ML20133J199
ML20133J199 | |
Person / Time | |
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Site: | North Anna |
Issue date: | 01/06/1997 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
To: | |
Shared Package | |
ML20133G865 | List: |
References | |
50-338-96-12, 50-339-96-12, NUDOCS 9701170433 | |
Download: ML20133J199 (40) | |
See also: IR 05000338/1996012
Text
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i U.S. NUCLEAR REGULATORY COMMISSION
REGION II
Docket Nos: 50 338, 50 339
i License Nos: NPF 4, NPF-7
Report Nos: 50 338/96 12, 50 339/96 12
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Licensee: Virginia Electric and Power Company (VEPC0)
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Facility: North Anna Power Station, Units 1 & 2
Location: 1022 Haley Drive
Mineral Virginia 23117
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Dates: November 3 through December 7, 1996
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- Inspectors
- R. McWhorter, Senior Resident Inspector
R. Gibbs, Resident Inspector
R. Chou, Reactor Inspector (Sections E1.1 and E2.1 through
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. E7.2)
P. Fillion. Reactor Inspector (Sections El.1 and E2.1
through E7.2)
L. Garner, Project Engineer (Sections 06.1, M2.1. E1.4 and
E8.1)
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P. Hopkins, Project Engineer (Sections M8.1 and M8.2)
D. Jones, Senior Radiation Specialist (Sections R1 and R8)
J. York, Reactor Inspector (Sections E1.1 and E2.1 through
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E7.2)
Approved by: G. Belisle, Chief, Reactor Projects Branch 5
Division of Reactor Projects
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ENCLOSURE 2
9701170433 970106
PDR ADOCK 05000338
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EXECUTIVE SUMMARY i
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North Anna Power Station. Units 1 & 2
NRC Inspection Report Nos. 50 338/96 12, 50 339/96 12
This integrated inspection included aspects of licensee operations,
engineering, maintenance, and plant support. The report covers a five week
period of resident insaection. In addition, it includes the results of
announced inspections ay regional specialists and regional projects
inspectors. I
Operations
. Daily operations were generally conducted in accordance with regulatory
requirements and plant procedures (Section 01.1). l
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. Safety system and oaerator response to a Unit 2 reactor trip was good.
Minor equipment pro)1 ems were promptly corrected. The trip's cause, a
main generator failure due to damage caused by foreign material,
required an extended unit shutdown for repairs (Section 01.2).
. Initial reviews of cold weather protection procedures found that
activities were properly completed (Section 02.1). l
. One NRC notification required by 10 CFR 50.72 was properly made by the
licensee (Section 02.2).
An Operator Work Around (0WA) meeting was an effective mechanism for
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keeping plant management informed of the status of each open 0WA i
(Section 06.1). '
. The Oversight organization continued to assess station performance
effectively. A Hanagement Safety Review Committee meeting complied with
TS requirements, and substantive assessment issues were addressed in
committee discussions (Section 07).
Maintenance
. Service Water Restoration Project work activities were well controlled.
Supporting system manipulations were performed in accordance with
regulatory requirements and commitments (Section M1.1).
. Debris was observed on the ledges above the radiator fans for three of
the four emergency diesel generators (Section M2.1).
. A Non Cited Violation (NCV) was identified for a failure to meet TS
surveillance requirements for testing reactor trip bypass breakers. Two
previous violations and three Licensee Event Reports (LERs) were closed
(Section M8).
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Enaineerino
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A violation was identified for a failure to ensure proper facility
design control. Unit 2 safeguards area walls were found to not meet
their design basis for controlling safeguards pump leakage since early <
in plant life. One Unresolved Item was closed (Section 08.1).
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The licensee's operability evaluation for non conforming bolts in a
recently installed pump was reasonable, and completed in a timely
manner. The scheduled date for correcting the non conformance was
acceptable. Even though the problem was primarily caused by the
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manufacturer, problems in the licensee's design control program
contributed to the wrong bolts being installed. For this reason a
Notice of Violation was issued (Section E1.1). -
The licensee appropriately analyzed the impact of service water system
restoration activities on a shutdown unit and made conservative
decisions concerning shutdown unit status (Section E1.2).
An NCV was identified for a failure to meet American Society of
Mechanical Engineers Code Section XI recuirements for testing the check
valve functions of six steam generator cecay heat removal isolation
valves (Section E1.3). ;
- The Minor Modification Review Team meeting was professionally conducted.
The inspectors had no concerns involving the disposition of the items i
(Section E1.4). ;
- The licensee's approach to resolving a potential problem with
microbiological influenced corrosion in stainless steel service water
piaing was reviewed. One section of four inch diameter pipe was
scleduled for replacement based on findings to date. The licensee was
at the investigation stage, and the total corrective action plan was l
under development. No concerns were identified by the inspectors
(Section E2.1).
. The engineering design change package was well prepared for implementing '
a carbon steel piping replacement in the service water system and the
quality of work being performed by the craftsmen was good
(Section E2.2).
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. A detailed cell inspection was performed on each cell of all the
safety related batteries. The inspectors concluded that battery
maintenance was good. However, the inspectors observed significant
sedimentation in two cells. The inspectors concluded that the
sedimentation had been present on June 4, the time of the last
surveillance inspection. Therefore, the fact that the surveillance did
not record any problems with sedimentation was considered a weakness in
the implementation of the inspection procedure (Section E2.3).
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. A review of six Deviation Reports and one Potential Problem Report
related to mechanical and structural engineering indicated good support
for facilities and equipment by engineers (Section E2.4).
. The alarm response procedure for bus overvoltage was a workable
procedure, and was consistent with statements made in letters to the NRC
on the subject of overvoltages. The safety evaluation supporting the
change in maximum allowable response time for performing tap changer
manipulations was accurate and complete.
Some corrective actions were proposed by the licensee to address NRC l
comments with regard to reading voltage at the 480 volt bus, but this
did not represent any programmatic weakness. The overvoltage relays
with alarms were a conservative design in relation to standard industry
practice (Section E2.5).
. The inspectors reviewed a Deviation Report involving the failure of
safety related vital battery 1 I to meet one acceptance criterion during
performance of the last service test. The inspectors agreed that the
subsequent Operability Evaluation was reasonable, and that the
requirement of the Technical Specification was met. An Inspection
Follow up Item was established to ensure review of certain procedure
enhancements and future test results (Section E2.6). l
. Review of a 1996 modification package to reinforce the supports for the
component cooling water surge tank to resolve concerns about the seismic
integrity of the tank indicated that the design was correctly
accomplished, but that the actual installation did not meet specified
dimensional tolerances. Also, a pipe support was installed at a point
where no support was shown on the drawings. A Notice of Violation was
issued (Section E3.1).
. The licensee's test procedure for the molded case circuit breakers was
good, in that, it checked that the magnetic element tripped within a
specified band around the set )oint. The controls for establishing and
verifying the set points for t1e magnetic elements were minimal. There
was no set point document, drawing, or specific instructions to help
ensure proper set >oints were maintained. Based on a sample of two
newer circuit brea(ers, the licensee's informal method resulted in
correct settings. Nevertheless, the lack of formal controls on the set
point for the magnetic element of molded case circuit breakers was a
weakness in the licensee's design control 3rogram in that continued use
of the informal method has increased proba)ility to result in incorrect
set points. Whether the lack of formal controls represents a violation
of NRC requirements in the area of design control or procedures is under i
further review by the NRC. The issue is identified as an Unresolved i
Item concerning the control of set points for molded case circuit !
breakers (Section E3.2).
. The safety and oversight committees were conducting their duties in an i
efficient and productive manner (Section E7.1).
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. The engineering self assessment program was only recently defined, and
very few self assessments were completed (Section E7.2).
. An Inspection Followup Item was opened to review functional tests that
will be conducted on either new or old snubbers in the upcoming Unit 1
refueling outage. One Unresolved Item was closed (Section E8.1).
Plant Support
. The licensee was closely monitoring collective and individual radiation
dose exposure and meeting established As Low As Reasonably Achievable
goals and occupational dose limits (Section R1.1).
The licensee's water chemistry control program for monitoring primary
and secondary water quality had been implemented in accordance with the ,
TS requirements and the Electric Power Research Institute guidelines for i
pressurized water reactor water chemistry (Section R1.2).
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. One non cited violation was identified by the licensee for failure to
comply with the conditions of the Certificate of Compliance for an
NRC approved shipping package (Section R1.3).
- Two previous violations were closed (Section R8).
. Security systems were in good working order and security manning was
appropriate (Section S1).
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Report Details
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Summary of Plant Status
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Unit 1 began the inspection period at full power and operated the entire
inspection period at or near full power.
i Unit 2 began the inspection period at full power and operated at or near full
i power until November 12. On that date, the unit tripped from full power due
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to a main generator fault. The unit was cooled down and entered hot shutdown !
on November 13, and cold shutdown on November 29. At the inspection period's l
end, the unit remained shutdown for main generator repairs.
I. Operations l
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01 Conduct of Operations
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01.1 Daily Plant Status Reviews (71707)
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The inspectors conducted frequent control room tours to verify proper ,
staffing, operator attentiveness, and adherence to approved procedures. l
The inspectors attended daily plant status meetings to maintain
i awareness of overall facility operations and reviewed operator logs to
i verify operational safety and compliance with Technical Specifications
(TSs). Instrumentation and safety system lineups were periodically
- reviewed from control room indications to assess operability. Frequent
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)lant tours were conducted to observe equipment status and housekeeping. i
)eviations Reports (DRs) were reviewed to ensure that potential safety
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concerns were properly reported and resolved. The inspectors found that
- daily operations were generally conducted in accordance dth regulatory
requirements and plant procedures.
01.2 Unit 2 Reactor Trio
a. Insoection Scope (71707. 93702)
On November 12, the inspectors in the field observed plant equipment
. responding to a Unit 2 reactor trip from full power. The inspectors
4 proceeded to the control room and observed operations immediately
following the trip. Additionally, the inspectors observed immediate
post trip equipment conditions in the turbine building, switchgear
rooms Auxiliary Feedwater (AFW) pump house, and Main Steam Valve House
(MSVH). The inspectors attended the licensee's post-trip review and
reviewed trip data to independently verify that safety systems and
operator performance were as expected throughout the event.
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b. Observations and Findinas
The inspectors found that the reactor tripped from full power following
a main generator trip. The main generator trip was caused by an
actuation of the generator protective system. A review of trip data
found that the trip signal was valid, and the inspectors verified that
safety systems performed as designed for plant conditions during the
trip. Operator response to the trip was appropriate and emergency
procedures were properly followed. One intermediate range nuclear
instrument was observed to be overcompensated, and one individual rod
position instrument indicated slightly greater than 10 steps after the
tri ). Operators initiated emergency boration for the rod position
pro)1em in accordance with abnormal procedures. The rod position
indication problem was corrected, and rod drop time testing was later
aerformed as required by NRC Bulletin 96 01, Control Rod Insertion
)roblems.
Plant equipment conditions immediately following the trip were good
except for the turbine building where numerous secondary relief valves
lifted following the reactor trip. Most of the relief valves lifted due
to the sudden increase in feedwater pressure, and all exce)t one
reseated when pressure was reduced. The relief valve whic1 did not
reseat was manually gagged by maintenance personnel. Additionally, the
ins)ectors observed that a large amount of water was discharged from the
turaine-driven AFW pump exhaust line during pump startup. No adverse
effects upon pump response were observed.
The main generator trip was found to be initiated by actuation of the
neutral ground fault relay. Testing confirmed that an actual fault
condition occurred on the A phase of the generator. On November 14,
generator inspections found that foreign material, a section of clear
plastic, had lodged on the cooling tubes for several generator coils.
The alastic cut off hydrogen cooling flow and allowed the coils to
overleat and fail. The generator required major disassembly for coil
replacement, and an extended forced outage was in progress at the
inspection period's end.
On November 13, the unit was cooled to hot shutdown, and secondary
systems were secured. The unit remained in hot shutdown until
previously ongoing repair activities on the Service Water (SW) system
were completed (Section E1.2). On November 29, the unit was cooled to
cold shutdown.
c. Conclusions
The inspectors concluded that safety system and operator response to the
Unit 2 reactor trip was good. Minor equipment problems were promptly
corrected. The trip's cause, a main generator failure due to damage
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caused by foreign material, required an extended unit shutdown for
repairs.
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02 Operational Status of Facilities and Equipment
02.1 Cold Weather Preparations
a. Insoection Scope (71714)
On several occasions during the inspection period, the inspectors
reviewed the initial implementation of the licensee's cold weather
protection procedures.
b. Observations and Findinos
The inspectors performed initial reviews of the licensee's procedures
for cold weather protection and their implementation. Procedure
0 G0P 4, Cold Weather Operations, Revision 9, was performed monthly
during cold weather or as directed by shift supervision. The inspectors
reviewed the procedure completed on November 15 and found that operators
had documented completing the actions necessary to protect
safety-related systems from freezing. For components v,ivere operators
identified material discrepancies, the inspectors verified that
corrective actions were initiated.
The inspectors also walked down the status of freeze protection
equipment near the Refueling Water Storage Tanks (RWSTs) and in various
buildings containing safety-related equipment. On November 24, the
inspectors identified that an a) proximately three inch section of piaing
to RWST level transmitter 2 05 _T 200D was wrapped in heat tracing, )ut
was not fully insulated. The inspectors reported the discrepancy to
shift supervision, and verified on December 6 that the discrepancy had
been corrected. Additionally, the inspectors discussed with station
managers the fact that with Unit 2 shutdown for a forced outage, the
Unit 2 MSVH temperature was much lower than normal. The managers
informed the inspectors that the Unit 2 MSVH temperature was being
monitored and that action would be taken (e.g., installing temporary
heaters) if MSVH temperature approached freezing.
At the inspection period's end, the inspectors were continuing their
reviews of the licensee's cold weather protection activities.
c. Conclusions
Initial reviews of cold weather protection procedures found that
activities were properly completed.
02.2 NRC Notifications
a. Inspection Scope (71707)
The inspectors reviewed the following licensee notifications to the NRC
to ascertain if the required reports were adequate, timely and proper
for the events.
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. b. Observations and Findinas
On November 12, the NRC was notified as required by 10 CFR 50.72
concerning reactor protection system and engineered safety feature
actuations generated when Unit 2 tripped from full power. The
inspectors found that the licensee's reporting actions were appropriate.
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Additional inspection activities and findings are discussed in
Section 01.2.
j c. Conclusions
l One NRC notification required by 10 CFR 50.72 was properly made by the
licensee.
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06 Operations Organization and Administration
- 06.1 Operator Work Arounds (0WAs) (71707)
l On December 5, the ins actors attended an 0WA status meeting conducted
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at the conclusion of t1e morning management meeting. There were 18
active 0WAs, 2 items assigned as high priority (may affect nuclear
safety), 7 assigned as medium priority (important but do not directly
affect nuclear safety) and 9 assigned as low priority (minimal impact on
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plant operations). Each item's status was reviewed in sufficient detail
j to determine the progress in resolving the item. The meeting was an
effective mechanism for keeping plant management informed of the status
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of each open 0WA.
07 Quality Assurance in Operations
07.1 Oversicht Meetina (40500)
On November 6. the inspectors met with Oversight personnel. Issues
discussed included Oversight activities and findings since previous
meetings. Copies of recent audits were provided for review. The
inspectors also observed Oversight personnel observing plant activities
on numerous other occasions during the inspection period and met briefly
with them to discuss their observations. The inspectors concluded that
the Oversight organization was continuing to assess station performance
effectively.
07.2 Manaaement Safety Review Committee (MSRC) Meetina (40500)
On November 20, the inspectors attended a regularly scheduled MSRC
meeting at the North Anna site and observed Station Manager's plant
- status reports. The inspectors found that the MSRC meeting met TS 6.5.2
requirements for member composition and quorum and that the agenda
appropriately included review items required by TS 6.5.2.7. The
- inspectors observed that the Station Manager's reports generated
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significant self critical discussions of station performance. The
inspectors concluded that the HSRC meeting was in compliance with TS
requirements and that substantive assessment issues were being addressed
in the discussions.
08 Miscellaneous Operations Issues (92901, 92700)
08.1 (Closed) Unresolved Item (URI) 50 339/96004 01, review significance of
safeguard area ventilation not meeting design basis
(Closed) Licensee Event Report (LER) 50 339/96001, potential unfiltered
release path from the quench spray pump house to the environment
a. Scope -
As a result of questions asked by the inspectors, on May 15, 1996, the
licensee identified and reported to the NRC a potential unfiltered
release path to the environment following a design basis accident. As a
result of the problem, both trains of safeguards area ventilation
systems were declared inoperable. During this inspection period, the
inspectors reviewed the problem's significance.
b. Observations and Findinas
The problem identified by the insaectors was that a flowpath existed
between the safeguards area and t1e Quench Spray (QS) area sumps. The
safeguards area contained the Low Head Safety Injection (LHSI) pumps,
Outside Recirculation Spray pumps, and associated piping and valves.
Leakage from these components was directed to a sump described in
Updated Final Safety Analysis Report (UFSAR), Section 15.4.1.8, as sized
to accommodate the design basis leakage from area components, including
a 50 gallons )er minute (gpm) LHSI pump seal leak lasting 10 minutes.
The size of t1e safeguards sump and sump drainage were important because
credit was taken that operators would notice any leakage of radioactive
water to the sump and take action to isolate the leakage. The
safeguards sump was found to be directly tied to the QS sump via a
six inch pipe connected between the two areas. The connection
potentially allowed a portion of the design basis radioactive leakage to
flow to the QS sump. This leakage could have inhibited prompt operator
identification of leakage into the sump. Additionally, the QS area
ventilation system was not designed to handle radioactive effluents, and
an unfiltered and unmonitored release could result.
The inspectors reviewed the licensee's corrective action for this
problem. Along with making a 10 CFR 50.72 report, the licensee resorted
this event in LER 50 339/96001. A temporary cap was placed over t1e
pipe until a permanent repair was prepared. Later, a Design Change
Package (DCP) was implemented to permanently plug the pipe and to
install a pump in the QS sump.
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The inspectors reviewed the event's significance. The LER stated that,
"The event posed no significant safety implications because any increase
in dose through the unfiltered release path would be well within the
- limits of 10 CFR 100." The inspectors reviewed the above statement with
the licensee's nuclear fuels group personnel on September 5. The
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inspectors found that the pump seal leak contribution to off-site dose
i was small compared to total off site dose referred to in UFSAR
Section 15. With no filtration, the calculated dose associated with a
LHSI pump seal leak was increased by a factor of 10, but was still only
i a small contributor to total dose. The ins
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safety consequence of the cross tied sumps,pectors concluded
with regards to off sitethat the
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dose, was minimal.
The inspectors also questioned the potential increase in control room
dose due to the cross tied sumps. Licensee engineers postulated that
the expected control room doses would be similar to those estimated
following a separate problem identified with inadequate operator
arocedures for responding to a fuel handling accident (NRC Inspection
leport Nos. 50 338, 339/96 09). Similar to that problem, the control
room doses could possibly exceed 10 CFR 50 General Design Criteria (GDC) 19 limits for operators. However, such estimates contained
numerous conservative assumptions which meant that if an accident had
actually occurred with the leakage path through the QS area, the actual
dose to control room operators would not likely exceed the GDC 19
limits.
While reviewing the above problem on May 23, 1996, the ins)ectors also
identified that the floor drain hole that permitted the B _HSI pump
leakage to drain from its pump cubicle to the safeguards area sump was ,
grouted closed. The grouted ends had been covered with paint indicating l
the drain hole had been in this condition for a long time period. The
inspectors noted that the UFSAR Section 15. Accident Analysis, Condition
IV - Limiting Faults for a Loss of Coolant Accident (LOCA) assumed a
aump seal failure. Specifically, Section 15.4.1.8, Doses From Leakage
Trom Emergency Core Cooling System Components, stated, "The 50 gpm
leakage due to the pump seal failure is assumed to last 10 minutes
subsequent to initiation of the leak. The leakage is limited to 10
minutes (500 gallons of total leakage) because the leak will be quickly
detected by the safeguards area sump level monitor and alarm." The
grouted hole prevented the sump level monitor and alarm from performing
its function for a pump seal leak on the B LHSI pump.
This issue was discussed with system engineers. After review, DR )
N 96-1059 was issued to document the problem and track corrective
actions. The licensee found that the drain holes were plugged in both
the B LHSI and the B Outside Recirculation Spray pump cubicles. The
licensee also found that with the drain holes plugged, seal leakage
could accumulate to ap3roximately 1500 gallons before draining over to
the safeguards sump w1ich was three times that analyzed in the UFSAR. l
The holes had apparently been plugged since initial construction.
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The licensee reviewed this issue for reportability to the NRC and
j concluded the following as documented in response to the DR:
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The condition was not outside of the design basis since
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maintaining off site doses within 10 CFR 100 limits met design
j basis criteria.
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The associated safety equipment was not affected by the condition,
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and the ability to process the ventilation discharge through the
i charcoal filters was not altered. Therefore, the ability to
mitigate the consequences of an accident was not significaro iy
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! The inspectors found that the licensee's assessments of the significance
- of the plugged cubicle drain holes were appropriate. Shortly after
- discovery, the licensee unplugged the drain holes in both cubicles and
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verified that drains for all other cubicles were open.
The inspectors concluded that since early in plant life, the safeguards
area configuration did not match that described in the plant design
basis. The licensee's failure to ensure proper facility design was a
violation of 10 CFR 50, Appendix B, Criterion III, which required the
licensee to establish measures to ensure that applicable regulatory
requirements for the design basis described in license documents be
implemented. Contrary to this requirement, since early in plant life
until May 1996, the licensee failed to ensure that safeguards area walls
met the design basis for containing pump seal leakage as described in ,
UFSAR Section 15.4.1.8. Specifically, a hole existed between the l
safeguards area and the QS area where the design required that the
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safeguards area be fully separated. Additionally, holes designed to 3
exist between pump cubicles and the safeguards area sump in order to j
allow drainage of pump seal leakage were found to be plugged. This is ;
identified as a violation of 10 CFR 50, Appendix B, Criterion III, l
requirements (50-339/96012 01). This violation is considered to have
occurred in the Engineering functional area.
c. Conclusions
A violation was identified for a failure to ensure proper facility
design control. Unit 2 safeguards area walls were found to not meet
their design basis for controlling safeguards pump leakage since early
in plant life. One URI was closed.
II. Maintenance
M1 Conduct of Maintenance I
M1.1 Maintenance Observations (62707)
Throughout most of the ins mction period, the inspectors reviewed
Service Water Restoration )roject (SWRP) efforts to replace sections of
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the Train B SW headers to the Component Cooling Water (CCW) heat
exchangers. During the SWRP, the licensee entered and exited various TS
Action Statements specifically approved for the SWRP. The inspectors
verified that TS compliance was maintained and that compensatory actions
required by the NRC Safety Evaluation Report for the TS Action
Statements were properly implemented by the licensee. The inspectors
also observed that the overall control of SWRP work activities was
approariate. The only deficiency noted by inspectors during the work
was t1at a flexible cable jacket was pulled out of a connector on valve
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1 SW-MOV 113A. Due to the large amount of work in the area of the
valve, it appeared that the jacket had probably been pulled out due to
unknown individuals stepping on the cable. DR N 96 2687 was initiated,
and the configuration was reviewed and found not to be an operability
concern. A work recuest was initiated for corrective action. The
inspectors concludec that overall the SWRP work activities were well
controlled, and supporting system manipulations were performed in
accordance with regulatory requirements and commitments.
M2 Maintenance and Material Condition of Facilities and Equipment
M2.1 Emeroency Diesel Generator (EDG) Radiator Fan Exhaust Comoartment
Housekeepino (71707)
On December 4, the inspectors, accompanied by a system engineer,
performed a walkdown of the EDG radiator fan exhaust compartments
located on the Service Building roof. Debris was observed on the ledges
above the radiator fans for three of the four EDGs. The debris included
two four by six inch metal )lates. With the radiator fan blades
exposed, a seismic event, w11ch results in EDG starts or occurs while an
EDG is operating, could cause the debris to fall onto the radiator fan
blades with unknown consequences. The system engineer notified the
shift supervisor of the observation so that the debris could be removed.
Deviation Report N 96 2749 was issued concerning this condition.
M8 Miscellaneous Maintenance Issues (92902, 92700)
M8.1 (Closed) Violation 50 338/95015 01, failure to follow procedures for
properly controlling safeguards area ventilation system (SAVS)
maintenance. This event involved the requirement of following
procedures to ensure that maintenance on safety related equipment be
properly preplanned and performed to minimize the impact on operability
of other associated safety equipment. Senior reactor operators failed
to verify whether maintenance work on one SAVS train would affect the
other redundant equipment train.
The inspectors verified that the licensee performed adequate
investigation and established the root causes for the event. Multiple
personnel errors in this case caused the process that would have ensured
the prevention of such an event to breakdown. The licensee took
remedial actions through the disciplinary process, and the event was
discussed at training sessions and shift turnovers and was instituted as
a part of the Licensed Operator Requalification Program.
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The inspectors verified that special training sessions took place, that
remedial action was taken, and the training materials and procedures
were reviewed in detail to ensure adequacy. The inspectors concluded
that the licensee's response dated October 12, 1995, and the corrective
actions were appropriate and had been adequately implemented.
M8.2 (Closed) Violation 50 339/95020 02, failure to comply with 3.6.1.3 for
air lock outer door rendered inoperable by open test connection. This
violation concerned an inoperable Unit 2 containment air lock outer door
due to valve 2 CE 4 being left uncapped. When the containment air lock
outer door became inoperable, unknowingly the plant was then under a TS
Limiting Condition for 0)erations. TS 3.6.1.3, Action A, required that
the operable door be locted within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> or that the plant be placed
in hot standby within the next six hours and placed in cold shutdown
within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.
The inspectors reviewed the licensee's response and commitments to this
event to determine the adequacy and appro)riateness of corrective
actions taken and the implementation of t1ose actions. The inspectors
verified that the licensee's response to the violation clearly
documented the efforts expended to preclude recurrence of the problem.
The inspectors reviewed procedure 2 PT-62.1, Containment Air Locks -
Leakage Rate, Revision 17, and verified that the procedure had been
revised and updated. The licensee's efforts to correct the causes of
the event included coaching the individuals who performed the procedure
on the importance of procedure implementation and self checking. The
event and lessons learned became part of the licensee's requalification
program. The inspectors concluded that the licensee's response dated
January 9, 1996, and corrective actions were appropriate and had been
adequately implemented.
M8.3 (Closed) LER 50 338, 339/96009, reactor trip bypass breaker missed
surveillance due to inadequate surveillance test procedure. This LER
reported the identification on October 10, 1996, that a surveillance
test was not being performed as required by TS 3.3.1.1. The
surveillance tests were not testing the reactor trip bypass breaker
manual shunt trip prior to placing the breaker in service. The shunt
tri) was instead being tested immediately after closing the normally
rac(ed in breaker. Licensee personnel identified the deficiency after
visiting another facility and noting differences in the testing
procedures. The licensee postulated that the procedure inadequacy was
caused by personnel mis interpreting TS wording and failing to identify
that a procedure change was needed following a 1986 TS change. A review
of NRC Generic Letter 85 09 Technical Specification for Generic Letter 83-28, Item 4.3, revealed that the prior interpretation was incorrect.
As corrective action, the licensee modified surveillance test procedures
to recuire that the bypass breaker be racked out and the shunt trip
testec prior to closing the breaker. The inspectors verified that these
procedure changes were completed. Additionally, a UFSAR change was
planned to update test sequence descriptions.
- _ - _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _
.
.
10
TS Surveillance Requirement 4.3.1.1.1. Table 4.3-1, Notation 8, requires
that the reactor trip bypass breaker local manual shunt trip be tested
prior to placing the breaker into service. Contrary to this
requirement, from approximately June 9,1986, until approximately
October 10, 1996, reactor trip bypass breakers were placed in service
without first testing the local manual shunt trip. This is identified
as a violation for an inadequate surveillance test, in that, the test
did not meet TS surveillance requirements. This licensee identified and
corrected violation is being treated as an NCV, consistent with
Section VII.B.1 of the NRC Enforcement Policy (50 338, 339/96012 02).
M8.4 (Closed) LER 50 338/96010, automatic reactor trip due to failure of a
generator negative phase sequence relay. This LER discussed an October
24,1996, Unit 1 tri) from full power due to a failure in the main
generator negative plase sequence relay. The licensee's response to the
event and corrective actions for the associated equipment failures were
reviewed and discussed in NRC Inspection Report Nos. 50 338, 339/96 10.
M8.5 (Closed) LER 50 339/96003, automatic reactor trip resulting from main
generator stator coil failure due to personnel error. This LER
discussed a November 12,1996, Unit 2 trip from full power due to a main
generator failure. The licensee's response to the event and initial
corrective actions for the event are reviewed and discussed in
Section 01.2. The inspectors also verified that appropriate corrective
actions were initiated for all associated minor equipment failures
following the trip.
III. Enaineerina
El Conduct of Engineering
El.1 Problem with Bolts - SW and Auxiliary Service Water Pumo
a. Insoection Scope (37550)
The inspectors reviewed a problem, documented in DR N-96 2359, involving
the seismic qualification for a replacement SW aump and stress on the
pump's flange bolts. Requirements related to t11s review included
American National Standards Institute (ANSI) B31.7, Power Piping.
b. Observations and Findinos
The licensee was in the process of replacing four safety related SW
pumps due to aging concerns. Replacement SW pump 2 SW P 1A was
installed in December 1995. The remainder were in manufacturing.
In October 1996, the manufacturer's Quality Control inspector, while
inspecting the second pump at the factory, identified a discrepancy in
the bolts at various column flanges and the bowls. The drawings
indicated one-inch diameter bolts were required, but the actual hardware
installed was three-quarter inch diameter bolts. The manufacturer
. - . - . . -- - _. .. . . - _ - - . - . -. - - - - . . -
,
-
'
,
11
l contacted the licensee to ask for approval to ship the pump with smaller
bolts about October 14, 1996. This prompted the licensee to review the
seismic qualification report (AR120N, Revision 1), the outline drawings,
a
and the bill of material for the pump received in 1995. The licensee
identified a discrepancy between the seismic report and the
- bill of-material regarding the bolts in question. The seismic
>
qualification report was based on one inch diameter, A325, high
strength, dynamic loading bolts, but the bill of material showed
one inch diameter, A307, low strength, non dynamic loading, structural
bolts.
.
Concerned about operability of the installed pump in light of the new
information, the license requested the manufacturer to perform a seismic
re analysis based on the actual bolts supplied with the new pump
.
(one inch diameter, A307). When the licensee reviewed this re analysis,
i
they identified errors. The re analysis used the wrong bolt tensile
>
strength area and compared calculated stresses to the wrong criteria
(wrong code), and therefore reached a wrong conclusion. Revision 1 of
the seismic report provided by the manufacturer did not have these
, errors. The licensee then performed their own re analysis on October
16.
T
The licensee's analysis showed a calculated stress for the Design Basis
-
Earthquake condition of 28.6 ksi on the bolts compared to ANSI B31.7
allowable stress of 16.8 ksi. ASME Section III, Appendix F, states that
the pump would be operable if the stress did not exceed 0.7 times the
Ultimate Tensile Strength or 42 ksi. Therefore, the licensee concluded
the pum) was operable. Replacement of the non conforming bolts with
proper aolts was scheduled for January 13, 1997. In addition, on
October 21, 1996, the licensee issued a revised aurchase specification
calling for A193 Group B7 high strength bolts to >e supplied with the
new pumps. Also, the licensee planned to inspect two Auxiliary Service
Water pumps, which were classified as important to safety, to determine
the bolt type used in these pumps. If necessary, those bolts would be
replaced as well.
The inspectors inquired whether a notification of defect would be issued
pursuant to 10 CFR 21. The licensee stated that evaluation of the need
for a report was in progress.
The licensee had documents, namely the seismic report and the
bill-of material, which contained a discrepancy and deficiency with
regard to the material of the bolts in question. However, the
licensee *s design reviews failed to identify these before installation
of the first replacement pump. This problem in the design control
program contributed to installation of non conforming bolts, and
constitutes a violation of 10 CFR 50, A)pendix B, Criterion III, Design
, Control, which requires that measures slall be established to ensure the
design basis are correctly translated into drawings. The matter is
'
identified as a violation (50 339/96012 03).
.
.
12
c. Conclusions
The inspectors concluded that the licensee's operability evaluation for
non conforming bolts in a recently installed pump reached a proper
conclusion in accordance with NRC guidance, and was completed in a
timely manner. The scheduled date for correcting the non conformance
was acceptable. Even though the problem was primarily caused by the
manufacturer, reviews in the licensee's design control program did not
identify that the wrong bolts were installed. For this reason a Notice
of Violation was issued.
E1.2 Review Sucoortina Plant Cooldown Durina SW Maintenance (37551)
During the licensee's SWRP to replace sections of the Train B SW piping i
going to the CCW heat exchangers (Section M1.1), a Unit 2 forced outage
was required for main generator repairs. The inspectors reviewed the
licensee's decisions with regard to the shut down status of Unit 2 to
ensure that regulatory recuirements were met and that Unit 2 was
maintained in a safe shutcown condition. The inspectors reviewed the
licensee's submittal for TS changes required to su) port the SWRP. In
the submittal documentation, the licensee stated t1at if an outage was
required for either unit during the SWRP, an assessment would be
performed. The inspectors found that shortly after shutdown, the
licensee completed the required assessment which was contained in an
Engineering Transmittal (ET) No. NAF 96201. The inspectors reviewed the
ET and found that it accurately assessed the situation. Specifically,
it analyzed the reliability of available SW equipment to support
shutdown operations and made appropriate recommendations for
compensatory actions. Additionally, the inspectors noted that managers
considered the ET and other available information and made a
conservative decision to keep Unit 2 in hot shutdown and not proceed to
cold shutdown until the SWRP was completed. The inspectors concluded
that the licensee appropriately analyzed the impact of the SWRP on the
unit shutdown and made conservative decisions concerning unit status.
E1.3 Inservice Testina of Decay Heat Release (DHR) Stoo Check Valves
a. Insoection Scope (37551)
During the week of November 12, the inspectors reviewed the engineering
basis for deleting Inservice Test (IST) requirements for DHR stop check
valves 1/2 MS 19 58, and 96.
b. Observations and Findinas
During the previous inspection period, the ins)ectors observed that
operators used the Unit 2 Decay Heat Release ()HR) valve to control
temperature during a forced outage. The DHR valve was an air operated
Steam Generator (SG) atmospheric relief valve located on a common header
supplied from all three SGs. The header was normally isolated by
manually operated stop-check valves 1/2 MS 19 58, and 96. On October
i
. . .
.
.
13
22, the inspectors observed that all three Unit 2 stop check valves were
open to allow DHR valve use. The inspectors questioned engineers
concerning the IST history for the stop check valves and were informed
that ISTs for the valves had been deleted in early 1996. Licensee
engineers provided the inspectors with a memorandum from C. Snow to B.
Foster dated October 24, 1996, describing the basis for deleting ISTs.
The inspectors reviewed the memorandum and found that it stated that the
ISTs were deleted because UFSAR Section 15.2.13.3 provided an analysis
of simultaneous blowdown of all three SGs due to a failure of the three
inch DHR line. The memorandum stated that American Society of
Mechanical Engineers (ASME) Code Section XI, paragraph IWV 1100,
required testing only for valves which were, " required to perform a
specific function in ... mitigating the consequences of an accident."
Since the UFSAR did not take credit for the valves' isolation in
analyzing for a DHR header break, the licensee concluded that ISTs were
not required. The inspectors accepted this conclusion for the accident
analyzed in UFSAR Section 15.2.13.3.
However, the inspectors identified that a different accident function
for the valve had not been properly considered by the licensee.
Specifically. UFSAR Section 15.4.2.1 described analyses for a Main Steam
Line Break (MSLB) occurring within the isolation boundaries for the SG
(e.g., upstream of the stop check valves). The analyses in that section
assumed that only one SG would be depressurized for such a failure. On
November 19, the inspectors informed licensee engineers that for this
assumption to be valid when the DHR valve is in use, the check valve
feature of the stop check valves must function correctly. The
stop check valves were needed to prevent backflow from intact SGs into a
faulted SG in order to prevent simultaneous blowdown of all SGs. The
stop check valves served a function similar to check valves in the steam
lines supplying the turbine driven AFW pump, for which ISTs were
performed. After reviewing the issue, licensee engineers submitted DR
N 96 2674 on November 22. The DR stated that IST testing for the
stop check valves should have been continued in order for operators to
be allowed to use the DHR valve for temperature control as was done on
October 22 through 24.
On November 26. licensee engineers provided the inspectors with a copy
of ET NAF 96207, Review of Decay Heat Removal Using the Decay Heat
Release Valve and Impact on the Plant Safety Analyses North Anna Power
Station Units 1 and 2, dated November 26, 1996. The ET evaluated the
effect of a failure of the check valve function on the accident analyses
for a MSLB. The ET concluded that for the plant situation existing on
October 22 through 24, (reactor in MODE 3, all rods in, main feed
isolation valves shut, and main steam non return valves shut), operation
of the DHR valve was acceptable and the licensing basis MSLB analysis
remained valid with an assumed failure of a DHR stop check valve. The
inspectors found that the ET prepared on November 26 demonstrated that
,
for the plant configuration actually occurring when the DHR valve was
used, the problem did not have major safety significance.
.
.
14
Overall, the inspectors found that the licensee had deleted the ISTs for
the DHR stop check valves without proper supporting analysis or controls
to prevent their use. In order to delete testing the check valve
functions of 1/2 MS 19. -58, and 96, use of the DHR valve should have
been prevented by modifications or procedural controls, or the licensing
basis MSLB analyses should have been re preformed assuming a stop check
valve failure. Neither of these actions were taken until questions were
raised by the inspectors. The licensee's failure to ensure proper IST
for the valves was a violation of TS 4.0.5 surveillance requirements
which required that ASME Code Class 1, 2 and 3 components be inspected I
and tested in accordance with ASME code Section XI. Contrary to this
requirement, the licensee deleted testing requirements for the ;
stop-check function for the six DHR isolation valves without properly )
evaluating or limiting their function during accident conditions. Three j
of the six valves were opened for use from October 22 through 24, 1996.
This failure constitutes a violation of minor significance and is being
treated as an NCV consistent with Section IV of the NRC Enforcement
Policy (50 338, 339/96012 04).
c. Conclusions
An NCV was identified for a failure to meet ASME code Section XI ,
requirements for testing the check valve functions of six steam I
generator DHR isolation valves. l
l
E1.4 Minor Modification Review Team (MMRT) Meetina (37551)
On December 4, the inspectors attended a MMRT meeting. Since these
meetings had been tem)orarily suspended after the October 16 meeting l
because of outages, t1ere were several new Requests for Engineering l
Assistance to be reviewed. The primary purpose of the meeting was for
management to approve, modify, or cancel proposed minor modifications.
The reviews considered nuclear plant safety, personnel safety, and
economic benefits, generally in that order. The discussions also
considered if a minor modification was the proper vehicle for addressing
an issue. The meeting was professionally conducted. The inspectors had
no concerns involving the disposition of the items.
E2 Engineering Support of Facilities and Equipment
E2.1 Resolution of Microbioloaical Influenced Corrosion (MIC) Corrosion of
Stainless Steel SW Pipina
a. Insoection Scope (37550)
The inspectors reviewed the licensee's ongoing activities in the area of
leaks in the SW piping. The regulatory requirement relevant to the
scope of inspection was 10 CFR 50, Appendix B, Criterion XVI, Corrective
Action.
-
- .-. . . - -
-
l
l
'
)
15 j
l
b. Observations and Findinas
l
The licensee was resolving the problem described in DR N 96-2492 which ,
identified the presence of two pin hole leaks on a four inch diameter l
stainless steel alloy 316 SW piping weld. The licensee inspected the ;
piping for the possibility of MIC since this form of corrosion had been
prominently identified in the carbon steel SW piping, and had been
identified in a stainless steel weld failure in the SW System in 1993.
A review was made by the inspectors of the Nondestructive Examination
(NDE) Procedure used for evaluating the MIC found in the stainless steel
SW line, No. NDE-RT-102, Radiographic Examination to Detect ...MIC, !
Revision 0, dated November 15, 1996. The attack.of MIC occurs in the
weld or in close proximity to the weld in stainless steel piping. The
procedure was discussed with a corporate NDE, Level III, radiographic :
specialist and the X ray film for welds WS 18E Line 4" WS 56163 03 Weld l
Nos. 60, 61, 64, and 65 were reviewed with the radiographer for the
presence of MIC attack. Further discussions were held with the
,
l
radiographer concerning the evaluation of the length of the MIC defect ;
size and the inspectors considered those evaluations to be conservative. I
Also, the licensee noted that any weld defects, lack of fusion, etc., .
were added to the defect size in this evaluation. The licensee l
radiographed 15 welds and only one of these welds did not have any areas
of HIC attack. The radiographer shot six film for each weld. The
defect sizes noted in the 14 welds varied from % inch to 18 inches in 2
length with the longest cumulative length being 38 inches in weld No. 89 l
in Line 4" WS 56-163-Q3.
!
The insmetors accompanied one of the licensee's inspectors performing l
the weecly visual examination of the welds in this service piping and l
discussed the results and inspection requirements for this examination. ;
While the licensee was still developing their SW action plan (some of
the actions would depend on inspections that had not yet been
completed), the inspectors reviewed the part that had been formulated as
of November 22, 1996. The licensee started preparation for replacement
of a section of four inch diameter pipe, and was preparing to visually
inspect all accessible welds in stainless steel SW piping. The licensee
stated that the visual inspections would include 18 , 3 , 4 , and 8 inch
diameter piping. The licensee was also considering selecting a sample
of welds for radiography.
c. Conclusions
The licensee's approach to resolving a potential problem with MIC in
stainless steel SW piping was reviewed. One section of 4 inch diameter
pipe was scheduled for replacement based on findings to date. The
licensee was at the investigation stage, and the total corrective action
plan was under development. Evaluations performed by the licensee were
reviewed and found to be conservative. No concerns were identified by
the inspectors.
1
_ _ _
.
.
16
E2.2 Repair Reclacement of Carbon Steel SW Pioina
a. Insoection Scope (37550)
The inspectors reviewed Design Change Notice (DCN) No. 94 010
Pepair/ Replacement of Exposed SW Piping to/from CCHXs, North Anna Units
1&2, and reviewed work being performed to implement the DCN.
Requirements for the scope of this inspection were 10 CFR 50,
Appendix B, Criterion III, Design Control; and Criterion V,
,
1
Instructions Procedures and Drawings.
b. Observations and Findinas
The inspectors reviewed DCN package No.94-010,. including written
descriptions of the change, isometric drawings for pipe support
locations, and the erection control isometric. The package was adequate
for the field implementation underway. The inspectors discussed the SW
repair / replacement project with the cognizant engineer, and accompanied
one of the assigned engineers into the auxiliary building basement where
some of the ex)osed SW piping was being replaced. Using the reviewed
DCN package, t1e inspectors reviewed some of the ongoing work.
The ins)ectors reviewed the welding technique sheet being used to weld
the car >on steel piping (Welding Technique No.103). The root passes
were welded using Gas Tungsten Arc Welding (GTAW) and the remaining part
of the weld was made using Shielded Metal Arc Welding (SMAW). The l
inspectors reviewed the material certifications of the bare wire used in ,
GTAW welding, the covered electrodes used in SMAW welding, and the l
certifications for one section of piping (piping is ASME SA106 Group B).
'
The welder performance qualification records were reviewed for three of l
the welders performing work on this modification. The welds appeared to
be of good quality and no problems were identified with the
documentation.
c. Conclusions
The engineering DCN package was well prepared for implementing a carbon
steel piping replacement in the SW System, and the quality of work being
performed by the craftsmen was good.
E2.3 Condition of Safety Related Batteries
a. Inspection Scope (37550)
The inspectors performed a detailed visual ins)ection of each cell in
the safety related vital and diesel generator aatteries for both units
(total of twelve battery banks). The inspectors also performed a
general inspection of the racks and environment for the batteries. The
inspection was pe-formed in accordance with Institute of Electrical and
Electronics Engineers (IEEE) 450, IEEE Recommended Practice for
Maintenance Testing of Large Lead Storage Batteries for Generating
Stations, Section 4.3 Inspections. This standard was not mentioned in
.
.
17
the UFSAR, but was used as a guide. This particular inspection item was
chosen, in part, because there have been several problems reported with
safety related batteries throughout the industry.
b. Observations and Findinas
The batteries and racks were well maintained. The rooms for the vital
batteries were well maintained and ambient conditions were acce) table.
The ambient conditions for the diesel generator batteries, whic1 were
located with the generators, were acceptable. All charger output
currents and voltages were normal. The electrolyte level was within
specification. No cracks or corrosion were observed. The last pilot
cell data was posted at each battery.
~
Cell No. 30 in bank 1-III and cell No. 60 in bank 1-IV had sedimentation
of significant depth below one or two plates. In response to this
observation, the licensee initiated DR N 96-2635. As part of the DR
resolution, the manufacturer's technical representative came to the site
and inspected the batteries. His report stated that the two cells
mentioned above were showing signs of reconversion to sponge lead from
the positive plate settlement.
The concern with sedimentation is that it could cause.the voltage to
decay. The inspectors reviewed co)ies of the data sheets from the last
surveillance tests which checked t1e voltage, specific gravity and level
of all cells. The surveillance had been performed on June 4, 1996,
according to PT-96 86B. The inspectors reviewed co)ies of the data
sheets for the most recent capacity test which had seen conducted on
September 24, 1994, according to PT 88D. The inspectors observed that
all the cells showed good voltage and capacity in the surveillances,
although tne cell inspections had not identified any problem with
sedimentation.
The licensee indicated to the insaectors that they would define an
enhanced monitoring program for t1e cells with excess sedimentation.
The 1-III battery had a date code February 1987, and the 1 IV battery
had a date code of January 1992.
DR N-96 0421 indicated that a short circuit had occurred at the main
terminals of battery 1 IV during preparations for a service test. The
inspectors examined the condition of the battery terminals. The
inspectors observed that some metal was melted away, but the damage was
of no consequence to future performance of the battery.
c. Conclusions
A detailed cell inspection was performed on each cell of all the
safety-related batteries. The inspectors concluded that battery
maintenance met requirements. However, the inspectors observed
significant sedimentation in two cells. The inspectors concluded that
- - - . . _ - - - - - - -
.
.
,
18
the sedimentation had been aresent on June 4, the time of the last
i
'
surveillance inspection. Tierefore, the fact that the surveillance did
not record any problems with sedimentation was considered a weakness in
the implementation of that inspection.
'
E2.4 Review of Mechanical and Structural Re_ lated Potential Problem Reoorts
and Deviation Reports
a. Inspection Scope (37550)
The inspectors reviewed the disposition and corrective actions for the
below listed Potential Problem Report (PPR) and DRs to determine if they ,
were adequately reviewed, evaluated, resolved and corrected. The items
reviewed were: -
l
'
'
Item No. Condition
PPR 96 018 Internal Pressure Concerns in Closed Piping in
,
Containment During a Design Basis Accident j
'
DR N 96 0384 A Pinhole Leak at Engine Sump of EDG '
i DR N 96-0450 Leakage on One-Inch Diameter Chemical Addition Piping ;
Expansion Joint
i
! DR N 96 0534 Response Spectra for Auxiliary Building
1
DR N 96 0843 Effects of Post-accident Temperature on the !
, Recirculation Spray (RS) and Quench Spray (QS) Systems
,
DR N 96 1169 Quench Spray System Pump Flow Uncertainty
DR N-96 2498 Steam Generator Blowdown Tank Supports
As appropriate, the inspectors verified corrective actions by reviewing
revised procedures, and drawings. The inspectors reviewed calculations
- and modifications as appropriate.
l b. Observations and Findinas
I
While some of the DRs were still in the process of evaluation or
analysis, the inspectors concluded that the performance of the engineers
was good. However, the inspectors had a comment on a tank isolation
sequence carried out by Operations personnel. The corrective action for
DR N 96 2498 included draining and isolating the steam generator
"
blowdown tank for each unit. When the inspectors verified this action,
he noted that one drain valve (1 BD 33) was in the correct position, but
it was not tagged. Review of the system revealed that the position of
valve 180 33 was of no consequence to accomplishing the intent of the
evolution as long as the other valves were in the correct position.
This represented an inattention to detail in preparing the evolution
instruction, since the tagging record did not include this valve.
+ - _ . _ . - - - - . . . - .
1
.
1
.
!
19
c. [pnclusions
A review of six Deviation Reports and one Potential Problem Report
related to mechanical and structural engineering indicated good support
for facilities and equipment by engineers.
E2.5 Overvoltaae on 480 V Bus
a. Insoection Scooe (37550)
The inspectors reviewed a situation where relatively frequent
overvoltages occurred on one or more 480 V buses. Most of the
overvoltage conditions occurred during plant shutdowns, but they
occurred during power operation as well. This situation involved
changing a previously submitted response to an NRC request for
information and performance of a safety evaluation (10 CFR 50.59).
Documents reviewed at the outset included the following: )
-
Letter, VEPC0 to NRC, dated June 4, 1982, on the subject of
" General Design Criterion 17 Analysis North Anna Units 1 and 2."
-
Letter VEPC0 to NRC, dated Seatember 10, 1996, on the subject of
" General Design Criterion 17: . Revised Commitment Related to
Response to Overvoltage Conditions."
-
Safety Evaluation 96 SE 0T-4B.
-
Type 1 Report NP 3085 (partial).
-
Alarm Response Procedure,1F-H5, 480 V or 4 kV Emergency Bus Volts ,
Hi/Lo.
'
Inspection activity of this item included a walkthrough of an alarm
response procedure involving manual operation of an on load transformer
tap changer and reading of voltage indicators and computer outputs.
Also, drawings, calibration data and voltage relays were inspected.
Requirements relevant to this inspection scope were: 10 CFR 50,
Appendix A, Criteria 13, 17, and 19: Regulatory Guide 1.33, Appendix A.
Item 5: Regulatory Guide 1.97 and 10 CFR 50.59.
b. Observations and Findinas
The source transformer had an on load automatic tap changer to maintain
the voltage on the 4 kV bus. Design basis loading scenarios dictated
that fixed taas on the 4160 480 V transformer must be set to boost
voltage. Witi voltage at the 4 kV bus at the low end of the tap changer
control band, voltage at the 480 V bus would be in saecification. With
voltage at the 4 kV bus at the high end of the tap c1 anger control band,
overvoltage would occur on a lightly loaded 480 V bus. Overvoltage
_ . _. - -- - - . - _ - -. . .- . -.
.
.
20
i
relays were installed on each 4 kV and main 480 V bus to warn operators
i of an overvoltage condition. The relays were wired to a common control
i
room annunciator point and individual computer points.
When an overvoltage alarm was received, the operator was prompted by the
alarm response procedure to determine which buses were normal and which
- were abnormal. This was done primarily through checking of voltmeters
i
and the relevant com) uter alarm points. In the case of 4 kV normal and
480 V overvoltage, tle procedure was to put the source transformer tap
.
changer in manual, and depress voltage on the 4 kV bus to the low end of
the acceptable range. The tap changer would then be returned to
- automatic mode. The tap changer control band was about 160 volts and
the tap changer made an adjustment of 26 volts per step.
. .
,
- '
The maximum calculated voltage on a 480 V bus with the 4 kV voltage in l
s)ecification was 521.9 V. Between 1982 and a recent procedure change, '
t1e operators were allowed 15 minutes to take the actions described
! above. The procedure was changed recently to allow a response time of !
,
two hours. The two hours applied only to performing the tap changer
"
manipulation.s. The change was supported by a safety evaluation, and the
NRC was notified of the procedure change by letter. The ;
- covered the case of diesel generator as the power source. procedure also
i The 480 V bus voltage could be read at a computer terminal in the main
- control room and other locations. This was accomplished through
- potential transformers, ac/dc transducers, a multiplexer and the
Emergency Response Facility computer. The transducers were wired to
read line to neutral voltage, and the multiplexer applied a factor of
- 1.73. The purpose of this factor was to present a line to line
magnitude voltage which was more recognizable to operators.
l The inspectors read the following voltages at the Emergency Response
. Facility terminal for the 1H1 bus: A=493, B=530 and C=519. These
8
voltages were significantly unbalanced and two of the three were above
the alarm set point of 515 V. The licensee initiated DR N 96 2634 to
resolve this apparent discrepancy. Using an accurate portable
1 voltmeter, the licensee read voltages directly on the 480 V bus and at
l various points in the potential circuit. These readings indicated that
- voltages were normal and balanced -- 507, 504 and 506. The readings
also indicated that the multiplexer was introducing an error in the
computer readout of voltage. The inspectors requested a co)y of the
last calibration of the voltage loop at the multiplexer. T1e last
, calibration had been performed on April 26, 1996. One of the phases had
4
a significant error, and was adjusted at that time. Since that time,
the multiplexer had drifted out of calibration. As a result of the
, inspection findings related to reading voltage at the 480 bus, the
! licensee was considering the following three actions:
2
1 -
Re wire the transducers to read line to line voltage.
- - In the interim, revise the ERF nomenclature to indicate the
reading is line to neutral multiplied by 1.73.
4
l
-- -. - .
.
.
21
-
Reduce the calibration interval of the multiplexer.
c. Conclusions
The alarm response procedure for bus overvoltage was a workable
procedure, and was consistent with statements made in letters to the NRC
on the subject of overvoltages. The safety evaluation supporting the
change in maximum allowable response time for performing tap changer
manipulations was accurate and complete.
Some corrective actions were proposed by the licensee to address NRC
comments with regard to reading voltage at the 480 V bus, but this did
not represent any programmatic weakness. The overvoltage relays with
alarms were a conservative design in relation to standard industry
practice.
E2.6 Adecuacy of Voltaae for Diesel Generator Breaker Close Coil
a. Insoection Scope (37550)
From a summary of DRs written on electrical systems since November 1995,
the inspectors selected DR N 96 0334 for further review. This DR,
initiated February 19, 1996, involved the failure of safety related
vital battery 1-I to meet one acceptance criterion during performance of
the last service test.
The relevant requirements for this inspection item were TS 4.8.2.3.2.d
(battery service test) and 10 CFR 50, Appendix A, Criterion 17. Electric
Power Systems.
b. Observations and Findinas
The acceptance criterion from 1-PT 87H, DC Distribution System' Service
Test (Train A), that was not met in the last service test was to have at
least 115.6 VDC at the battery terminals at t=10 seconds. The measured
voltage was 115.3 VDC.
The reason for this criterion was to demonstrate that the breaker close
coil for diesel generator 1H was operable. The criterion was determined
by calculation and directly related to the close coil rated minimum
operating voltage of 70 VDC. As confirmed by the inspectors, the source
of this value was a letter from Brown Boveri Co., to VEPC0, dated June
24, 1986, on the subject of " Reliable Minimum Close Coil Voltage." A
similar criterion applied to battery 2-I, but the other vital batteries
did not have a corresponding criterion because calculations indicated
that the voltage at t=10 seconds was not critical.
The licensee completed an Operability Determination on February 20,
1996. The report, which was reviewed by the inspectors, concluded that
the battery was operable based primarily on the logic that the service
.
.
22
test result was only 0.3 V less than the conservatively calculated
minimum voltage. Also, the report referenced a test conducted on an i
identical breaker in December 1985 which demonstrated breaker operation I
with a control voltage of about 40 VDC.
The Operability Determination also recommended that the output breaker
for diesel generator 1H be tested to demonstrate operability at control
voltages less than 70 V. This was expeditiously done, and the breaker
was demonstrated to operate with a minimum control voltage of about
40 V. The inspectors asked about the test methodology to determine a
minimum operating voltage. The test engineer explained that he slowly
increased voltage to the close coil being tested with a rheostat. The
inspectors commented that a similar test conducted at another site had
resulted in damaging a close coil which had a rated minimum operating '
voltage of 100 VDC and a rated energize time of one minute. The test
engineer recollected that he increased from zero to operate voltage in
about 15 seconds. The rated energize time was not readily available.
The breaker in question operated several times during diesel generator
surveillance tests since the special test was conducted. While the l
inspectors agreed that the diesel generator output breaker was OPERABLE,
there still remained the question of whether the test procedure affected
the useful life of the close coil.
The inspectors noted that the criterion for battery voltage at t=10
seconds did not provide margin above the calculated value. Should the
service test result be only slightly above the criterion, the procedure
would not require any further evaluation. However, in such a case,
given an 11 year old battery, normal aging could very possibly result in
below criterion results at the next scheduled test. To address this
concern, the inspectors reviewed results of the last service test on
battery 2-I, which supplied diesel generator 2H output breaker control
power. The test result was 118.5 VDC as compared to a required 111.4
VDC. Therefore, there was sufficient margin in the last test results to i
offset normally expected aging. The licensee stated they would I
re consider their t=10 second criterion in light of battery aging.
Given the importance of the components involved, the inspectors decided
that this issue should be re visited at a future date. The specific
items to review are:
- Enhancement to the voltage criterion in the service test procedure
to account for aging.
-
Enhancement to the test procedure which demonstrated close coil
operating voltage.
- Evaluation of the close coil ratings versus the test procedure
used in February 1996.
-
Evaluation of future service test results versus the close coil
rating.
.
.
.
23
The issue will be tracked under an Inspection Follow up Item (50 338,
339/96012-05).
c. Conclusions
The inspectors reviewed a DR involving the failure of safety related
vital battery 1-I to meet one acceptance criterion during performance of
the last service test. .The inspectors agreed that the subsequent
Operability Evaluation was reasonable, and that the requirement of the
TS was met. An Inspection Follow up Item was established to ensure
review of certain procedure enhancements and future test results.
E3 Engineering Procedures and Documentation
.
E3.1 Modification of the CCW Surae Tank Suocort
a. Inspection Scooe (37550)
From a summary of DRs assigned to structural engineers, the inspectors
selected randomly DR N 96 2095 for review. Resolution of this DR
involved a modification, and the inspectors reviewed that modification
as well. The upper level requirement applicable to review of the DR was
10 CFR 50, Appendix B, Criterion XVI, Corrective Action. The
requirement applicable to review of the modification was 10 CFR 50,
Appendix B, Criterion III, Design Control. The DR and modification
involved 10 CFR 50 Appendix A. Criterion 2, Design Bases for Protection
Against Natural Phenomena.
b. Observaticns and Findinas
DCN 96 014 reinforced the supports for the CCW surge tank to resolve
concerns about the seismic integrity of the tank. From a design
wrspective, this DCN met the requirements, and resolved the DR.
iowever, inspection of the completed work by the inspectors identified
that the dimensional tolerances indicated on Drawing No.
N 96014 3-S 001, Sheets 1 through 8 were exceeded. For example, the
dimensions for certain anchor bolts carried a tolerance of minus 0
inches, plus 2 inches. Actual dimensions varied from the specified
minus tolerance by ly inches and the plus tolerance by IV inches. Also,
the inspectors observed that one pipe support for a 3 inch diameter pipe
was attached to the original un reinforced portion of the tank support
and that pipe support did not show on the modification drawings. DCN
96 014 was signed as completed on October 11, 1996, by the Operational
Readiness Review. The licensee did not produce any documentation
indicating that the discrepancies were noted or evaluated. The
inspection finding described above constitutes a violation of 10 CFR 50,
Appendix B, Criterion V, which requires that activities affecting
quality shall be accomplished in accordance with documented drawings.
The matter was identified as a Violation (50 338, 339/96012-06).
1
I
)
!
.
.
24
c. Conclusions
Review of a 1996 modification package (DCN) to reinforce the supports
for the CCW surge tank to resolve concerns about the seismic integrity
of the tank indicated that the design was correctly accomplished, but
that the actual installation did not meet specified dimensional
tolerances. Also, a pipe support was installed at a point where no
support was shown on the drawings. A Notice of Violation was issued.
E3.2 Set Points for Molded Case Circuit Breakers
a. Insoection Scope (37550)
The inspectors reviewed the control of set points for safety related
molded case circuit breakers. This inspection topic was chosen, in
part, because lack of controls on molded case circuit breaker set points
at other sites resulted in breakers inadvertently tripping during
starting.
Relevant requirements for this inspection topic included 10 CFR 50,
Appendix B, Criterion III, Design Control and Criterion V. Instructions.
Procedures and Drawings. Guidance was provided by IEEE std 741 1986,
IEEE Standard Criteria for the Protection of Class 1E Power Systems and
Equipment in Nuclear Power Generating Stations, Sections 5.1.3.1 and
6.1.4. Also, the inspectors referenced IEEE std 242 1986, IEEE
Recommended Practice for Protection and Coordination of Industrial and
Commercial Power Systems Section 9.3.3.5, Instantaneous Settings.
b. Observations and Findinas
The great majority of motor control centers at the site were furnished
by Klockner Moeller Co. The original circuit breakers had an adjustable
inverse-time (thermal) element and a fixed instantaneous (magnetic)
element. Many of the original circuit breakers had been replaced with a
newer style due to a problem described in a 10 CFR 21 report (NRC
Information Notice 93 22) and other age related failures. The newer
style circuit breakers had an adjustable thermal element and an
adjustable magnetic element.
The frame size and thermal element set point were shown on the one line
diagrams which depicted the 480 V motor control centers and loads. The
magnetic set point was not shown on the drawings. The inspectors
inquired as to how the set points for the magnetic element were
established and controlled. The engineers responded that the
craftsperson or technician installing a new breaker would know (i.e.,
skill of the craft) to make the settings the same as the one being
replaced. The validity of this method was based on the philosophy that
operating experience has shown the set points to be a>propriate (i.e.,
no inadvertent tri) ping). The licensee pointed out t1at the magnetic
set point, althoug1 fixed, was indicated on the nameplate of the
original style circuit breakers. This was confirmed by the inspectors.
- . _- - - -. ._ . - - - - . - - . . .
.
t
6
25
i
The licensee stated that the method by which a craftsperson or
technician set up a new breaker was not explicitly covered in any
procedure nor was it covered in any required training.
The inspectors reviewed Electrical Maintenance Procedure 0 EPM 0304 01.
Testing Non Containment Isolation 480 V Breaker Assemblies, Revision 18.
The inspectors noted that both the thermal and magnetic elements were
tested. The magnetic element was checked to carry 70 percent of the set
- point value and trip at 125 to 140 percent of the set point value.
,
The inspectors examined six safety melated in service circuit breakers,
- four original style and two newer style. The examination confirmed that
the thermal element set point matched the one-line diagram. The
magnetic element set points were recorded from the nameplate for the
original style and from the setting dial for the newer style. The
inspectors concluded that the set points for the magnetic element of the
newer style breakers matched what would have been the fixed setting on
the original style breaker having that thermal set point. The
inspectors also compared the set points to the motor full load current
] and locked rotor current of the respective loads, and concluded that the
4
set points were correct. The circuit breakers inspected were:
Comoartment No. Load Breaker Style
2H1 2N-J3 MOV-2890C original
2H12N B3 2 CV-P 03A original
2H12N A4 2-HC-F-01 original
2H1 25 C1 MOV-2720A original
2H1-2S C3 2 RS P 3A newer
c. Conclusions
The licensee's test procedure for the molded case circuit breakers was
good, in that, it checked that the magnetic element tripped within a
specified band around the set point. The controls for establishing and
verifying the set point for the magnetic element were minimal. There
was no set point document, drawing or specific instructions to help
ensure proper set mints were maintained. Based on a sample of two
newer circuit brea(ers, the licensee's informal method resulted in
correct settings. Nevertheless, the lack of formal controls on the set
point for the magnetic element of molded case circuit breakers was a
weakness in the licensee's design control program, in that, the
continued use of the informal method has increased the probability to
result in incorrect set points. Whether the lack of formal controls
represents a violation of NRC requirements in the area of design control
or procedures is under further review by the NRC. The issue is
identified as Unresolved Item (50 338, 339/96012 07).
._ ._ _ _ . _ . . _ _ . _ . _ _ _ _ _ _._. _ -
_ _ . _ _ . _ _ _ . . _
~ !
!
.
4
-
26
!
] E7 Quality Assurance in Engineering Activities l
E7.1 Safety Committees j
a. Insoection Scope (37550) l
i
'
The inspectors reviewed the functioning of the two safety and oversight
committees.
,
!
,
b. Observations and Findinas
i
The inspectors reviewed some of the minutes of past meetings for the two
safety and oversight committees and attended meetings of both of these ;
committees. During the meeting of the Station Nuclear Safety and 1
2
Operating Committee, the inspectors observed the review and a> proval of
a temporary modification (required 10 CFR 50.59 screening), t1e ap3roval )
of a special report on SW/ ground water levels, the approval of eig1t ,
l procedure changes, and a change to a curve for nuclear fuel burnup rate. '
'
A review was made of the last three MSRC meeting minutes, and it was l
4 noted by the inspectors that the committee was performing the functions
delineated in the committee's procedures. This committee is the !
off-site oversight review committee. The inspectors attended a part of
l the meeting held at the North Anna Station on November 20. 1996. Three 1
- root cause evaluations (two involving unit trips) and various
i improvement initiatives for North Anna were discussed. The items were ,
- well presented and resulted in lively and productive discussions.
{
c. Conclusions l
The safety and oversight committees were conducting their duties in an
efficient and productive manner.
E7.2 Enaineerina Self-Assessment
a. Inspection Scooe (40500)
A review of the licensee's engineering self assessment 3rogram was
conducted by the inspectors to see if strengths and wea(nesses were
identified and if corrective actions were initiated for the weaknesses.
b. Observations and Findinas
The ins)ectors reviewed the procedure for engineering self assessments,
NASES (iorth Anna Station Engineering Services) 1.12. Controlling
Procedure for Engineering Self Assessment, Revision 0. Site Engineering i
Services performs a wide variety of services and the procedure is !
intended as a guideline only. The Engineering Review Board is
responsible for controlling the scope of the proposed self assessments.
Since this program was recently implemented, very few self assessments
were completed. The inspectors reviewed two partially completed j
!
I
_ _ _ _ _ _ _ . _ _ - _ . _ _ _ . _ . . - _ _ _ _
. _ _ . _ _-.
.
.
27
4
assessments, one on System Engineering and one on Post Maintenance
Testing. The inspectors noted during the MSRC meeting that the Nuclear
Oversight Group had identified that an upper tier document which
addresses self-assessment (PAP 0104) was under modification because it
did not spell out management's expectations for self assessments.
. c. Conclusions
The engineering self assessment program was only recently defined, and
very few self assessments were completed.
'
E8 Miscellaneous Engineering Issues (92903)
.
E8.1 (Closed) URI 50-339/96009 03, review anomalies in large bore snubber
test data. The inspectors completed their review of large bore snubber
functional test data. No other anomalies were identified. Snubbers
i with anomalies in test data were either repaired, replaced or
subsequently satisfactorily tested.
The licensee plans to procure replacement large bore snubbers from a
different vendor prior to the next refueling outage, i.e., the Unit 1 1
,
refueling outage scheduled to begin in May 1997. Testing of the new I
i
snubbers will use different test equipment and test techniques. An
Inspection Followup Item is opened to review functional tests that will i
!
be conducted on either new or old snubbers in the upcoming Unit 1 ,
refueling outage (50 338, 339/96012 08). l
i
(
IV. Plant Support '
'
R1 Radiological Protection and Chemistry (RP&C) Controls
R1.1 As low As Reasonably Achievable (ALARA) j
a. Inspection Scope (83750)
The inspectors reviewed licensee records of personnel radiation exposure
and discussed ALARA program details, implementation and goals with the
1
licensee. The site collective dose and individual exposures were
compared to licensee established ALARA goals and occupational dose
limits, respectively.
b. Observations and Findinas
The licensee provided the inspectors with reports of personnel radiation
exposure for calendar year (CY) 1995 and the first three quarters of
. 1996. Those reports indicated that the licensee had initially
established an ALARA goal of 459 person roentgen equivalent man (rem)
for the 1995 site collective dose. That goal included a projected 425
2 person rem for the Unit 2 SG Replacement Project and related outage
,
activities. After the actual exposure for that outage was determined to
have been 340 person rem, the annual goal was reduced from the initial
_ _.
- _ _ - .. .- . . . .- ... . _ - - - . . - . - . ..
.
.
28
goal of 459 person rem to 367 3erson rem. The final collective dose for
CY 1995 was 359 person rem. T1e annual goal for the 1996 site
collective dose was established at 364 person rem. That goal included a
projected 188 person rem for the Unit 1 Refueling Outage (RF0) and 149
person rem for the Unit 2 RF0. The actual ex>osures for those outages
were 184 and 117 person rem, respectively. T1e actual exposure during
the first three quarters of 1996 was 305 )erson rem. The licensee
indicated that, given the current work scledule for the remainder of the j
1
year, the 1996 annual goal was not expected to be exceeded. The
inspectors determined that the licensee was meeting their established
ALARA goals. The licensee's personnel radiation exposure records also
indicated that the maximum individual exposures for 1995 and the first
three quarters of 1996 were less than 2.6 rem and within the limits
specified in 10 CFR 20.1201(a). >
c. Conclusions
i
Based on the above reviews and observations, the inspectors concluded
that the licensee was closely monitoring collective and individual
radiation dose exposure, and that the licensee was meeting established
ALARA goals and occupational dose limits. ,
R1.2 Water Chemistry Controls
a. Inspection ScoDe (84750)
The inspectors reviewed implementation of selected elements of the
licensee's water chemistry control program for monitoring primary and
secondary water quality. The review included examination of program
guidance and implementing procedures, and analytical results for
selected chemistry parameters. Those procedures and data were compared
to specific ard programmatic requirements, i.e., the TSs required the
licensee to monitor primary coolant for specific chemistry aarameters
and to implement a program for monitoring secondary water clemistry to
inhibit steam generator tube degradation.
b. Observations and Findinas
The inspectors reviewed VPAP 2201 Nuclear Plant Chemistry Program,
Revision 1, and determined that it included provisions for sampling and
analyzing reactor coolant at the prescribed frequency for the parameters
required to be monitored by the TSs. That procedure also included
provisions for monitoring primary and secondary water quality based on
established industry guidelines and standards. Although the licensee's
procedure did not s)ecifically indicate that their program included
implementation of t1e Electric Power Research Institute (EPRI)
guidelines for Pressurized Water Reactor (PWR) primary and secondary
water chemistry, the inspectors used those guides as references for
evaluating the effectiveness of the licensee's program. The inspectors
noted that VPAP 2201 listed the sampling frequency and typical values
for each parameter to be monitored. Action levels applicable to various
operational modes were given where appropriate. Guidance was also
.
.
29
provided for actions to be taken if analytical results exceeded
prescribed limits. The inspectors determined that the above guidance
and procedures were consistent with the applicable TS requirements and
EPRI guidelines.
The inspectors also reviewed trend plots and records of analytical
results for selected parameters generated during the period April i
through October 1996. The parameters selected included dissolved l
oxygen, chloride, fluoride, sulfate, and dose equivalent iodine-131 in l
reactor coolant and dissolved oxygen, iron, copper, sodium, hydrazine, j
silica, and sulfate in secondary systems. Those parameters were
maintained well within the relevant TS limits and within the EPRI
guidelines for power operations.
c. Conclusions i
Based on the above reviews, the inspectors concluded that the licensee's
water chemistry control program for monitoring primary and secondary
water quality had been implemented in accordance with the TS
requirements and the EPRI guidelines for PWR water chemistry.
R1.3 Transoortation of Radioactive Materials
l
a. Insoection Scope (TI 2515/133) '
The inspectors evaluated the licensee's transportation of radioactive
materials programs for implementing the revised Department of
Transportation and NRC transportation regulations for shipment of
radioactive materials as required by 10 CFR 71.5 and 49 CFR Parts 170
through 179.
b. Observations and Findinos
1
The inspectors reviewed the licensee's actions regarding a shipment of
licensed material which exceeded the limit for specific activity
delineated in the Certificate of Compliance (CoC) for the cask used to
transport the material. On October 31, 1996, the licensee's radioactive
waste shipping personnel were reviewing shipping records and found that
the most recent revision of the CoC for the shipping cask had not been
properly filed in the cask's reference notebook. The licensee maintains
a cask reference notebook for each NRC licensed cask used by the
facility and licensee 3ersonnel use those notebooks when preparing
radioactive material slipments. On April 16, 1996. CoC No. 6601,
Revision 25, for the Model No. CNS 8 120A package was issued by the NRC
Office of Nuclear Material Safety and Safeguards, and was received at
the site on or about May 6, 1996. Further review of shipping records by
the licensee on November 5,1996, revealed that on July 9,1996, the
cask was used for a shipment (No. 96 05) of radioactive waste to the
Chem-Nuclear waste disposal site at Barnwell, SC. 10 CFR 71.12(c)(2)
authorizes any licensee to trans) ort licensed material in a package for
which a CoC has been issued by tie NRC, provided that the licensee
complies with the terms and conditions of the CoC. Condition 5
- - - ~. - - . - - - - . ._ -. . - . - - .
.
.
30
(b)(1)(1) of CoC No. 6601 specifies that the average concentration of
the package contents shall not exceed 0.3 millicurie per gram of
radionuclides for which the A2 quantity in A)pendix A of 10 CFR Part 71
is more than 1 curie. Contrary to that concition, the average
'
concentration of radionuclides for which the A2 quantity in Appendix A
of 10 CFR Part 71 is more than 1 curie for the package contents of
Shipment No 96-05 was 0.495 millicurie per gram. On November 6, 1996,
the licensee called the NRC Region II Office to report the violation of
10 CFR 71.12(c)(2) and indicated that shipments of radioactive waste for
disposal had been immediately suspended and that an investigation had
- been initiated. During this inspection the licensee's report
documenting that investigation was reviewed by the inspectors. That
report indicated that the root cause of the violation was poor document
control of the CoC. Other contributing factors identified by the
investigation were incomplete procedural checklist guidance for
preparing and inspecting shipments, and incomplete guidance for
a) plication of the software used as an aid in shipping preparations.
T1e report also included recommendations for corrective actions to
prevent recurrence of this event. Those recommendations were:
delineating the CoC requirements in the cask shipping checklists used by
the personnel who prepare the casks for shipment and in the checklists
used by Quality Assurance / Quality Control personnel who inspect the
shipments; filing the CoCs in their proper location in the cask
reference notebooks immediately upon receipt; and establishing a
required reading program and signoff system for revised shipping
3rocedures. The licensee indicated that those corrective actions would
>e implemented prior to the resumption of radioactive uste shipments
planned for December 6, 1996. This licensee identified violation for
failure to comply with the conditions of the Certificate of Compliance
for an NRC approved shipping package is being treated as an NCV.
consistent with Section VII.B.1 of the Enforcement Policy (50 338,
339/96012-09).
c. Conclusions
Based on the above reviews, the inspectors determined that the
licensee's efforts in identifying and initiating corrective actions for
the violation were adequate. One NCV was identified by the licensee for
failure to comply with the conditions of the CoC for an NRC-approved
shipping package.
R8 Miscellaneous RC&P Issues (92904)
R8.1 (Closed) Violation 50 338, 339/96007-04, failure to label a container of
licensed material. During a previous inspection, the inspectors
observed a trailer in the outside protected area which contained
contaminated scaffolding but did not bear a completed radioactive
material label. The licensee's response to the violation indicated that
the container was relabeled properly, that other containers were
ins)ected to ensure proper labeling, and that this event was discussed
witi Health Physics (HP) personnel during departmental meetings and
subsequent training sessions. During this inspection no further
1
.
.
31
examples of improper container labeling were observed by the inspectors.
Licensee records of attendance and discussion topics for the referenced
departmental meetings and training sessions were also reviewed by the
inspectors. The inspectors concluded that the licensee's response dated
October 8, 1996, and the corrective actions were appropriate and had
been adequately implemented.
R8.2 (Closed) Violation 50 338, 339/96007 05, failure to follow procedures
for minimizing the potential spread of radioactivity to unrestricted
areas. During a previous inspection it was determined that a individual
was released from the protected area with clothing which exceeded the
licensee's procedural release limit for radioactive contamination. The
licensee's response to the violation indicated that the contaminated
clothing had been retrieved, that HP procedures had been revised to
provide additional guidance to HP personnel for dealing with personnel !
that alarm portal or personal contamination monitors, and that HP
personnel were trained in those procedural changes. During this
inspection the licensee's revised HP procedures were reviewed and found
to include specific guidance for responding to alarms by portal and
personal contamination monitors. The inspectors also reviewed the
licensee's records for training on those procedure changes. The
inspectors concluded that the licensee's response dated October 8,1996,
and the corrective actions were appropriate and had been adequately
impirmented.
S1 Conduct of Security and Safeguards Activities (71750)
On November ll, the inspectors toured various plant security systems I
with a security team leader. Specifically, selected protection area
perimeter fencing and isolation zones, Central and Secondary Alarm l
Stations, various vital area accesses, and the secondary power supply l
were inspected. The inspectors observed that the protected area j
perimeter fencing was in good condition with no o)enings. Isolation :
zones were free of objects and clearly marked. T1e inspectors observed l
'
that the Central and Secondary Alarm Stations were properly manned and
that intrusion systems were functioning properly. Various vital area
accesses and boundaries were inspected and found to be in good working
order. The inspectors concluded that security systems were in good
working order and security manning was appropriate.
VI. Manaoement Meetinas
X1 Exit Meeting Summary
The inspectors ) resented the inspection results to members of licensee ,
management at t1e conclusion of the inspection on December 20, 1996. The l
licensee acknowledged the findings presented.
i
. -. - . . .... ... - . -_ - ..- -..- _. - .-. - . - __ . . - _ .-.-.. .... . ._ - .- - .. _ _ . . - .
4
J .
- .
1 :
- -
l
32
i The inspectors asked the licensee whether any materials examined during the !
i inspection should be considered proprietary. No proprietary information was :
-
identified.
.
!
. - -. - - - _-. - . _ _ _ . . _ _ _ _ _
.
!*
33
PARTIAL LIST OF PERSONS CONTACTED
Licensee
W. Anthes, Superintendent, Outage and Planning
'
B. Foster, Superintendent Station Engineering
,
~
E. Grecheck, Assistant Station Manager, Operations and Maintenance
J. Hayes, Superintendent, Operations
D. Heacock, Assistant Station Manager, Nuclear Safety and Licensing
M. Kansler, Vice President, Nuclear Operations
,
P. Kemp, Supervisor, Licensing
i
T. Maddy, Superintendent, Security
W. Matthews, Station Manager
M. McCarthy, Director, Nuclear Oversight
D. Roberts, Supervisor, Station Nuclear Safety !
H. Royal, Superintendent, Nuclear Training !
D. Schappell, Superintendent, Site Services l
R. Shears, Superintendent, Maintenance
A. Stafford, Superintendent, Radiological Protection
NRC
I
B. Buckley, Project Manager '
F. Reinhart, Acting Project Director
INSPECTION PROCEDURES USED
IP 37550: Engineering ;
IP 37551: Onsite Engineering
IP 40500: Effectiveness of Licensing Controls in Identifying, Resolving, and
Preventing Problems
IP 62707: Maintenance Observations '
IP 71707: Plant Operations
IP 71714: Cold Weather Preparations
IP 71750: Plant Support Activities
IP 83750: Occupational Radiation Exposure !
IP 84750: Radioactive Waste Treatment, and Effluent and Environmental
Monitoring
IP 92700: Onsite Followup of Written Reports of Nonroutine Events at Power
Reactor Facilities
IP 92901: Followup Plant Operations
- -- _ - . . _ - - - _ _ - - - - - _ - .
.
l
34
IP 92902: Followup - Maintenance
IP 92903: Followup - Engineering
IP 92904: Followup Plant Support
IP 93702: Prompt Onsite Response to Events at Operating Power Reactors
TI 2515/133: Implementation of Revised 49 CFR Parts 100 179 and 10 CFR Part
71
ITEMS OPENED AND CLOSED
Opened
50-339/96012 01 VIO Failure to Meet 10 CFR 50 Appendix B
Criterion III Recuirements for Design Control of
Safeguards Area kalls (Section 08.1)
50 338, 339/96012-02 NCV Inadequate Surveillance Test Procedure for i
Placing Reactor Trip Breakers in Service '
(Section M8.3) j
50-339/96012-03 VIO Inadequate Design Controls Contribute to
Non Conforming Bolts in Column Flange for
Service Water Pump 2-SW P 1A (Section El.1)
50-338, 339/96012 04 NCV Improper Deletion of DHR Isolation Valve !
Inservice Testing (Section E1.3)
50-338, 339/96012 05 IFI Battery Service Test and Rating of Diesel
Generator Breaker Close Coil (Section E2.6)
50 338, 339/96012-06 VIO Component Cooling Surge Tank 1 CC-TK 1 Support
Structure not Installed Per Drawings
(Section E3.1)
1
50 338, 339/96012-07 URI Control of Set Points for Molded-Case Circuit
Breakers (Section E3.2)
50 338, 339/96012 08 IFI Review Functional Tests That Will Be Conducted
On New or Old Snubbers During Unit 1 Refueling
Outage (Section E8.1)
50 338, 339/96012 09 NCV Failure to Comply With Conditions of CoC for NRC
Approved Shipping Package (Section R1.3)
. . - . . ._ - - _ - . . - - - - -_ - . .-.
.
.
35
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Closed
50 338/95015 01 VIO Failure To Follow Procedures For Properly
Controlling Safeguards Area Ventilation System
(SAVS) Maintenance (Section M8.1)
50 339/95020 02 VIO Failure to Comply With 3.6.1.3 for Air Lock
Outer Door Rendered Inoperable by Open Test
Connection (Section M8.2)
50 339/96001 LER Potential Unfiltered Release Path From the
Quench Spray Pump House to the Environment
(Section 08.1) -
50-339/96003 LER Automatic Reactor Trip Resulting From Main
Generator Stator Coil Failure Due to Personnel
Error (Section M8.5)
50 339/96004 01 URI Review Significance of Safeguard Area
Ventilation Not Meeting Design Basis
(Section 08.1)
50 338, 339/96007-04 VIO Failure to Label a Container of Licensed
Material (Section R8.1)
50 338, 339/96007-05 VIO Failure to Follow Procedures for Minimizing the
Potential Spread of Radioactivity to 1
'
Unrestricted Areas (Section R8.2)
50 338, 339/96009 LER Reactor Trip Bypass Breaker Missed Surveillance
Due to Inadequate Surveillance Test Procedure
(Section M8.3) l
50 339/96009 03 URI Review Anomalies in Large Bore Snubber Test Data
(Section E8.1) i
50 338/96010 LER Automatic Reactor Trip Due to Failure of a
Generator Negative Phase Sequence Relay
'
(Section M8.4)
50 338, 339/96012 02 NCV Inadequate Surveillance Test Procedure for 1
Placing Reactor Trip Breakers in Service
(Section M8.3)
50 338, 339/96012 04 NCV Improper Deletion of DHR Isolation Valve
Inservice Testing (Section E1.3)
50 338, 339/96012 09 NCV Failure to Comply With Conditions of CoC for NRC
Approved Shipping Package (Section R1.3)