999-007, Forwards LER 99-007-00,providing Details of Operation Outside Tornado Missile Protection Licensing Basis for turbine-driven Emergency Feedwater Pump Exhaust Stack & Steam Supply Piping.All Commitments Identified on Attached1999-07-23023 July 1999 Forwards LER 99-007-00,providing Details of Operation Outside Tornado Missile Protection Licensing Basis for turbine-driven Emergency Feedwater Pump Exhaust Stack & Steam Supply Piping.All Commitments Identified on Attached ML20210D8701999-07-23023 July 1999 Forwards Safety Evaluation Re First 10-yr Interval Inservice Insp Plan Requests for Relief ISI-018 Through ISI-020 for Entergy Operations,Inc,Unit 3 ML20210B1521999-07-15015 July 1999 Forwards Insp Rept 50-382/99-13 on 990523-0703.Three Violations Being Treated as Noncited Violations ML20209G9771999-07-13013 July 1999 Forwards Objectives & Guidelines for Waterford 3 Emergency Preparedness Exercise Scheduled for 991013.List of Objectives cross-referenced Where Applicable to Relevant Sections of NUREG-0654 IR 05000382/19990081999-07-12012 July 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-382/99-08 Issued on 990503 ML20209E5231999-07-0909 July 1999 Informs That as Result of NRC Review of Util Responses to GL-92-01,rev 1 & Suppl 1,staff Revised Info in Reactor Vessel Integrity Database & Releasing Database as Rvid Version 2.This Closes Staff Efforts Re TAC MA0583 ML20209D4051999-07-0707 July 1999 Forwards Revised TS Pages to Replace Attachment C,Entirely in Original TS Change Request NPF-38-207,per 990519 Discussion with C Patel of Nrc.Changes to Action 20 Delete Word Requirement & Revise Word Modes to Mode 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217L0101999-10-18018 October 1999 Provides Update of Waterford 3 Effort for Review of Ufsar. Info Listed Includes Background Mgt Expectations,Review Status & Results,Clarifications Re Review & Conclusions ML20217L0141999-10-18018 October 1999 Submits Update to NRC Staff Re Circumstances & Plans for Submitting Certification Rept on Waterford 3 Plant Specific Simulator ML20217G7051999-10-14014 October 1999 Forwards Comments on Four of NRC RO Examination Questions for Exam Administered During Week of 991004 05000382/LER-1999-014, Forwards LER 99-014-00,providing Details of Reactor Shutdown Due to Loss of RCP Controlled bleed-off Flow.Attached Commitment Identification/Voluntary Enhancement Form Identifies All Commitments Contained in Submittal1999-10-12012 October 1999 Forwards LER 99-014-00,providing Details of Reactor Shutdown Due to Loss of RCP Controlled bleed-off Flow.Attached Commitment Identification/Voluntary Enhancement Form Identifies All Commitments Contained in Submittal ML20217D5151999-10-0707 October 1999 Forwards Application for Renewal of SRO License for C Fugate License SOP-43039-3,IAW 10CFR55.57.Without Encls 05000382/LER-1999-013, Forwards LER 99-013-00,providing Details of Exceeding TS Limits for RCS Cooldown Rates.All Commitments Contained in Submittal Are Identified on Encl Commitment Identification/ Voluntary Enhancement Form1999-09-23023 September 1999 Forwards LER 99-013-00,providing Details of Exceeding TS Limits for RCS Cooldown Rates.All Commitments Contained in Submittal Are Identified on Encl Commitment Identification/ Voluntary Enhancement Form ML20212C2391999-09-16016 September 1999 Requests Cancellation of SRO Licenses for Bn Coble,License SOP-43835,due to Job Assignment Location & CA Rodgers, License SOP-43537-1,due to Resignation from Company, Effective 990901 ML20212C2471999-09-16016 September 1999 Forwards Five Final Applications for RO Licenses for G Esquival,Jm Hearn,Md Lawson,Re Simpson & PI Wood.Written Exam & Operating Test to Be Administered,Is Requested. Encls Withheld ML20211P4121999-09-0707 September 1999 Requests NRC Staff Review & Approval of Integrated Nuclear Security Plan (Insp) & Integrated Security Training & Qualification Plan (Ist&Q), for Use by All Entergy Operations,Inc.Encl Withheld,Per 10CFR2.790(d) ML20211M8391999-09-0303 September 1999 Forwards Revised Epips,Including Rev 25 to EP-001-020,rev 24 to EP-001-030,rev 25 to EP-001-040,rev 30 to EP-002-100,rev 22 to EP-001-010,rev 27 to EP-002-010,rev 26 to EP-002-102 & Rev 16 to EP-002-190.Listed Proprietary Revs to Epips,Encl ML20211L3681999-09-0202 September 1999 Forwards Five Preliminary Applications for Reactor Operator Licenses for Individuals Listed,Iaw 10CFR55.31.Encls Withheld 05000382/LER-1999-011, Forwards LER 99-011-00,providing Details of Reactor Shutdown Due to Loss of Controlled bleed-off Flow.All Commitments Contained in Submittal Identified on Attached Commitment Identification/Voluntary Enhancement Form1999-08-31031 August 1999 Forwards LER 99-011-00,providing Details of Reactor Shutdown Due to Loss of Controlled bleed-off Flow.All Commitments Contained in Submittal Identified on Attached Commitment Identification/Voluntary Enhancement Form ML20211M3641999-08-30030 August 1999 Forwards Written Examination,Operating Tests & Supporting Ref Matl Identified in Attachment 2 of ES-210,in Response to NRC .Encl Withheld ML20211E3281999-08-26026 August 1999 Forwards fitness-for-duty Performance Data for Period of 990101-0630,IAW 10CFR26.71(d).Ltr Does Not Contain Commitments 05000382/LER-1999-010, Forwards LER 99-010-00,providing Details of Inadequate Pumping Capacity in Dry Cooling Tower Area.All Commitments Contained in Submittal Are Identified on Attached Commitment Identification Voluntary Enhancement Form1999-08-26026 August 1999 Forwards LER 99-010-00,providing Details of Inadequate Pumping Capacity in Dry Cooling Tower Area.All Commitments Contained in Submittal Are Identified on Attached Commitment Identification Voluntary Enhancement Form 05000382/LER-1999-009, Forwards LER 99-009-00 Re Discovery of Condition of Noncompliance with App R Involving Inadequate Separation of Essential Cables Routed in Fire Area RAB-30 in Rab. Compensatory Measures Were Established Immediately1999-08-26026 August 1999 Forwards LER 99-009-00 Re Discovery of Condition of Noncompliance with App R Involving Inadequate Separation of Essential Cables Routed in Fire Area RAB-30 in Rab. Compensatory Measures Were Established Immediately ML20211F3561999-08-24024 August 1999 Forwards CTS Pages & TS Proposed marked-up Pages for Insertion Into TS Change Request NPF-38-207 Re Efas, Originally Submitted on 980702.Original NSHC Determination Continues to Be Applicable ML20211F5421999-08-24024 August 1999 Forwards Proposed marked-up TS Page Xviii, Index Administrative Controls, Correcting Page Number Re TS Change Request NPF-38-220.Editorial Changes for TS Change NPF-38-221 Discussed ML20211C5101999-08-19019 August 1999 Forwards Certified Copies of Liability Insurance Policy Endorsements Issued in First Half of 1999 for Each Entergy Operations,Inc Nuclear Unit,Per 10CFR140.15 ML20210Q6161999-08-12012 August 1999 Forwards Corrected Copy of Monthly Operating Rept for July 1999 for Waterford 3.Original Rept,Submitted with ,Contained Typos ML20210S0561999-08-12012 August 1999 Submits Voluntary Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for NRC Fys 2000 & 2001 for Waterford 3 ML20217F2661999-08-12012 August 1999 Forwards Copy of 1999 Waterford 3 Biennial Exercise Package to Be Performed Using Waterford 3 CR Simulator 05000382/LER-1999-008, Forwards LER 99-008-00,re Failure to Perform Testing of ESF Filtration Units Per TS Srs.Commitments Made by Util Also Encl1999-07-29029 July 1999 Forwards LER 99-008-00,re Failure to Perform Testing of ESF Filtration Units Per TS Srs.Commitments Made by Util Also Encl ML20210H4291999-07-29029 July 1999 Forwards Response to NRC Rai,Associated with TS Change Request NPF-38-208,proposing to Replace Ref to Supplement 1 with Ref to Supplement 2 of Calculative Methods for CE Small Break LOCA Evaluation Model, in ACs Section of TSs ML20210F9451999-07-27027 July 1999 Forwards Proprietary & non-proprietary Version of Rev 29 to EPIP EP-002-100, Technical Support Ctr Activation,Operation & Deactivation. Proprietary Info Withheld,Per 10CFR2.790 ML20210D3171999-07-23023 July 1999 Submits Proposal for Final Resolution of Reracking Spent Fuel Pool at Plant,Per License Amend 144,issued by NRC in .No New Commitments Are Contained in Ltr 05000382/LER-1999-007, Forwards LER 99-007-00,providing Details of Operation Outside Tornado Missile Protection Licensing Basis for turbine-driven Emergency Feedwater Pump Exhaust Stack & Steam Supply Piping.All Commitments Identified on Attached1999-07-23023 July 1999 Forwards LER 99-007-00,providing Details of Operation Outside Tornado Missile Protection Licensing Basis for turbine-driven Emergency Feedwater Pump Exhaust Stack & Steam Supply Piping.All Commitments Identified on Attached ML20209G9771999-07-13013 July 1999 Forwards Objectives & Guidelines for Waterford 3 Emergency Preparedness Exercise Scheduled for 991013.List of Objectives cross-referenced Where Applicable to Relevant Sections of NUREG-0654 ML20209D4051999-07-0707 July 1999 Forwards Revised TS Pages to Replace Attachment C,Entirely in Original TS Change Request NPF-38-207,per 990519 Discussion with C Patel of Nrc.Changes to Action 20 Delete Word Requirement & Revise Word Modes to Mode ML20209B6081999-06-30030 June 1999 Submits Response to NRC GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants. Disclosure Encl 05000382/LER-1999-005, Forwards LER 99-005-00,providing Details of Discovery of Untested Electrical Contacts in safety-related Logic Circuits1999-06-24024 June 1999 Forwards LER 99-005-00,providing Details of Discovery of Untested Electrical Contacts in safety-related Logic Circuits ML20196G5731999-06-24024 June 1999 Forwards Operator Licensing Exam Outlines Associated with Exam Scheduled for Wk of 991004.Exam Development Is Being Performed in Accordance with NUREG-1021,Rev 8 ML20212J4121999-06-23023 June 1999 Responds to NRC Re Reconsideration of EA 98-022. Details Provided on Actions Util Has Taken or Plans to Take to Address NRC Concerns with Ability to Demonstrate Adequate Flow Availability to Meet Design Requirements ML20196E9371999-06-22022 June 1999 Forwards Revs Made to EP Training Procedures.Procedures NTC-217 & NTC-217 Have Been Deleted.Procedure NTP-203 Was Revised to Combine Requirement Previously Included in Procedures NRC-216 & NTC-217 ML20196A1021999-06-17017 June 1999 Provides Supplemental Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, Per 990513 Request of NRC Project Manager ML20195F3671999-06-0909 June 1999 Forwards Rev 21,Change 0 to EP-001-010, Unusual Event. Rev Reviewed in Accordance with 10CFR50.54(q) Requirements & Determined Not to Decrease Effectiveness of Emergency Plan ML20195C7801999-06-0303 June 1999 Submits Response to Violations Noted in Insp Rept 50-382/99-08.Corrective Actions:All Licensee Access Authorization Personnel Were Retrained Prior to Completion of Insp ML20195C2951999-05-28028 May 1999 Forwards Annual Evaluation of Changes & Errors Identified in Abb CE ECCS Performance Evaluation Models Used for LOCA Analyses.Results of Annual Evaluation for CY98 Detailed in Attached Rept,Based Upon Suppl 10 to Abb CE Rept ML20195C0241999-05-28028 May 1999 Notifies NRC of Operator Medical Condition for Waterford 3 Opertaor Sp Wolfe,License SOP-43723.Attached NRC Form & Memo Contain Info Concerning Condition.Without Encls ML20196L3281999-05-24024 May 1999 Informs That Entergy Is Withdrawing TS Change Request NPF-38-205 Re TS 3.3.3.7.1, Chlorine Detection Sys & TS 3.3.3.7.3, Broad Range Gas Detection Submitted on 980629 ML20206S4691999-05-17017 May 1999 Requests Waiver of Exam for SRO Licenses for an Vest & Hj Lewis,Iaw 10CFR55.47.Both Individuals Have Held Licenses at Plant within Past Two Year Period,But Licenses Expired Upon Leaving Util Employment.Encl Withheld 05000382/LER-1999-004, Forwards LER 99-004-00 Re Discovery That Response Time Testing Had Not Been Performed for ESFAS Containment Cooling Function,As Required by TS SR 4.3.2.31999-05-14014 May 1999 Forwards LER 99-004-00 Re Discovery That Response Time Testing Had Not Been Performed for ESFAS Containment Cooling Function,As Required by TS SR 4.3.2.3 ML20206N1921999-05-10010 May 1999 Provides Revised Attachment 2 for Alternative Request IWE-02,originally Submitted 990429 Re Bolt Torque or Tension Testing of Class Mc pressure-retaining Bolting as Specified in Item 8.20 of Article IWE-2500,Table IWE-2500-1 ML20206J1471999-05-0606 May 1999 Requests That Implementation Date for TS Change Request NPF-38-211 Be within 90 Days of Approval to Allow for Installation of New Monitoring Sys for Broad Range Gas Detection Sys ML20206J1721999-05-0606 May 1999 Notifies That Proposed Schedule for Plant 1999 Annual Exercise Is Wk of 991013.Exercise Objective Meeting Scheduled for 990513 at St John Baptist Parish Emergency Operations Ctr ML20206G8021999-05-0404 May 1999 Provides Revised Response to NRC Re Violations Noted in Insp Rept 50-382/99-01.Licensee Denies Violation as Stated.Change Made Is Denoted by Rev Bar & Does Not Materially Impact Original Ltr ML20206E7811999-04-29029 April 1999 Proposes Alternatives to Requirements of ASME B&PV Code Section XI,1992 Edition,1992 Addenda,As Listed.Approval of Alternative Request on or Before 990915,requested ML20205T2531999-04-22022 April 1999 Forwards LER 99-S02-00,describing Occurrence of Contract Employee Inappropriately Being Granted Unescorted Access to Plant Protected Area ML20205R2611999-04-20020 April 1999 Forwards Rev 19 to Physical Security Plan,Submitted in Accordance with 10CFR50.54(p).Plan Rev Was Approved & Implemented on 990407.Rev Withheld,Per 10CFR73.21 ML20205Q3241999-04-16016 April 1999 Submits Addl Info Re TS Change Request NPF-38-215 for Administrative Controls TS Changes.Appropriate Pages from New Entergy Common QA Program Manual Provided as Attachment to Ltr 1999-09-07
[Table view] Category:UTILITY TO NRC
MONTHYEARW3P90-1505, Forwards Proposed Operator Licensing Exam Schedule & Proposed Requalification Exam Schedule,Per Generic Ltr 90-071990-09-17017 September 1990 Forwards Proposed Operator Licensing Exam Schedule & Proposed Requalification Exam Schedule,Per Generic Ltr 90-07 W3P90-1163, Forwards Relief Requests Associated w/10-yr Inservice Insp Program Per Section 50.55a(g)(6)(i) of 10CFR501990-09-0606 September 1990 Forwards Relief Requests Associated w/10-yr Inservice Insp Program Per Section 50.55a(g)(6)(i) of 10CFR50 W3P90-1191, Responds to Violations Noted in Insp Rept 50-382/90-15. Corrective Actions:Tech Spec Surveillance Procedure PE-005-004 Will Be Revised to Ensure That Normally Closed Valves Opened & Verified to Close for Toxic Gas Signal1990-08-31031 August 1990 Responds to Violations Noted in Insp Rept 50-382/90-15. Corrective Actions:Tech Spec Surveillance Procedure PE-005-004 Will Be Revised to Ensure That Normally Closed Valves Opened & Verified to Close for Toxic Gas Signal W3P90-1194, Submits Fitness for Duty Performance Data for 6-month Period from Jan-June 19901990-08-29029 August 1990 Submits Fitness for Duty Performance Data for 6-month Period from Jan-June 1990 W3P90-1184, Responds to Violations Noted in Insp Rept 50-382/90-14. Corrective Actions:Local Leak Rate Test Activities Shall Be Administratively Controlled to Require Use of Test Method Other than Pressure Decay1990-08-20020 August 1990 Responds to Violations Noted in Insp Rept 50-382/90-14. Corrective Actions:Local Leak Rate Test Activities Shall Be Administratively Controlled to Require Use of Test Method Other than Pressure Decay W3P90-1187, Forwards Booklet Entitled, Safety Info - Plans to Help You During Emergencies, Recently Distributed to General Public1990-08-17017 August 1990 Forwards Booklet Entitled, Safety Info - Plans to Help You During Emergencies, Recently Distributed to General Public W3P90-1189, Forwards Waterford 3 Steam Electric Station Emergency Preparedness Exercise for 901024. Annual Exercise Will Be Performed Using Control Room Simulator1990-08-17017 August 1990 Forwards Waterford 3 Steam Electric Station Emergency Preparedness Exercise for 901024. Annual Exercise Will Be Performed Using Control Room Simulator W3P90-1162, Forwards Rev 4 to 10-Yr Inservice Insp Program First Interval 1985-19951990-08-16016 August 1990 Forwards Rev 4 to 10-Yr Inservice Insp Program First Interval 1985-1995 W3P90-1174, Forwards Rev to Emergency Plan & QA Program,Consisting of Chart Indicating Changes to Util Organization1990-08-0707 August 1990 Forwards Rev to Emergency Plan & QA Program,Consisting of Chart Indicating Changes to Util Organization W3P90-1177, Forwards Revised Objectives for Emergency Preparedness Exercise Scheduled for 9010241990-08-0303 August 1990 Forwards Revised Objectives for Emergency Preparedness Exercise Scheduled for 901024 W3P90-1164, Forwards Waterford Steam Electric Station Unit 3 Basemat Monitoring Program Special Rept 3. Rept Documents Continued Integrity of Basemat as Verified by Program from Time of Inception of Monitoring in 1985 Through Mar 19901990-08-0303 August 1990 Forwards Waterford Steam Electric Station Unit 3 Basemat Monitoring Program Special Rept 3. Rept Documents Continued Integrity of Basemat as Verified by Program from Time of Inception of Monitoring in 1985 Through Mar 1990 W3P90-1167, Forwards Rev 12 to Emergency Plan Implementing Instruction EP-001-001, Recognition & Classification of Emergency Conditions, Reflecting Name Change of State Agency to Louisiana Radiation Protection Div1990-07-19019 July 1990 Forwards Rev 12 to Emergency Plan Implementing Instruction EP-001-001, Recognition & Classification of Emergency Conditions, Reflecting Name Change of State Agency to Louisiana Radiation Protection Div W3P90-1148, Responds to NRC 900503 Submittal Concerning Review of Util Rev 6,Change 1 to Inservice Testing Program for Pumps & Valves1990-07-17017 July 1990 Responds to NRC 900503 Submittal Concerning Review of Util Rev 6,Change 1 to Inservice Testing Program for Pumps & Valves W3P90-1143, Advises That 900404 Request for Addl Info Re Tech Spec Change Request NPF-38-103 Will Be Provided by 900803.Change Will Extend Test Frequency of Channel Functional Tests for ESF Actuation Sys & Reactor Protection Sys Instrumentation1990-07-0606 July 1990 Advises That 900404 Request for Addl Info Re Tech Spec Change Request NPF-38-103 Will Be Provided by 900803.Change Will Extend Test Frequency of Channel Functional Tests for ESF Actuation Sys & Reactor Protection Sys Instrumentation W3P90-1379, Provides Notification That Util Has Consolidated Operation of All Nuclear Facilities,Effective 9006061990-07-0202 July 1990 Provides Notification That Util Has Consolidated Operation of All Nuclear Facilities,Effective 900606 ML20044A5541990-06-26026 June 1990 Forwards Response to Generic Ltr 90-04 Requesting Info on Status of Licensee Implementation of Generic Safety Issues Resolved W/Imposition of Requirements or Corrective Actions ML20044A5551990-06-22022 June 1990 Describes Changes Required to Emergency Plan as Result of Transfer of Operations to Entergy Operations,Inc. Administrative Changes to Plan Necessary to Distinguish Support Functions to Be Retained by Louisiana Power & Light W3P90-1365, Provides Notification of Change in Operator Status Per 10CFR50.74 Due to Entergy Corp Consolidating Operation of All Nuclear Generating Facilities,Including Plant Under Util1990-06-19019 June 1990 Provides Notification of Change in Operator Status Per 10CFR50.74 Due to Entergy Corp Consolidating Operation of All Nuclear Generating Facilities,Including Plant Under Util ML20043G3431990-06-14014 June 1990 Requests That All NRC Correspondence Re Plant Be Addressed to RP Barkhurst at Address Indicated in 900523 Ltr ML20043F5121990-06-0808 June 1990 Forwards List of Directors & Officers of Entergy Operations, Inc.Operation of All Plants Transferred to Entergy on 900606 ML20043F2621990-06-0606 June 1990 Requests Withdrawal of 900504 Request to Extend Implementation Date of Amend 60 Re Transfer of Operations to Entergy,Inc.All Necessary Regulatory Approvals Obtained & License Conditions Implemented ML20043C1861990-05-29029 May 1990 Submits Response to 900426 Comments Re Investigation Case 4-88-020.Util Issued P.O. Rev Downgrading Order of Circuit Breakers & Eliminating Nuclear Requirements ML20043E5441990-05-24024 May 1990 Forwards Public Version of Change 1 to Rev 2 to EPIP EP-002-015, Emergency Responder Activation. Release Memo Encl ML20043B3501990-05-23023 May 1990 Forwards Response to Concerns Noted in Insp Rept 50-382/90-02.Response Withheld ML20043B3781990-05-23023 May 1990 Requests Change in NRC Correspondence Distribution List, Deleting Rt Lally & Adding DC Hintz,Gw Muench & RB Mcgehee. All Ref to Util Changed to Entergy Operations,Inc.Proposed NRC Correspondence Distribution List Encl W3P90-1314, Requests NRC Concurrence That Design/Controls/Testing to Minimize Potential for Common Header Blockage Acceptable Per 900510 Meeting.Tap Alternatives for Shutdown Cooling Level Indication Sys Discussed1990-05-21021 May 1990 Requests NRC Concurrence That Design/Controls/Testing to Minimize Potential for Common Header Blockage Acceptable Per 900510 Meeting.Tap Alternatives for Shutdown Cooling Level Indication Sys Discussed ML20043B3271990-05-21021 May 1990 Forwards Justification for Continued Operation Re Taped Splice for Use in Instrument Circuits,Per 900517 Request ML20042F5251990-05-0404 May 1990 Requests Extension of 90 Days to Implement Amend 60 to License NPF-38 in Order to Provide Securities & Exchange Commission Time to Review Transfer of Licensed Activities to Entergy Operations,Inc ML20042E5501990-04-17017 April 1990 Responds to Request for Addl Info Re Feedwater Isolation Valve Bases Change Request Dtd 891006 ML20012F4551990-04-10010 April 1990 Forwards Rev 10,Change 4 to Physical Security Plan.Encl Withheld ML20012F5491990-04-0606 April 1990 Advises That Util Installed Two Addl Benchmarks for Use as Part of Basemat Surveillance Program to Increase Efficiency of Survey Readings.New Benchmarks Will Be Shown on FSAR Figure 1.2.1 as Part of Next FSAR Rev ML20012F3181990-04-0606 April 1990 Forwards Util,New Orleans Public Svc,Inc & Entergy Corp 1989 Annual Repts ML20012E8971990-03-30030 March 1990 Submits Results of Evaluation of Util 900414 Response to Station Blackout Rule (10CFR50.63).Station Mod May Be Required to Change Starting Air Sys to Accomodate Compressed Bottled Air ML20012E2551990-03-27027 March 1990 Responds to Violation Noted in Insp Rept 50-382/90-01. Corrective Actions:Qa Review of Licensed Operator Medical Exam Records Conducted & Sys Implemented to Track Types & Due Dates of Medical Exams Required for Operators ML20012E0511990-03-27027 March 1990 Forwards Rev 10,Change 3 to Physical Security Plan.Rev Withheld ML20012D5461990-03-22022 March 1990 Forwards Documentation from Nuclear Mutual Ltd,Nelia & Nuclear Electric Insurance Ltd Certifying Present Onsite Property Damage Insurance ML20012D4911990-03-21021 March 1990 Responds to NRC 900208 Ltr Re Violations Noted in Investigation Rept 4-89-002.Corrective Action:Proper Sequence of Insp Hold Point Placed in Procedure Under Change Implemented on 880425 ML20012C0691990-03-14014 March 1990 Advises That Util Intends to Address Steam Generator Overfill Concerns (USI A-47) Utilizing Individual Plant Exam Process,Per Generic Ltr 89-14 ML20012C0421990-03-12012 March 1990 Forwards Questionnaire in Response to Generic Ltr 90-01, Request for Voluntary Participation in NRC Regulatory Impact Survey. Results Not Reflective of Particular Calendar Yr ML20012B6731990-03-0707 March 1990 Responds to NRC Bulletin 88-011,Action 1.a Re Insp of Surge Line to Determine Discernible Distress or Structural Damage & Advises That Neither Surge Line Nor Affiliated Hardware Suffered Any Discernible Distress or Structural Damage ML20006F5321990-02-22022 February 1990 Forwards Payment for Order Imposing Civil Monetary Penalty in Response to Enforcement Action EA-89-069 ML20011F1401990-02-21021 February 1990 Responds to Violations Noted in Insp Rept 50-382/89-41. Corrective Action:Review of Independent Verification Requirements Re Maint Activities Performed ML20006F1731990-02-19019 February 1990 Forwards Corrected Pages 9.2-21 & 9.2-22 of Rev 3 to FSAR, Per 891214 Ltr ML20006E5781990-02-13013 February 1990 Forwards Third Refueling Inservice Insp Summary Rept for Waterford Steam Electric Station Unit 3. ML20006D0571990-02-0202 February 1990 Responds to SALP Rept for Aug 1988 - Oct 1989.Contrary to Info Contained in SALP Rept,Civil Penalty Not Assessed by State of Nv for Radioactive Matl Transport Violations.Issue Resolved W/State of Nv W/O Issuance of Civil Penalty ML20006C1631990-01-30030 January 1990 Requests Extension of Commitment Dates in Response to Violations Noted in Insp Repts 50-382/89-17 & 50-382/89-22 to 900222 & 19,respectively.Violations Covered Use of Duplex Strainers & Missing Seismic Support for Cabinet ML20006C1581990-01-29029 January 1990 Forwards Response to Generic Ltr 89-13 Re safety-related Open Svc Water Sys.Instruments in Place on Component Cooling Water Sys/Auxiliary Component Cooling Water Sys HXs Which Connect to Plant Monitor Computer ML20006C1611990-01-29029 January 1990 Responds to NRC Bulletin 89-003 Re Potential Loss of Required Shutdown Margin During Refueling Operations. Instructions for Determining Acceptable Refueling Boron Concentration Provided in Procedure RF-005-001 ML20006B4121990-01-26026 January 1990 Informs That Photographic Surveys Discontinued,Per Basemat Monitoring Program.Monitoring Program Implementing Procedure Will Be Revised to Reflect Change ML20006A7091990-01-22022 January 1990 Forwards List of Individuals That No Longer Require Reactor Operator Licenses at Plant 1990-09-06
[Table view] |
Text
a -I LO U 181 A N A / 44. oeuao~o. .ra. r P O W E R & L I G H T / New cat Ana toVSANA
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70174-800G . (504]386-9345 hiuklNSYS June 13, 1985 W3P85-2115 3-A1.01.04 A4.05 Director of Nuclear Reactor Regulation Attention: Mr. G.W. Knighton, Chief Licensing Branch No. 3 Division of Licensing U.S. Nuclear Regulatory Commission Washington, D.C. 20555
SUBJECT:
Waterford SES Unit 3 Docket No. 50-382 Operating License NPF-38 Condition 12 LP&L Report: Depressurization Capability with Degraded Auxiliary Pressurizer Spray
Dear Sir:
LP&L hereby submits the subject report. The report provides the information required to satisfy License Condition 12. The results of LP&L testing and analysis demonstrate that the auxiliary spray system can perform the necessary depressurization to meet the SGTR accident acceptance criteria with a charging loop isolation valve postulated failed open.
Please feel free to contact me or Robert J. Murillo should you have any questions.
Yours very truly,
{.O~.-- (j'Y K.W. Cook )!V Nucicar Support & Licensing Manager KWC/RJM/pc1 Attachment cc: B.W. Churchill, W.M. Stevenson, R.D. Martin, D.M. Crutchficid, J. Wilson, T.A. P11ppo G506170205 050613 ap PDR ADOCK 050003G2
L
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'. n i DEPRESSURIZATION CAPABILITY WITH DEGRADED AUXILIARY PRESSURIZER SPRAY l
1.0 INTRODUCTION
l While reviewing information to address NRC questions concerning the l
Decay Heat Removal Capability at Waterford 3, a potential single failure vulnerability in the pressurizer auxiliary spray system was identified.
Auxiliary spray would be used to depressurize the RCS during a Steam Generator Tube Rupture (SGTR) event with main spray unavailable (reactor
^
' coolant pumps not running). To initiate auxiliary spray the operator must close both charging loop isolation valves, CVC-218A and CVC-218B (See l
Figure 1-1). If one of the valves fails to close (i.e., mechanically sticks open), then some of the flow would be diverted to the charging line instead of to the pressurizer due to differences in elevation and flow resistance. Thus the spray flow might be insufficient to depressurize the RCS and minimize the radiological consequences of the event.
To respond to this concern, LP&L has performed a test at the Waterford -
3 plant to determine the depressurization rate using auxiliary pressurizer spray with one charging loop isolation valve open. In addition, a SGTR analysis with degraded auxiliary spray has been performed to verify that the V~
acceptance criteria given in SRP 15.6.3 and 10 CFR 100 can be met. This report addresses the license requirement imposed by NRC to submit the results of a confirmatory depressurization test and demonstrate that the '
auxiliary pressurizer spray can perform the necessary depressurization to meet the SGTR acceptance criteria (SRP 15.6.3) with a charging loop isolation valve failed open.
1
, o
. g Section 2 provides a susunary of the results of both the test and analysis. Section 3 describes the degraded auxiliary spray flow test performed at Waterford 3. Section 4 describes the SGTR analysis performed with a degraded auxiliary spray flow. Section 5 provides the conclusions from this study. A comparison of the analysis given in this' report to the SGTR analysis in Section 15.6 of the FSAR is presented in Appendix A.
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SUMMARY
This report confirms that if a charging loop isolation valve failed open during a SGTR event, the' acceptance criteria (radiological dose consequences) would be met. Test results showed that an auxiliary spray flow rate of about 37 gpm was achieved with a charging loop isolation valve open. Analysis of a SGTR with an auxiliary spray flow rate of only
~
10 gpm showed that the offsite radiological dose released.was well below the
-acceptance criteria given in 10 CFR 100. Thus, since the actual spray flow rate was much greater than the acceptable spray flow rate from the analysis,
. the auxiliary spray system can perform its function during a SGTR event with one charging loop isolation valve failed open such that the acceptance criteria are' met.
The analysis showed that depressurization during a SGTR with a degraded spray flow rate of 10 gpm was controlled predominately by adjusting HPSI flow.
The spray flow served to initiate the drop in pressure that allowed HPSI flow to increase and fill the pressurizer. With an adequate level in the pressurizer (and subcooling), the operator would throttle the HPSI flow according to the Emergency Operating Procedures and depressurize the RCS. .
Shutdown cooling conditions were reached with the radiological dose consequences well below the acceptance criteria given in 10 CFR 100, e-This report confirms thar *he acceptance criteria for radiological release during a SGTR with a tharging loop isolation valve failed open can be met with the existing Waterford 3 design. The results show that the public health and safety are satisfactorily protected ,ithout any plant
. modifications.
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s 3.0 AUXILIARY SPRAY FLOW TEST A test was performed at Waterford 3 to measure the depressurization rate using auxiliary spray with one charging loop isolation valve open. The test was performed during the startup test program with the RCS at 545'F and 2250 psia. Two charging pumps were used to provide spray flow. This is based on the Technical Specification requirement that two charging pumps be operable and the operator uses both pumps to maximize the spray flow rate during the postulated SGTR. The charging isolation valve CVC-218B was opened because this line has a slightly lower flow resistance than the other charging line.
.This minimizes the auxiliary spray flow. The reactor coolant pumps were tripped and not running during the test. The initial test conditions are given in Table 3-1.
The test was initiated by starting auxiliary spray flow from two charging pumps (88 gpm) with both charging loop isolation valves closed.
After the pressure decreased about 100 psi, one charging loop isolation valve (CVC-218B) was opened. The depressurization with the degraded spray flow continued until the pressurizer pressure decreased to 2000 psia.
The depressurization from this test is shown in Figure 3-1 and Table 3-2.
The initial depressurization rate with full flow from two charging pumps was about 60 psi / min. When a charging loop isolation valve was opened, the e depressurization rate dropped to 24 psi / min.
A calculation was performed using the RETRAN-02 computer code to deter-mine the degraded auxiliary spray flow rate corresponding to the measured depressurization rate.
For a flow rate of 88 gpm, the calculated depressur-Tzation rage was 59 psi / min. This agrees well with the measured rate for the
. a initial part of the test and therefore verifies the adequacy of the calculation. A depressurization rate of 24 psi / min. was calculated with an auxiliary, spray flow rate of 37 gpm. Thus, with a charging loop isolation valve open, an auxiliary spray flow rate of about 37 gpm was achieved. This matches the average spray flow of 36 gpm measured by a sonic flow measurement device during a portion of the time with degraded spray.
The test was performed with a pressurizer level of about 35% (10.5 ft.).
A lower level would reduce the elevation head seen by the charging flow. This would result in a higher charging flow and lower spray flow when the charging isolation valve was open. A difference of 10.5 ft. however would reduce the auxiliary spray flow rate by only a small amount (less than 5 gpm).
6 I
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TABLE 3.1 DEGRADED AUXILIARY SPRAY INITIAL TEST CONDITICNS Pressurizer Pressure, psia 2243 Pressurizer Level, % 34.6 Average Cold Leg Temperature. *F 535 Average Hot Leg Temperature. 'F 535 Regenerative' Heat Exchanger Outlet (Charging / Spray)
Temperature. *F' 354 Reactor Coolant Pumps Not Running Charging Pumps B, A/B Running 1
. o TABLE 3.2 DEGRADED AUXILIARY SPRAY TEST DEPRESSURIZATION Time (Min.) Pressurizer Pressure (PSIA) 0 2242.7 1.0 2241.7 2.0 2241.0 3.0 2239.5 3.5 2214.0 4.0 2181.7 4.5 2154.0 5.0 2135.2 5.5 2128.5 6.0 2121.0
. 6.5 2107.5 7.0 2094.0 7.5 2080.5 8.0 2067.0 8.5 2054.2 9.0 2041.0 9.5 2029.5 10.0 2016.7 10.5 2004.7 Auxiliary Spray valve opened at 3.1 minutes.
Charging loop isolation valve opened at 4.8 minutes.
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FIGURE 3-1 DEPRESSURIZATION FOR DEGRADED AUXILIARY SPRAY TEST (MARCH 11, 1985)- ,
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-pPENSPRAYVALVE 2200 - 60 Psi Min Q
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-END TEST v
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4.0 SGTR ANALYSIS An analysis of a single double ended Steam Generator Tube Rupture (SGTR) event with degraded auxiliary spray flow has been performed.
Degraded spray flow would result in a reduced RCS depressurization capability 1
and, therefore^ would increase the time needed to minimize the primary to secondary' leak rate. It would also increase the time necessary for the RCS to reach shutdown cooling conditions. The analysis was performed to determine that, with degraded auxiliary pressurizer spray, the acceptance criteria (radiological dose released) for the SGTR event can be met.
4.1 Analysis Method and Assumptions The SGTR analysis presented in this report assumed that with two charging pumps operating, an auxiliary spray flow rate of only 10 gpm was achieved. The remaining 78 gpm flowed to the RCS cold leg through the failed 1,
open charging loop isolation valve. The transient simulation was run for 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. ,
The radiological dose to the thyroid at the exclusion area boundary (2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />, EAB), and the low population zone (8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />, LPZ) were calculated. The dose for both the Preaccident Iodine Spike (PIS) and the accident Generated i Iodine Spike (GIS) were calculated as identified in Standard Review Plan Section 15.6.3 e.
The analysis was done using the CESEC-III computer code prior to and shortly after reactor trip. The CEPAC code, which is a long term cooldown
, algorithm based on CESEC-III, was used after reactor trip during plant cooldown. CESEC-III is used by Combustion Engineering for licensing analyses presented in Chapter 15 of the FSAR and support of plant start-up tests.
CEPAC was used for the cooldown because of its ability to simulate operator actions and calculate the offsite dose release.
The method and assumptions of the analysis are given below:
- 1. Reactor trip was initiated by the Core Protection Calculators (CPCs) on the approach of the RCS hot legs to saturation conditions. Reactor trip could also have been initiated by CPCs on a pressurizer pressure out of range low (1845 psia) signal with no change in results since the two trip signals occurred at
~
almost the same time.
- 2. Offsite power was assumed to be available.
- 3. The steam bypass system, although available, was not credited in the calculation of radiological doses. This maximized the radiological consequences for the event since steam was released directly to the atmosphere.
- 4. The Waterford 3 Emergency Operating Procedure, OP-902-007, (EOP) for a SGTR (which is based on the NRC approved guidelines developed by the CE Owner's Group in CEN-152) was followed in simulating e
operator actions during the plant cooldown. A concise summary of the operator actions is given in Figure 4-1.
. +
- 5. Subsequent to reactor trip, it was assumed that five minutes passed (wherein the operators perform the Emergency Entry Procedure) before the operators determined that a SGTR event occurred.
Also,'a minimum of two minutes was assumed between a set of related operator actions. For instance, if the operator detected that the subcooling margin was too high he may do one or all of the following simultaneously (which are considered a related set of operator i
actions): throttle HPSI flow, turn on auxiliary spray, or turn off pressurizer heaters. These " timing" assumptions are consistent with ANSI-N660.
- 6. The RCPs were tripped by the operator when the RCS pressure dropped to 1621 psia. The RCPs (and main pressurizer spray) were 4
not available for the duration of the event.
- 7. Consistent with the E0P, the RCS hot legs were cooled to 550*F (at 100*F/HR per the Technical Specifications) using the Atmospheric Dump Valves (ADVs) for both steam generators before isolating the affected steam generator.
- 8. High Pressure Safety Injection (HPSI) flow was throttled only
.when all the termination criteria were satisfied (Subcooling 1 28*F, and PZR level 1 28%, and available SG wide range level is y both 1 50% and constant or rising).
- 9. Control of the affected steam generator level was performed with '
the steam generator blowdown system to maintain level at 85-90%
4 Wide Range. The unaffected steam generator level was maintained r
using the main feedwater control system at about 68% Narrow Range.
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- 10. It was assumed that the operator did not stop the depressurization in order to collapse the steam void formed in the reactor vessel upper head.
- 11. The discharge.of fluid through the blowdown system was accounted for in the radiological release calculation in the same manner as the leak from the RCS. The flashed fraction of steam in the blowdown flash' tank is treated as steam released directly to the atmosphere with a partition coefficient of 0.01.
- 12. The assumptions used for the radiological dose calculation are given in Table 4-1 and are the same as that specified in the FSAR and Standard Review Plan Section 15.6.3
- 13. The enthalpy of the auxiliary pressurizer spray was held constant at a value based on normal operating conditions with letdown.
The decrease in spray temperature as letdown (RCS) temperature decreased was not accounted for. The high spray temperature reduced the effectiveness of the spray to depressurize the RCS.
- 14. Nominal full power values were used for the initial conditions as listed in Table 4-2.
t 4.2 Analysis Results The radiological thyroid dose results are given in Table 4-3. As can be seen, the dose released for a SGTR with only 10 gpm auxiliary spray is
well below the 10 CFR 100 limit for both GIS and PIS assumptions. The major contribution to the dose is due to steam released from the affected steam generator. This is a conservatively high dose release due to the analysis assumptions and operator actions.
The thermal-hydraulic response for a SGTR with 10 gpm auxiliary spray flow is shown in Figures 4-2 to 4-8. Table 4-4 lists the sequence of events.
The reactor coolant system began to depressurize when the tube rup-ture was initiated (Figure 4-2). The pressure continued to decrease until a reactor trip signal was generated at 13 minutes by the CPC on the approach to hot leg saturation conditions. After reactor trip, the RCS pressure decreased rapidly and initiated safety injection. The pressurizer emptied (Figure 4-3) shortly af ter reactor trip due to the leak flow and RCS shrinkage. The RCPs were tripped by the operator due to low RCS pressure
At about 20 minutes the operator started to cool the RCS until the hot leg temperature (Figure 4-4) was below 550 F using ADVs in both steam generators. The affected steam generator was then isolated and the cooldown to an unaffected loop hot leg temperature of 500*F was continued using the e unaffected steam generator. During this time the pressure remained i
relatively constant with pressurizer level near zero and subcooling increasing. At 80 minutes, RCS hot leg temperature reached 500 F and auxi-liary spray was initiated to depressurize the RCS.
Pressurizer pressure decreased due to the auxiliary spray flow. This allowed HPSI flow (Figure 4-5) to increase and begin filling the pressurizer.
The rise in pressurizer level compressed the steam space causing pressure to increase slightly. The pressure leveled out at a value where compression of the steam space was balanced by condensation from the auxiliary spray.
Pressure remained constant until pressurizer level increased to the value that the HPSI flow could be throttled according to the termination criteria in the E0P. The reduced HPSI flow caused the pressure to drop, but also caused the pressurizer level to decrease below the safety injection termination criteria.
The HPSI flow was therefore increased to reestablish the pressurizer level
, which caused the RCS pressure to increase. Subsequent throttling of the HPSI flow, governed by the need to maintain adequate pressurizer level and sub-cooling (Figure 4-6), controlled the depressurization rate. The oscillations in the pressurizer pressure and level were due to these adjustments in the HPSI flow rate. The primary to secondary leak rate (Figure 4-7) decreased as RCS pressure decreased. Shutdown cooling conditions were reached at 5.8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> after the tube rupture.
Throughout the natural circulation cooldown (as specified in the E0P),
the optimum temperature difference between the secondary sides of the steam generators was maintained. This was done in a conservative manner by assuming that the operator periodically opened the ADV on the affected steam generator to reduce its temperature (Figure 4-8). The increased steam ,.
release from the affected steam generator causes a higher radiological dose to be calculated than if the affected steam generator ADV were kept closed.
This is a conservative analysis assumption since the Waterford 3 E0P does not call for the affected steam generator ADV to be opened in this situation.
Instead, the operator would use feedwater and blowdown to feed and drain the affected steam generator, thereby reducing its temperature.
4.3 Analysis Conservatisms The SGTR analysis described above includes conservative assumptions and methods. Some of these conservatisms are identified below.
- 1. The auxiliary spray temperature was maintained constant at 375'F.
Not accounting for the decrease in spray temperature as RCS letdown temperature decreased resulted in a reduced depressurization capability for auxiliary spray as shutdown cooling conditions were approached.
- 2. The auxiliary spray flow rate used for the analysis (10 gpm) was well below the calculated spray flow rate achieved during the test (37 gpm).
- 3. Steam was periodically released during the cooldown from the affected steam generator through the ADV to cool the steam generator and maintain the optimum temperature difference between steam generators. This resulted in a higher radiological dose release than if the affected ADV were kept closed.
- 4. The Steam Bypass Control System, which directs steam to the condenser, was not credited. This would reduce the radioactivity e released due to scrubbing and dilution with the condenser water.
Releasing steam directly to the atmosphere through the ADV maximized the radiological dose release.
. +
- 5. Conservative atmospheric dispersion factors were used that are
/
consistent with the SGTR analysis in FSAR Section 15.6 and SRP 1
15.6.3. Best estimate values would significantly reduce the cal-4 culated offsite dose.
- 6. Initial activity levels in the RCS and steam generator were taken to be at the Technical Specification limit. Typical values would be much lower.
- 7. The Shutdown Cooling (SDC) System was not used as soon as the RCS conditions would allow SDC to be entered. The additional steam released from the steam generators during the two hours af ter SDC conditions were reached resulted in a higher radiological dose release than if SDC had been entered as soon as possible.
4
Table F1 ' -
Radiological Considerations PIS - Coincident (existing) 1317 spike 60 uCi/gm 2
GIS - Spiking Factor (Increase in Iodine Release Rate From Fuel Rods Due to Reactor Trip) 500 131 Ao -
Initial Primary Fluid Activity 7 2
Dose Equivalent 1.0 uCi/gm 131 A
gg Initial Secondary Fluid Activity 7 2
Dose Equivalent 0.1 uCi/gm H -
Partition Coefficient (ratio of iodine concentration in vapor to iodine concentration in water within affected steam generator) 0.01 BR -
Breathing Rate -4 3 M
3.47 x 10 sec X/Q -
Exclusion Area Boundary (0-2 HR) Atmospheric -4 Dispersion Factor se 6.3 x 10 3 M
X/Q -
Low Population Zone Outer Boundary (0-8 HR) -5 Atmospheric Dispersion Factor 7.1 x 10 sec M
Leak Rate - Primary to Secondary Leak Rate Within yM Intact Steam Generator min
+
,, _ _ _ _ _ _ ,y.
Table 4-2 Initial Conditions for the Steam Generator Tube Rupture Analysis with Degraded Auxiliary Spray Assumed Parameter Value
' Core Power Level, MWt 3410 Core Inlet Coolant Temperature, 'F 553 Reactor Coolant System Pressure, psia 2250 6
Core Mass Flow Rate, 10 lbm/hr 143 Steam Generator Pressure, psia 900 Moderator Temperature Coefficient, 10-4 ao/*F -0.68 ,
Pressurizer Water Level, percent 55 Core Protection Calculator (CPC) Temperature Margin Necessary to Generate Reactor Trip Signal, *F 13 Trip Delay Time from CPC Generated Signal to Time When Reactor Trip Breakers Open, seconds 0.70
^
1 .
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TABLE 4-3 RADIOLOGICAL DOSE TO THYROID, REM 2 HR, EAB 2 HR, EAB 8 HR, LP3 8 HR, LP3 GIS PIS GIS PIS SGTR with Degraded Spray-(10 GPM) 3.9 15. 2.8 3.7
~
Acceptance Criteria from 10 CFR 100 and Standard Review Plan 15.6.3 GIS = 30 REM PIS = 300 REM
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TABLE 4-4 SEQUENCE OF EVENTS 10 GPM AUXILIARY PRESSURIZER SPRAY TIME SETPOINT (sec) EVENT OR VALUE 0.0 Tube rupture occurs 15 Letdown Control Valve throttled to minimum position ---
28 2nd Charging Pump On, pER level, feet below programmed level -0.75 28 Full Output Proportional Heaters, PER pressure, psia 2225 42 3rd Charging Pump On, PER level, feet below programmed level -1.16 57 Back-Up Heaters On, Pressurizer pressure, psia 2200 445 All heater cut off, pressurizer liquid water volume, Ft % 334/28 774 CPC Hot Leg Saturation Trip Signal Approximately 13*F away from sr.turation temperature --
775 Turbine Stop Valves closed, CEAs begin to drop Minimum SG 1evel, % Wide Range 70 Main Feedwater Control System begins to ramp down to 5% (Reactor Trip Override Setting) ---
780 Main Steam Safety Valves (MSSVs) open, psia 1070 783 Maximum steam generator pressure, both SGs, psia 1100 789 Pressurizer empties ___
790 RCPs tripped manually on low RCS pressure, psia
- 1621 794 Main Feedwater Control System supplying 5%
Flow 827 MSSVs closed, psia (Cycle thereafter until ADVs are opened) 1017 840 SIS starts to supply flow, psia 1400
TABLE 4-4 (C:ntinued)
SEQUENCE OF EVENTS 10 GPM AUXILIARY PRESSURIZER SPRAY TIME (sec) SETPOINT EVENT OR VALUE 1195 Operator starts to use ADV's to cool RCS temperature (hot legs) to 550*F. Cooldown rate = 100*F/HR ---
2808 Operator isolates the damaged steam generator, RCS hot leg temperature. *F '
i 550 4810 Unaffected SG hot leg temperature equals 500*F. Operator re-establishes letdown flow (letdown control valves in "AUT0") . Operator initiates auxiliary PER spray to depressurize RCS to 1000 psia ---
8946 Operator detects RCS pressure equal to 1000 psia ---
Operator starts to cool RCS at 50*F/HR using unaffected steam generator Operator controls auxiliary spray flow, pro-portional heater output, and HPSI flow to reduce RCS pressure, control subecoling, and maintain primary system inventory 20,808 Operator detects shutdown cooling conditions, unaffected hot leg temperature, *F/RCS pressure, psia 343/391 SDC Entry Conditions = cold leg temperature unaffected SG g 350*F and PER pressure between 392 psia and 350 psia.
Subsequently, operator tries to maintain these conditions 28,800 End of Transient #
FIGURE 4-1 ;
, OPERATOR ACTIONS FOR A SGTR !
FROM WATERFORD 3 OP-902-007 Cooldown RCS to below 550*F with both SGs u
Isolate Affected SG h
Cooldown RCS to 500*F (at 100*F/hr) using ADV on unaffected SG n
When RCS at 500*F, depressurize to 1000 psia uring auxiliary spray, Re-establish letdown flow.
u
~
Cooldown and depressurize RCS to Shutdown cooling conditions. Maintain optimum 4T between SGs.
Too Rapid: Too Slow:
Close ADV on :
Control Cooldown to650*F/hr x Open ADV on Unaffected SG Unaffected SGl Too High: y -
Too Low:
Aux. Spray on Aux. Spray off Heaters off : Control subcooling ?!: 28'F n Heaters on Decrease HPSI Increase HPSI Close ADV Open ADV Too High: '
Too Low:
Decrease HPSI -: Control pressurizer level 2: 28% :-- Increase HPSI h
Control SG 1evel to 77% - 94% WR using the blowdown system for the affected SG and 60% ~70% NR using main feedwater for ,,
the unaffected SG.
v Achieve Shutdown cooling conditions at 350*F and 392 psia
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5.0 CONCLUSION
This report confirms that if a charging loop isolation valve failed open during a SGTR event, the acceptance criteria (radiological dose consequences) would be met. Test results showed that an auxiliary spray flow rate of about 37 gpm was achieved with a charging isolation valve open.
This flow rate is much greater than the 10 gpm assumed in a SGTR analysis that showed the radiological dose released was well below.the acceptance criteria limits. Thus, the auxiliary spray system can perform its function
'. during a SGTR event such that the acceptance criteria are met.
This report confirms the inherent safety capability of the Waterford 3 plant to cope with various operational events and accidents.
k
Appendix A COMPARISON TO FSAR RADIOLOGICAL RELEASE RESULTS The radiological consequences calculated for the SGTR analysis presented in this report are compared to the results given in Section 15.6 of the FSAR in Table A-1. The results for this analysis show a higher radiological dose release then was calculated for the FSAR. This is not due to degraded auxiliary pressurizer spray, but is caused by.other analysis assumptions related to operator actions. Although a meaningful comparison between an FSAR analysis done for the purpose of licensing the plant and a more realistic analysis can not be made, the following describes the differences from the FSAR calculation that result in higher radiological dose.
The SGTR analysis presented in the FSAR is for a " stylized" event done with a prescribed set of assumptions. An important assumption for this comparison is that the operator takes no action for the first 30 minutes of the event. This means that the steam released to the atmosphere from the affected steam generator (the major cont * ".bution to the radiological dose) comes from a brief period where the tea safety valves popped open to limit steam pressure. After 30 minute. it i. s;sumed that the operator isolates the affected steam generator so there is no more steam released from it.
In the SGTR analysis presented in this report, operator action as identified in the SGTR Emergency Operating Procedure is accounted for. The key action for this comparison is that the operator opens an Atmospheric Dump Valve (ADV; assuming that the turbine steam bypass valves are not available) in both steam generators to cool the RCS hot legs before the
affected steam generator is isolated. The ADV in the affected steam generator was also opened periodically during the cooldown to maintain the optimum steam generator temperature differential (AT). This increases the amount of steam released to the atmosphere from the affected steam generator which increases the radiological dose consequences. Also, this analysis conservatively accounts for the release of activity from water removed from the affected steam generator through the blowdown system.
The basis for the first operator action is to quickly cool the RCS below the temperature at which heat transfer from the RCS would cause the steam generator safety valves to open. If the safety valves opened, there is a risk that one or more might fail open. With no block valve in this release path, the radiological dose consequence would be much more severe.
T,hus, the safer action is to cool the RCS quickly, using the ADVs if necessary, even though this results in a higher dose than calculated for the FSAR event. This action is consistent with CE's Emergency Procedure Guidelines that have been reviewed in detail and approved by NRC.
The optimum steam generator 6T is maintained to assure that natural circulation continues in the RCS loop with the affected steam generator.
In order to maximize the radiological dose released, this analysis assumed that the ADV was opened to cool the affected steam generator within the optimum AT. This is conservative analysis assumption since the Waterford 3 e-E0P does not allow the affected steam generator ADV to be opened af ter the initial RCS cooldown. Although these actions result in more steam being j released from the affected steam generator, the calculated dose is still l well below the acceptance criteria given to 10 CFR 100.
1 1
, o In conclusion, the_ higher radiological dose calculated for this analysis compared to the FSAR SGTR analysis is due not to degraded auxiliary spray, but rather, analysis assumptions related to operator actions.
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_ TABLE A-1 SGTR THYROID DOSE RESULTS, REM Y
2 HR, EAB 2 HR, EAB 8 HR, LPE '8 HR, LPE GIS PIS g73 pyg d
Degraded Spray 3.9 15 2.8 3.7
- FSAR 0.8 0.51
. 03 .06 4
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