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{{#Wiki_filter:MONTHLY" PORTS iFOR GRAY BOOK PREPARATT0%
{{#Wiki_filter:MONTHLY   " PORTS   iFOR GRAY BOOK PREPARATT0%
NRC bsoTRIBUTION FOR PART 50 DOCKE.'IATERIAL (TEMPORARY FORM)CONTROL NO: FILE MONTHLY REPORT FILE oc ester Gas&Elec.C rg,qTEOF DOC Rochester; N.Y.C.E.P1att ORIG DATE R EC'D LTR CC OTHER TWX RPT.OTHER s NRC CLASS UNCLASS PROPINFO XXX DESCRIPTION:
NRC bsoTRIBUTION FOR PART 50 DOCKE                 .'IATERIAL (TEMPORARY FORM)
'Ltr trans the following:
CONTROL NO:
1 Si ned INPUT LO NO CYS REC'D DOCKET NO: ENCLOSURES:
FILE MONTHLY     REPORT FILE oc ester Gas & Elec. C rg,qTEOF DOC       DATE    R EC'D      LTR    TWX    RPT      .OTHER Rochester; N.Y.                                                                                       s C.E. P1att ORIG       CC     OTHER NRC                             1  Si ned                                        LO CLASS       UNCLASS         PROPINFO             INPUT       NO CYS REC'D           DOCKET NO:
Monthly Report for DeCember 1975 Plant&Component Operability
XXX DESCRIPTION:                                                  ENCLOSURES:
&Availability This Report to be used in preparing Gray Book by Plans&Operations.
'Ltr trans      the following:                                Monthly Report for                     DeCember 1975 Plant & Component Operability & Availability This Report to be used in preparing Gray Book by Plans & Operations.
NUMBER OP COPIES REC'D: PLANT NAME: FOR ACTION/INFORMATION BUTLER (L)W/Copies CLARK (L)\A//Copssss'ARR (L)W/Copies KNtEt (L)W/Copies G FI~NR DR OGC, ROOM P-506A.GOSSI CK/STAF F CASE/BOYD MOORE (L)DEYOUNG (L)SKOVHOLT (L)GOLLER{L){Ltr)P.COLLINS DENISE REG OPR FI I.F.6 REGION (2)STEELE SCHWENCER (L)W/Copies STOLZ (L)W/Copies VASSALLO (L)-W pies RPLE (L)W/Copies TECH REVIEW SCHROEDER MACCARY KNIGHT PAWLI CKI SHAO STE LLO HOUSTON NOVAK ROSS IPPOLI TO TEDESCO J.COLLINS LAI NAS BENAROYA VOLLMER tNTERNAL DtSTRIBUTION LIC ASST R.DIGGS (L)H.GEAR IN (L)E.GOULBOURNE P.KREUTZER (E)J.LEE (L)M.RUSHBROOK (L)FNVIRO S.REED (EI MULLER'.S VICE (t)DICKER.SHEPPARD (L)KNIGHTON M.SLATER (E)YOUNGBLOOD H.SMITH (L)REGAN S.TEETS (L)PROJECT LDR G.WILLIAMS (E)V.WILSON (L)HARLESS R.INGRAM (L)M DUN A~N EXTERNAL DISTRIBUTION A/T I ND~8 RAITMAN SALTZMAN (L)MELTZ DENTON GRIMES GAMM ILL KASTNER BALLARD SPANGLER PLANS~MCDONALD~CHAPMAN DUBE (Ltr)E.COUP.E PETERSON HARTFIELD (2)KLECKER E ISENHUT Wl GG INl ON K.PARRISH L ZIEMANN (L)BEGAN (E)W/Copies Vil/Copies+0 NOT REMO~DICKER (E)LEAR (L)KNIGHTON (Ei SPELS W/.Copies W/Copies YOUNGBLOOD (E)>>MIPC/PE W/Copies W,4 Copies~1-LOCAL PDR~~Mm Rochester, N.Y.~'l-TIC (ABERNATHY)
NUMBER OP COPIES       REC'D:
(1}(2)('IO)
PLANT NAME:
-NATIONAL LABS~1-NSIC (BUCHANAN) 1-W.PENNINGTON, Rm E-201 GT 1-ASLB 1-CONSULTANTS s 1-Newton Anderson NEWMARK/BLUME/AG BABI AN-ACRS HOLDING/SENT 1-P D R-SAN/LA/N Y 1-BROOKIHAVEN NAT LAB 1-G.ULRIKSON, ORNL 1-AGMED (RUTH GUSSMAN)Rm B-127.GT 1-J.D.RUNKLES, Rm E-201 GT P~  
FOR ACTION/INFORMATION BUTLER (L)                 SCHWENCER (L)        ZIEMANN (L)            BEGAN (E)
', t ZW///SIXES//I/IIII'ZFiH':
W/ Copies                   W/ Copies            W/ Copies              Vil/ Copies  +0 NOT REMO~
/////I//8'///I///////
CLARK (L)                   STOLZ (L)            DICKER (E)            LEAR (L)
ROCHESTER GAS AND ELECTRIC CORPO cj T AVENUE, ROCHESTER, N.Y.14649 URIEL JP, ge.lBES.>~-.r TELEIIHONE AREA coDE 7ld 546-2700 Ginna Station January 8, 1976~ReguTatorP
    \A// Copssss               W/ Copies
'Ajtk.N<'irector, Office of Inspection and Enforcement U.S.Nuclear Regulatory Commission Washington, D.C.20555 1 (P i~l/N e  
'ARR (L)                     VASSALLO (L)-        KNIGHTON (Ei          SPELS W/ Copies                  W    pies            W/. Copies            W/ Copies KNtEt (L)                     RPLE (L)          YOUNGBLOOD (E)>> MIPC/PE W/ Copies                  W/ Copies            W/ Copies             W,4 Copies tNTERNAL DtSTRIBUTION G FI                   TECH REVIEW          DENTON                LIC ASST                  A/T I ND  ~
~NR         DR               SCHROEDER            GRIMES            R. DIGGS (L)                    8 RAITMAN OGC,     ROOM     P-506A. MACCARY              GAMM ILL          H. GEAR IN (L)                  SALTZMAN GOSSI CK/STAF F             KNIGHT              KASTNER          E. GOULBOURNE (L)              MELTZ CASE                       PAWLICKI              BALLARD          P. KREUTZER (E)
BOYD MOORE (L)
DEYOUNG (L)
SKOVHOLT (L)
GOLLER {L) {Ltr)
                    /       SHAO STE LLO HOUSTON NOVAK ROSS IPPOLI TO SPANGLER FNVIRO MULLER DICKER KNIGHTON
                                                                  '. J. LEE (L)
M. RUSHBROOK S. REED (EI M.
                                                                        .
S (L)
VICE (t )
SHEPPARD (L)
SLATER (E)
PLANS
                                                                                                  ~MCDONALD
                                                                                                  ~CHAPMAN DUBE (Ltr)
E. COUP.E PETERSON P. COLLINS                  TEDESCO              YOUNGBLOOD       H. SMITH (L)                 HARTFIELD (2)
DENISE                      J. COLLINS            REGAN             S. TEETS (L)                 KLECKER REG OPR                    LAINAS                PROJECT LDR     G. WILLIAMS(E)               E ISENHUT FI I.F. 6 REGION (2)        BENAROYA                              V. WILSON (L)                 Wl GG INl ON VOLLMER              HARLESS           R. INGRAM (L)
STEELE                                                            M DUN       A~N           K. PARRISH L EXTERNAL DISTRIBUTION
~1     LOCAL PDR~~Mm Rochester, N.Y.
P D R-SAN/LA/NY
~'l TIC (ABERNATHY) (1}(2)('IO) NATIONALLABS                                            1
~1     NSIC (BUCHANAN)                 1   W. PENNINGTON,     Rm E-201 GT             1 BROOKIHAVEN NAT LAB 1 ASLB                               1   CONSULTANTS                     s           1 G. ULRIKSON, ORNL 1 Newton Anderson                           NEWMARK/BLUME/AGBABIAN                    1 AGMED (RUTH GUSSMAN)
ACRS HOLDING/SENT                                                                        Rm B-127.GT 1 J. D. RUNKLES, Rm E-201 GT
 
P ~
  ',   t                 ZW/// SIXES
        //I/IIII'ZFiH':
    / ////I//8'///I///////
ROCHESTER GAS AND ELECTRIC CORPO                                     T AVENUE, ROCHESTER, N.Y. 14649 cj TELEIIHONE URIEL                   AREA coDE  7ld                  546-2700 Ginna    Station JP,   ge.lBES.>~-           January 8, 1976
                                                                                    ~ReguTatorP
                                                                        .r                          'Ajtk.N<'irector,
                                                                                                                  ~
1 Office of Inspection and Enforcement                         (P    i                      l U. S.                   Nuclear Regulatory Commission                                                                       /N Washington, D. C. 20555                                                               e


==Subject:==
==Subject:==
Monthly Report for December, 1975 (Revised)Operating Status Information R.E.Ginna Nuclear Power Plant Unit No.1 Docket No.50-244 Gentlemen:
Monthly Report for December, 1975 (Revised)
Pursuant to Technical Specification 6.9.1c attached herewith is a re-vised unit shutdown and power reduction data sheet, to correct previous error in reporting reasons for reductions in reactor power levels on 12/13, 12/21 and 12/23.Very truly yours, gtP Charles E.Platt Superintendent CEP:fah Attachments 1 cc: Mr.James P.O'Reilly, NRC (1)Mr.William G.McDonald, NRC (2) t I 11 DOCKET NO.50-244  
Operating Status Information R. E. Ginna Nuclear Power Plant Unit No. 1 Docket No. 50-244 Gentlemen:
Pursuant to Technical Specification 6.9.1c attached herewith is a re-vised unit shutdown and power reduction data sheet, to correct previous error in reporting reasons for reductions in reactor power levels on 12/13, 12/21 and 12/23.
Very truly yours, gtP Charles E. Platt Superintendent CEP:fah Attachments 1
cc:     Mr. James P. O'Reilly, NRC (1)
Mr. William G. McDonald, NRC (2)
 
t I
11
 
DOCKET NO.       50-244


==SUMMARY==
==SUMMARY==
: The reactor power levels averaged 99%during the period.The major exceptions were the power reduc-tions and Outage 814 detailed below.REPORT MONTH GINNA STATION, UNIT PI January 8, 1976(Revision)
: The reactor power levels averaged                                                                                   GINNA STATION, UNIT PI 99% during the period. The major exceptions were the power reduc-                                                                               January 8, 1976(Revision)
DATE COMPLETED BY Andrew E.McNamara, Operations Aide TELEPHONE Ext.291-214, at Ginna UNIT SHUTDOWN AND POWER REDUCTIONS NO.DATE TYPE F-FORCED S-SCHEDULED DURATION (HOURS)REASON (I)METHOD OF SHUTTING DOWN THE REACTOR OR REDUCING POWER (2)CORRECTIVE ACTIONS/COMMENTS N/A 75 12 13 Reactor power level reduction to~47%=to perform T-'8B, Turbine Main Steam Stop Valves test.N/A 75 12 21 A Reactor power level reduction to~47%to perform M-54.2, Check condenser 1B-1 Water Box for Leaks with Freon.N/A 75 12 23 A Reactor power level reduction to~47%to perform M-54.2, Check condenser 1B-1 Water Box for Leaks, with Freon.14 75 12 30 43.75 See Note)"B" Steam Generator-Tube Leak NOTE: Unit remained shutdown through the end of report month.(I)REASON: (2)METHOD: A-EOUIPMENT FAILURE (EXPLAIN)I-MANUAL B-MAINT.OR TEST 2-MANUAL SCRAM C-REFUELING 3-AUTOMATIC SCRAM D-REGULATORY RESTRICTION 4-OTHER (EXPLAIN)E-OPERATOR TRAINING AND LICENSE EXAMINATION F-ADMINISTRATIVE G-OPERATIONAL ERROR (EXPLAIN)H-OTHER (EXPLAIN).+Power reductions were not previously reported.Data not available.
DATE tions  and Outage 814  detailed below.                                                                                              COMPLETED BY Andrew E. McNamara, Operations Aide TELEPHONE Ext. 291-214, at Ginna REPORT MONTH UNIT SHUTDOWN AND POWER REDUCTIONS METHOD OF TYPE                                     SHUTTING DOWN F-FORCED       DURATION                                                          CORRECTIVE ACTIONS/COMMENTS THE REACTOR OR NO. DATE      S-SCHEDULED     (HOURS)   REASON (I)   REDUCING POWER (2)
Commencing January 1, 1976, this data wig bp pegprteg.~9 0 L'~,
N/A   75 12 13                                                                 Reactor power level reduction to~47%=to perform T-'8B, Turbine Main Steam Stop Valves test.
DOCKET RO.50-2i:C 5!ARY I The reactor power levels averaged 99Z durirg the period.The ma)or exceptions vere the power reduc-tions and Oueage F'14 deeailed be'v.REPORT MONTH UVIT RAvE DATE GIRRA STATlos, UR'T AI January 8, 1976(Revision)
N/A 75 12 21                                     A                             Reactor power level reduction to ~ 47% to perform M-54.2, Check condenser 1B-1 Water Box for Leaks with Freon.
COMPLETED SY Andzev E.McNamara, Operations Aide TELEPHONE-7 4 Ext.291-214, at Ginra UNIT S-uTDOIY'N AND POWER REDUCTIONS NO.DATE TYP E F-FORCED S-SCHEDUI.ED DURAT I OiN (HOURS)REASON (I)METHOD OF SHUTTING DOWN THE REACTOR OR REDUCING POWER (2)CORRECT I VE ACT I ONS/COLNENTS N/A 75 12 13 Reactor power level reduction toL 47Z to perform T-18B, Turbine venin Seeam Stop Ualves test.N/A 75 12 21 0 Reactor power level reduction to&#x17d;47Z to perform M-54.2, Check condenser 1B-1 Mater Box for Leaks vith Freon.N/A 75 12 23 Reactor power level reduceion to I47Z to perform N-54.2, Check condenser 1B-1 Mater Box for Leaks, with Freon.75 12 30 43.75 See Note)"B" Steam Generator-Tube Leak NOTE: Unit remained shutdown thzough the end of zeport onth.(I)REASORI (2)MEiHOOI A EOUIPME.T FAILURE (EXPLAIII)
N/A 75 12 23                                     A                             Reactor power level reduction to~47% to perform M-54.2, Check condenser 1B-1 Water Box for Leaks, with Freon.
I VARUAL S MAINT.OR TEST 2-MARUA'cRAv.
14   75 12 30                     43.75                                       "B" Steam Generator       Tube Leak See Note)
C-REFUELING 3-AUTOVATIC SCRAM 0-REGUlATORY RESTRICTION 4-OTHER (EXPLAIN)E OPERATOR TRAII<IRG ARO lICEiiSE EXAvlRATIOR F-ADMINISTRATIVE OPERATIONAL ERROR (EXPLAIN)H OTHER (EXPL*III)
NOTE:   Unit remained shutdown through the           end of report month.
RPower reducti'ons were not previously reported.Data not available.
(I) REASON:                                 (2) METHOD:
Commencing Januazy 1, 1976, this data I<p bp geQrteg.>>  
A - EOUIPMENT FAILURE (EXPLAIN)             I - MANUAL B - MAINT. OR TEST                         2 - MANUAL SCRAM C - REFUELING                               3 - AUTOMATIC SCRAM D - REGULATORY RESTRICTION                 4 - OTHER (EXPLAIN)
E - OPERATOR TRAINING AND LICENSE EXAMINATION F - ADMINISTRATIVE G - OPERATIONAL ERROR (EXPLAIN)
H - OTHER (EXPLAIN) .
                                                                                      +Power   reductions were not previously reported.             Data not available. Commencing January 1, 1976,         this data wig   bp pegprteg.~9
 
0 L'~,
 
DOCKET RO.       50-2i:C 5!ARY I The reactor power levels averaged                                                                   UVIT RAvE      GIRRA  STATlos, UR'T AI 99Z durirg the period. The ma)or exceptions vere the power reduc-                                                                   DATE January 8, 1976(Revision) tions and Oueage F'14 deeailed be'v.                                                                                               COMPLETED SY Andzev E. McNamara, Operations Aide TELEPHONE     -7       4 Ext. 291-214, at Ginra REPORT MONTH UNIT S-uTDOIY'N AND   POWER REDUCTIONS METHOD OF TYP E                                     SHUTTING  DOWN F-FORCED       DURAT I OiN              THE REACTOR OR                          CORRECT I VE ACT I ONS/COLNENTS NO.      DATE    S-SCHEDUI.ED     (HOURS)   REASON (I)   REDUCING POWER (2)
N/A 75 12 13                                                                   Reactor power level reduction toL 47Z to perform T-18B, Turbine venin Seeam Stop Ualves test.
N/A 75 12 21                         0                                       Reactor power level reduction to '47Z to perform M-54.2, Check condenser 1B-1 Mater Box for Leaks vith Freon.
N/A 75 12 23                                                                   Reactor power level reduceion to I47Z to perform N-54.2, Check condenser 1B-1 Mater Box for Leaks, with Freon.
75 12 30                   43.75                                       "B" Steam Generator - Tube Leak See  Note)
NOTE: Unit remained shutdown thzough the end of zeport                   onth.
(I) REASORI                                 (2)   MEiHOOI A   EOUIPME .T FAILURE   (EXPLAIII)           I   VARUAL S   MAINT. OR TEST                           2 - MARUA'cRAv.
C - REFUELING                                 3 - AUTOVATIC SCRAM 0 - REGUlATORY RESTRICTION                     4 - OTHER (EXPLAIN)
E   OPERATOR TRAII<IRG ARO lICEiiSE EXAvlRATIOR F - ADMINISTRATIVE OPERATIONAL ERROR (EXPLAIN)
H   OTHER (EXPL*III)
RPower reducti'ons were not previously reported. Data not available. Commencing Januazy 1, 1976, this data I<p bp geQrteg.>>
 
DOCKET NO.      50-244 PIARYI  The reactor power levels averaged                                                                                        GIMNA STATION  OMIT <I 99X during the period. The ma/or exceptions were the power reduc-                                                                                  January 8, 1976(Revision) tions below.
and Outage 814  detailed DATE COMPLETED 8Y Andrew E. )(cNamara, Operations Aide A
TELEPHONE    -7 Ext. 291-214, at Ginna REPORT MONTH UNIT Sl-uTDONI AND    POWER RFDUCTIOIMS METHOD OF TYPE                                      SHUTTING  DOWN F-FORCED        DURAT I OII              THE REACTOR OR                              CORRECTIVE ACTIONS/COSDIENTS DATE    S-SCHEDUI.ED      (HOURS)    REASON (I)    REDUCING POWER (2)
N/A 75 12 13                          0                                        Reactor power level reduction to'~47X to perform T-18B, Turbine )win Steam Stop Valves test.
N/A 75 12 21                          0                                        Reactor power level reduction to L"47X to perform )(-54.2, Check condenser 1B-1 Water Box for Leaks with Freon.
N/A .75 12 23                          0                                        Reactor power level reduction to~47X to perform H-54.2, Check condenser 1B-1 Water Box for Leaks, with Freon.
75 12 30                      43.75                                        "B" Steam Generator        -  Tube Leak See Note)
NOTE:    Unit remained shutdown through the            end of report onth.
(I)  REASOMI                                (2)  METHOD:
A    EQUIPME:.'T FAILURE (EXPLAIN)                MANUAL 8  - MAINT. OR TEST                              MANUAL SCRAM C  - REFUELING                                3 - AUTOMATIC SCRAM
                                                                                        ~ D    REGULAiORY RESTRICTION                  4 - OTHER (EXPLAIII)
E    OPFRATOR TRAINING AND LICENSE EXAMINATION F  - ADMINISTRATIVE G  - OPERATIONAL ERROR (EXPLAIN)
H    OTHER (EXPI.AIM)
                                                                                      *Power reductions were not          previously reported.        Data not available.      Commencing January      1, 1976, this data wiQ bp gepprtegt
 
DOCKET NO.        50 2i:4 W!ARYI  The reactor power levels averaged                                                                                        GINNA STATIDN, CNIT LI 99X during the period. The ma)or exception~ were the power reduc-                                                                        DATE January 8, 1976(Revision) tions  and Outage I~14 detailed below.                                                                                                  CDMPLETED ST Andrew E. MCNanara, Operations Aide TELEPHONE              4 Ext. 291-214, at Ginna REPORT MONTH LID IT SI.IUTDONN AND POWER REDUCTIONS METHOD OF TYPE                                        SHUTTING DOWN F-FORCED        DURATION                    THE REACTOR OR                            CORRECT I VE ACT I Oi(S/COMMENTS DATE      S-SCHEDULED      (HOURS)    REASOiI (I )  REDUCING POWER (2)
'(/A  75 12 13                        0                                          Reactor power level reduction toL 47X to perform T-18B, Turbine            Yogin Steam Stop Valves test.
N/A 75 12 21                                                                      Reactor power level reduction to '47X to perform )(-54.2, Check condenser 1B-1 Vater Box for Leaks with Freon.
N/A 75 12 23                          0            A                            Reactor power level reduction to I47X to perform M-54.2, Check condenser 1B-1 Mater Box for Leaks, with Freon.
14    75 12 30                    43.75                                          "B" Stean Generator        Tube Leak See  Note)                                                                                                  of report onth.
NOTE:    Unit remained shutdown through the            end (I)  REASONI A  - EQUIPME:.'T FAILURE (EXPLAIN) 8  - MAINT. OR TEST C  - REFIIELING D  - REGULATORY RESTRICTION E  - OPERATOR TRAINING AND LICENSE EXA'iIINATION C  - ADXIINISTRATIVE G  - OPERATIONAL ERROR (EXPLAIN)
H  - OTHE'R (EXPLAIN)
                                                                                      ~power  reductions were not previously reported. Data not available.      Com encing January 1, 1976, this data wig bp geQrteg.>>
 
~ .
DOCKET NO.      50-244 DIARYI  The reactor pover levels averaged                                                                  UNIT  NAME    GINNA STATIDN. UNIT <I 99Z during the period. The ma)or exceptions 'were the power reduc-                                                                DATE January 8, 1976(Revision) tions and Outage  814 detailed belov.                                                                                            COVPLETEO SY Andrew E. McNamara, Operations Aide TELEPHONE      7 6- 4 Ext. 291-214, at Ginna REPORT MONTH UNIT SI-QTDOWN AND POWER REDUCTIONS METHOD OF TYPE                                    SHUTTING DOWN F-FORCED        DURATION                THE REACTOR OR                          CORRECTIVE ACTIONS/COAIVENTS DATE    S-SCHEDULED      (HOURS)  REASON (I)    REDUCING POWER (2)
N/A 75 12 13                          0          B                            Reactor power level reduction to~47Z to            perfo~    T-18B, Turbine Yogin Steam Stop Valves test.
N/A 75 12 21                          0                                      Reactor power level reduction to '47Z to perform iM.-54.2, Check condenser 1B-1 Mater Box for Leaks with Freon.
N/A 75 12 23                          0                                      Reactor power level reduction to~47Z to perform if-54.2, Check condenser 1B-1 Vater Box for Leaks, with Freon.
14    75 12 30                    43.75                                      "B" Steam Generator  Tube Leak See  Note)                                  NOTE: Unit remained shutdown through the end of report                onth.
(I) REASON!                                (2)  METNODI A - EQUIPME::T FAILURE (EXPLAIN)            I - VasuaL D - MAINT. OR TEST                        2 - MANUA'cRav.
C - REFUELING                              3 - AUTGvaTIc scpav D - REGULATORY RESTRICTION                4 - OTNER (EXPLA!N)
E  OPERATOR TRAINING ANO I.ICENSE EXAMINaTION F - ADMINISTRATIVE G - OPERATIONAL ERROR (EXPLAIN)
H  OTIIER'(EXPLAIN)
                                                                                  ~power reductions were not .previouslv reported. Data not available. Connencing January 1, 1976, this data wiQ bp,ge@rte<I
 
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DDGKET No.      50-2>>'c The reactor power levels averaged                                                                          UNIT NAVE      GINNA STATION, UNIT AI 99K during the period. The na)or exceptions were the power reduc-                                                                        DATE January 8, 1976(Revision) tions  and Outage J)14  detailed below.                                                                                                  COMPLETED 8Y Andrew E. McNamara, Operations Aide TELEPHONE      7      4 Ext. 291-214, at Ginna REPORT MONTH UNIT S.uTDOWN AND    POWER  REDVCTI(NS METHOD OF TYPE                                      SHUTTING DOWN F-FORCED        DURATION                THE REACTOR OR                            CORRECT I VE ACT I ONS/CO.'i'MENTS NO.
      "
DATE      S-SCHEDUI.ED      (HOURS)  REASON (I)    REDUCING POWER (2)
N/A 75 12 13                            0          B                            Reactor power level reduction toL"47X to perform T-18B, Turbine Main Steam Stop Valves test.
N/A 75 12 21                            0                                      Reactor power level reduction to ~ 47X to perform M-54.2, Check condenser lB-1 Water Box for Leaks with Freon.
N/A 75 12 23            S.            0          A                            Reactor power level reduction to I47/ to perform M-54.2, Check condenser 1B-1 Water Box for Leaks, with Freon.
14  75 12 30                        43.75*                                      "B" Steam Generator      -  Tube Leak See Note)
NOTE:    Unit remained shutdown through the              end  of report =anth.
(I) REASON:                                    (2)  METHOOr A  - EOUIPMENT FAILURE (EXPLAIN)                I -  MANUAL 8  - MAINT. OR TEST                            2    MANUAL scRAV C  - REFUELING                                  3    AU OuATIC SCRAu D  - REGVLATORY RE'STRICTION                    4  - OTHER (EXPL*III)
F.  - OPERATOR TR*INI:IG ANO LICENSE EXAul>>lATION F  - ADMINISTRATIVE G    OPERATIONAL ERROR (EXPLAIN)
H  - OTHER  (EXPLAI.'I)
                                                                                    ~Power    reductions were not previously reported. Data not aVailable. CODmreneing January 1, 1976, thiS data WiQ bp pep>rtegr
 
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DOCKET NO.
50-24'.!ARY I  The reactor pover levels averaged                                                                    UNIT  NAME    GLNVA STATIOV, UNIT        LI 99X during the period. The ma)or exceptions vere the power reduc-                                                                    DATE January 8, 1976(Revision) tions  and Outage II14 detailed below.                                                                                              COMPLETED SY Andrew E. McNamara, Operations Aide TEIEPHONE    -7            - 4 Ext. 291-214, at Ginna REPORT MONTH UNIT 3-uTDOII AND    POWER REDUCTIONS METHOD OF TYPE                                    SHUTTING  DOWN F-FORCED        DURATION                THE REACTOR OR                            CORRECT I VE ACTIONS/COIN!ENTS DATE      S-SCHEDULED      (HOURS)  REASON (I)    REDUCING POWER (2)
N/A 75 12 13                          0        B                            Reactor power level reduction to'A 47X to perform T-18B, Turbine venin Steam Stop Ualves test.
N/A 75 12 21                          0                                      Reactor power level reduction to '47K to perform )(-54.2, Check condenser 1B-1 Water Box for Leaks vith Ereon.
N/A 75 12 23                          0                                      Reactor power level reduction to~47X to perform M-54.2, Check condenser 1B-1 Water Box for Leaks, with Freon.
14  75 12 30                    43.75                                      "B" Steam Generator      -  Tube Leak See  Note)                                                                                                      of report onth.
NOTE:    Unit remained shutdown through the                    end (I)  REASOV:
A    EOUIPAtE;:T FAILURE (EXPLAIN) 8  - MAINT. OR TEST C  - REFUELING D  - REGULATORY RESTRtCTION E    OPERATOR TRAINING AND LICENSE EXAMINATION F    ADAIINISTRATIVE G    OPERATIONAL ERROR (EXPLAIN)
H  - OTHER  (EXPLAIN)
                                                                                  ~Power  reductions vere not previously reported. Data not available. Commencing January 1, 1976, this data viQ bp,ge@rtegt>>
 
~ .
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DOCKET NO.          50-244
'MARY:  The  reactor power levels averaged                                                                  UV I 'T VAilE      Gl NNA STA'Tl OV, UV I ~ <I 99%  during the period. The ma)or exceptions were the power reduc-                                                                  DATE January 8, 1976(Revision) tions  and Outage 814  detailed below.                                                                                            CO'MPLETEO SY Andrew E. NcNamara, Operations Aide TEt.EPHOVE            4 Ext. 291-214, at Ginna REPORT MONTH UNIT 3-UTDOMN AND POMER REDVCTIGVS METHOD OF TYPE                                    SHUTTING DOWN F-FORCED        DURATION                THE REACTOR OR                          CORRECT I VE ACT I ONS/COSMENTS NO. DATE      S-SCHEDULED      (HOURS)  REASON (I)    REDUCING POWER (2)
N/A 75 12 13                          0        B                            Reactor power level reduction to'L"47% to perform T-18B, Turbine Muin Steam Stop Valves test.
N/A 75 12 21                                                                  Reactor power level reduction to ~ 47% to perform )("54.2, Check condenser 1B-1 Water Box for Leaks with Freon.
N/A 75 12 23            S.                                                    Reactor po~er level reduction to~47% to perform H-54.2, Check condenser 1B-1 Water Box for Leaks, with Freon.
75 12 30                    43. 75                                      "B" Steam Generator  Tube Leak See Note)
NOTE: Unit remained shutdown through the end of report month.
(I) REASONI                                  (2)  NE'THDD:
A - EOUIPME::T FAILURE (EXPLAIN)                I  NANUAI.
8 - MAINT. OR TEST                                  MANUAL SCRAM C - REFUELING                                  3 - AUTOUATIC SCRAu D - REGULATORY RESTRICTION                    4 - OTHER (EXPLAIN)
E  OPERATOR TRAINING AVD LICENSE EXAUINATION F - ADXIINISTRATI YE G - OPERATIONAL ERROR (EXPI.*IN)
H - OTIIER (EXPLAIN)
                                                                                    *Power reductions were not          previouslv reported.            Data not available. Commencing January        1, 1976, this data whap bp,~e)iprtegl
 
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DOCKET NO.        50-2ra e!ARYI  The reactor power levels averaged                                                                            NAyE      GINNA STATIO.'I. UNIT UI 99X during the period. The ma)or exceptions were the power reduc-                                                                    DATE January 8, 1976(Revision) tions  and Outage 814  detailed below.                                                                                              COIJIPLETED BY Andrew E. McNamara, Operations Aide TELEPHONE        7      4 Ext. 291-214, at Ginna REPORT MONTH UNIT S.uTDOWN AND    POWER REDUCTIONS METHOD OF TYPE                                    SHUTTING DOWN F-FORCED        DURATION                THE REACTOR OR                            CORRECTIVE ACTIONSICOSIyENTS DATE      S-SCHEDULED      (HOURS)  REASON (I)    REDUCING POWER (2)
M/A 75 12 13                          0                                      Reactor power level reduction to'~47X to perform T-18B, Turbine Ywin Steam Stop Valves test.
N/A 75 12 21                          0                                      Reactor power level reduction to ~47X to perform M-54.2, Check condenser 1B-1 Water Box for Leaks with Freon.
N/A 75 12 23                          0                                      Reactor power level reduction to~47X to perform M-54.2, Check condenser lB-1 Water Box for Leaks, with Preon.
14  75 12 30                    43. 75                                      "B" Steam Generator  Tube Leak See Note)
NOTE: Unit remained shutdown through the end of report                      onth.
(I)  REASON:                                  (2)  NETHODI A    EOUIPMERT FAILURE (EXPLAIN)                I - yANUAL B    NAINT. OR TEST                            2  - yANUAL SCRAy C  - REFUELING                                  3    AUTOyATIC SCRAil D  - REGULATORY RESTRICTION                          OTHER (EXPLAIN)
E    OPERATOR TRAINI'NG AND LICENSE EXAA'IINATION F  - ADIIINISTRATIVE G    OPERATIONA'L ERROR (EXPLAIN)
H    OTHER  (EXPLAIN)
                                                                                    +Power  reductions were not previously reported. Data not available. Commencing January 1, 1976, this data wig bp gegrtegl>>


DOCKET NO.50-244 PIARYI The reactor power levels averaged 99X during the period.The ma/or exceptions were the power reduc-tions and Outage 814 detailed below.REPORT MONTH DATE GIMNA STATION OMIT<I January 8, 1976(Revision)
DOCKET NO.       50-2(4 t.'!PRY I  The reactor power levels averaged                                                                       UVIT VAvE      GINVA STATIOV.    ~ v! T =',
COMPLETED 8Y A Andrew E.)(cNamara, Operations Aide TELEPHONE-7 Ext.291-214, at Ginna UNIT Sl-uTDONI AND POWER RFDUCTIOIMS DATE TYPE F-FORCED S-SCHEDUI.ED DURAT I OII (HOURS)REASON (I)METHOD OF SHUTTING DOWN THE REACTOR OR REDUCING POWER (2)CORRECTIVE ACTIONS/COSDIENTS N/A 75 12 13 0 Reactor power level reduction to'~47X to perform T-18B, Turbine)win Steam Stop Valves test.N/A 75 12 21 0 Reactor power level reduction to L"47X to perform)(-54.2, Check condenser 1B-1 Water Box for Leaks with Freon.N/A.75 12 23 0 Reactor power level reduction to~47X to perform H-54.2, Check condenser 1B-1 Water Box for Leaks, with Freon.75 12 30 43.75 See Note)"B" Steam Generator-Tube Leak NOTE: Unit remained shutdown through the end of report onth.(I)REASOMI (2)METHOD: A EQUIPME:.'T FAILURE (EXPLAIN)MANUAL 8-MAINT.OR TEST MANUAL SCRAM C-REFUELING 3-AUTOMATIC SCRAM~D REGULAiORY RESTRICTION 4-OTHER (EXPLAIII)
99X during the period. The ma)or exceptions vere the power reduc-                                                                       DATE January 8, 1976(Revision) tions and Outage f14 detailed below.                                                                                                  COMPLETED 8Y Andrew E. McNamara, Operations Aide TELEPHONE     4 Ext. 291-214, at Ginna REPORT NORTH UNIT SI-IUTOOWiil AND POWER RFOUCTIGMS METHOD OF TYP E                                    SHUTTING DOIlVN F-FORCED       DURATION                  THE REACTOR OR                                CORRECTIVE ACTIONS/CONTENTS DATE    S-SCHEDULED    (HOURS)   REASON (I)   REDUCING POPOVER (21 N/A>> 75 12 13                                                                   Reactor power level reduction toA"47X to perform T-18B, Turbine Ruin Steam Stop Valves test.
E OPFRATOR TRAINING AND LICENSE EXAMINATION F-ADMINISTRATIVE G-OPERATIONAL ERROR (EXPLAIN)H OTHER (EXPI.AIM)
N/A 75 12 21                         0                                         Reactor power level reduction to ~ 47X to perform )(-54.2, Check condenser lB-1 Mater Box for Leaks with Preon.
*Power reductions were not previously reported.Data not available.
N/A 75 12 23                         0                                         Reactor power level reduction to~47! to perform H-54.2, Check condenser 1B-1 Vater Box for Leaks, with Freon.
Commencing January 1, 1976, this data wiQ bp gepprtegt
14    75 12 30                   43.75                                         "BH Steam   Generator     - Tube Leak See  Note)                                      NOTE:   Unit remained shutdown through the             end of report       onth.
(I) REASOMI                                   (2) A!ETHOD:
A - EOUIPUE::t  FAII.ORE (EXPLAIN)           I    UAVQAI.
8 - MAINT. OR TEST                         2 - MANUAL SCPAv.
C - REFUELING                                 3 - AUTOVATIC SCRAM D - REGULATORY RESTRICTION                   C  - OTHER   (EXPLAIN)
E - OPERATOR TRAINING AND LICENSE EXAvIMATIOV F - ADA'llNI STRATI YE G   OPERATIONAL ERROR     (EXPLAIN)
H - OTHER   (EXPI.AIN)
                                                                                        ~power  reductions were not previously reported. Data not available.       Commencing January 1, 1976, this data w'QT bp ge+rtegt>>


W!ARY I The reactor power levels averaged 99X during the period.The ma)or exception~
DOCKET NO.       50 AC VARY: The reactor power levels averaged                                                                       UV IT NAVE      GINNA STAT I OV, UN I T ~l 99%  during the period. The ma)or exceptions were the power reduc-                                                                         DATE January 8, 1976(Revision) t'ons  and Outage LB14 detailed below.                                                                                                   COMPLETED BY Andrew E. McNamara, Operations Aide TELEPMONE      7     4 Ext. 291-214, at Ginna REPORT MONTH uwtT 3.RJTOORM AND POMER REOUCTIGQS hIETHOD OF TYPE                                       SHUTTING DOWN F-FORCED         DURATION                 THE REACTOR OR                             CORRECTIVE ACTIONS/COI'MENTS NO. DATE     S-SCHEDULED       (HOURS)   REASON (I)   REDUCING POWER (2)
were the power reduc-tions and Outage I~14 detailed below.REPORT MONTH DOCKET NO.50 2i:4 DATE GINNA STATIDN, CNIT LI January 8, 1976(Revision)
N/A 75 12 13                           0                                       Reactor power level reduction toL            47%   to perform T-18B, Turbine wain Steam Stop Valves test.
CDMPLETED ST Andrew E.MCNanara, Operations Aide TELEPHONE 4 Ext.291-214, at Ginna LID IT SI.IUTDONN AND POWER REDUCTIONS DATE TYPE F-FORCED S-SCHEDULED DURATION (HOURS)REASOiI (I)METHOD OF SHUTTING DOWN THE REACTOR OR REDUCING POWER (2)CORRECT I VE ACT I Oi(S/COMMENTS
N/A 75 12 21                           0                                        Reactor power level reduction to ~ 47% to perform )(-54.2, Check condenser 1B-1 Water Box for Leaks with Preon.
'(/A 75 12 13 0 Reactor power level reduction toL 47X to perform T-18B, Turbine Yogin Steam Stop Valves test.N/A 75 12 21 Reactor power level reduction to&#x17d;47X to perform)(-54.2, Check condenser 1B-1 Vater Box for Leaks with Freon.N/A 75 12 23 0 A Reactor power level reduction to I47X to perform M-54.2, Check condenser 1B-1 Mater Box for Leaks, with Freon.14 75 12 30 43.75 See Note)"B" Stean Generator-Tube Leak NOTE: Unit remained shutdown through the end of report onth.(I)REASONI A-EQUIPME:.'T FAILURE (EXPLAIN)8-MAINT.OR TEST C-REFIIELING D-REGULATORY RESTRICTION E-OPERATOR TRAINING AND LICENSE EXA'iIINATION C-ADXIINISTRATIVE G-OPERATIONAL ERROR (EXPLAIN)H-OTHE'R (EXPLAIN)~power reductions were not previously reported.Data not available.
N/A 75 12 23                           0                                        Reactor power level reduction to~47% to perform "(-54.2, Check condenser 1B-l Water Box for Leaks, with Freon.
Com encing January 1, 1976, this data wig bp geQrteg.>>
14  75 12 30                     43.75         A                            "B" Steam Generator       -   Tube Leak See Note)
~.
NOTFI    Unit remained shutdown through the               end of repozt    onth.
DIARY I The reactor pover levels averaged 99Z during the period.The ma)or exceptions
(I) REASON:                                   (2) METNODI A - EOUIPME .T FAILURE (EXPLAIN)               I   VANDAL B  - MAINT. OR TEST                             2   - VANUA'CRAV C   REFUELING                                 3     AUTOVATIC SCRAM D - REGULATORY RESTRICTION                           OTHER (EXPLAIN)
'were the power reduc-tions and Outage 814 detailed belov.REPORT MONTH DOCKET NO.50-244 UNIT NAME GINNA STATIDN.UNIT<I January 8, 1976(Revision)
E - OPERATOR   TRAltllNG  AND LICENSE EXAVINATION F - ADXIINISTRATI YE G   OPERATIOVAL ERROR (EXPLAIN)
DATE COVPLETEO SY Andrew E.McNamara, Operations Aide TELEPHONE 7 6-4 Ext.291-214, at Ginna UNIT SI-QTDOWN AND POWER REDUCTIONS DATE TYPE F-FORCED S-SCHEDULED DURATION (HOURS)REASON (I)METHOD OF SHUTTING DOWN THE REACTOR OR REDUCING POWER (2)CORRECTIVE ACTIONS/COAIVENTS N/A 75 12 13 0 B Reactor power level reduction to~47Z to perfo~T-18B, Turbine Yogin Steam Stop Valves test.N/A N/A 75 12 21 75 12 23 0 0 Reactor power level reduction to&#x17d;47Z to perform iM.-54.2, Check condenser 1B-1 Mater Box for Leaks with Freon.Reactor power level reduction to~47Z to perform if-54.2, Check condenser 1B-1 Vater Box for Leaks, with Freon.14 75 12 30 43.75 See Note)"B" Steam Generator-Tube Leak NOTE: Unit remained shutdown through the end of report onth.(I)REASON!(2)METNODI A-EQUIPME::T FAILURE (EXPLAIN)I-VasuaL D-MAINT.OR TEST 2-MANUA'cRav.
H - OTHER   (EXPLAIN)
C-REFUELING 3-AUTGvaTIc scpav D-REGULATORY RESTRICTION 4-OTNER (EXPLA!N)E OPERATOR TRAINING ANO I.ICENSE EXAMINaTION F-ADMINISTRATIVE G-OPERATIONAL ERROR (EXPLAIN)H OTIIER'(EXPLAIN)
IIPower  reductions were not previouslv reported.                 Data not available.       COIImIencing Januazy    I,   1976,     this data wig bp,gegrtegt
~power reductions were not.previouslv reported.Data not available.
Connencing January 1, 1976, this data wiQ bp,ge@rte<I O.
The reactor power levels averaged 99K during the period.The na)or exceptions were the power reduc-tions and Outage J)14 detailed below.REPORT MONTH DDGKET No.50-2>>'c UNIT NAVE GINNA STATION, UNIT AI January 8, 1976(Revision)
DATE COMPLETED 8Y Andrew E.McNamara, Operations Aide TELEPHONE 7 4 Ext.291-214, at Ginna UNIT S.uTDOWN AND POWER REDVCTI(NS NO." DATE TYPE F-FORCED S-SCHEDUI.ED DURATION (HOURS)REASON (I)METHOD OF SHUTTING DOWN THE REACTOR OR REDUCING POWER (2)CORRECT I VE ACT I ONS/CO.'i'MENTS N/A 75 12 13 0 B Reactor power level reduction toL"47X to perform T-18B, Turbine Main Steam Stop Valves test.N/A 75 12 21 0 Reactor power level reduction to~47X to perform M-54.2, Check condenser lB-1 Water Box for Leaks with Freon.N/A 75 12 23 S.0 A Reactor power level reduction to I47/to perform M-54.2, Check condenser 1B-1 Water Box for Leaks, with Freon.14 75 12 30 43.75*See Note)"B" Steam Generator-Tube Leak NOTE: Unit remained shutdown through the end of report=anth.(I)REASON: (2)METHOOr A-EOUIPMENT FAILURE (EXPLAIN)I-MANUAL 8-MAINT.OR TEST 2 MANUAL scRAV C-REFUELING 3 AU OuATIC SCRAu D-REGVLATORY RE'STRICTION 4-OTHER (EXPL*III)
F.-OPERATOR TR*INI:IG ANO LICENSE EXAul>>lATION F-ADMINISTRATIVE G OPERATIONAL ERROR (EXPLAIN)H-OTHER (EXPLAI.'I)
~Power reductions were not previously reported.Data not aVailable.
CODmreneing January 1, 1976, thiS data WiQ bp pep>rtegr t O.
DOCKET NO.50-24'.!ARY I The reactor pover levels averaged 99X during the period.The ma)or exceptions vere the power reduc-tions and Outage II14 detailed below.REPORT MONTH UNIT NAME GLNVA STATIOV, UNIT LI January 8, 1976(Revision)
DATE COMPLETED SY Andrew E.McNamara, Operations Aide TEIEPHONE-7-4 Ext.291-214, at Ginna UNIT 3-uTDOII AND POWER REDUCTIONS DATE TYPE F-FORCED S-SCHEDULED DURATION (HOURS)REASON (I)METHOD OF SHUTTING DOWN THE REACTOR OR REDUCING POWER (2)CORRECT I VE ACTIONS/COIN!
ENTS N/A 75 12 13 0 B Reactor power level reduction to'A 47X to perform T-18B, Turbine venin Steam Stop Ualves test.N/A 75 12 21 0 Reactor power level reduction to&#x17d;47K to perform)(-54.2, Check condenser 1B-1 Water Box for Leaks vith Ereon.N/A 75 12 23 0 Reactor power level reduction to~47X to perform M-54.2, Check condenser 1B-1 Water Box for Leaks, with Freon.14 75 12 30 43.75 See Note)"B" Steam Generator-Tube Leak NOTE: Unit remained shutdown through the end of report onth.(I)REASOV: A EOUIPAtE;:T FAILURE (EXPLAIN)8-MAINT.OR TEST C-REFUELING D-REGULATORY RESTRtCTION E OPERATOR TRAINING AND LICENSE EXAMINATION F ADAIINISTRATIVE G OPERATIONAL ERROR (EXPLAIN)H-OTHER (EXPLAIN)~Power reductions vere not previously reported.Data not available.
Commencing January 1, 1976, this data viQ bp,ge@rtegt>>
~.>A DOCKET NO.50-244'MARY: The reactor power levels averaged 99%during the period.The ma)or exceptions were the power reduc-tions and Outage 814 detailed below.REPORT MONTH UV I'T VAilE Gl NNA STA'Tl OV, UV I~<I DATE January 8, 1976(Revision)
CO'MPLETEO SY Andrew E.NcNamara, Operations Aide TEt.EPHOVE
--4 Ext.291-214, at Ginna UNIT 3-UTDOMN AND POMER REDVCTIGVS NO.DATE TYPE F-FORCED S-SCHEDULED DURATION (HOURS)REASON (I)METHOD OF SHUTTING DOWN THE REACTOR OR REDUCING POWER (2)CORRECT I VE ACT I ONS/COSMENTS N/A 75 12 13 0 B Reactor power level reduction to'L"47%to perform T-18B, Turbine Muin Steam Stop Valves test.N/A 75 12 21 Reactor power level reduction to~47%to perform)("54.2, Check condenser 1B-1 Water Box for Leaks with Freon.N/A 75 12 23 S.Reactor po~er level reduction to~47%to perform H-54.2, Check condenser 1B-1 Water Box for Leaks, with Freon.75 12 30 43.75 See Note)"B" Steam Generator-Tube Leak NOTE: Unit remained shutdown through the end of report month.(I)REASONI (2)NE'THDD: A-EOUIPME::T FAILURE (EXPLAIN)I NANUAI.8-MAINT.OR TEST MANUAL SCRAM C-REFUELING 3-AUTOUATIC SCRAu D-REGULATORY RESTRICTION 4-OTHER (EXPLAIN)E OPERATOR TRAINING AVD LICENSE EXAUINATION F-ADXIINI STRATI YE G-OPERATIONAL ERROR (EXPI.*IN)
H-OTIIER (EXPLAIN)*Power reductions were not previouslv reported.Data not available.
Commencing January 1, 1976, this data whap bp,~e)iprtegl
'1$r DOCKET NO.50-2ra e!ARYI The reactor power levels averaged 99X during the period.The ma)or exceptions were the power reduc-tions and Outage 814 detailed below.REPORT MONTH NAyE GINNA STATIO.'I.
UNIT UI January 8, 1976(Revision)
DATE COIJIPLETED BY Andrew E.McNamara, Operations Aide TELEPHONE 7 4 Ext.291-214, at Ginna UNIT S.uTDOWN AND POWER REDUCTIONS DATE TYPE F-FORCED S-SCHEDULED DURATION (HOURS)REASON (I)METHOD OF SHUTTING DOWN THE REACTOR OR REDUCING POWER (2)CORRECTIVE ACTIONSICOSIyENTS M/A 75 12 13 0 Reactor power level reduction to'~47X to perform T-18B, Turbine Ywin Steam Stop Valves test.N/A 75 12 21 0 Reactor power level reduction to~47X to perform M-54.2, Check condenser 1B-1 Water Box for Leaks with Freon.N/A 75 12 23 0 Reactor power level reduction to~47X to perform M-54.2, Check condenser lB-1 Water Box for Leaks, with Preon.14 75 12 30 43.75 See Note)"B" Steam Generator-Tube Leak NOTE: Unit remained shutdown through the end of report onth.(I)REASON: (2)NETHODI A EOUIPMERT FAILURE (EXPLAIN)I-yANUAL B NAINT.OR TEST 2-yANUAL SCRAy C-REFUELING 3 AUTOyATIC SCRAil D-REGULATORY RESTRICTION OTHER (EXPLAIN)E OPERATOR TRAINI'NG AND LICENSE EXAA'IINATION F-ADIIINISTRATIVE G OPERATIONA'L ERROR (EXPLAIN)H OTHER (EXPLAIN)+Power reductions were not previously reported.Data not available.
Commencing January 1, 1976, this data wig bp gegrtegl>>


DOCKET NO.50-2(4 t.'!PRY I The reactor power levels averaged 99X during the period.The ma)or exceptions vere the power reduc-tions and Outage f14 detailed below.REPORT NORTH UVIT VAvE GINVA STATIOV.~v!T=', DATE January 8, 1976(Revision)
'0 OOCKET NO.       50-24C YI  The eactor power levels averaged                                                                   UNIT NAVE      GINNA STATION,  "NIT <<I 99X dur'ng the period. The ma)or exceptions were the power reduc-                                                                               January 8, 1976{Revision) tions and Outage i14 detailed below.                                                                                             CovPLETEO 8Y Andrew E. YicNa'ara, Operations Aide TELEPiIONE    -7 ai - FI Ext. 291-214, at Ginna REPORT MONTH Uii)IT S.VTDORN AND POMER REDUCTIGMS kETHOD OF TYPE                                      SHUTTING DOWII F-FORCED       DURATION                  THE REACTOR OR                          CORRFCTI VE ACTIONS/COIsIENTS DATE    S-SCHEDULED     (HOURS)     REASON (I)   REDUCING POWER (2) 75 12 13                       0                                        Reactor power level reduction to'L"47% to perform T-18B, Turbine Uain Steam Stop Valves test.
COMPLETED 8Y Andrew E.McNamara, Operations Aide TELEPHONE-7-4 Ext.291-214, at Ginna UNIT SI-IUTOOWiil AND POWER RFOUCTIGMS DATE TYP E F-FORCED S-SCHEDULED DURATION (HOURS)REASON (I)METHOD OF SHUTTING DOIlVN THE REACTOR OR REDUCING POPOVER (21 CORRECTIVE ACTIONS/CONTENTS N/A>>75 12 13 Reactor power level reduction toA"47X to perform T-18B, Turbine Ruin Steam Stop Valves test.N/A 75 12 21 0 Reactor power level reduction to~47X to perform)(-54.2, Check condenser lB-1 Mater Box for Leaks with Preon.N/A 75 12 23 0 Reactor power level reduction to~47!to perform H-54.2, Check condenser 1B-1 Vater Box for Leaks, with Freon.14 75 12 30 43.75 See Note)"BH Steam Generator-Tube Leak NOTE: Unit remained shutdown through the end of report onth.(I)REASOMI (2)A!ETHOD: A-EOUIPUE::t FAII.ORE (EXPLAIN)I UAVQAI.8-MAINT.OR TEST 2-MANUAL SCPAv.C-REFUELING 3-AUTOVATIC SCRAM D-REGULATORY RESTRICTION C-OTHER (EXPLAIN)E-OPERATOR TRAINING AND LICENSE EXAvIMATIOV F-ADA'll NI STRATI YE G OPERATIONAL ERROR (EXPLAIN)H-OTHER (EXPI.AIN)
75 12 21                       0                                         Reactor power level reduction to '47% to perfom M;54.2, Check condenser 1B-1 4'ater Box for Leaks with Freon.
~power reductions were not previously reported.Data not available.
A                                 0                                         Reactor power level reduction to~47% to perform M-54.2, Check condenser 1B-1 Vater Box for Leaks, with Preon.
Commencing January 1, 1976, this data w'QT bp ge+rtegt>>  
75 12 30                   43. 75                                       "B" Steam Generator Tube Leak See Note)
NOTE: Unit remained shutdown through the end of report "onth.
('I) REASON:                                (2) METHOO:
A   EOUIPME::I'AILURE (EXPLAIN)             I   MANUAL 8 - vAINT. OR TEST                             hQNVAL SCPAV C - REFUELING                               3 - AVTGVATIC SCRAM REGULATORY RESTRICTION                     OTHER {EXPLAI.I)
E   OPERATOR TRAINIIIG ANO LICENSE EXAMINATION F - ADMINISTRATIVE G  OPERATIONA'RROR (EXPLAIN)
H   OTHER (EXPI.AIN)
IIPower  reductions were not previouslv reported. Data not available. Commencing January 1, 1976, this data wig bp ge+rtegI>>


DOCKET NO.50 AC VARY: The reactor power levels averaged 99%during the period.The ma)or exceptions were the power reduc-t'ons and Outage LB14 detailed below.REPORT MONTH UV IT NAVE GINNA STAT I OV, UN I T~l January 8, 1976(Revision)
DATE COMPLETED BY Andrew E.McNamara, Operations Aide TELEPMONE 7 4 Ext.291-214, at Ginna uwtT 3.RJTOORM AND POMER REOUCTIGQS NO.DATE TYPE F-FORCED S-SCHEDULED DURATION (HOURS)REASON (I)hIETHOD OF SHUTTING DOWN THE REACTOR OR REDUCING POWER (2)CORRECTIVE ACTIONS/COI'MENTS N/A 75 12 13 0 Reactor power level reduction toL 47%to perform T-18B, Turbine wain Steam Stop Valves test.N/A 75 12 21 0 Reactor power level reduction to~47%to perform)(-54.2, Check condenser 1B-1 Water Box for Leaks with Preon.N/A 75 12 23 0 Reactor power level reduction to~47%to perform"(-54.2, Check condenser 1B-l Water Box for Leaks, with Freon.14 75 12 30 43.75 See Note)A"B" Steam Generator-Tube Leak NOTFI Unit remained shutdown through the end of repozt onth.(I)REASON: (2)METNODI A-EOUIPME.T FAILURE (EXPLAIN)I VANDAL B-MAINT.OR TEST 2-VANUA'CRAV C REFUELING 3 AUTOVATIC SCRAM D-REGULATORY RESTRICTION OTHER (EXPLAIN)E-OPERATOR TRAltllNG AND LICENSE EXAVINATION F-ADXIINI STRATI YE G OPERATIOVAL ERROR (EXPLAIN)H-OTHER (EXPLAIN)IIPower reductions were not previouslv reported.Data not available.
COIImIencing Januazy I, 1976, this data wig bp,gegrtegt
'0 OOCKET NO.50-24C YI The eactor power levels averaged 99X dur'ng the period.The ma)or exceptions were the power reduc-tions and Outage i14 detailed below.REPORT MONTH UNIT NAVE GINNA STATION,"NIT<<I January 8, 1976{Revision)
CovPLETEO 8Y Andrew E.YicNa&#x17d;ara, Operations Aide TELEPiIONE ai-FI Ext.291-214, at Ginna Uii)IT S.VTDORN AND POMER REDUCTIGMS DATE TYPE F-FORCED S-SCHEDULED DURATION (HOURS)REASON (I)kETHOD OF SHUTTING DOWII THE REACTOR OR REDUCING POWER (2)CORRFCTI VE ACTIONS/COIsIENTS 75 12 13 0 Reactor power level reduction to'L"47%to perform T-18B, Turbine Uain Steam Stop Valves test.75 12 21 0 Reactor power level reduction to&#x17d;47%to perfom M;54.2, Check condenser 1B-1 4'ater Box for Leaks with Freon.A 0 Reactor power level reduction to~47%to perform M-54.2, Check condenser 1B-1 Vater Box for Leaks, with Preon.75 12 30 43.75 See Note)"B" Steam Generator-Tube Leak NOTE: Unit remained shutdown through the end of report"onth.('I)REASON: (2)METHOO: A EOUIPME::I'AILURE (EXPLAIN)I MANUAL 8-vAINT.OR TEST hQNVAL SCPAV C-REFUELING 3-AVTGVATIC SCRAM O REGULATORY RESTRICTION OTHER{EXPLAI.I)
E OPERATOR TRAINIIIG ANO LICENSE EXAMINATION F-ADMINISTRATIVE G OPERATIONA'RROR (EXPLAIN)H OTHER (EXPI.AIN)
IIPower reductions were not previouslv reported.Data not available.
Commencing January 1, 1976, this data wig bp ge+rtegI>>
Ce}}
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Revision as of 02:21, 21 October 2019

R. E. Ginna - Forwards Revised Unit Shutdown and Power Reduction Data Sheet for Monthly Operating Report for December 1975
ML18142B390
Person / Time
Site: Ginna Constellation icon.png
Issue date: 01/08/1976
From: Platt C
Rochester Gas & Electric Corp
To:
NRC/IE
References
Download: ML18142B390 (28)


Text

MONTHLY " PORTS iFOR GRAY BOOK PREPARATT0%

NRC bsoTRIBUTION FOR PART 50 DOCKE .'IATERIAL (TEMPORARY FORM)

CONTROL NO:

FILE MONTHLY REPORT FILE oc ester Gas & Elec. C rg,qTEOF DOC DATE R EC'D LTR TWX RPT .OTHER Rochester; N.Y. s C.E. P1att ORIG CC OTHER NRC 1 Si ned LO CLASS UNCLASS PROPINFO INPUT NO CYS REC'D DOCKET NO:

XXX DESCRIPTION: ENCLOSURES:

'Ltr trans the following: Monthly Report for DeCember 1975 Plant & Component Operability & Availability This Report to be used in preparing Gray Book by Plans & Operations.

NUMBER OP COPIES REC'D:

PLANT NAME:

FOR ACTION/INFORMATION BUTLER (L) SCHWENCER (L) ZIEMANN (L) BEGAN (E)

W/ Copies W/ Copies W/ Copies Vil/ Copies +0 NOT REMO~

CLARK (L) STOLZ (L) DICKER (E) LEAR (L)

\A// Copssss W/ Copies

'ARR (L) VASSALLO (L)- KNIGHTON (Ei SPELS W/ Copies W pies W/. Copies W/ Copies KNtEt (L) RPLE (L) YOUNGBLOOD (E)>> MIPC/PE W/ Copies W/ Copies W/ Copies W,4 Copies tNTERNAL DtSTRIBUTION G FI TECH REVIEW DENTON LIC ASST A/T I ND ~

~NR DR SCHROEDER GRIMES R. DIGGS (L) 8 RAITMAN OGC, ROOM P-506A. MACCARY GAMM ILL H. GEAR IN (L) SALTZMAN GOSSI CK/STAF F KNIGHT KASTNER E. GOULBOURNE (L) MELTZ CASE PAWLICKI BALLARD P. KREUTZER (E)

BOYD MOORE (L)

DEYOUNG (L)

SKOVHOLT (L)

GOLLER {L) {Ltr)

/ SHAO STE LLO HOUSTON NOVAK ROSS IPPOLI TO SPANGLER FNVIRO MULLER DICKER KNIGHTON

'. J. LEE (L)

M. RUSHBROOK S. REED (EI M.

.

S (L)

VICE (t )

SHEPPARD (L)

SLATER (E)

PLANS

~MCDONALD

~CHAPMAN DUBE (Ltr)

E. COUP.E PETERSON P. COLLINS TEDESCO YOUNGBLOOD H. SMITH (L) HARTFIELD (2)

DENISE J. COLLINS REGAN S. TEETS (L) KLECKER REG OPR LAINAS PROJECT LDR G. WILLIAMS(E) E ISENHUT FI I.F. 6 REGION (2) BENAROYA V. WILSON (L) Wl GG INl ON VOLLMER HARLESS R. INGRAM (L)

STEELE M DUN A~N K. PARRISH L EXTERNAL DISTRIBUTION

~1 LOCAL PDR~~Mm Rochester, N.Y.

P D R-SAN/LA/NY

~'l TIC (ABERNATHY) (1}(2)('IO) NATIONALLABS 1

~1 NSIC (BUCHANAN) 1 W. PENNINGTON, Rm E-201 GT 1 BROOKIHAVEN NAT LAB 1 ASLB 1 CONSULTANTS s 1 G. ULRIKSON, ORNL 1 Newton Anderson NEWMARK/BLUME/AGBABIAN 1 AGMED (RUTH GUSSMAN)

ACRS HOLDING/SENT Rm B-127.GT 1 J. D. RUNKLES, Rm E-201 GT

P ~

', t ZW/// SIXES

//I/IIII'ZFiH':

/ ////I//8'///I///////

ROCHESTER GAS AND ELECTRIC CORPO T AVENUE, ROCHESTER, N.Y. 14649 cj TELEIIHONE URIEL AREA coDE 7ld 546-2700 Ginna Station JP, ge.lBES.>~- January 8, 1976

~ReguTatorP

.r 'Ajtk.N<'irector,

~

1 Office of Inspection and Enforcement (P i l U. S. Nuclear Regulatory Commission /N Washington, D. C. 20555 e

Subject:

Monthly Report for December, 1975 (Revised)

Operating Status Information R. E. Ginna Nuclear Power Plant Unit No. 1 Docket No. 50-244 Gentlemen:

Pursuant to Technical Specification 6.9.1c attached herewith is a re-vised unit shutdown and power reduction data sheet, to correct previous error in reporting reasons for reductions in reactor power levels on 12/13, 12/21 and 12/23.

Very truly yours, gtP Charles E. Platt Superintendent CEP:fah Attachments 1

cc: Mr. James P. O'Reilly, NRC (1)

Mr. William G. McDonald, NRC (2)

t I

11

DOCKET NO. 50-244

SUMMARY

The reactor power levels averaged GINNA STATION, UNIT PI 99% during the period. The major exceptions were the power reduc- January 8, 1976(Revision)

DATE tions and Outage 814 detailed below. COMPLETED BY Andrew E. McNamara, Operations Aide TELEPHONE Ext. 291-214, at Ginna REPORT MONTH UNIT SHUTDOWN AND POWER REDUCTIONS METHOD OF TYPE SHUTTING DOWN F-FORCED DURATION CORRECTIVE ACTIONS/COMMENTS THE REACTOR OR NO. DATE S-SCHEDULED (HOURS) REASON (I) REDUCING POWER (2)

N/A 75 12 13 Reactor power level reduction to~47%=to perform T-'8B, Turbine Main Steam Stop Valves test.

N/A 75 12 21 A Reactor power level reduction to ~ 47% to perform M-54.2, Check condenser 1B-1 Water Box for Leaks with Freon.

N/A 75 12 23 A Reactor power level reduction to~47% to perform M-54.2, Check condenser 1B-1 Water Box for Leaks, with Freon.

14 75 12 30 43.75 "B" Steam Generator Tube Leak See Note)

NOTE: Unit remained shutdown through the end of report month.

(I) REASON: (2) METHOD:

A - EOUIPMENT FAILURE (EXPLAIN) I - MANUAL B - MAINT. OR TEST 2 - MANUAL SCRAM C - REFUELING 3 - AUTOMATIC SCRAM D - REGULATORY RESTRICTION 4 - OTHER (EXPLAIN)

E - OPERATOR TRAINING AND LICENSE EXAMINATION F - ADMINISTRATIVE G - OPERATIONAL ERROR (EXPLAIN)

H - OTHER (EXPLAIN) .

+Power reductions were not previously reported. Data not available. Commencing January 1, 1976, this data wig bp pegprteg.~9

0 L'~,

DOCKET RO. 50-2i:C 5!ARY I The reactor power levels averaged UVIT RAvE GIRRA STATlos, UR'T AI 99Z durirg the period. The ma)or exceptions vere the power reduc- DATE January 8, 1976(Revision) tions and Oueage F'14 deeailed be'v. COMPLETED SY Andzev E. McNamara, Operations Aide TELEPHONE -7 4 Ext. 291-214, at Ginra REPORT MONTH UNIT S-uTDOIY'N AND POWER REDUCTIONS METHOD OF TYP E SHUTTING DOWN F-FORCED DURAT I OiN THE REACTOR OR CORRECT I VE ACT I ONS/COLNENTS NO. DATE S-SCHEDUI.ED (HOURS) REASON (I) REDUCING POWER (2)

N/A 75 12 13 Reactor power level reduction toL 47Z to perform T-18B, Turbine venin Seeam Stop Ualves test.

N/A 75 12 21 0 Reactor power level reduction to '47Z to perform M-54.2, Check condenser 1B-1 Mater Box for Leaks vith Freon.

N/A 75 12 23 Reactor power level reduceion to I47Z to perform N-54.2, Check condenser 1B-1 Mater Box for Leaks, with Freon.

75 12 30 43.75 "B" Steam Generator - Tube Leak See Note)

NOTE: Unit remained shutdown thzough the end of zeport onth.

(I) REASORI (2) MEiHOOI A EOUIPME .T FAILURE (EXPLAIII) I VARUAL S MAINT. OR TEST 2 - MARUA'cRAv.

C - REFUELING 3 - AUTOVATIC SCRAM 0 - REGUlATORY RESTRICTION 4 - OTHER (EXPLAIN)

E OPERATOR TRAII<IRG ARO lICEiiSE EXAvlRATIOR F - ADMINISTRATIVE OPERATIONAL ERROR (EXPLAIN)

H OTHER (EXPL*III)

RPower reducti'ons were not previously reported. Data not available. Commencing Januazy 1, 1976, this data I

> DOCKET NO. 50-244 PIARYI The reactor power levels averaged GIMNA STATION OMIT > ~ . DOCKET NO. 50-244 DIARYI The reactor pover levels averaged UNIT NAME GINNA STATIDN. UNIT <I 99Z during the period. The ma)or exceptions 'were the power reduc- DATE January 8, 1976(Revision) tions and Outage 814 detailed belov. COVPLETEO SY Andrew E. McNamara, Operations Aide TELEPHONE 7 6- 4 Ext. 291-214, at Ginna REPORT MONTH UNIT SI-QTDOWN AND POWER REDUCTIONS METHOD OF TYPE SHUTTING DOWN F-FORCED DURATION THE REACTOR OR CORRECTIVE ACTIONS/COAIVENTS DATE S-SCHEDULED (HOURS) REASON (I) REDUCING POWER (2) N/A 75 12 13 0 B Reactor power level reduction to~47Z to perfo~ T-18B, Turbine Yogin Steam Stop Valves test. N/A 75 12 21 0 Reactor power level reduction to '47Z to perform iM.-54.2, Check condenser 1B-1 Mater Box for Leaks with Freon. N/A 75 12 23 0 Reactor power level reduction to~47Z to perform if-54.2, Check condenser 1B-1 Vater Box for Leaks, with Freon. 14 75 12 30 43.75 "B" Steam Generator Tube Leak See Note) NOTE: Unit remained shutdown through the end of report onth. (I) REASON! (2) METNODI A - EQUIPME::T FAILURE (EXPLAIN) I - VasuaL D - MAINT. OR TEST 2 - MANUA'cRav. C - REFUELING 3 - AUTGvaTIc scpav D - REGULATORY RESTRICTION 4 - OTNER (EXPLA!N) E OPERATOR TRAINING ANO I.ICENSE EXAMINaTION F - ADMINISTRATIVE G - OPERATIONAL ERROR (EXPLAIN) H OTIIER'(EXPLAIN) ~power reductions were not .previouslv reported. Data not available. Connencing January 1, 1976, this data wiQ bp,ge@rte>'c The reactor power levels averaged UNIT NAVE GINNA STATION, UNIT AI 99K during the period. The na)or exceptions were the power reduc- DATE January 8, 1976(Revision) tions and Outage J)14 detailed below. COMPLETED 8Y Andrew E. McNamara, Operations Aide TELEPHONE 7 4 Ext. 291-214, at Ginna REPORT MONTH UNIT S.uTDOWN AND POWER REDVCTI(NS METHOD OF TYPE SHUTTING DOWN F-FORCED DURATION THE REACTOR OR CORRECT I VE ACT I ONS/CO.'i'MENTS NO. " DATE S-SCHEDUI.ED (HOURS) REASON (I) REDUCING POWER (2) N/A 75 12 13 0 B Reactor power level reduction toL"47X to perform T-18B, Turbine Main Steam Stop Valves test. N/A 75 12 21 0 Reactor power level reduction to ~ 47X to perform M-54.2, Check condenser lB-1 Water Box for Leaks with Freon. N/A 75 12 23 S. 0 A Reactor power level reduction to I47/ to perform M-54.2, Check condenser 1B-1 Water Box for Leaks, with Freon. 14 75 12 30 43.75* "B" Steam Generator - Tube Leak See Note) NOTE: Unit remained shutdown through the end of report =anth. (I) REASON: (2) METHOOr A - EOUIPMENT FAILURE (EXPLAIN) I - MANUAL 8 - MAINT. OR TEST 2 MANUAL scRAV C - REFUELING 3 AU OuATIC SCRAu D - REGVLATORY RE'STRICTION 4 - OTHER (EXPL*III) F. - OPERATOR TR*INI:IG ANO LICENSE EXAul>>lATION F - ADMINISTRATIVE G OPERATIONAL ERROR (EXPLAIN) H - OTHER (EXPLAI.'I) ~Power reductions were not previously reported. Data not aVailable. CODmreneing January 1, 1976, thiS data WiQ bp pep>rtegr t O. DOCKET NO. 50-24'.!ARY I The reactor pover levels averaged UNIT NAME GLNVA STATIOV, UNIT LI 99X during the period. The ma)or exceptions vere the power reduc- DATE January 8, 1976(Revision) tions and Outage II14 detailed below. COMPLETED SY Andrew E. McNamara, Operations Aide TEIEPHONE -7 - 4 Ext. 291-214, at Ginna REPORT MONTH UNIT 3-uTDOII AND POWER REDUCTIONS METHOD OF TYPE SHUTTING DOWN F-FORCED DURATION THE REACTOR OR CORRECT I VE ACTIONS/COIN!ENTS DATE S-SCHEDULED (HOURS) REASON (I) REDUCING POWER (2) N/A 75 12 13 0 B Reactor power level reduction to'A 47X to perform T-18B, Turbine venin Steam Stop Ualves test. N/A 75 12 21 0 Reactor power level reduction to '47K to perform )(-54.2, Check condenser 1B-1 Water Box for Leaks vith Ereon. N/A 75 12 23 0 Reactor power level reduction to~47X to perform M-54.2, Check condenser 1B-1 Water Box for Leaks, with Freon. 14 75 12 30 43.75 "B" Steam Generator - Tube Leak See Note) of report onth. NOTE: Unit remained shutdown through the end (I) REASOV: A EOUIPAtE;:T FAILURE (EXPLAIN) 8 - MAINT. OR TEST C - REFUELING D - REGULATORY RESTRtCTION E OPERATOR TRAINING AND LICENSE EXAMINATION F ADAIINISTRATIVE G OPERATIONAL ERROR (EXPLAIN) H - OTHER (EXPLAIN) ~Power reductions vere not previously reported. Data not available. Commencing January 1, 1976, this data viQ bp,ge@rtegt>> ~ . > A DOCKET NO. 50-244 'MARY: The reactor power levels averaged UV I 'T VAilE Gl NNA STA'Tl OV, UV I ~ > DOCKET NO. 50-2(4 t.'!PRY I The reactor power levels averaged UVIT VAvE GINVA STATIOV. ~ v! T =', 99X during the period. The ma)or exceptions vere the power reduc- DATE January 8, 1976(Revision) tions and Outage f14 detailed below. COMPLETED 8Y Andrew E. McNamara, Operations Aide TELEPHONE 4 Ext. 291-214, at Ginna REPORT NORTH UNIT SI-IUTOOWiil AND POWER RFOUCTIGMS METHOD OF TYP E SHUTTING DOIlVN F-FORCED DURATION THE REACTOR OR CORRECTIVE ACTIONS/CONTENTS DATE S-SCHEDULED (HOURS) REASON (I) REDUCING POPOVER (21 N/A>> 75 12 13 Reactor power level reduction toA"47X to perform T-18B, Turbine Ruin Steam Stop Valves test. N/A 75 12 21 0 Reactor power level reduction to ~ 47X to perform )(-54.2, Check condenser lB-1 Mater Box for Leaks with Preon. N/A 75 12 23 0 Reactor power level reduction to~47! to perform H-54.2, Check condenser 1B-1 Vater Box for Leaks, with Freon. 14 75 12 30 43.75 "BH Steam Generator - Tube Leak See Note) NOTE: Unit remained shutdown through the end of report onth. (I) REASOMI (2) A!ETHOD: A - EOUIPUE::t FAII.ORE (EXPLAIN) I UAVQAI. 8 - MAINT. OR TEST 2 - MANUAL SCPAv. C - REFUELING 3 - AUTOVATIC SCRAM D - REGULATORY RESTRICTION C - OTHER (EXPLAIN) E - OPERATOR TRAINING AND LICENSE EXAvIMATIOV F - ADA'llNI STRATI YE G OPERATIONAL ERROR (EXPLAIN) H - OTHER (EXPI.AIN) ~power reductions were not previously reported. Data not available. Commencing January 1, 1976, this data w'QT bp ge+rtegt>> DOCKET NO. 50 AC VARY: The reactor power levels averaged UV IT NAVE GINNA STAT I OV, UN I T ~l 99% during the period. The ma)or exceptions were the power reduc- DATE January 8, 1976(Revision) t'ons and Outage LB14 detailed below. COMPLETED BY Andrew E. McNamara, Operations Aide TELEPMONE 7 4 Ext. 291-214, at Ginna REPORT MONTH uwtT 3.RJTOORM AND POMER REOUCTIGQS hIETHOD OF TYPE SHUTTING DOWN F-FORCED DURATION THE REACTOR OR CORRECTIVE ACTIONS/COI'MENTS NO. DATE S-SCHEDULED (HOURS) REASON (I) REDUCING POWER (2) N/A 75 12 13 0 Reactor power level reduction toL 47% to perform T-18B, Turbine wain Steam Stop Valves test. N/A 75 12 21 0 Reactor power level reduction to ~ 47% to perform )(-54.2, Check condenser 1B-1 Water Box for Leaks with Preon. N/A 75 12 23 0 Reactor power level reduction to~47% to perform "(-54.2, Check condenser 1B-l Water Box for Leaks, with Freon. 14 75 12 30 43.75 A "B" Steam Generator - Tube Leak See Note) NOTFI Unit remained shutdown through the end of repozt onth. (I) REASON: (2) METNODI A - EOUIPME .T FAILURE (EXPLAIN) I VANDAL B - MAINT. OR TEST 2 - VANUA'CRAV C REFUELING 3 AUTOVATIC SCRAM D - REGULATORY RESTRICTION OTHER (EXPLAIN) E - OPERATOR TRAltllNG AND LICENSE EXAVINATION F - ADXIINISTRATI YE G OPERATIOVAL ERROR (EXPLAIN) H - OTHER (EXPLAIN) IIPower reductions were not previouslv reported. Data not available. COIImIencing Januazy I, 1976, this data wig bp,gegrtegt '0 OOCKET NO.50-24C YI The eactor power levels averaged UNIT NAVE GINNA STATION, "NIT <> Ce