ML20134G907

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Insp Repts 50-338/96-09 & 50-339/96-09 on 960811-0921. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML20134G907
Person / Time
Site: North Anna  
Issue date: 10/21/1996
From: Mcwhorter R, Taylor D, Vandorn P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20134G755 List:
References
50-338-96-09, 50-338-96-9, 50-339-96-09, 50-339-96-9, NUDOCS 9611130429
Download: ML20134G907 (27)


See also: IR 05000338/1996009

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Report Details

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Summary of Plant Status

Unit 1 began the inspection period at full power. On August 27, the unit

tripped from full power due to a rod control system failure (Sections 01.2 and

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02.3). The reactor was restarted on August 28, and the unit returned to

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commercial service on August 29. The unit returned to full power on August 30

and remained at or near full power for the remainder of the inspection period.

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Unit 2 began the inspection period at full >ower. On August 16. the unit

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began a coast down to a refueling outage.

_ ate on September 7 a unit

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shutdown was commenced from 85 percent power, and early on September 8, the

unit was removed from commercial service and the reactor was shut down for a

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scheduled refueling outage. On September 16, reactor defueling was completed,

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and the reactor remained defueled for the remainder of the inspection period.

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I. Operations

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Conduct of Operations

01.1 Daily Plant Status Reviews (71707)

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The inspectors conducted frequent control room tours to verify proper

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staffing, operator attentiveness, and adherence to approved procedures.

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The inspectors attended daily plant status meetings to maintain

awareness of overall facility operations and reviewed operator logs to

verify operational safety and compliance with Technical Specifications

(TSs).

Instrumentation and safety system lineups were periodically

reviewed from control room indications to assess operability.

Frequent

plant tours were conducted to observe equipment status and housekeeping.

Deviation Reports (DRs) were reviewed to assure that potential safety

concerns were properly reported and resolved. The inspectors found that

daily operations were generally conducted in accordance with regulatory

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requirements and plant procedures.

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01.2 Prompt On Site Response to Events (93702)

a.

Insoection Scope

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On August 27, the licensee notified the inspectors concerning a Unit 1

reactor trip. The unit tripped from full power while operators were

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performing 10P-17.1, Control Rod Operability, Revision 17. The

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inspectors reviewed control room conditions and operations following the

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trip. Additionally, the inspectors attended the licensee's post trip

review and reviewed trip data to independently verify that safety system

and operator performance was as expected throughout the event.

b.

Observations and Findinas

The inspectors found that the automatic trip was generated from the

Reactor Protective System (RPS) when a nuclear instrument negative rate

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condition was detected. The trip occurred as o)erators began to move

the B control rod bank inward in accordance wit 1 1 0P-17.1. The

inspectors observed that operator response following the trip was good,

and procedures for responding to the trip were a3propriately

implemented. Although the inspectors observed t1at a large number of

people were present in the control room soon after the trip,

communications remained formal and the extra personnel were not

distracting to the operators.

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A review of trip data found that the trip signal was valid and was

caused by one or more dropped control rods. All safety systems

performed as designed for plant conditions during the trip.

During the

trip recovery, main condenser vacuum was lost. Operators were required

to use the main steam atmospheric dump valves to control reactor coolant

system temperature.

Plant startup and subsequent corrective actions are

discussed in Sections 01.3, 02.1 and M2.1.

c.

Conclusions

The inspectors concluded that safety system and operator response to the

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Unit 1 reactor trip was proper.

01.3 Unit 1 Restart Followina Reactor Trio (71707)

a.

Insoection Scoce

On August 28, after a reactor trip the day before, the inspectors

reviewed the licensee's corrective actions for the reactor trip's root

cause. Additionally, the inspectors observed operators performing

Unit 1 restart activities to ensure that operational activities were

conducted in accordance with plant procedures and TS requirements.

b.

Observations and Findinas

The inspectors observed that the licensee's investigations into the root

cause for the Unit 1 reactor trip found that a failure in the rod

control system had caused a drop of one group of the B control rod bank

when the rods were moved when performing 1 0P-17.1.

Repair efforts

identified a discrepancy in the signal from the rod control system logic

cabinet to the aower cabinet supplying the group

An interface card was

replaced, and t1e problem was corrected.

However, the problem could not

be duplicated by placing the suspect card back into the system. The

investigation )ostulated that the sus)ect card had either intermittently

failed or had aroken the circuit at tie card's edge connector. After

replacing the suspect card, technicians completed current order traces

for the entire system, and no other problems were found. The inspectors

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reviewed the current (amaerage) order traces before and after the card

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changeout and verified t1e problem's identification and correction.

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Additionally, the licensee conservatively decided to perform rod drop

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timing tests prior to unit restart, although test performance was not

recuired by TS or the licensee *s response to NRC Bulletin 96-01, Control

Roc Insertion Problems. The inspectors observed that tests were

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successfully completed (Section M1.2).

Formal root cause evaluations

were continuing at the inspection period's end. Additional reviews of

restart issues are discussed in Section 02.1.

The inspectors observed operators performing the Unit I reactor startup

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and found that o)erators properly used appropriate procedures. and were

cautious and metlodical during startup operations.

No significant

problems were encountered during the startup, and control room

communications and formality were good. The inspectors noted that

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appropriate supervisory and management personnel, as well as Oversight

personnel, were present to review startup activities.

c.

Conclusions

The inspectors concluded that the licensee's actions to correct the

cause of the Unit 1 trip and operator performance during reactor startup

were appropriate. A conservative decision was made to perform rod drop

timing tests prior to unit restart.

01.4 Trooical Storm Fran Response (71707)

a.

Insoection Scope

On September 5 and 6, the inspectors reviewed the licensee's response to

severe weather from Tropical Storm Fran. The inspectors compared the

licensee's response to plans for severe weather contained in the

Hurricane Response Plan, the site Emergency Plan, and in 0 AP 41, Severe

Weather Conditions, Revision 12.

b.

Observations and Findinas

The inspectors found that the licensee adequately reviewed the status of

alant equi > ment and activities in anticipation of the severe weather.

)rior to tie storm's arrival, outside areas were inspected for loose

equipment and debris. Outside efforts appropriately focused on areas

temporarily staged with equipment in pre >aration for the Unit 2

refueling outage. Additionally, althougl entry conditions were not met,

the Hurricane Response Plan was implemented as a precaution to ensure

that all appropriate actions were taken.

During the storm, the inspectors found that the licensee ap3ropriately

monitored the storm's progress and remained alert for possiale effects

on the facility. 0-AP-41 was entered as required during tornado

watches, and actions were taken to protect the facility from moderate

winds and heavy rains. As a result of local power outages caused by the

storm, power was lost to numerous emergency sirens (Section P1). No

site damage was sustained due to the storm.

c.

Conclusions

The inspectors concluded that the licensee properly prepared for and

responded to severe weather caused by Tropical Storm Fran.

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01.5 Unit 2 Shutdown for Refuelina (71707)

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a.

Inspection Scope

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On September 8, the inspectors observed operators placing Unit 2 in

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MODE 3 from MODE 2 in preparation for refueling. The inspectors

reviewed activities to ensure operations were conducted in accordance

with plant procedures TS requirements, and commitments made in response

to NRC Bulletin 96 01, Control Rod Insertion Problems.

b.

Observations and Findinas

The inspectors found that operators effectively controlled unit shutdown

activities.

Operating procedures were followed, and TS requirements

were complied with during the mode changes. Communications during

shutdown evolutions were good.

The inspectors observed that the unit was shutdown by manually tripping

all control rods into the core, and control rod drop time tests were

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performed immediately following the shutdown. On September 16, the

inspectors also observed rod drag tests being performed on approximately

ten control rods in the spent fuel pit (Section M1.2). These actions

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met licensee's commitments made in response to NRC Bulletin 96-01. No

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problems were identified during the rod control system testing.

c.

Conclusions

The inspectors concluded that operator control of 31 ant shutdown

activities was good, and the licensee complied wit1 commitments made in

response to NRC Bulletin 96 01, Control Rod Insertion Problems.

01.6 Control of Reactor Coolant System (RCS) Drain Down (71707)

On September 10, the inspectors observed RCS drain down activities

including observation of the pre job briefing and actual drain down to

the 74 inches above mid loop level. A thorough briefing was conducted

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which included an overview of the procedure, a review of drain down

curves, expectations of instrumentation during drain down,

communications, cautions, and specific personnel assignments. The

licensee exhibited good sensitivity to risks associated with drain down.

This was evidenced by excellent involvement between Reactor Operators

and Senior Reactor Operators (SR0s) and by careful procedural

compliance.

Several Shift Technical Advisors were also involved and

accurately predicted when instrumentation would come on scale. The

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prediction for when level would be observed in the sight glass was

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within approximately one minute and for the control room instrument,

which comes on scale at 95 inches above mid loop, was within ten

minutes. Two good initiatives were also noted. One was a rolling lit

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sign highlighting the time to boiling. Also, the licensee developed a

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recorder to do an inventory balance by measuring various tank levels

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involved in the drain down. The recorder did not calculate the total

inventory as expected, but did record the data to do so. Also the

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recorder did not print out digital information as originally intended.

The licensee indicated they intended to continue this initiative and

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modify the recorder as necessary to perform the calculation and to print

the calculation's results.

In summary, the RCS drain down was well

coordinated and personnel exhibited a good sensitivity to risk.

01.7 Unit 2 Refuelina Activities (71707)

a.

Inspection Scope

On September 14, the inspectors observed operators performing Unit 2

refueling activities to ensure that plant operations were conducted in

accordance with procedures and TS requirements.

b.

Observations and Findinas

During core off load, the inspectors verified that operators in

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containment properly used procedures 2-0P 4.1, Controlling Procedure for

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Refueling, Revision 32-P2: 2 0P 4.13 Fuel Transfer System. Revision 1:

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and 2 0P 4.15. Manipulator Crane, Revision 2.

Applicable TS

requirements were reviewed and found to be complied with for operable

equipment and for containment integrity. The inspectors observed that

communications were properly established between all stations and that

evolutions were supervised by a licensed SR0 in containment. Also, the

inspectors observed that fuel movements were being continuously tracked

by a reactor engineer in the control room.

c.

Conclusions

The inspectors concluded that refueling activities were properly

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conducted by operators.

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Operational Status of Facilities and Equipment (71707)

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02.1 Unit 1 Startuo Reviews

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a.

Insoection Scope

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On August 28, the inspectors attended a Station Nuclear Safety and

0)erating Committee (SNSOC) meeting to ascertain if problems following

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t1e August 27 Unit 1 trip were being adequately reviewed and resolved.

b.

Observations and Findinas

Prior to discussing the Unit 1 startup, the inspectors observed the

SNSOC discussing a proposed revision to security procedure SPIP 12.

Refueling / Major Maintenance Measures. The revision proposed changes to

the requirements for security badge display to allow wearing badges

inside Protective Clothing (PC) in containment. The inspectors observed

that a long discussion was generated by the proposed revision. The

discussion eventually led to members of the SNSOC proposing that the

procedure should be further revised to delete the requirement for

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displaying badges in other situations and/or throughout the plant

entirely. The inspectors observed that throughout the long discussions,

neither the individual presenting the revision nor the SNSOC members

displayed a knowledge of the actual requirements for badge display

contained in the Physical Security Plan (Revision 0, dated April 1,

1996). After the discussions appeared to be moving towards referring

the revision back to security for additional reviews, the inspectors

informed the SNSOC members that several of their pro)osals did not meet

the requirements of the Physical Security Plan and t1at they had failed

to recognize this due to their apparent lack of knowledge of the plan's

requirements.

The inspectors then observed the SNS0C consideration of the Unit 1 Post

Trip Review Report. The report was presented to the SNSOC for approval

following its completion by Shift Technical Advisors. As presented, the

inspectors observed that the report accurately analyzed alant

aerformance during the trip and corrective actions for t1e trip's cause.

iowever, the report's analyses of secondary plant equipment problems

encountered during the trip led to much discussion in the SNSOC meeting.

In discussing these failures, the SNS0C determined that the report

inadequately stated that a loss of secondary vacuum would be addressed

through the DR closeout process and inaccurately stated that a reheat

flow control valve,1-MS FCV-104C, had been repaired. The discussions

then centered on deciding what corrective actions were necessary for the

loss of secondary vacuum and for the failure of 1 MS FCV 104C to shut

following the trip. The SNS0C decided not to approve the report until

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additional corrective actions were taken for the loss of vacuum and

until a safety evaluation was completed for 1 MS FCV 104C being left in

a degraded condition.

Later that same day, the additional corrective

actions were completed, and the report was approved by the SNSOC.

The inspectors found that the SNSOC adequately ensured that problems

were being resolved prior to unit startup. However, the inspectors

questioned station management concerning the appropriateness of the

SNSOC directly making decisions about corrective actions to be taken for

equipment problems. The inspectors expressed concern that such active

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decision making was more appropriate for station management discussions

than for the SNSOC, which was intended to be a safety review authority.

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Licensee management stated that they believed the deliberations took the

track they did because the Post Trip Review Report should have been more

thoroughly reviewed prior to being presented to the SNS0C. Management

stated that they expected that such problems would be identified and

resolved by the Supervisor, Station Nuclear Safety (SNS) prior to the

SNSOC presentation. The inspectors also noted that the Post Trip Review

Report presented to the SNSOC had not been presented to the

Su)erintendent, Operations for concurrence signature prior to its

su) mission to the SNSOC.

In the SNSOC meeting, both the Supervisor,

SNS, and the Superintendent, Operations were seeing the report for the

first time as SNS0C members.

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Additionally, the inspectors found that VPAP 1404, Reactor Control.

Revision 0. Section 6.8.1.a. stated that the decision to re start a

reactor after a trip shall be made in accordance with VPAP-2804,

Start-Up Assessment. However, VPAP-2804 had never been issued although

four years had elapsed since the time that VPAP 1404 had been issued

(June 1992). This fact was noted in a supplemental page in VPAP 1404

which stated that until VPAP 2804 was issued, the " Start up Assessment

Review Package distributed by Nuclear Safety and Licensing" shall be

used. The inspectors noted that the Start up Assessment Review Package

was a document normally used for startup following refueling outages and

was not used for startups following reactor tri)s. The inspectors

discussed this issue with licensee management w1o directed station

personnel to complete VPAP 2804 as soon as possible.

c.

Conclusions

The inspectors concluded that the SNS0C considered a security procedure

revision without having an accurate knowledge of the applicable Physical

Security Plan requirements. The SNSOC ensured that adequate corrective

actions were completed prior to restart of Unit 1 following a reactor

tri ).

However, a Post Trip Review Report was not fully reviewed prior

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to >eing presented to the SNSOC which required the SNSOC to depart from

its normal review functions and plan and direct additional corrective

actions. An administrative procedure formally delineating the startup

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assessment process following a reactor trip did not exist.

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02.2 Unit 2 Containment Conditions

On September 9, the inspectors entered Unit 2 containment shortly

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following the shutdown to ascertain the status of equipment following

the long operating cycle. The inspectors found that material conditions

and cleanliness were good. A few small system leaks were identified.

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The inspectors noted that these small leaks had already been identified

by licensee personnel performing RCS leak identification surveillance

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tests. The inspectors concluded that safety systems in the Unit 2

containment were in good overall condition immediately following

shutdown.

On September 18 and 19, the inspectors reviewed activities inside Unit 2

containment. These activities did not promote good housekeeping

practices and potentially represented a challenge to personnel assigned

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to cleanup containment prior to restart.

Specifically, the inspectors

observed that cloth rags were on the pressurizer head in places where

insulation had been removed: materials such as plastic bottle tops and

work gloves were on top of supports and raceways below deck gratings:

and, tools and miscellaneous debris were laid on supports or dropped on

the floor. The inspectors observed no designated trash receptacles in

use in areas Aere work was being performed on the lower two levels of

containment. Housekeeping conditions and practices were discussed with

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plant management.

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02.3 NRC Notifications

a.

Insoection Scope

The inspectors reviewed the following licensee notifications to the NRC

to ascertain if the required reports were adequate, timely and proper

for the events.

b.

Observations and Findinas

On August 27. the NRC was notified as required by 10 CFR 50.72

concerning RPS and engineered safety feature actuations generated when

Unit 1 tripped from full power. The inspectors found that the

licensee's reporting actions were appropriate. Additional inspection

activities and findings are discussed in Sections 01.2, 01.3, 02.1 and

H2.1.

On September 6, the NRC was notified as required by 10 CFR 50.72

concerning the notification of off site authorities. Specifically, the

licensee notified surrounding counties and individuals of flood warnings

downstream of the Lake Anna Dam due to heavy rains from Tropical Storm

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Fran. The inspectors found that the licensee's reporting actions were

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appropriate.

On September 6, the NRC was notified as required by 10 CFR 50.72

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concerning a loss of a significant portion of the offsite emergency

notification system. Specifically, the licensee notified the NRC and

the Commonwealth of Virginia concerning the fact that 28 of 55 emergency

sirens were inoperable. The inspectors found that the licensee's

reporting actions were appropriate. Additional reviews are discussed in

Section Pl.

On September 8, the NRC was notified as required by 10 CFR 50.72

concerning the identification of a condition which could have prevented

the fulfillment of a system safety function needed for accident

mitigation. While shutting down Unit 2 for a refueling outage,

o)erators identified during a routine surveillance test that feedwater

cleck valve, 2 FW 62, would not prevent backflow.

The ins)ectors found

that the licensee's reporting actions were appropriate. T1e licensee

was required to submit a Licensee Event Report (LER) for this event, and

the inspectors will review the licensee's corrective actions after LER

issuance and prior to unit restart.

On September 10, the NRC was notified as required by 10 CFR 50.72

concerning a loss of emergency assessment capability lasting greater

than one hour. At 6:52 p.m., the Safety Parameter Display System (SPDS)

computer failed and could not be restored within one hour. Maintenance

personnel successfully returned the SPDS computer to operation at 10:24

p.m.

The inspectors monitored the licensee's reporting and corrective

actions and found them to be appropriate for the situation.

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On September 19, the NRC was notified concerning the identification of a

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condition which could have prevented the fulfillment of a system safety

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function needed for accident mitigation.

Due to questions raised by the

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inspectors, the licensee identified a procedural deficiency that could

have resulted in the dose to the control room personnel exceeding Fuel

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Handling Accident (FHA) analysis assumption. After further review the

licensee retracted this notification on October 15, 1996. The

inspectors reviewed the licensee's reporting actions and found that they

were appropriate. Additional reviews are discussed in Section E2.1.

c.

Conclusions

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Five NRC notifications required by 10 CFR 50.72 were properly made by

the licensee.

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Operator Knowledge and Performance (71707)

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04.1 Operator Error Durina Charoina Pumo Breaker Manioulation

a.

Insoection Scope

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On September 10 the inspectors reviewed an event in which all Unit 2

charging pumps were found to be simultaneously inoperable while the unit

was in MODE 5.

b.

Observations and Findinas

At approximately 12:35 p.m. on September 10, operators attempted to

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start charging pum) 2-CH P 1C and received a breaker disagreement light.

At the time, 2-CH-) 1C was considered to be the only aump operable to

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meet TS requirements.

Pump 2 CH P-1A was available, aut its emergency

power supply, the 2H Emergency Diesel Generator, was inoperable. Pum)

2 CH-P 1B was unavailable due to a tagout. Operators dispatched to t1e

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breaker identified that the charging motor )ower control switch was in

"off", and the breaker springs indication slowed that the springs were

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discharged. Operators ) laced the power control switch in "on", but the

springs still did not c1arge as expected. The pump was declared

inoperable and TS 3.1.2.1 and 3.1.2.3 action statements were reviewed

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and complied with. The inspectors responded to the control room shortly

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after identification of the problem and verified that TS action

statement compliance was maintained throughout the time that all

charging pumps were inoperable.

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Initial investigations into the problem found that the breaker was

racked into the cubicle earlier the same day during an evolution to swap

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the pump power supply from the H to the J bus. Pump 2-CH P-1C was

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declared as the only operable pump after racking in the breaker at

5:25 a.m.

The operator performing the evolution completed procedure

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0 0P-26.9, 4160 volt Breaker Operation, Revision 9, including initialing

steps indicating that the switch was "on" and that the springs indicated

charged.

In accordance with the procedure, since repositioning the

switch was not required, no independent verification of switch position

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was required. After finding and verifying that the breaker

configuration was incorrect, the licensee concluded that the operator

erred when signing off the ste)s.

During interviews, the operator

informed his supervision that le did not remember the details concerning

procedure performance.

The licensee also investigated the reason for the springs failing to

charge when the switch was re positioned to "on".

The breaker was found

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to have an intermittent problem which was preliminarily determined to be

caused by a slight misalignment in the internal relay switch crank. The

breaker was replaced with a spare breaker which operated satisfactorily.

The pump was returned to operable status at 3:07 p.m.

The inspectors found that the operator's error led to the plant

operating without any charging pumps. Although the breaker had an

intermittent mechanical problem which prevented the springs from

charging, the operator error was a missed opportunity to identify the

problem. As corrective action, the operator was disciplined in

accordance with the licensee's programs, and the procedure was enhanced

to require independent verification for the power control switch.

The inspectors reviewed the procedural requirements for the evolution.

Unit 2 TS 6.8.1 requires that written arocedures be established

implemented and maintained, including Jy reference to Appendix A of NRC

Regulatory Guide 1.33. Revision 2, procedures for operation of the

chemical and volume control systems. This requirement was implemented

in part by 0 0P 26.9, Section 5.2.5, which required operators racking in

4160 volt breakers to verify the power control switch in "on" and to

verify that the breaker springs are charged. Contrary to this

requirement, the operator did not verify the power control switch in

"on" or the breaker springs charged. As a result, the only available

Unit 2 charging pump was unknowingly inoperable for approximately seven

hours. This licensee identified and corrected violation is being

treated as an NCV, consistent with Section VII.B.1 of the NRC

Enforcement Policy (50 339/96009 01).

c.

Conclusions

An NCV was identified for an operator's failure to follow procedures

when racking in a charging pump breaker. As a result, the only

available Unit 2 charging pump was unknowingly inoperable for

approximately seven hours during shutdown conditions.

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Quality Assurance in Operations (40500)

07.1 Oversicht Meetina

On September 18, the inspectors met with Oversight personnel.

Issues

discussed included Oversight activities and findings since previous

meetings. Copies of recent audits were provided for review. The

inspectors also observed Oversight personnel observing plant activities

on numerous other occasions during the inspection period and met briefly

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with them to discuss their observations. The inspectors concluded that

the Oversight organization was continuing to assess station performance

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effectively.

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Miscellaneous Operations Issues (92901, 92700)

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08.1

(Closed) Unresolved Item (URI) 50 339/96007-01 (EA 96 292): Review

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Comoliance With 10 CFR 50.54k Reouirements For Operator Presence at

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a.

Inspection Scope

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On August 5, the inspectors were informed by licensee managers that a

licensed operator had inadvertently left the Unit 2 controls area for a

short time period. During this inspection period, the inspectors

reviewed the event's details, the licensee's administrative controls

over Operator at the Controls (0ATC) movements, and compliance with

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regulatory requirements.

b.

Observations and Findinas

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The inspectors ascertained the following event details through

interviews with operators and management:

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On August 5, at approximately 3:30 p.m., the Backboards Operator

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properly relieved the 0ATC for a meal break.

The individual

carried the Backboards Operator's portable phone to the 0ATC area.

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A) proximately two minutes after relief, the 0ATC made a personal

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pione call using the Backboards Operator's portable phone.

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During the OATC's call, the other party requested a phone number

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for calling back, and the 0ATC proceeded to the portable

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base unit at the Backboards Operator's desk to retrieve t1e phone

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number. The Backboards Operator's desk was a few feet outside the

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0ATC's designated work area.

It was estimated that the individual

was away from the 0ATC's work area for less than five seconds.

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The OATC's actions were observed by an observer who had entered

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the control room to gather information related to a licensee

self assessment activity. The observer informed the Unit SR0

concerning the OATC's actions. The Unit SR0 had not directly

observed the OATC's actions due to involvement in discussions with

maintenance personnel.

- After the problem was identified, the 0ATC was relieved of the

0ATC and Backboards Operator duties pending further

investigations. Deficiency Report N 96140 was initiated to

identify and track corrective action.

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The next day, August 6, the individual was directed to report for

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Fitness for Duty (FFD) chemical testing.

FFD chemical testing

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results were later found to be negative. The individual's access

to the protected area and qualification for licensed duties were

temporarily suspended pending further corrective and disciplinary

action.

On August 20 and 21, the inspectors discussed these findings with

licensee management. The inspectors were informed that the licensee

concluded that the individual's actions were negligent of duty and were

probably influenced by outside personal problems.

Individual

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disciplinary actions were taken in accordance with the licensee's

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established program.

>

Additionally, the inspectors discussed with licensee management

administrative requirements and policies regarding conducting wrsonal

business while at the controls.

Procedure OPAP-0007. Control

Room

Activities, Revision 6 Paragraph 6.2.3, stated, "Only activities

essential to sup)orting station o>eration should be conducted in the

control room."

rurther, Paragrap16.2.4 stated, "Non-job related

2

discussions should be minircized to prevent any possible interference

with conduct of the shift or monitoring of station parameters." No

clear requirements were identified prohibiting the placement of personal

calls by OATCs. Station management stated that the individual's actions

2

in this case were clearly unacceptable, but that there were instances

where personal phone calls to or from the 0ATC would be acceptable

(e.g., urgent or emergency situations). Management indicated that

policies for phone use while on duty were being reviewed, and additional

j

guidance would be issued. Management also informed the inspectors of

i

additional actions which were being taken to evaluate on shift 0ATC

4

activities to ensure that the event did not reflect a widespread problem

with inappropriate activities being performed by 0ATCs.

.

i

The inspectors reviewed the licensee's controls over 0ATC movements. To

ensure that an operator remained present at the controls, the licensee

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had an established program for controlling 0ATC movements delineated in

OPAP-0007.

Procedure OPAP-0007, Section 6.3.6 and Attachment 1, defined

i

three areas for operator movements: the work area, the limited time

area, and the restricted work area. The 0ATC was allowed to leave the

work area and enter the limited time area only to acknowledge

annunciators, initiate corrective actions, to obtain reactor coolant

'

pump vibration readings, or to obtain drawings. The 0ATC was not

.

'

allowed to enter the restricted work area unless properly relieved.

The inspectors found that the 0ATC's movements during the event took him

out of the designated work area through the limited time area and

approximately two feet into the restricted work area. There were no

'

valid reasons for the 0ATC to enter the limited time area, and a proper

l

turnover was not conducted before the 0ATC entered the restricted work

~

area. During the time the 0ATC was absent from the work area, no other

licensed operators were present in the work area.

The nearest other

licensed operator was the Unit 2 SR0 who was ) resent at the SR0 desk a

few feet outside and overlooking the 0ATC wort area.

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10 CFR 50.54k requires that licensed operator be present at the controls

.

at all times during facility operation. This requirement is implemented

in part, by 0 PAP 0007 Section 6.3.6, which designates areas where a

licensed operator must be present during facility operation. Contrary

to this requirement, a licensed operator was not present in the

'

designated Unit 2 controls area for a short time period. This

licensee identified and corrected violation is being treated as an NCV,

consistent with Section VII.B.1 of the NRC Enforcement Policy

(50-339/96009 02).

'

c.

Conclusions

An NCV was identified involving a licensed operator not being present at

the Unit 2 controls for a short time period contrary to 10 CFR 50.54k

requirements.

08.2 (Closed) LER 50 338/96005:

Reactor Trio on Hiah Neaative Flux Rate

This LER discussed the August 27 Unit 1 trip from full power due to a

rod control system failure. The licensee's response to the event and

corrective actions for the associated equipment failures were reviewed

and are discussed in Sections 01.2, 01.3, 02.1, 02.3 and H2.1.

II. Maintenance

M1

Conduct of Maintenance

M1.1 2H Emeraency Diesel Generator (EDG) Post Maintenance Insoection and

Testina

a.

Insoection Scoce (627071

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On September 18 and 19, the inspectors observed inspection activities

and testing performed on the 2H EDG.

b.

Observations and Findinas

During the routine refueling outage inspection of the 2H EDG, the

licensee identified that the top and middle compression rings on number

seven lower piston were worn. All three compression rings were replaced

on this piston. The inspectors observed the 2H EDG operate during the

break-in period and witnessed visual examination of new rings by an

engineer and the vendor representative after the 2H EDG had operated at

65 percent load.

After the 65 percent load run, the 2H EDG exhaust manifold for the

number seven cylinder was removed to allow inspection of the new rings.

The inspectors observed that the number seven cylinder walls and lower

1

piston skirt were less lubricated that the other cylinders. This was

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discussed with the engineer and vendor representative. They also

examined the upper piston for proper lubrication. They concluded that

i

there was no problem.

'

After the 100 percent load run, the inspectors again looked at the

number seven cylinder. This time the oil coating appeared normal. The

inspectors had no further concerns in this area. Based upon operating

,

data, including crank case vacuum, taken during the break-in runs and

the licensee's and inspectors' examinations, there were no indications

'

of a problem with the new compression rings.

c.

Conclusions

i

The 2H EDG post-maintenance inspections and testing were adequate to

demonstrate that the new compression rings on the number seven lower

piston were functioning correctly.

M1.2 Control Rod Surveillance Observations (61726)

a.

InsDection Scooe

On August 28 and September 8 and 16. the inspectors observed technicians

and engineers performing 1/2 PT-17.2, Rod Drop Time Measurement,

>

Revision 13/12 P1. The test was performed, on Unit 1 prior to rectart

following a reactor trip and on Unit 2 immediately following a shutdown

for a refueling outage, to meet the licensee's commitments made in

'

response to NRC Bulletin 96 01.

In addition, the inspectors observed

control rod drag testing of Unit 2 discharged fuel assemblies.

b.

Observations and Findinas

The inspectors observed that technicians properly followed procedures in

obtaining the rod drop traces.

Formal communications between the

control room, the relay room, and the rod drive room were maintained

throughout the repetitive rod drop sequences. The inspectors reviewed a

sampling of rod drop traces and verified that measurements were being

accurately recorded and that the traces were correctly shaped. The

inspectors also observed that reactor engineers were reviewing the

traces to verify that rod recoil was recorded. The inspectors reviewed

the test procedure and verified that the licensee was meeting

commitments made in response to NRC Bulletin 96 01. The test results

were satisfactory for all rods.

On September 16, the inspectors observed drag testing of the final eight

control rods being tested from the Unit 2 off loaded core.

In addition,

the c'?ta for the other 40 control rods and fuel assembly pairs were

reviewed. The maximum force required to move the control rod through

the dash pot region and the area just above this region was recorded.

All measured values were 40 lbs or less which was well below the 100 lb

acceptance criteria.

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c.

Conclusions

The inspectors concluded that rod drop timing tests were aroperly

performed for both units. The inspectors also verified t1at the Unit ?.

control rod drag testing results were well within the acceptance

criteria.

M1.3 Larae Bore Snubber Testina (61726)

a.

Inspection Scope

During the Unit 2 refueling outage, the first two large bore snubbers

functionally tested failed to lockup in one or both directions. The

inspectors observed subsequent test activities, reviewed test

procedures, previous test records, procurement documents,

specifications, engineering test reports, and TS requirements.

b.

Observations and Findinas

On September 15, 1,000 kip snubber 2-RC-HSS-11A failed to lockup during

both the compression and tension activation tests conducted in the

field. On September 16, 1,900 kip snubber 2 RC HSS 01A failed to lockup

during its field compression activation. The inspectors observed the

bench test of snubber 2-RC HSS-11A. Although the snubber locked up in

both directions during the bench test, the acceptance criteria was not

met. The speed at which lockup occurred was a> proximately 28 inches per

minute as compared to a maximum allowed 20 incies per minute. A spare

snubber replaced this snubber in Unit 2.

Testing was subsequently performed on other installed and spare snubbers

with various results.

However, the licensee noted that more recent

tests were more likely to have acceptable results. Thus, except for

snubber 2-RC-HSS-11A, it was hyaothesized that earlier test results may

have resulted from problems wit 1 the test apparatus or testing

technique.

On September 19, the ins)ectors observed a spare 1,900 kip snubber,

designated as spare 06, aeing field tested. The snubber met the

acceptance criteria and performed satisfactorily.

Subsequent to the report period, snubber 2-RC HSS 11A was disassembled

and found to contain metal shavings in the hydraulic fluid. These metal

shavings apparently caused this snubber's improper functioning. Based

on this result, all 12 large bore snubbers installed in Unit 2 were

tested. The inspectors were informed that the data from these twelve

test, as well as, test results taken during previous outages were

reviewed by engineering and the results presented to the SNS0C prior to

restart of Unit 2.

The inspectors' review of data taken during 3reviously outages indicated

that snubber 2 RC HSS 001B in 1992 and 2-RC iSS-001C in 1993 did not

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clearly demonstrate that lockup had occurred during compression

activatlen testing. An Unresolved Item (URI) is being identified to

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perform additional reviews of the anomalies observed in large bore

snubber test data (50 339/960009 03).

c.

Conclusions

i

The licensee functionally tested all 12 large bore snubbers installed in

Unit 2 and considered that they were operable. An URI was identified to

review anomalies in large bore snubber test data taken early in this

refueling outage and during previous outages.

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M2

Maintenance and Material Condition of Facilities and Equipment

M2.1 Eauioment Problems Followina Unit 1 Reactor Trio (62703. 62707)

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a.

Inspection Scope

On August 27 and 28, the inspectors reviewed conditions following a

Unit 1 reactor trip to ensure the licensee was taking appropriate

actions to identify and resolve equipment problems.

b.

Observations and Findinas

The inspectors found that after the trip, the following significant

equipment problems occurred:

i

Main Feedwater Regulating Valves (MFRVs) leaked by the seats.

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Operator action was required to isolate two of the three MFRVs.

,

Steam dump 1 MS-TCV 1408B indication limit switch failed.

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Operators were momentarily concerned that the dump was not

o>ening, and operator action was required to locally verify that

t1e dump was properly responding.

Extraction steam flow control valve 1-MS FCV-104C failed to close.

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Operator action was required to manually isolate the valve to

limit RCS cooldown.

Condenser vacuum was lost due to inadequate turbine gland sealing

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steam. Operators were required to use the steam generator

atmospheric relief valves to control RCS temperature.

Several secondary reliefs lifted and several failed to properly

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reseat. Operators were required to locally isolate various

components to reduce the flow of water into the turbine building

sumps.

The inspectors verified that all the above problems were appropriately

resolved prior to unit restart. The ins >ectors noted that concerning

the loss of condenser vacuum, operators lad previously opened the gland

steam header dump bypass valve on both units in order to reduce gland

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steam pressure at full power. The pressure was postulated to be high

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due to excessive leakoff from the turbine valve glands. This

configuration required operator action on a trip to close the bypass

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valve to maintain gland steam header pressure. This had been identified

as an Operator Work Around (0WA) and added to the licensee's OWA list on

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June 11, 1996, as a low priority (category C) OWA.

However, trip

,

response or other procedures had not been modified to alert operators

concerning the need to shut the dump bypass valve following a trip.

.

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c.

Conclusions

The inspectors concluded that following the Unit 1 reactor trip, five

secondary plent equipment problems occurred requiring operator.

compensatory actions.

.

M4

Maintenance Staff Knowledge and Performance

.

M4.1 Foreian Material Exclusion (FME) Controls (71707)

On September 18, the inspectors observed that the limit switch

compartment cover for 2 SI-MOV 2865A, the Unit 2 A accumulator discharge

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isolation valve, was not installed. Approximately ten feet away (over

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to one side and above the valve), an individual was grinding on a

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support for the instrument tubing for this accumulator. This was called

to the attention of a nearby Health Physics (HP) technician who stopped

the work until the valve switch compartment could be covered. The

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inspectors subsequently observed personnel performing "V0TES" testing on

another accumulator discharge valve and discussed the missing cover with

them. The individuals indicated that they had removed the cover earlier

in the day to do testing and were not aware of the grinding work in the

area. The individuals returned to 2 SI MOV-2865A and replaced the

cover. This item was discussed with Maintenance supervision as

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representing a lack of sensitivity to FME issues and as a potential for

equi) ment degradation. The licensee indicated that the valve would be

chec(ed out prior to its return to service.

III. Enaineerina

E2

Engineering Support of Facilities and Equipment (37551)

E2.1 Seismic Concerns Reaardina Containment Particulate and Gaseous Radiation

Monitors (RMs)

a.

Insoection ScoDe

The inspectors reviewed concerns raised by the licensee involving the

seismic qualifications for the containment particulate and gaseous RMs

to ascertain if the licensee complied with equipment operability

requirements.

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b.

Observations and Findinas

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On September 10, the inspectors found that DR N 96 1743 was originated

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by engineers to document identification of a concern with the

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qualification of containment particulate and gaseous RMs to remain

operable following a seismic event. The DR originated from reviews of

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Potential Problem Report (PPR) 96 019 which questioned how the RMs could

remain operable followiw a seismic event given that a loss of the

non seismically qualified instrument air supplies to the system's

l

containment su) ply and return trip valves could result in isolation of

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the RMs. The )PR originated from questions raised during training on

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lessons learned from an event earlier in 1996 where the RMs were

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identified to be inoperable to meet TS 3.4.6.1 requirements for

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seismically qualified leakage detection systems due primarily to

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non safety related power supplies (LER 50-338, 339/96004: NRC Inspection

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Report 50 338, 339/96 07). On Seatember 11, a second DR, DR N 96 1783,

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Jas originated by Nuclear Oversig1t personnel who identified that a

similar issue existed for the containment air recirculation fan dampers

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which were a supporting system to the RMs, but were not classified as

safety related or seismically qualified.

After identifying the problem, the inspectors verified that the licensee

took actions required by TS 3.4.6.1 for inoperable leakage detection

systems on Unit 1.

The licensee planned to modify the system to ensure

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the system met seismic requirements prior to exceeding the 30 day TS

!

allowed outage time. The TS 3.4.6.1 requirement was applicable only in

MODES 1 - 4 and did not apply at the time to Unit 2 which was in MODE 5.

'

The licensee was required to submit an LER for the problem, and the

inspectors will further review the problem's significance when closing

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the LER.

The licensee also reviewed the issue prior to Unit 2's entry into MODE 6

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and concluded that seismic qualification was not required for the

'

monitors to meet TS 3.3.3.1 and 3.9.9 requirements for operability as a

part of the automatic containment isolation system. The inspectors

reviewed the basis for this conclusion with licensee engineers. The

engineers provided the inspectors with the licensee's proposed TS change

and the NRC's Safety Evaluation Report (SER) related to a February 1996

.

TS change which allowed refueling to be conducted with the containment

,

l

personnel air lock doors open.

In those documents the design bases for

'

a Fuel Handling Accident (FHA) were clarified. The clarification also

stated that the containment isolation system was non safety related.

Additionally, the documents referenced a facility original licensing

SER, NUREG 0053 Supplement 7, which, in the context of discussing a FHA

in containment, referred to the monitors as non safety grade. The

inspectors concluded that the licensee was correct in stating that the

RMs did not have to be seismically qualified to support TS operability

requirements in MODE 6.

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During the review of the documents related to the February 1996 TS

change, the inspectors found a discrepancy with the licensee's

implementation of the change.

In the change request (Virginia Power

,

letter to the NRC from J. O'Hanlon dated October 17, 1995), the licensee

stated that upon verbal notification of a FHA or upon receipt of a high

radiation signal, the control room would be manually isolated and the

bottled air su) ply initiated. The inspectors reviewed procedure

0 AP 30, Fuel r ilure During Handling, Revision 4, and found that it did

a

not direct operators to initiate the control room bottled air su3 ply

during a FHA. The inspectors informed the licensee concerning t11s

j

finding. After review, the licensee concluded that this was a

i

discrepancy and changed 0 AP 30 to correct the discrepancy prior to

commencing core on load for Unit 2.

i

The inspectors also reviewed the licensee *s Safety Evaluation (SE) for

the TS change, 95 SE 0T-34, and found that it made several assumptions

in concluding that the change did not represent an unreviewed safety

question.

Included in these assumptions were that actions would be

taken to develop an abnormal procedure to require operator action to

manually isolate the control room and initiate bottled air. Also, the

SE indicated that action would be taken to train operators on the

i

importance of isolating the control room within two minutes. Neither of

these actions were completed by the licensee from the time of

implementing the change on February 27, 1996, until identified by the

inspectors.

During that period, the licensee had performed core

alterations on at least two occasions: Unit 1 core on load from

February 29 to March 3,1996, and Unit 2 core off load from September

14 to 16, 1996. On both occasions, core alterations were performed with

the personnel hatch doors open.

The inspectors then reviewed the significance of not pressurizing the

control room bottled air system during a FHA. The inspectors found that

the TS change request used this assumption during basis calculations to

demonstrate that the dose to control room operators during a FHA would

remain less that the limit required by 10 CFR 50 General Design Criteria (GDC) 19. The licensee's amendment request analysis found that with

control room pressurization, inleakage was assumed to be 10 cfm and the

resultant estimated dose to the thyroid of control room operators was

19 rem. The inspectors concluded that for the assumptions made in the

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amendment analysis, without control room pressurization, the inleakage

l

would be significantly higher, and the dose to the thyroid of control

i

room operators would likely go from 19 rem to a value exceeding the

GDC 19 design criteria of 30 rem (5 rem whole body equivalent).

!

On September 24, the inspectors discussed the safety significance with

licensee fuel and analysis engineers. The engineers conceded that

without pressurization, the control room inleakage would likely be

significantly higher. As a result, if the basis calculation was

performed with all other factors the same, the GDC 19 design criteria

for dose to the thyroid would probably be exceeded.

However, the

engineers pointed out numerous conservative assumptions in the analyses.

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These included:

The analysis assumed containment was not isolated.

Procedures

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included direction to immediately isolate containment manually.

The analysis took no credit for control room ventilation charcoal

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filters during the first hour.

Procedures included direction to

immediately start the fans / filters on recirculation during the

first hour.

The analysis assumed containment release concentrations were

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present at the control room intake. Weather and plant layout

,

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would actually reduce the concentrations likely to leak into the

control room.

The analysis contained numerous additional conservative source

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term assumptions with regard to fuel composition and amount of

!

radioactivity released.

l

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The inspectors found that the conservative assumptions meant that had a

FHA actually occurred, the dose to control room operators would likely

not exceed the GDC 19 limits. However, if all assumptions used in the

basis calculation actually occurred, the GDC 19 limit would likely have

been exceeded.

TS 6.8.1 requires that written procedures be established, implemented

and maintained, including by reference to Appendix A of Regulatory

Guide 1.33. Revision 2, procedures for irradiated fuel damage while

refueling. The licensee's TS change request and the NRC's TS Amendment

Nos.198 and 179, stated that upon notification of a FHA, the control

room bottled air supply would be initiated by operators within two

minutes. Contrary to these requirements, from February 27, 1996, until

September 19, 1996, procedure 0 AP 30 was inadequate in that it did not

,

l

direct operators to initiate the control room bottled air supply within

two minutes of notification of a FHA. This is identified as Violation

(VIO) 50 338, 339/96009 04.

c.

Conclusions

A violation was identified concerning an inadequate abnormal procedure.

The procedure did not contain direction to operators to initiate the

control room bottled air system during a FHA as assumed in the bases for

a TS amendment allowing refueling with the containment personnel hatches

l

open.

E7

Quality Assurance in Engineering Activities

E7.1 Review of Vodated Final Safety Analysis Report (UFSAR) Commitments

'

A recent discovery of a licensee o>erating their facility in a manner

contrary to the UFSAR description lighlighted the need for a special

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focused review that compared plant practices, procedures and/or

parameters to the UFSAR descriptions. While performing the inspections

l

discussed in this report, the inspectors reviewed the applicable

i

portions of the UFSAR that related to the areas inspected. The

l

inspectors verified that the UFSAR wording was consistent with the

1

observed plant practices, procedures and/or parameters.

j

l

IV. Plant Support

R1

Radiological Protection and Chemistry (RP&C) Controls (71750)

,

a.

Inspection Scope

l

On Se)tember 14, the inspectors observed technicians performing portions

!

of a ligh radiation area survey on the refueling deck in containment.

b.

Observations and Findinas

l

The inspectors observed that during off load of the first fuel assembly,

the assembly was sto) ped in the transfer tube and radiation surveys were

l

performed to verify ligh radiation area boundaries in containment. The

l

inspectors observed portions of these surveys on the refueling deck in

i

containment. No discrepancies were noted in survey techniques.

l

However, the inspectors observed several ina)propriate work practices by

l

a contract HP technician.

In an area near t1e fuel transfer system

operating panel, the technician attempted to remove a radiation area

sign from the plastic mesh FME area barrier in order to place it on a

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high radiation barrier rope. When the technician found that the sign

was attached to the mesh with tie wraps and could not be pulled loose by

'

hand, the technician unzipped both life jacket and PC coverall and

reached inside the PCs to obtain a pocketknife. The technician then

i

used the small knife to cut the tie wraps and remove the sign. When

cut, one of the tie wraps flew approximately twenty feet in the air and

fell through a grating near the refueling cavity transfer canal and into

4

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the lower containment levels. The other tie wrap fell near the sign and

was retrieved. This event was observed by an inspector and a reactor

o>erator who was part of the refueling crew. The ins)ectors notified

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tie refueling SR0 and HP supervision concerning the caservation, and DR

,

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N-96-1902 was submitted documenting the event.

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The inspectors reviewed the requirements for FME controls. Unit 2 TS

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6.8.1 requires that written procedures be established imalemented and

maintained, including by refarence to Appendix A of NRC Regulatory Guide

,

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1.33, Revision 2, procedures for refueling and core alterations. This

l

requirement was implemented in part by VPAP 1302. Foreign Material

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Exclusion Program, Revision 8, and 2 0P 4.1 which delineated the

licensee *s FME controls in the reactor cavity area during refueling.

Procedures VPAP-1302 and 2 0P-4.1 required that all items which fit

through a 2 3/4 inch hole must be logged by the cavity watch prior to an

individual's entry into the FME control area. Contrary to these

requirements, the HP technician had failed to inform the ca'lity watch

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that the small pocketknife was in his aossession prior to entry to the

.

FME controls area and prior to using t1e knife inside the area. This

failure constitutes a violation of minor significance and is being

treated as an NCV consistent with Section IV of the NRC Enforcement

Policy (50 339/96009 05).

i

c.

Conclusions

A non cited violation was identified for an HP Technician's failure to

follow procedures for FME control during refueling.

P1

Conduct of Emergency Preparedness Activities (71750)

On September 6 and 7, the inspectors reviewed the licensee's res)onse to

the discovery that 28 of 55 emergency sirens were inoperable. T1e

.

sirens were found to be ino>erable when they failed to respond during a

i

test during Tropical Storm

ran (Section 02.3). The sirens were

degraded due arimarily to losses of local power to the sirens caused by

'

damage from t1e storm. The licensee contacted the Virginia State

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Department of Emergency Services and verified that alternate

notification means (route alerting) remained available in accordance

with the site Emergency Plan. The licensee informed the inspectors when

a

a majority of the sirens were returned to service the following day.

The inspectors concluded that the licensee properly resolved the

.

problem.

,

S1

Conduct of Security and Safeguards Activities (71750)

S1.1 Unescorted Visitor (71750)

On September 19 at approximately 12:45 p.m., the inspectors entered the

2H EDG room and observed that the vendor representative, visitor badge

V-0018, was not with his escort.

He was on the control side of the EDG

and was not observable by the three badged employees on the other side

of the EDG. The unescorted visitor accom3anied the inspectors to the

other side of the EDG where a member of t1e plant staff assumed escort

responsibilities for the individual. The person who had been watching

the visitor re entered the 2H EDG room a few moments later. The person

had left the area to obtain work materials.

The inspectors reported the event to security supervision.

Security

personnel subsequently counseled the involved personnel on

escort / visitor responsibilities. When the licensee issued a DR

concerning this observation, another example was included which had been

identified by the licensee on September 15. This second example also

involved personnel in the 2H EDG room.

Pending additional review of

3revious unescorted visitor occurrences, this item is identified as an

JRI (50 339/96009 06).

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V. Manaaecent Meetinas

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4

X1

Exit Meeting Summary

The inspectors 3 resented the inspection results to members of licensee

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management at t1e conclusion of the inspection on September 27 and

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October 18, 1996. The licensee acknowledged the findings presented.

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The inspectors asked the licensee whether any materials examined during the

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inspection should be considered proprietary. No proprietary information was

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identified.

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

C. Funderburk, Superintendent, Outage and Planning

E. Grecheck, Assistant Station Manager, Operations and Maintenance

,

J. Hayes. Superintendent. Operations

.

D. Heacock, Assistant Station Manager, Nuclear Safety and Licensing

'

.

P. Kemp, Supervisor, Licensing

,

T. Maddy, Superintendent, Security

'

W. Matthews, Station Manager

M. McCarthy, Director, Nuclear Oversight

'

D. Roberts, Supervisor, Station Nuclear Safety

4

H. Royal, Superintendent, Nuclear Training

i

3

R. Saunders, Vice President. Nuclear Operations

i

D. Schappell, Superintendent, Site Services

,

'

R. Shears, Superintendent, Maintenance

J. Smith, Superintendent, Station Engineering

i

l

A. Stafford, Superintendent, Radiological Protection

,

i

INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 40500: Effectiveness of Licensing Controls in Identifying, Resolving, and

j

.

Preventing Problems

IP 61726:

Surveillance Observations

IP 62703:

Maintenance Observations

-

IP 62707: Maintenance Observations

-

IP 71707:

Plant Operations

!

IP 71750:

Plant Support Activities

IP 92700: Onsite Follow up of Written Reports of Nonroutine Events at Power

,

Reactor Facilities

i

IP 92901:

Followup

Plant Operations

IP 93702:

Prompt Onsite Response to Events at Operating Power Reactors

!

ITEMS OPENED, CLOSED, AND DISCUSSED

,

i

Opened

50 339/96009 01

NCV

Failure to Follow Procedure for Racking In

Charging Pump Breaker (Section 04.1).

50 339/96009 02

NCV

Failure to Meet 10 CFR 50.54k Requirements for

Operator Presence at Unit Controls

(Section 08.1) (EA 96 292).

50 339/96009 03

URI

Review Anomalies in Large Bore Snubber Test Data

(Section M1.3).

.

. . . .

-

-. . - -

.

_ - . - -

.

. . . - . .

.

_ . -

. _ - .

--

. .

.

'

,

'

,

,

25

r

50 338, 339/96009 04

VIO

Inadequate Procedure for Fuel Handling Accident

(Section E2.1).

'

50 339/96009 05

NCV

Failure to Follow Procedures For FME Control By

HP Technician Near Reactor Cavity (Section R1).

>

50 339/96009 06

URI

Review occurrences of unescorted visitors

,

(Section S1.1).

'

Closed

,

i

50-339/96007 01

URI

Review Compliance With 10 CFR 50.54k-

'

Requirements For Operator Presence at

l

Unit Controls (Section 08.1) (EA 96 292).

l

'

50-339/96009 01

NCV

Failure to Follow Procedure for Racking In

Charging Pump Breaker (Section 04.1).

l

50 339/96009 02

NCV

Failure to Meet 10 CFR 50.54k Requirements for

Operator Presence at Unit Controls

j

(Section 08.1) (EA 96 292).

i

50 339/96009 05

NCV

Failure to Follow Procedures For FME Control By

HP Technician Near Reactor Cavity (Section R1).

L

j ',

50 338/96005 LER

Reactor Trip on High Negative Flux Rate

l

(Section 08.2).

.

I

!

!

i

l

'

1

i