05000272/LER-1982-055, Forwards LER 82-055/03L-0.Detailed Event Analysis Encl

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Forwards LER 82-055/03L-0.Detailed Event Analysis Encl
ML20063J441
Person / Time
Site: Salem PSEG icon.png
Issue date: 08/18/1982
From: Midura H
Public Service Enterprise Group
To: Haynes R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20063J443 List:
References
NUDOCS 8209020406
Download: ML20063J441 (3)


LER-2082-055, Forwards LER 82-055/03L-0.Detailed Event Analysis Encl
Event date:
Report date:
2722082055R00 - NRC Website

text

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O PSIEG Public Service Electric and Gas Company P.O. Box E Hancocks Bridge, New Jersey 08038 Salem Generating Station August 18, 1982 Mr. R. C. Haynes Regional Administrator USNRC Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406

Dear Mr. Haynes:

LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 82-055/03L Pursuant to the requirements of Salem Generating Station Unit No. 1, Technical Specifications, Section 6.9.1.9.b, we are submitting Licensee Event Report for Reportable Occurrence 82-055/03L. This report is required within thirty (30) days of the occurrence.

Sincerely yours, H. J. Midura General Managet -

Salem Operations RH:ks ,&

CC: Distribution i

4 8209020406 820sts gDRADOCK 05000272 PDR V i The Energy People M 21E9 (2]V) 1081

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( Report Number: 82-055/03L Report Date: 08-18-82 Occurrence Date: 08-01-82 Facility: Salem Generating Station, Unit 1 Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:

Fire Protection System - No. 1 Fire Pump - Inoperable.

This report was initiated by Incident Report 82-206.

CONDITIONS PRIOR TO OCCURRENCE:

Mode 1 - Rx Power 98% - Unit Load 1050 MWe.

DESCRIPTION OF OCCURRENCE:

At 1005 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.824025e-4 months <br />, August 1, 1982, during surveillance testing of the Fire Suppression System, the operator discovered that No. 1 Fire Pump would not start from automatic initiation.

The fire pump was declared inoperable and Technical Specification Limiting Condition for Operation Action Statement 3.7.10.la was entered at 1015 hours0.0117 days <br />0.282 hours <br />0.00168 weeks <br />3.862075e-4 months <br />.

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

! Investigation revealed that a fuse was blown on No. 1 Battery Charger, preventing it from keeping the required charge on'the battery. Previous surveillance on the battery had shown the battery to be satisfactory.

j ANALYSIS OF OCCURRENCE:

The operability of the fire suppression systems ensures that adequate fire suppression capability is available to confine and extinguish fires occurring in any portion of the facility, where safety related equipment is located. Due to redundancy in the fire suppression system, one pump being inoperable did not result in any loss of protection. No. 2 Fire Pump was tested and was capable of meeting system requirements in the event of a fire. Therefore, this occurrence involved no risk to the health and safety of the general public.

f

, LEB 82-055/03L ANALYSIS OF OCCURRENCE: (continued)

Action Statement 3.7.10.la requires:

With one pump and or water supply inoperable, restore the inoperable equipment to operable status within 7 days or, in lieu of any other report required by Specification 6.9.1, prepare and submit a special report to the Commission pursuant to Specification 6.9.2 within the next 30 days, outlining the plans and procedures to be used to provide for the loss of redundancy in this system.

Inoperability of No. 1 Fire Pump, therefore, constituted operation in a degraded mode, permitted by a limiting condition for operation, and is reportable in accordance with Technical Specification 6.9.1.9.b.

CORRECTIVE ACTION:

The fuse was replaced and the battery charger was used to recharge the battery. The surveillance test was satisfactorily performed, and No. 1 Fire Pump was declared operable. Action Statement 3.7.10.la was terminated at 1900 hours0.022 days <br />0.528 hours <br />0.00314 weeks <br />7.2295e-4 months <br />, August 1, 1982.

FAILURE DATA:

Lexington Standard Corporation Model LX1000 Fire Pump Controller Prepared By R. Heller / sc[e- "#

General Ma6ager -

SORC Meeting No. 82-77