ML020860427

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February 2002 Monthly Operating Report for R.E. Ginna Nuclear Power Plant
ML020860427
Person / Time
Site: Ginna Constellation icon.png
Issue date: 03/08/2002
From: Widay J
Rochester Gas & Electric Corp
To:
Document Control Desk, NRC/NRR/DLPM/LPD1
References
Download: ML020860427 (3)


Text

ROCHESTER GAS AND ELECTRIC CORPORATiON # 89 EAST AVENUE, ROCHESTER, N. Y 14649-0001 AREA CODE 716 546-2700 March 8, 2002 US Nuclear Regulatory Commission Document Control Desk Attn:

Robert Clark Project Directorate I-1 Washington, DC 20555

Subject:

Monthly Report for February, 2002 Operating Status Information R.E. Ginna Nuclear Power Plant Docket No. 50-244

Dear Mr. Clark:

Pursuant to Ginna Improved Technical Specifications Section 5.6.4, attached is the monthly operating status report for Ginna Station for the month of February, 2002.

Very truly yours,

ýaqn A. Widaya Plant Manager xc:

U.S. Nuclear Regulatory Commission Mr. Robert Clark (Mail Stop O-8E9)

Project Directorate I-1 Washington, D.C. 20555 U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 U.S. NRC Ginna Senior Resident Inspector Attachments

OPERATING DATA REPORT 50-244 March 8, 2002 COMPLETED BY:

JO W

/John V. Walden TELEPHONE (585) 771-3588 OPERATING STATUS

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Unit Name:

R.E. GINNA NUCLEAR POWER PLANT Reporting Period:

February, 2002 Design Electric Rating (Net MWe):

470 Maximum Dependable Capacity (Net MWe):

480 Notes:

Number of hours Reactor Was Critical Hours Generator On-line Unit Reserve Shutdown Hours Net Electrical Energy Generated (MWH)

This Month 653.7 637.2 0.0 310159.1 Yr.-to-Date 1397.7 1381.2 0.0 679595.1 Cumulative**

232419.9 228543.3 8.5 104165155.9

    • CUMULATIVE TOTAL COMMENCING NOVEMBER 8,1969
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DOCKET NO: 50-244 UNIT NAME: R.E. GINNA NUCLEAR POWER PLANT DATE: March 8, 2002 COMPLETED BY: John V. Walden TELEPHONE: (585) 771-3588 UNIT SHUTDOWN REPORTING PERIOD:

February, 2002 (Month/Year)

NO.

DATE TYPE DURATION REASON(1 )

METHOD OF CAUSE/CORRECTIVE ACTIONS F: FORCED (HOURS)

SHUTTING 5: SCHEDULED DOWN(2)

COMMENTS 1

020205 F

34.8 A

2

'A' Circulating Water Pump Trip

SUMMARY

The unit operated at full power until February 5, 2002. A manual reactor trip occurred on February 5, 2002 at 0911. The cause of the trip was due to a DC field cable failure on the 'A' Circulating Water Pump motor rotor. The unit was place on-line on February 6, 2002 at 2001.

Full power operations continued from February 7, 2002 to February 23, 2002. End of Fuel Cycle 29 coastdown began on February 23, 2002 and continued through the end of the month.

(1) Reason A - Equipment Failure (Explain)

B - Maintenance or Test C - Refueling D - Regulatory Restriction E - Operator Training/License Examination F - Administrative G - Operational Error (Explain)

H - Other (Explain)

(2) Method 1 - Manual 2 - Manual Trip/Scram 3 - Automatic Trip/Scram 4 - Continuation 5 - Other (Explain)