IR 05000338/1987036

From kanterella
Jump to navigation Jump to search
Insp Repts 50-338/87-36 & 50-339/87-36 on 871020-1119. Violations Noted.Major Areas Inspected:Plant Status, Unresolved Items,Ler Followup,Esf Walkdown,Verification of Containment Integrity & Security
ML20235A260
Person / Time
Site: North Anna  Dominion icon.png
Issue date: 12/28/1987
From: Caldwell J, Cantrell F, King L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20235A188 List:
References
50-338-87-36, 50-339-87-36, NUDOCS 8801120172
Download: ML20235A260 (14)


Text

_ _ _ - _ . - _ _ _ _ ._ ,- _ _ _ _ _ _ __. _ . _ _ _ _ _ _ _ _ _ _ .. _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ .____

-'

( BRECO UNITED STATES

  1. o MUCLEAR REGULATORY COMMISSION

",*

.!' N s REGION 11 l h ' I MARIETTA STREET, N.W.

,

"'

[t '

~

ATLANTA, GEORGI A 30323

,o

.....  ;

,

Report Nos.: 50-338/87-36 and 50-339/87-36 )

y Licensee: Virginia Electric & Power Company  !

Richmond, VA 23261 g Dock'et Nos.: 50-338 and 50-339 Facility Name: North Anna 1 and 2 Inspection Conducted: October 20 - November 19, 1987 Inspectors: f' W /

. J. L. aldwell 7M, /2[28!b)

Dhte Signed h b , SRIAA - /z/28/B7 L.~ P: g, RI '/ j Date Signed Approved by:

'

/l% a O 9 7

~

/F CantrelT, Section ef // Date S'igned ivision of Reactg P ojects SUMMARY Scope: This routine inspection by the resident inspectors involved the following areas: plant status, unresolved items, licensee event report (LER followup), review of inspector follow-up items, monthly maintenance observation, monthly surveillance observation, ESF walkdown, verification of containment integrity, operator safety verification, operating reactor events; instruments- l tion problems related to startup of Unit 2 from refueling, and securit During the performance of this inspection, the resident inspectors conducted reviews of the- licensee's backshift operations on the following days'-

, October' 21, 22, 27 and 29 and November 2, 3, 4, 6, 17 and 1 Results: Three violations were identified: Two of these violations, one with five examples, were for inadequate procedures and failure to follow procedures (paragraphs 6, 8,10, 11 and 13). The third violation was for changing the intent of a surveillance procedure without prior approva {DR ADOCK 05000338 PDR

_ - _ _ _ _ . - - _ - _ _ - _ _ _ _ _ _ - ._ _ _ _ _ _ _ _ _ _ _ _ _ _ - -

l

l REPORT DETAILS Licensee Employees Contacted ,

  • E. W. Harrell, Station Manager

. C. Driscoll, Quality Control (QC) Manager

  • G. E. Kane, Assistant Station Manager M. L'. Bowling, Assistant Station Manager
  • R. O. Enfinger, Superintendent, Operations
  • R. Kansler, Superintendent, Maintenance
  • A. H. Stafford, Superintendent, Health Physics J. A. Stall, Superintendent, Technical Services J. L. Downs, Superintendent, Administrative Services

~

J. R. Hayes, Operations Coordinator D. A. Heacock, Engineering Supervisor D. E. Thomas, Mechanical Maintenance Supervisor G. D. Gordon, Electrical Supervisor

  • L. N. Hartz, Instrument Supervisor F. T. Terminella, QA Supervisor J. P. Smith, Superintendent, Engineering D. B. Roth, Nuclear Specialist J. H. Leberstein, Engineer
  • G. G. Harkness, Licensing Coordinator i
  • T. Johnson, Supervisor, Quality Other licensee employees contacted include technicians, operators, mechanics, security force members, and office personne * Attended exit interview ,

NRC Regional Management Site Visit: J. N. Grace and F. S. Cantrell visited North Anna Power Station on November 19, to present certificates to recently licensed operator i Exit Interview (30703)

The inspection scope and findings were summarized on November 19, 1987, with those persons indicated in paragraph 1 abov The licensee acknowledged the inspectors findings. The licensee did not identify as proprietary any of the material provided to or reviewed by the inspectors during this inspectio (0 pen) Unresolved Item (338,339/87-3. 11) Potential Flooding of Safety Related Equipment (paragraph 5).

(0 pen) Violation (338,339/87-36-02) Violation of Technical Specification 6.8.1 for failure to follow procedures and inadequate procedures with five examples (paragraphs 6, 8,11 and 13),

(0 pen) Unresolved Item (338,339/87-36-03) Potential Inadequate Post Maintenance Testing (paragraph 12).

L-_-_______

- _ _ _ _ - _ _ _

.

.

i

'

l (0 pen) Violation (339/87-36-04) Inadequate Procedure Resulting in the Overloading of the 2J Emergency Diesel Generator (paragraph 10).

(0 pen) Violation (339/87-36-05) Viciation of Technical Specification 6. by changing the intent of a surveillance procedure without prior safety committee approval, f 3. Plant Status Unit 1 l Unit 1 began the inspection period operating at approximately 49fs power, waiting on NRC concurrence in the acceptability of steam generator repairs and the surveillance program to promptly detect steam generator tube leaks at full power. On October 26, the lower radial bearing of the "B" Reactor Coolant Pump (RCP) was damaged while manipulating the oil level to. clear an alarm. The "B" RCP is being monitored by the licensee and the bearing temperature and. vibration monitors indicate that the pump is stable and j acceptable-for continued operation (See Section 10 for details). '

On November 5, the NRC issued a revised Confirmation of Action Letter 1 (CAL) allowing the licensee to increase power to 100?;. On November 9, the Region and Headquarters Staff briefed the Commissioners in Washington on the Steam Generator Tube Rupture (SGTR) event of July 1 At the end of the inspection period Unit I was operating at 100?4 powe Unit 2 j Unit 2 began the inspection period in Mode 5, day 59, of the refueling outage. On October 22, the "C" accumulator was injected into the Reactor

'

Coolant System (RCS) (which was partially drained at the time) while performing a . valve stro ki ng surveillance procedure (See Section 8 for details). On October 23, the licensee was informed by the NRC that the ,

e only acceptable retest for the overhaul of the Inside Recirculation Spray I Pumps (IRSP) was a hydraulic test' (See Section 7 for details). On .

October 26, while performing an 18-month surveillance test, the 2J  !

Emergency Diesel Generator (EDG) was electrically overloaded due to an ,

inadequate procedure (See Section 10 for details). Also, on October 26, I while performing a valve stroking surveillance test, the operating charging pump discharge was aligned to the RCS which was solid and 4 resulted in the lifting of the pressurizer PORV (See Section 8 for ,

details). On October 27, the licensee satisfactorily completed the hydraulic retest of the IRSPs. On October 31, while in Mode 4 with the scram Dreakers closed, the engineering staff performed a surveillance test which resulted in an unexpected reactor trip signal and opened the scram breakers (See Section 11 for details).

On November 3, Unit 2 commenced a reactor startup. During the startup and i performance of reactor physics testing, power range instrument N44, which

'

had previously been made inoperable to support physics testing, was i discovered by the operator to not have been placed in trip as required by technical specification When the instrument was placed in trip, the method used caused an inadvertent cooldown of the RCS to less than 541 i

__ ___ _ _ _ _ _ _ _ _ _ ___

___

.

degrees F which is also in noncompliance with technical specification (See Section 13 for details). On November 4 with the unit in Mode 1, less than 10% power, the licensee was unable to trip the turbine without using the local mechanical trip lever (See Section 10 for details). Aiao on ~

November 4, the TS 3.0.3 shutdown statement was entered due to inoperable reactor protection system instrumentation (See Section 12 for for details).

This instrumentation was corrected and the shutdown was terminated at 0032 on November Unit 2, as of the end of the inspection period, was operating at approximately 100% powe !

4. Unresolved Items An Unresolved Item is a matter about which more information is required to determine whether it is acceptable.or may involve a violation or devia-tio Two unresolved items were identified during this inspection and are discussed in paragraphs 5 and 1 . Licensee Event Report (LER) Follow-Up (90712 & 92700)  ;

The following LERs were reviewed and closed. The inspector verified that reporting requirements had been met, that causes had been identified, that corrective actions appeared appropriate, that generic applicability had been considered, and that the LER forms were complete. Additionally, the inspectors confirmed that no unreviewed safety questions were involved and that violations of regulations or Technical Specification (TS) conditions had been identifie (Closed) 338,339/P2186-03: BBC Brown Boveri K600/K800 Circuit Breakers Wire Harness Packing Gear In Contact With Wiring Harness and Wore a Hole Thru Insulation and Severed a Wire In Harness. The licensee has inspected  !

the breakers and they were found to have no wiring harness damag l (Closed) 338,339/P2187-01: Diaphragm Seal Plate Welded to Recirc Spray )

Heat Exchanger Head Flange Could Exceed Fatigue Life on a Limited Number l of Overpressurizations The licensee has replaced the diaphragm plates on I Units 1 and 2 Recirculation Spray Heat Exchangers with much thicker j plate .

'

l (Closed) LER 338/85-03 and Rev.1: Flooding Potential Not Previously i Evaluated. The inspector had reviewed this LER previously and determined I that the licensee had not taken any permanent corrective actio The licensee was requested to determine if any permanent corrective action was required. The licensee's evaluation concluded that a concrete wall would have to be constructed on the west wall of the turbine building to ensure the turbine building equipment and some safety related equipment would not be damaged during a worst case flood. This wall is scheduled to be constructed in 198 In the mean time the licensee has procedures covering lake level control, shutting down the reactors if the level gets too high and emergency procedures covering damage to safety related l

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ -

_ _ _ _ - _ _ _

!

equipment. Long term corrective action had not been developed promptly by the licensee. This LER will be closed and identified as an Unresolved Item (338,339/87-36-01) pending further evaluation by the inspecto !

!

(Closed) LER 339/86-09: Reactor Trip - June 29, 1986. The licensee has evaluated the 500-230KV transformers isolation. A new breaker was installed and a wiring change has been made to. isolate bus 2 by taking its feed from Ladysmith line 52 (Closed) LER 338/87-08: High Lift Pressure Setpoint on Pressurizer Safety Valves. The licensee analyzed the "as found" high lift setpoint using the most limiting overpressurization analysis. The design basis for the unit and the safety valves was still me (Closed) LER 338/87-05: I-131 Dose Equivalent Greater Than Microcurie / Gram. The increase of I-131 dose equivalent specific activity was caused by minor fuel cladding defects which were present- in the reactor core during a rapid power decreas (Closed) LER 338/87-02 (Rev. 1): . Malfunctioning Cardreaders Resulted in Potential for Unauthorized / Undetected Access -Into Vital Areas. The licensee has taken corrective actio . Review of Inspector Follow-up Items (92701)

(Closed) Unresolved Item 338/87-34-02: Potential failure to follow procedure violation which resulted in the draining of the Refueling Water Storage Tanks (RWST) below the TS limi This unresolved item is classified as a violation based on the inspector's review of the even The operator, while securing makeup to the Unit 1 RWST from the Unit 2 blender, did not follow the lineup sequence established by 1-0P-7.7, Operation of RWST Systems. This f ailure to follow procedure resulted in the inadvertent draining of the RWST below the TS limits and is identified as'the first example of violation 338,339/87-36-0 e 7. Monthly Maintenance (62703)

Station maintenance activities affecting safety related systems and components were observed / reviewed, to ascertain that the activities were conducted in accordance with approved procedures, regulatory guides and industry codes or standards, and in conformance with the Technical Specification The inspectors reviewed MMP-C-RS-1, the mechanical maintenance procedure for containment inside recirculation spray pump The inspectors also observed portions of :the disassembly of the pumps. The "B" inside recirculation spray pump had a bearing replaced during the outage and both pumps were torn down for the five year inspectio The licensee had committed to performing a hydraulic test of the pumps  !

'

following the inspection This commitment was made back in 198 However, following this inspection the licensee informed the NRC that they were not going to flow test the pumps with water but just dry test the pumps to prove operabilit This dry test is the method used by the l

- --__________j

_- _ _ _

-

i

'

l

5

[

licensee to comply with the ASME Section II testing requirements and was submitted to the NRC as a relief request. However, this relief request .

had not been reviewed by the NRC. After several discussions with the l Region and Headquarters staff, the inspectors informed the licensee on '

October 23 that the dry test was not adequate to determine operability of the pumps following major maintenanc The inspectors witnessed the pump operability recirculation test of both inside recirculation spray pumps on October 27. This test was completed without any major impact on the outage schedul The 2A charging pump had been removed from service to perform maintenan'

on the seals and discharge check valve during performance of 2-PT-21 The pressure had dropped off when the discharge valve was opened indicating that the check valve was not seating. Maintenance opened up the valve and verified freedom of movement and the pump was reteste The pressure-still dropped of The pump was tagged out and the check valve blue  ;

checke It will be ground in to reseat it and reteste Previous problems with the discharge check valve on pump 2C (Inspection Report 87-06) indicated grit in the swingarm and it was cleaned and reteste No violations or deviations were identifie . Monthly Surveillance (61726)

The inspectors observed / reviewed technical specification required testing and verified that testing was performed in accordance with adequate procedures, that test instrumentation was calibrated, that limiting conditions for operation (LCO) were met and that any deficiencies identified were properly reviewed and resolve ,

The inspectors observed 2-PT-61.4, RCS Pressure Isolation Valves Leakage Test. Portions of the test included testing of the low head safety injection discharge header valves to the hot and cold legs of the RC Also, the valves off the charging pump alternate discharge header were observe No problems were identifie On October 22, the licensee notified the inspectors that the Unit 2 "C" accumulator had been inadvertently injected into the RCS. At the time of the injection, Unit 2 was in Mode 5, with the RCS drained to approximately 10 inches above vessel nozzle center line. The injection occurred when an operator stroked the "C" accumulator discharge valve per surveillance test 2-PT-21 The inspector reviewed the surveillance procedure and determined that the procedure was established to perform the valve stroking with the RCS pressurizer between 800 and 1000 psig. This would prevent the accumulator from injecting into the plant. The operator had deviated the procedure to allow performance with the RCS depressurized but did not add any precautionary steps to ensure the accumulator was depressurize This deviation, which changed the intent of the procedure, was not reviewed by the safety committee prior to performance as required by TS. Also, to complicate matters, the pressure and level instruments for the "C" accumulator were out of service for maintenance. Therefore, the operators had no idea of the actual status of the accumulator prior to stroking the I

discharge valv !

________________w

_ _ - _ _ ._ _ __ _ _ _ _ - _ _ . - - - _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ - _ _ _ = _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ - e

At the time of the valve stroking, the operators assumed that the "C" accumulator was depressurized because that was condition that had existed 7 previously. However, earlier that day, the nitrogen system in containment  !

had been pressurized and even though the nitrogen isolation valve to the l

"C" accumulator had been shut, the licensee concluded that the valve must have leaked by pressurizing the "C" accumulator to greater than 30 psi This pressure was enough to overcome the height of the injection line and caused the "C" accumulator to inject into the depressurized RCS when the discharge valve came ope Following the injection, the licensee determined that the shutdown margin was still being maintaine Also, the -licensee monitored the Residual Heat Removal (RHR) pump operation to ensure that the pump was not affecte The operating RHR pump was subsequently vented ano determined not to have contained any accumulation of gase TS 6.8.3 states that temporary changes to procedures may be made provided the intent of the original procedure is not altere TS 6.8.2 requires that changes which do not meet the temporary change criteria above shall j be reviewed by the safety committee prior to implementatio Contrary to the above, the temporary change to 2-PT-211.6, which allowed the accumulator discharge valve to be operated with the RCS depressurized was an intent change which was not reviewed by the safety committee prior to implementatio This improper temporary change which resulted in an inadequate procedure, will be identified as a Violation (339/87-36-05) of TS 6. The licensee informed the inspectors that on October 26, the Unit 2 Pressurizer Power Operated Relief Valve (PORV) lifted. The unit was in Mode 5 with the RCS full of water (solid plant operation) at the time of the event. The operators had just stroked MOV-28698 per 2-PT-211.2 and inadvertently aligned the operating charging pump discharge directly to the RCS through the safety injection lin This resulted in the RCS pressure exceeding the low pressure lift setpoint of the pressurizer PORV and lifting of the valve to relieve the pressur The setpoint for the e PORVs with the unit in Mode 5 is approximately 375 psig. This setpoint is j established to prevent overpressurization of the RCS during low temperature )

and low pressure operatio The PORVs opened when the RCS pressure exceeded approximately 375 psig maintaining RCS pressure below the NDT ,

design limits until the lineup to the charging pump was secure .

The inspector reviewed the procedure 2-PT-211.2 and determined that one of )

the initial conditions required all the charging pumps to be s! cured. The j initial conditions had been established a couple of days earlier and were ]a no longer applicable.- The operator performing the procedure did not I

reverify the initial conditions prior to performing the valve stroking; however, he did realize the potential for overpressurizing the RCS by stroking the valve. Therefore, prior to stroking the valve, the operator reviewed the drawings associated with the charging system and incorrectly determined that the valve which he intended to stroke was isolated from the charging pump.

- - _ _ = _ _ _ . _ _ _ - _- -_ ._ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ -

- - _ _ - _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ - _ _ _

.

-

\

The failure of the operator to follow the procedure and ensure that the initial conditions were established prior to stroking the valve is a violation of TS 6. This failure to follow procedure will be identified as the second example of Violation (338,339/87-36-02). ESF System Walkdown (71710), Verification of Containment Integrity (61715)

The inspectors locally observed the positioning of ten penetration valves inside and outside the containment on Unit 2. The inspectors walked down the valve alignment for the low head safety injection system on Unit 2 using 2-0P-7.1 No problems were identifie No violations or deviations were identifie . Operational Safety Verification (71707)

, By observations during the inspection period, the inspectors verified that l the control room manning requirements were being met. In addition, the i inspectors observed shift turnover to verify that continuity of system

'

status was maintaine The inspectors periodically questioned shift personnel relative to their awareness of plant condition Through log review and plant tours, the inspectors verified compliance with selected Technical Specification (TS) and Limiting Conditions for Operation The inspectors kept informed, on a daily basis, of overall status of both units and of any significant safety matter related to plant operation Discussions were held with plant management and various members of the operations staff on a regular basis. Selected port,io'ns of operating logs and data sheets were reviewed dail The inspectors conducted various plant tours and made frequent visits to the control room. Observations included: witnessing work activities in progress; verifying the status of operating and standby safety systems and equipment; confirming valve positions, instrument and recorder readings, annuciator alarms, and housekeepin The following comments were noted:

On October 28, 1987, the operators were draining oil from the Reactor Coolant Pump (RCP),1-RCP-1B, lower radial bearino reservoir to correct a level alarm when the RCP lower radial bearing temperature went from 146 degrees F to 324 degrees F in a three to five minute perio Pump vibration was unchanged and following oil being added to the reservoir the temperature decreased back to 172 degrees F. Also dur.ing this event the seal water leakoff increased from 2.3 to 3.3 gpm at the same time as the temperature increase. Oil was added to the lower reservoir several more time On October 29, 1987, an oil sample was taken. Based on the sample results and the bearing temperature at the time of the event, Westinghouse informed the licensee that the bearing had been damaged. However, Westinghouse

_ _ _ _ - _ _ _ _

l

..

l: .

(

!

stated that as long as the bearing temperature and vibration monitors are indicating in specification then the RCP was acceptable for continued operation. As of the end of the inspection period 1-RCP-1B bearing temperature was approximately 169 degrees F and the vibration monitor was indicating norma '

}

During a review of plant deviation reports on October 30, the inspector I discovered that the licensee had exceeded the technical specification  ;

surveillance limits of 3000 kw during surveillance testing of the 2J l Emergency Diesel Generator (EDG). On October 26, 1987, the licensee  ;

operated the 2J EDG at 3100 kw for approximately 10 minutes during the

'

performance of 2-PT-83.4, Blackout of Emergency Bus for Shutdown Load This violation of TS 4.8.1.1.2.d.7 loading requirements was due to an inadequate surveillance procedur The surveillance procedure 2-PT-83.4 was inadequate because it incorrectly established a test equipment voltage range to be monitored which was  !

supposed to be equivalent to 2900 to 3000 kw, but was actually equivalent to 3050 to 3150 kw. Approximately 10 minutes into the test, an engineer realized that the test equipment voltage range had been incorrectly calculate The voltage range cciculation had been. based on a percentage of 'all scale of the kw ' meter which was incorrectly assumed to be 0 to 4000 k The engineer observed that the actual meter range was 0 to 4200 kw which made the test equipment voltage rarce incorrect. The diesel load was reduced to less than 3000 kw by the kw meter and the licensee determined thet the EDG had been actually operating at approximately 3100 k On October 30, following the discovery by the inspector, the licensee was requested to perform an engineering evaluation to determine operability of the 2J EDG. This evaluation had been committed to by the licensee as documented in Inspection Report 87-04, to be performed following an inadvertent overloading of the EDG. The evaluation which was performed and discussed with Colt on October 30 concluded that the 2J EDG was fully e operable based on the original design rating of 3100 kw for 168 hour0.00194 days <br />0.0467 hours <br />2.777778e-4 weeks <br />6.3924e-5 months <br /> !

A review of previous violations revealed that curing the last performance of 2-PT-83.4, in February 1986, the licensee received a violation for electrically overloadi.1g the 2J EDG. The corrective action for ensuring that the diesels are not overloaded during testing was to place a dedicated operator on the diesel panel to monitor the kw meter and to reduce the load anytime it exceeded the TS limits. However, even though the operator was monitoring the panel, he allowed the '.1 EDG to operate at an indicated load of 3100 kw for 10 minutes because the test engineer informed him that the more accurate indication provided by the test equipment instrumentation, using the voltage data in the procedire, ensured that the diesel was not loaded above 3000 k The licensee determined that the data provided in the procedure was incorrect and the kw meter was actually indicating correctl !

ANSI N18.7-1976, Administrative Control and Quality Assurance for the Operational Phase of Nuciear Power Plants, Step 5.2.1, states in part that it is the responsibility of operating personnel to believe and respond l conservatively to instrument indications unless they are proved to be

'

___ - -

w \

. i

!

9 incorrec This~LANSI. standard is implemented by the ' licensee in Administrative Procedure 19.26, Instrumentation and Controls, which states in part, unless an instrument, instrument channel or instrument-train has been proven ,to be ~ inaccurate' or inoperable, it is the responsibility of-.

operating. personnel.to believe'the instruments. However, 19.26 goes on.to say that operating personnel should' not' make operational decisions based solely on a' single parameter indication when one or more . redundant ,

indications are available. In 'this case, even though the diesel kw meter !

had ' not been proven inoperable, the licensee felt the test equipment 1

' instrumentation was more accurat Based on the' requirements' of ' ANSI-N18.7-1976, Step 5.2.1.and Administrative Procedure 19.26, _ operators should always question instrumentation indications which are outside operating criter_ia and believe those. indications are correct until- given appropriate evidence showing the contrary, i

The licensee's corrective action' for violation '86-04-01 was not adequate to ensure that during subsequent performances of 2-PT-38.4, the EDGs.would not be overloaded. The inadequate procedure 2-PT-83.4, which resulted in the electrical overloading of'the 2J EDG is a violation of:TS 6.8.1, which requires that wri_tten procedures be established, implemented and maintaine This inadequate procedure will be identified' as' Violation-(339/87-36-04). .This violation 'will also be identified as similar to Violation (339/86-04-01).

On November 4,1987, at 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br />, with Unit 2 at 5% power and while performing :2-0P-15.1 " Main Turbine Operation", the turbine did not trip from the control room and had ' to be tripped locally._ It was' later discovered that a part of anc "0" ring was discovered lodged in the auto-stop oil dump line preventing the pressure from dropping sufficiently -

to trip the turbine. The debris was removed and th,e turbine was tripped successfully from the control room at 1542 hour0.0178 days <br />0.428 hours <br />0.00255 weeks <br />5.86731e-4 months <br /> Following a discussion with the ' licensee and a review of the operation i of the main turbine trip system,.the inspector-concluded that the position .

of _- the '0-ring in the auto-stop oil system would not have affected the 'I operation of the mechanical overspeed trip system, the backup master trip !

solenoid valve, the backup emergency trip valve or the overspeed protection-solenoid valves. Consequently, for the major automatic turbine trip signals; overspeed, reactor trip, steam generator high-high water level, safety' injection, feedwater pump trip, high level in feedwater heaters,

'

j low ' auto-stop oil pressure, EHC oil- reservoir low-low level', switchyard -l backup lockout and main generator breaker failure, the turbine trip system

'

would have still functioned properly and tripped the turbine. Based on the

-

above information, the turbine trip system was = still in compliance with 3

'

the TS requirement During a review of licensee deviation reports, the inspector discovered ;

that both of the Unit 2 EDGs were inoperable on November 10 with the unit

'

in Mode 1 operating at approximately 45% power. The 2J EDG had been

! . tagged out to perform preventative maintenance and was therefore declared ;

'

inoperable at 0534 on November 10. The 2H EDG was operational with only one starting air tank and compressor because the -other starting air tank i and compressor had been blown down and tagged out. At approximately 1645 on November 10, the licensee discovered the only pressurized starting air i

~ a

-- - _ _

L

,

.

tank.on the 2H diesel to be approximately 100 psig below the required pressure. This made the 2H EDG technically inoperable; however, the EDG

! would still have started accordirig to the license The licensee stated I that the starting air tank was repressurized to above 240 psig within one hour, meeting the TS Action Statement 3.8.1.1.e limit of two hours. Also, the inspector reviewed a completed copy of 2-PT-80, Offsite AC Sources, that was completed within an hour of the discovery of both diesels being inoperable. This surveillance complies with the TS Action Statement 3.8.1.1.e for performing .TS surveillance requirement 4.8.1.1.1.a within one hou . Operating Reactor Events (93702)

The inspectors reviewed activities associated with the below listed reactor event The review included determination of cause, safety significance, performance of personnel and systems, and corrective actio The inspectors examined instrument recordings, computer printouts, operations journal entries, scram v1 ports and had discussions with operations, maintenance and engineering support personnel as appropriat On October 31, the licensee notified the NRC via the ENS phone of a Reactor Protection System (RPS) actuation on Unit 2. The unit was in Mode 4 with the scram breakers closed and the engineering staff was performing a surveillance procedure 2-PT-71.4 at the time of the The purpose of the surveillance procedure was to test the actuatio auxiliary .feedwater pump time response to an automatic start signa However, unknown to the engineer and to the reactor operator, the test t signal required by the procedure not only started the auxiliary feedwater pumps, but also generated a reactor trip signal. This resulted in the

'

unexpected cycling of the reactor trip breakers. The failure of the procedure to recognize and provide a caution that a reactor trip signal would be generated is a violation of TS 6.8.1 for an inadequate procedur This inadequate procedure will be identified as the third example of e Violation (338,339/87-36-02).

12. Instrumentation Problems Related to Startup of Unit 2 on November 4 and 5, 1987 (71707)

At 1915 on November 4 the Unit 2 "B" Loop delta T protection was placed in trip due to it being out of calibration with "A" and "C" loops. Due to a prior failure of the B loop RTD, the spare RTD was.being utilized and the generic calibration data was inputed to calibrate channel "B". Also during the increase to power, neither flow indicator F1-2474 ("A" Steam Generator Steam flow Channel 3) or F1-2485 ("B" Steam Generator Channel 4)

were reading on scal At 2153 the steam flow instruments FI-2474 and FI-2485 were declared inoperable and the licensee entered Technical Specification 3. which requires shutdown in six hours. The decision to enter Technical Specification 3.03 and not place the steam flow channels in trip was taken by the licensee as a precautionary measure. The licensee felt that with y

_ _ _ _ _ _ _ _ _ . _ _ _ . _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ . _ _ __ __]

. _ _ _ - _ _ _ _ _ _ - - _ - _ _ _

'

.

the "B" delta T channel in trip and two steam flow channels in trip that a

'

single channel failure could cause a safety injection and resulting reactor tri At 2200 shutdown was commenced per OP 2.2 and an unusual event was declare A containment entry was made and mechanical agitation of FI-2485 sensing lines caused it to return to servic .A decision was then made to deviate 2-AP-3.7, Loss of Vital Instrumentation Steam Flow, to allow placing steam flow channel 3 FI-2474 in trip' with

"B" loop delta T in trip. At 0012, FI-2474 was placed in trip and at 0026, the Notification of Unusual Event was terminate Power was returned to 20% at 010 At 0206, an instrument technician found the field wiring to cabinet 3 terminal board "J" contacts 10 and 11 for the F1-2474 instrument to be reversed between the cabinet and the transmitter FT-2474. The licensee is investigating to determine if this happened while the Ray Chem splices were being corrected during the overhaul. The inspectors will investigate to determine if modifications had been made without required post

. maintenance testin This will be identified as Unresolved Item (338,339/87-36-03).

At 0220, FI-2474 was returned to servic The abnormal procedures were exited and the action statement cleare The channel was removed from tri At 0539, new cross calibration data was used to calibrate "B" loop channel II TAVE and delta T. The action statement was cleare This action removed the last of the channels from trip. ,

1 Plant Startup From Refueling (71711)

The low head safety injection and core flood system lineup was walked down to ensure proper lineu The inspectors also witnessed portions of 2-PT-61.4 (See surveillance, Section 8) and 2-PT-83.1 " Simulated Blackout and SI-H-Bus"'

The inspectors witnessed portions of the Unit 2 refueling outage startup physics testing. The following portions of 2-PT-94.0, Refueling Nuclear Design Check Tests, were witnesse .1-Determine zero power testing flux range and establish the zero power testing flux level . .3-Establish initial conditions for determination of the All-Rods-Out Critical Boron Concentratio On October 30, prior to the performance of 2-PT-94.0 " Refueling Nuclear Design Check" Instrumentation and Control (I&C) techanicans connected a meter to power range instrument N44 per procedure ICP-2-N44, to support the test. At some point following the connection of this meter, N44 was adjusted to 0 which made it inoperabl Neither, the I&C procedure nor

_ _ _ _ _ _

'

'

! l 1  !

j 2-PT-94.0 required N44 protection signals to be placed in trip or inform the operators that the instrument was inoperable. On November 3, 1987, with the unit in Mode 2 the operators realized that N44 was inoperable and ,

the protection signals had not been placed in trip as required by TS. The '

unit had been in Mode 2 for over six. hours before the operator discovered the problem. TS, Table 3.3-1 requires an inoperable power range instrument to be placed in trip within one hour when in Modes 1 or 2, to allow f startup or power operation to continue. Neither the instrument department i procedures nor the physics t st procedures required that the channel be i placed 'in trip. The procedures were revised to preven't a reccurence. A plant deviation was submitted for being in Mode 2 without N44 in tri ,

'

The failure of the procedures to require N44 protection signals to be placed in the trip condition resulting in the licensee being in noncompliance with TS is a violation of TS 6.8.1 for an inadequate procedur These inadequate procedures will be identified as the fourth I example of Violation (338,339/87-36-02).

Following the operator's discovery, a signal was dialed into the N44 1 circuitry which was the equivalent of 120?s powe This was performed, instead of the requirements of Abnormal Procedure (AP) 4.3, Malfunction of Nuclear Instrumentation (Power Range), to place N44 protection signals in the trip condition. In prior tests, the instrument department had placed .

the channel in test when installing the meter. The steam generator (S/G) I startup feedwater regulator valves for "A" and "B" S/Gs were in the auto position and opened as a result of the anticipatory power increase. This caused an inadvertent reactor cooldown which resulted in TAVE dropping below 541 degrees F which is in noncompliance of the technical specification limits. The licensee was able to increase TAVE to above 541  !

degrees F prior to exceeding the TS action limit of 15 minutes preventing the unit from having to be shutdow The failure of the licensee to follow AP-4.3 when placing the power range instrument in the trip condition, resulting in an inadvertent cooldown of the RCS below the TS limits is a violation of TS 6.8.1 for failure to follow procedure. This i failure to follow procedure will be identified as the fifth example of

,. Violation (338,339/87-36-02).

The inspectors reviewed the test data on the. rod drop test including the retest of rod K-8 which would not move during testing. The licensee discovered the rod circuity had a loose connector and successfully tested the rod following correction of the loose connecto . Unit 2 Startup Problem Inspection Report 87-19 identified several problems associated with the Unit I refueling outage and startup following the outag Examples of ,

these problems include: reactor trip from 18?; power due to an improperly performed non-safety related tagout, while at 50?; power; di scovery of improperly installed moisture seperator reheat stop valve which prevented the valve from going fully shut as required by TS, and prior to the startup in Mode 6 core alterations were performed without a fully operable charging pump as required by TS. The licensee has conducted an aggressive study of those problems along with several others they have identifie The study has provided the licensee with several generic root causes and

- -_ . _ _ - _ _ _ _ __ ___- _ __ -

, . . - _ _ _ _ _ _ - _ _ - _ _ _ ___ _-_ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ ._

-

.

13 i

.

'

the licensee is establishing corrective actions to prevent recurrence.

) One of the corrective actions involves increased station management involvement in plant activities and providing more supervision involvement ,

of all ?evels at the job site l The corrective actions taken in response to the previous Unit 1 problems were not sufficiently in place to prevent the Unit 2 outage and startup J errors described in this report. The licensee has had several of the i personnel involved in the errors discuss the problems with the Vice President of Nuclear Operations . demonstrating the significance being placed on these errors by licensee managemen The inspectors have observed that the licensee has a good system of identifying their problems and mistakes; however, corrective action to prevent recurrence needs improvemen The licensee is also trying to determine if there are any generic root causes associated with their errors. However, based on the recent experience with the Unit I restart attempts'in June and July and the Unit 2 problems, the licensee must place increased emphasis on establishing corrective actions to prevent recurrenc .- Security Inspection (71881)

The resident made a tour with security of all the vital area The inspector identified to security that the condition of the security batteries needed to be corrected. Corrosion deposits were visible on several of the terminal .The inspectors verified that the minimum amount of armed guards required by the Physical Security Plan (PSP) were on site for each shift and that at least one of the individuals authorized by the PSP to direct security was on site each shif The inspectors made a tour with Quality Assurance and Security to

,. determine the status of illumination in the protected are No violations or deviations were identifie i L-_--____--._