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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217L0421999-10-21021 October 1999 Forwards Insp Rept 50-382/99-20 on 990815-0925 & Notice of Violation.Two Severity Level IV Violations of NRC Requirements Identified & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20217N2111999-10-19019 October 1999 Forwards Insp Rept 50-382/99-14 on 990913-17 & 1004-08.No Violations Noted.Licensed Operator Requalification Program, Effective,Utilized Systems Approach to Training & Showed Continued Improvements Over Previous Insp Findings ML20217L0101999-10-18018 October 1999 Provides Update of Waterford 3 Effort for Review of Ufsar. Info Listed Includes Background Mgt Expectations,Review Status & Results,Clarifications Re Review & Conclusions ML20217L0141999-10-18018 October 1999 Submits Update to NRC Staff Re Circumstances & Plans for Submitting Certification Rept on Waterford 3 Plant Specific Simulator ML20217G7051999-10-14014 October 1999 Forwards Comments on Four of NRC RO Examination Questions for Exam Administered During Week of 991004 05000382/LER-1999-014, Forwards LER 99-014-00,providing Details of Reactor Shutdown Due to Loss of RCP Controlled bleed-off Flow.Attached Commitment Identification/Voluntary Enhancement Form Identifies All Commitments Contained in Submittal1999-10-12012 October 1999 Forwards LER 99-014-00,providing Details of Reactor Shutdown Due to Loss of RCP Controlled bleed-off Flow.Attached Commitment Identification/Voluntary Enhancement Form Identifies All Commitments Contained in Submittal ML20217D5151999-10-0707 October 1999 Forwards Application for Renewal of SRO License for C Fugate License SOP-43039-3,IAW 10CFR55.57.Without Encls ML20217C6251999-10-0505 October 1999 Informs That NRC Reviewed Util Ltr & Encl Exercise Scenario Package for Waterford 3 Emergency Plan Exercise Scheduled for 991013.Based on Review,Nrc Determined That Exercise Appropriate to Meet Objectives ML20212J6921999-09-29029 September 1999 Forwards Insp Rept 50-382/99-18 on 990830-0902.One Noncited Violation Identified Re Failure to Follow Procedural Instructions to Ensure That Members on Fire Brigade Shift Were Qualified ML20216G2441999-09-27027 September 1999 Forwards Insp Rept 50-382/99-19 on 990830-0903.No Violations Noted 05000382/LER-1999-013, Forwards LER 99-013-00,providing Details of Exceeding TS Limits for RCS Cooldown Rates.All Commitments Contained in Submittal Are Identified on Encl Commitment Identification/ Voluntary Enhancement Form1999-09-23023 September 1999 Forwards LER 99-013-00,providing Details of Exceeding TS Limits for RCS Cooldown Rates.All Commitments Contained in Submittal Are Identified on Encl Commitment Identification/ Voluntary Enhancement Form IR 05000382/19993011999-09-21021 September 1999 Informs That NRC License Exam Previously Associated with NRC Insp Rept 50-382/99-301 Will Be Incorporated Into NRC Insp Rept 50-382/99-14 ML20212D8761999-09-16016 September 1999 Informs That on 990818,NRC Staff Completed Midcycle PPR of Waterford 3.During Assessment Period,Number of Personnel Errors Occurred,Which Demonstrated Lack of Attention to Detail by Plant Personnel.Historical Listing of Issues,Encl ML20212C2471999-09-16016 September 1999 Forwards Five Final Applications for RO Licenses for G Esquival,Jm Hearn,Md Lawson,Re Simpson & PI Wood.Written Exam & Operating Test to Be Administered,Is Requested. Encls Withheld ML20212C2391999-09-16016 September 1999 Requests Cancellation of SRO Licenses for Bn Coble,License SOP-43835,due to Job Assignment Location & CA Rodgers, License SOP-43537-1,due to Resignation from Company, Effective 990901 ML20212C5881999-09-14014 September 1999 Forwards Insp Rept 50-382/99-15 on 990719-23 with Continuing in Ofc Insp Until 0819.No Violations Noted ML20211Q4421999-09-0909 September 1999 Forwards Insp Rept 50-382/99-07 on 990601-11.Three Violations Being Treated as Noncited Violations ML20211P4121999-09-0707 September 1999 Requests NRC Staff Review & Approval of Integrated Nuclear Security Plan (Insp) & Integrated Security Training & Qualification Plan (Ist&Q), for Use by All Entergy Operations,Inc.Encl Withheld,Per 10CFR2.790(d) ML20211M8391999-09-0303 September 1999 Forwards Revised Epips,Including Rev 25 to EP-001-020,rev 24 to EP-001-030,rev 25 to EP-001-040,rev 30 to EP-002-100,rev 22 to EP-001-010,rev 27 to EP-002-010,rev 26 to EP-002-102 & Rev 16 to EP-002-190.Listed Proprietary Revs to Epips,Encl ML20211L3681999-09-0202 September 1999 Forwards Five Preliminary Applications for Reactor Operator Licenses for Individuals Listed,Iaw 10CFR55.31.Encls Withheld ML20211K9741999-09-0101 September 1999 Forwards Insp Rept 50-382/99-16 on 990704-0814.Two Severity Level IV Violations Identified & Being Treated as Noncited Violations,Consistent with App C of Enforcement Policy 05000382/LER-1999-011, Forwards LER 99-011-00,providing Details of Reactor Shutdown Due to Loss of Controlled bleed-off Flow.All Commitments Contained in Submittal Identified on Attached Commitment Identification/Voluntary Enhancement Form1999-08-31031 August 1999 Forwards LER 99-011-00,providing Details of Reactor Shutdown Due to Loss of Controlled bleed-off Flow.All Commitments Contained in Submittal Identified on Attached Commitment Identification/Voluntary Enhancement Form ML20211M3641999-08-30030 August 1999 Forwards Written Examination,Operating Tests & Supporting Ref Matl Identified in Attachment 2 of ES-210,in Response to NRC .Encl Withheld ML20211G5751999-08-27027 August 1999 Forwards RAI Re IPEEE Submittal.Please Provide RAI within 60 Days of Receipt of Ltr,Per Util Response to GL 88-20,suppl 4 ML20211E3281999-08-26026 August 1999 Forwards fitness-for-duty Performance Data for Period of 990101-0630,IAW 10CFR26.71(d).Ltr Does Not Contain Commitments 05000382/LER-1999-009, Forwards LER 99-009-00 Re Discovery of Condition of Noncompliance with App R Involving Inadequate Separation of Essential Cables Routed in Fire Area RAB-30 in Rab. Compensatory Measures Were Established Immediately1999-08-26026 August 1999 Forwards LER 99-009-00 Re Discovery of Condition of Noncompliance with App R Involving Inadequate Separation of Essential Cables Routed in Fire Area RAB-30 in Rab. Compensatory Measures Were Established Immediately 05000382/LER-1999-010, Forwards LER 99-010-00,providing Details of Inadequate Pumping Capacity in Dry Cooling Tower Area.All Commitments Contained in Submittal Are Identified on Attached Commitment Identification Voluntary Enhancement Form1999-08-26026 August 1999 Forwards LER 99-010-00,providing Details of Inadequate Pumping Capacity in Dry Cooling Tower Area.All Commitments Contained in Submittal Are Identified on Attached Commitment Identification Voluntary Enhancement Form ML20211F5421999-08-24024 August 1999 Forwards Proposed marked-up TS Page Xviii, Index Administrative Controls, Correcting Page Number Re TS Change Request NPF-38-220.Editorial Changes for TS Change NPF-38-221 Discussed ML20211F3561999-08-24024 August 1999 Forwards CTS Pages & TS Proposed marked-up Pages for Insertion Into TS Change Request NPF-38-207 Re Efas, Originally Submitted on 980702.Original NSHC Determination Continues to Be Applicable ML20211F4611999-08-24024 August 1999 Informs That NRC Reviewed Ltr & Encl Objectives for Waterford 3 Emergency Plan Exercise Scheduled for 991013.Exercise Objectives Appropriate to Meet Emergency Plan Requirements ML20211G1731999-08-23023 August 1999 Informs That Info Submitted in ,B&W Rept 51-1234900-00,will Be Withheld from Public Disclosure,Per 10CFR2.790 ML20211C5101999-08-19019 August 1999 Forwards Certified Copies of Liability Insurance Policy Endorsements Issued in First Half of 1999 for Each Entergy Operations,Inc Nuclear Unit,Per 10CFR140.15 ML20210T9791999-08-18018 August 1999 Discusses Which Responded to Reconsideration of Violation Denial (EA 98-022) Enforcement Action Detailed in .Concludes That Violation Occurred as Stated ML20211A9501999-08-12012 August 1999 Discusses 990720-21 Workshop Conducted in Region IV Ofc,Re Exchange of Info in Area of Use of Risk Insights in Regulatory Activities.List of Attendees,Summary of Topic & Issues,Agenda & Copies of Handouts Encl ML20210S0561999-08-12012 August 1999 Submits Voluntary Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for NRC Fys 2000 & 2001 for Waterford 3 ML20210Q6161999-08-12012 August 1999 Forwards Corrected Copy of Monthly Operating Rept for July 1999 for Waterford 3.Original Rept,Submitted with ,Contained Typos ML20217F2661999-08-12012 August 1999 Forwards Copy of 1999 Waterford 3 Biennial Exercise Package to Be Performed Using Waterford 3 CR Simulator ML20210R9231999-08-11011 August 1999 Forwards Insp Rept 50-382/99-10 on 990719-23.Violations Noted.Nrc Has Determined That One Severity Level IV Violation of NRC Requirements Occurred ML20210L1461999-08-0303 August 1999 Informs That NRC Plans to Administer Gfes of Written Operator Licensing Exam on 991006.Requests Submittal of Ltr Identifying Individuals Taking Exam,Personnel Allowed Access to Exams & Mailing Address for Exams 05000382/LER-1999-008, Forwards LER 99-008-00,re Failure to Perform Testing of ESF Filtration Units Per TS Srs.Commitments Made by Util Also Encl1999-07-29029 July 1999 Forwards LER 99-008-00,re Failure to Perform Testing of ESF Filtration Units Per TS Srs.Commitments Made by Util Also Encl ML20210H4291999-07-29029 July 1999 Forwards Response to NRC Rai,Associated with TS Change Request NPF-38-208,proposing to Replace Ref to Supplement 1 with Ref to Supplement 2 of Calculative Methods for CE Small Break LOCA Evaluation Model, in ACs Section of TSs ML20210F9451999-07-27027 July 1999 Forwards Proprietary & non-proprietary Version of Rev 29 to EPIP EP-002-100, Technical Support Ctr Activation,Operation & Deactivation. Proprietary Info Withheld,Per 10CFR2.790 ML20210D3171999-07-23023 July 1999 Submits Proposal for Final Resolution of Reracking Spent Fuel Pool at Plant,Per License Amend 144,issued by NRC in .No New Commitments Are Contained in Ltr 05000382/LER-1999-007, Forwards LER 99-007-00,providing Details of Operation Outside Tornado Missile Protection Licensing Basis for turbine-driven Emergency Feedwater Pump Exhaust Stack & Steam Supply Piping.All Commitments Identified on Attached1999-07-23023 July 1999 Forwards LER 99-007-00,providing Details of Operation Outside Tornado Missile Protection Licensing Basis for turbine-driven Emergency Feedwater Pump Exhaust Stack & Steam Supply Piping.All Commitments Identified on Attached ML20210D8701999-07-23023 July 1999 Forwards Safety Evaluation Re First 10-yr Interval Inservice Insp Plan Requests for Relief ISI-018 Through ISI-020 for Entergy Operations,Inc,Unit 3 ML20210B1521999-07-15015 July 1999 Forwards Insp Rept 50-382/99-13 on 990523-0703.Three Violations Being Treated as Noncited Violations ML20209G9771999-07-13013 July 1999 Forwards Objectives & Guidelines for Waterford 3 Emergency Preparedness Exercise Scheduled for 991013.List of Objectives cross-referenced Where Applicable to Relevant Sections of NUREG-0654 IR 05000382/19990081999-07-12012 July 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-382/99-08 Issued on 990503 ML20209E5231999-07-0909 July 1999 Informs That as Result of NRC Review of Util Responses to GL-92-01,rev 1 & Suppl 1,staff Revised Info in Reactor Vessel Integrity Database & Releasing Database as Rvid Version 2.This Closes Staff Efforts Re TAC MA0583 ML20209D4051999-07-0707 July 1999 Forwards Revised TS Pages to Replace Attachment C,Entirely in Original TS Change Request NPF-38-207,per 990519 Discussion with C Patel of Nrc.Changes to Action 20 Delete Word Requirement & Revise Word Modes to Mode 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217L0101999-10-18018 October 1999 Provides Update of Waterford 3 Effort for Review of Ufsar. Info Listed Includes Background Mgt Expectations,Review Status & Results,Clarifications Re Review & Conclusions ML20217L0141999-10-18018 October 1999 Submits Update to NRC Staff Re Circumstances & Plans for Submitting Certification Rept on Waterford 3 Plant Specific Simulator ML20217G7051999-10-14014 October 1999 Forwards Comments on Four of NRC RO Examination Questions for Exam Administered During Week of 991004 05000382/LER-1999-014, Forwards LER 99-014-00,providing Details of Reactor Shutdown Due to Loss of RCP Controlled bleed-off Flow.Attached Commitment Identification/Voluntary Enhancement Form Identifies All Commitments Contained in Submittal1999-10-12012 October 1999 Forwards LER 99-014-00,providing Details of Reactor Shutdown Due to Loss of RCP Controlled bleed-off Flow.Attached Commitment Identification/Voluntary Enhancement Form Identifies All Commitments Contained in Submittal ML20217D5151999-10-0707 October 1999 Forwards Application for Renewal of SRO License for C Fugate License SOP-43039-3,IAW 10CFR55.57.Without Encls 05000382/LER-1999-013, Forwards LER 99-013-00,providing Details of Exceeding TS Limits for RCS Cooldown Rates.All Commitments Contained in Submittal Are Identified on Encl Commitment Identification/ Voluntary Enhancement Form1999-09-23023 September 1999 Forwards LER 99-013-00,providing Details of Exceeding TS Limits for RCS Cooldown Rates.All Commitments Contained in Submittal Are Identified on Encl Commitment Identification/ Voluntary Enhancement Form ML20212C2391999-09-16016 September 1999 Requests Cancellation of SRO Licenses for Bn Coble,License SOP-43835,due to Job Assignment Location & CA Rodgers, License SOP-43537-1,due to Resignation from Company, Effective 990901 ML20212C2471999-09-16016 September 1999 Forwards Five Final Applications for RO Licenses for G Esquival,Jm Hearn,Md Lawson,Re Simpson & PI Wood.Written Exam & Operating Test to Be Administered,Is Requested. Encls Withheld ML20211P4121999-09-0707 September 1999 Requests NRC Staff Review & Approval of Integrated Nuclear Security Plan (Insp) & Integrated Security Training & Qualification Plan (Ist&Q), for Use by All Entergy Operations,Inc.Encl Withheld,Per 10CFR2.790(d) ML20211M8391999-09-0303 September 1999 Forwards Revised Epips,Including Rev 25 to EP-001-020,rev 24 to EP-001-030,rev 25 to EP-001-040,rev 30 to EP-002-100,rev 22 to EP-001-010,rev 27 to EP-002-010,rev 26 to EP-002-102 & Rev 16 to EP-002-190.Listed Proprietary Revs to Epips,Encl ML20211L3681999-09-0202 September 1999 Forwards Five Preliminary Applications for Reactor Operator Licenses for Individuals Listed,Iaw 10CFR55.31.Encls Withheld 05000382/LER-1999-011, Forwards LER 99-011-00,providing Details of Reactor Shutdown Due to Loss of Controlled bleed-off Flow.All Commitments Contained in Submittal Identified on Attached Commitment Identification/Voluntary Enhancement Form1999-08-31031 August 1999 Forwards LER 99-011-00,providing Details of Reactor Shutdown Due to Loss of Controlled bleed-off Flow.All Commitments Contained in Submittal Identified on Attached Commitment Identification/Voluntary Enhancement Form ML20211M3641999-08-30030 August 1999 Forwards Written Examination,Operating Tests & Supporting Ref Matl Identified in Attachment 2 of ES-210,in Response to NRC .Encl Withheld ML20211E3281999-08-26026 August 1999 Forwards fitness-for-duty Performance Data for Period of 990101-0630,IAW 10CFR26.71(d).Ltr Does Not Contain Commitments 05000382/LER-1999-010, Forwards LER 99-010-00,providing Details of Inadequate Pumping Capacity in Dry Cooling Tower Area.All Commitments Contained in Submittal Are Identified on Attached Commitment Identification Voluntary Enhancement Form1999-08-26026 August 1999 Forwards LER 99-010-00,providing Details of Inadequate Pumping Capacity in Dry Cooling Tower Area.All Commitments Contained in Submittal Are Identified on Attached Commitment Identification Voluntary Enhancement Form 05000382/LER-1999-009, Forwards LER 99-009-00 Re Discovery of Condition of Noncompliance with App R Involving Inadequate Separation of Essential Cables Routed in Fire Area RAB-30 in Rab. Compensatory Measures Were Established Immediately1999-08-26026 August 1999 Forwards LER 99-009-00 Re Discovery of Condition of Noncompliance with App R Involving Inadequate Separation of Essential Cables Routed in Fire Area RAB-30 in Rab. Compensatory Measures Were Established Immediately ML20211F3561999-08-24024 August 1999 Forwards CTS Pages & TS Proposed marked-up Pages for Insertion Into TS Change Request NPF-38-207 Re Efas, Originally Submitted on 980702.Original NSHC Determination Continues to Be Applicable ML20211F5421999-08-24024 August 1999 Forwards Proposed marked-up TS Page Xviii, Index Administrative Controls, Correcting Page Number Re TS Change Request NPF-38-220.Editorial Changes for TS Change NPF-38-221 Discussed ML20211C5101999-08-19019 August 1999 Forwards Certified Copies of Liability Insurance Policy Endorsements Issued in First Half of 1999 for Each Entergy Operations,Inc Nuclear Unit,Per 10CFR140.15 ML20210Q6161999-08-12012 August 1999 Forwards Corrected Copy of Monthly Operating Rept for July 1999 for Waterford 3.Original Rept,Submitted with ,Contained Typos ML20210S0561999-08-12012 August 1999 Submits Voluntary Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for NRC Fys 2000 & 2001 for Waterford 3 ML20217F2661999-08-12012 August 1999 Forwards Copy of 1999 Waterford 3 Biennial Exercise Package to Be Performed Using Waterford 3 CR Simulator 05000382/LER-1999-008, Forwards LER 99-008-00,re Failure to Perform Testing of ESF Filtration Units Per TS Srs.Commitments Made by Util Also Encl1999-07-29029 July 1999 Forwards LER 99-008-00,re Failure to Perform Testing of ESF Filtration Units Per TS Srs.Commitments Made by Util Also Encl ML20210H4291999-07-29029 July 1999 Forwards Response to NRC Rai,Associated with TS Change Request NPF-38-208,proposing to Replace Ref to Supplement 1 with Ref to Supplement 2 of Calculative Methods for CE Small Break LOCA Evaluation Model, in ACs Section of TSs ML20210F9451999-07-27027 July 1999 Forwards Proprietary & non-proprietary Version of Rev 29 to EPIP EP-002-100, Technical Support Ctr Activation,Operation & Deactivation. Proprietary Info Withheld,Per 10CFR2.790 ML20210D3171999-07-23023 July 1999 Submits Proposal for Final Resolution of Reracking Spent Fuel Pool at Plant,Per License Amend 144,issued by NRC in .No New Commitments Are Contained in Ltr 05000382/LER-1999-007, Forwards LER 99-007-00,providing Details of Operation Outside Tornado Missile Protection Licensing Basis for turbine-driven Emergency Feedwater Pump Exhaust Stack & Steam Supply Piping.All Commitments Identified on Attached1999-07-23023 July 1999 Forwards LER 99-007-00,providing Details of Operation Outside Tornado Missile Protection Licensing Basis for turbine-driven Emergency Feedwater Pump Exhaust Stack & Steam Supply Piping.All Commitments Identified on Attached ML20209G9771999-07-13013 July 1999 Forwards Objectives & Guidelines for Waterford 3 Emergency Preparedness Exercise Scheduled for 991013.List of Objectives cross-referenced Where Applicable to Relevant Sections of NUREG-0654 ML20209D4051999-07-0707 July 1999 Forwards Revised TS Pages to Replace Attachment C,Entirely in Original TS Change Request NPF-38-207,per 990519 Discussion with C Patel of Nrc.Changes to Action 20 Delete Word Requirement & Revise Word Modes to Mode ML20209B6081999-06-30030 June 1999 Submits Response to NRC GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants. Disclosure Encl 05000382/LER-1999-005, Forwards LER 99-005-00,providing Details of Discovery of Untested Electrical Contacts in safety-related Logic Circuits1999-06-24024 June 1999 Forwards LER 99-005-00,providing Details of Discovery of Untested Electrical Contacts in safety-related Logic Circuits ML20196G5731999-06-24024 June 1999 Forwards Operator Licensing Exam Outlines Associated with Exam Scheduled for Wk of 991004.Exam Development Is Being Performed in Accordance with NUREG-1021,Rev 8 ML20212J4121999-06-23023 June 1999 Responds to NRC Re Reconsideration of EA 98-022. Details Provided on Actions Util Has Taken or Plans to Take to Address NRC Concerns with Ability to Demonstrate Adequate Flow Availability to Meet Design Requirements ML20196E9371999-06-22022 June 1999 Forwards Revs Made to EP Training Procedures.Procedures NTC-217 & NTC-217 Have Been Deleted.Procedure NTP-203 Was Revised to Combine Requirement Previously Included in Procedures NRC-216 & NTC-217 ML20196A1021999-06-17017 June 1999 Provides Supplemental Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, Per 990513 Request of NRC Project Manager ML20195F3671999-06-0909 June 1999 Forwards Rev 21,Change 0 to EP-001-010, Unusual Event. Rev Reviewed in Accordance with 10CFR50.54(q) Requirements & Determined Not to Decrease Effectiveness of Emergency Plan ML20195C7801999-06-0303 June 1999 Submits Response to Violations Noted in Insp Rept 50-382/99-08.Corrective Actions:All Licensee Access Authorization Personnel Were Retrained Prior to Completion of Insp ML20195C2951999-05-28028 May 1999 Forwards Annual Evaluation of Changes & Errors Identified in Abb CE ECCS Performance Evaluation Models Used for LOCA Analyses.Results of Annual Evaluation for CY98 Detailed in Attached Rept,Based Upon Suppl 10 to Abb CE Rept ML20195C0241999-05-28028 May 1999 Notifies NRC of Operator Medical Condition for Waterford 3 Opertaor Sp Wolfe,License SOP-43723.Attached NRC Form & Memo Contain Info Concerning Condition.Without Encls ML20196L3281999-05-24024 May 1999 Informs That Entergy Is Withdrawing TS Change Request NPF-38-205 Re TS 3.3.3.7.1, Chlorine Detection Sys & TS 3.3.3.7.3, Broad Range Gas Detection Submitted on 980629 ML20206S4691999-05-17017 May 1999 Requests Waiver of Exam for SRO Licenses for an Vest & Hj Lewis,Iaw 10CFR55.47.Both Individuals Have Held Licenses at Plant within Past Two Year Period,But Licenses Expired Upon Leaving Util Employment.Encl Withheld 05000382/LER-1999-004, Forwards LER 99-004-00 Re Discovery That Response Time Testing Had Not Been Performed for ESFAS Containment Cooling Function,As Required by TS SR 4.3.2.31999-05-14014 May 1999 Forwards LER 99-004-00 Re Discovery That Response Time Testing Had Not Been Performed for ESFAS Containment Cooling Function,As Required by TS SR 4.3.2.3 ML20206N1921999-05-10010 May 1999 Provides Revised Attachment 2 for Alternative Request IWE-02,originally Submitted 990429 Re Bolt Torque or Tension Testing of Class Mc pressure-retaining Bolting as Specified in Item 8.20 of Article IWE-2500,Table IWE-2500-1 ML20206J1471999-05-0606 May 1999 Requests That Implementation Date for TS Change Request NPF-38-211 Be within 90 Days of Approval to Allow for Installation of New Monitoring Sys for Broad Range Gas Detection Sys ML20206J1721999-05-0606 May 1999 Notifies That Proposed Schedule for Plant 1999 Annual Exercise Is Wk of 991013.Exercise Objective Meeting Scheduled for 990513 at St John Baptist Parish Emergency Operations Ctr ML20206G8021999-05-0404 May 1999 Provides Revised Response to NRC Re Violations Noted in Insp Rept 50-382/99-01.Licensee Denies Violation as Stated.Change Made Is Denoted by Rev Bar & Does Not Materially Impact Original Ltr ML20206E7811999-04-29029 April 1999 Proposes Alternatives to Requirements of ASME B&PV Code Section XI,1992 Edition,1992 Addenda,As Listed.Approval of Alternative Request on or Before 990915,requested ML20205T2531999-04-22022 April 1999 Forwards LER 99-S02-00,describing Occurrence of Contract Employee Inappropriately Being Granted Unescorted Access to Plant Protected Area ML20205R2611999-04-20020 April 1999 Forwards Rev 19 to Physical Security Plan,Submitted in Accordance with 10CFR50.54(p).Plan Rev Was Approved & Implemented on 990407.Rev Withheld,Per 10CFR73.21 ML20205Q3241999-04-16016 April 1999 Submits Addl Info Re TS Change Request NPF-38-215 for Administrative Controls TS Changes.Appropriate Pages from New Entergy Common QA Program Manual Provided as Attachment to Ltr 1999-09-07
[Table view] Category:UTILITY TO NRC
MONTHYEARW3P90-1505, Forwards Proposed Operator Licensing Exam Schedule & Proposed Requalification Exam Schedule,Per Generic Ltr 90-071990-09-17017 September 1990 Forwards Proposed Operator Licensing Exam Schedule & Proposed Requalification Exam Schedule,Per Generic Ltr 90-07 W3P90-1163, Forwards Relief Requests Associated w/10-yr Inservice Insp Program Per Section 50.55a(g)(6)(i) of 10CFR501990-09-0606 September 1990 Forwards Relief Requests Associated w/10-yr Inservice Insp Program Per Section 50.55a(g)(6)(i) of 10CFR50 W3P90-1191, Responds to Violations Noted in Insp Rept 50-382/90-15. Corrective Actions:Tech Spec Surveillance Procedure PE-005-004 Will Be Revised to Ensure That Normally Closed Valves Opened & Verified to Close for Toxic Gas Signal1990-08-31031 August 1990 Responds to Violations Noted in Insp Rept 50-382/90-15. Corrective Actions:Tech Spec Surveillance Procedure PE-005-004 Will Be Revised to Ensure That Normally Closed Valves Opened & Verified to Close for Toxic Gas Signal W3P90-1194, Submits Fitness for Duty Performance Data for 6-month Period from Jan-June 19901990-08-29029 August 1990 Submits Fitness for Duty Performance Data for 6-month Period from Jan-June 1990 W3P90-1184, Responds to Violations Noted in Insp Rept 50-382/90-14. Corrective Actions:Local Leak Rate Test Activities Shall Be Administratively Controlled to Require Use of Test Method Other than Pressure Decay1990-08-20020 August 1990 Responds to Violations Noted in Insp Rept 50-382/90-14. Corrective Actions:Local Leak Rate Test Activities Shall Be Administratively Controlled to Require Use of Test Method Other than Pressure Decay W3P90-1187, Forwards Booklet Entitled, Safety Info - Plans to Help You During Emergencies, Recently Distributed to General Public1990-08-17017 August 1990 Forwards Booklet Entitled, Safety Info - Plans to Help You During Emergencies, Recently Distributed to General Public W3P90-1189, Forwards Waterford 3 Steam Electric Station Emergency Preparedness Exercise for 901024. Annual Exercise Will Be Performed Using Control Room Simulator1990-08-17017 August 1990 Forwards Waterford 3 Steam Electric Station Emergency Preparedness Exercise for 901024. Annual Exercise Will Be Performed Using Control Room Simulator W3P90-1162, Forwards Rev 4 to 10-Yr Inservice Insp Program First Interval 1985-19951990-08-16016 August 1990 Forwards Rev 4 to 10-Yr Inservice Insp Program First Interval 1985-1995 W3P90-1174, Forwards Rev to Emergency Plan & QA Program,Consisting of Chart Indicating Changes to Util Organization1990-08-0707 August 1990 Forwards Rev to Emergency Plan & QA Program,Consisting of Chart Indicating Changes to Util Organization W3P90-1177, Forwards Revised Objectives for Emergency Preparedness Exercise Scheduled for 9010241990-08-0303 August 1990 Forwards Revised Objectives for Emergency Preparedness Exercise Scheduled for 901024 W3P90-1164, Forwards Waterford Steam Electric Station Unit 3 Basemat Monitoring Program Special Rept 3. Rept Documents Continued Integrity of Basemat as Verified by Program from Time of Inception of Monitoring in 1985 Through Mar 19901990-08-0303 August 1990 Forwards Waterford Steam Electric Station Unit 3 Basemat Monitoring Program Special Rept 3. Rept Documents Continued Integrity of Basemat as Verified by Program from Time of Inception of Monitoring in 1985 Through Mar 1990 W3P90-1167, Forwards Rev 12 to Emergency Plan Implementing Instruction EP-001-001, Recognition & Classification of Emergency Conditions, Reflecting Name Change of State Agency to Louisiana Radiation Protection Div1990-07-19019 July 1990 Forwards Rev 12 to Emergency Plan Implementing Instruction EP-001-001, Recognition & Classification of Emergency Conditions, Reflecting Name Change of State Agency to Louisiana Radiation Protection Div W3P90-1148, Responds to NRC 900503 Submittal Concerning Review of Util Rev 6,Change 1 to Inservice Testing Program for Pumps & Valves1990-07-17017 July 1990 Responds to NRC 900503 Submittal Concerning Review of Util Rev 6,Change 1 to Inservice Testing Program for Pumps & Valves W3P90-1143, Advises That 900404 Request for Addl Info Re Tech Spec Change Request NPF-38-103 Will Be Provided by 900803.Change Will Extend Test Frequency of Channel Functional Tests for ESF Actuation Sys & Reactor Protection Sys Instrumentation1990-07-0606 July 1990 Advises That 900404 Request for Addl Info Re Tech Spec Change Request NPF-38-103 Will Be Provided by 900803.Change Will Extend Test Frequency of Channel Functional Tests for ESF Actuation Sys & Reactor Protection Sys Instrumentation W3P90-1379, Provides Notification That Util Has Consolidated Operation of All Nuclear Facilities,Effective 9006061990-07-0202 July 1990 Provides Notification That Util Has Consolidated Operation of All Nuclear Facilities,Effective 900606 ML20044A5541990-06-26026 June 1990 Forwards Response to Generic Ltr 90-04 Requesting Info on Status of Licensee Implementation of Generic Safety Issues Resolved W/Imposition of Requirements or Corrective Actions ML20044A5551990-06-22022 June 1990 Describes Changes Required to Emergency Plan as Result of Transfer of Operations to Entergy Operations,Inc. Administrative Changes to Plan Necessary to Distinguish Support Functions to Be Retained by Louisiana Power & Light W3P90-1365, Provides Notification of Change in Operator Status Per 10CFR50.74 Due to Entergy Corp Consolidating Operation of All Nuclear Generating Facilities,Including Plant Under Util1990-06-19019 June 1990 Provides Notification of Change in Operator Status Per 10CFR50.74 Due to Entergy Corp Consolidating Operation of All Nuclear Generating Facilities,Including Plant Under Util ML20043G3431990-06-14014 June 1990 Requests That All NRC Correspondence Re Plant Be Addressed to RP Barkhurst at Address Indicated in 900523 Ltr ML20043F5121990-06-0808 June 1990 Forwards List of Directors & Officers of Entergy Operations, Inc.Operation of All Plants Transferred to Entergy on 900606 ML20043F2621990-06-0606 June 1990 Requests Withdrawal of 900504 Request to Extend Implementation Date of Amend 60 Re Transfer of Operations to Entergy,Inc.All Necessary Regulatory Approvals Obtained & License Conditions Implemented ML20043C1861990-05-29029 May 1990 Submits Response to 900426 Comments Re Investigation Case 4-88-020.Util Issued P.O. Rev Downgrading Order of Circuit Breakers & Eliminating Nuclear Requirements ML20043E5441990-05-24024 May 1990 Forwards Public Version of Change 1 to Rev 2 to EPIP EP-002-015, Emergency Responder Activation. Release Memo Encl ML20043B3501990-05-23023 May 1990 Forwards Response to Concerns Noted in Insp Rept 50-382/90-02.Response Withheld ML20043B3781990-05-23023 May 1990 Requests Change in NRC Correspondence Distribution List, Deleting Rt Lally & Adding DC Hintz,Gw Muench & RB Mcgehee. All Ref to Util Changed to Entergy Operations,Inc.Proposed NRC Correspondence Distribution List Encl W3P90-1314, Requests NRC Concurrence That Design/Controls/Testing to Minimize Potential for Common Header Blockage Acceptable Per 900510 Meeting.Tap Alternatives for Shutdown Cooling Level Indication Sys Discussed1990-05-21021 May 1990 Requests NRC Concurrence That Design/Controls/Testing to Minimize Potential for Common Header Blockage Acceptable Per 900510 Meeting.Tap Alternatives for Shutdown Cooling Level Indication Sys Discussed ML20043B3271990-05-21021 May 1990 Forwards Justification for Continued Operation Re Taped Splice for Use in Instrument Circuits,Per 900517 Request ML20042F5251990-05-0404 May 1990 Requests Extension of 90 Days to Implement Amend 60 to License NPF-38 in Order to Provide Securities & Exchange Commission Time to Review Transfer of Licensed Activities to Entergy Operations,Inc ML20042E5501990-04-17017 April 1990 Responds to Request for Addl Info Re Feedwater Isolation Valve Bases Change Request Dtd 891006 ML20012F4551990-04-10010 April 1990 Forwards Rev 10,Change 4 to Physical Security Plan.Encl Withheld ML20012F5491990-04-0606 April 1990 Advises That Util Installed Two Addl Benchmarks for Use as Part of Basemat Surveillance Program to Increase Efficiency of Survey Readings.New Benchmarks Will Be Shown on FSAR Figure 1.2.1 as Part of Next FSAR Rev ML20012F3181990-04-0606 April 1990 Forwards Util,New Orleans Public Svc,Inc & Entergy Corp 1989 Annual Repts ML20012E8971990-03-30030 March 1990 Submits Results of Evaluation of Util 900414 Response to Station Blackout Rule (10CFR50.63).Station Mod May Be Required to Change Starting Air Sys to Accomodate Compressed Bottled Air ML20012E2551990-03-27027 March 1990 Responds to Violation Noted in Insp Rept 50-382/90-01. Corrective Actions:Qa Review of Licensed Operator Medical Exam Records Conducted & Sys Implemented to Track Types & Due Dates of Medical Exams Required for Operators ML20012E0511990-03-27027 March 1990 Forwards Rev 10,Change 3 to Physical Security Plan.Rev Withheld ML20012D5461990-03-22022 March 1990 Forwards Documentation from Nuclear Mutual Ltd,Nelia & Nuclear Electric Insurance Ltd Certifying Present Onsite Property Damage Insurance ML20012D4911990-03-21021 March 1990 Responds to NRC 900208 Ltr Re Violations Noted in Investigation Rept 4-89-002.Corrective Action:Proper Sequence of Insp Hold Point Placed in Procedure Under Change Implemented on 880425 ML20012C0691990-03-14014 March 1990 Advises That Util Intends to Address Steam Generator Overfill Concerns (USI A-47) Utilizing Individual Plant Exam Process,Per Generic Ltr 89-14 ML20012C0421990-03-12012 March 1990 Forwards Questionnaire in Response to Generic Ltr 90-01, Request for Voluntary Participation in NRC Regulatory Impact Survey. Results Not Reflective of Particular Calendar Yr ML20012B6731990-03-0707 March 1990 Responds to NRC Bulletin 88-011,Action 1.a Re Insp of Surge Line to Determine Discernible Distress or Structural Damage & Advises That Neither Surge Line Nor Affiliated Hardware Suffered Any Discernible Distress or Structural Damage ML20006F5321990-02-22022 February 1990 Forwards Payment for Order Imposing Civil Monetary Penalty in Response to Enforcement Action EA-89-069 ML20011F1401990-02-21021 February 1990 Responds to Violations Noted in Insp Rept 50-382/89-41. Corrective Action:Review of Independent Verification Requirements Re Maint Activities Performed ML20006F1731990-02-19019 February 1990 Forwards Corrected Pages 9.2-21 & 9.2-22 of Rev 3 to FSAR, Per 891214 Ltr ML20006E5781990-02-13013 February 1990 Forwards Third Refueling Inservice Insp Summary Rept for Waterford Steam Electric Station Unit 3. ML20006D0571990-02-0202 February 1990 Responds to SALP Rept for Aug 1988 - Oct 1989.Contrary to Info Contained in SALP Rept,Civil Penalty Not Assessed by State of Nv for Radioactive Matl Transport Violations.Issue Resolved W/State of Nv W/O Issuance of Civil Penalty ML20006C1631990-01-30030 January 1990 Requests Extension of Commitment Dates in Response to Violations Noted in Insp Repts 50-382/89-17 & 50-382/89-22 to 900222 & 19,respectively.Violations Covered Use of Duplex Strainers & Missing Seismic Support for Cabinet ML20006C1581990-01-29029 January 1990 Forwards Response to Generic Ltr 89-13 Re safety-related Open Svc Water Sys.Instruments in Place on Component Cooling Water Sys/Auxiliary Component Cooling Water Sys HXs Which Connect to Plant Monitor Computer ML20006C1611990-01-29029 January 1990 Responds to NRC Bulletin 89-003 Re Potential Loss of Required Shutdown Margin During Refueling Operations. Instructions for Determining Acceptable Refueling Boron Concentration Provided in Procedure RF-005-001 ML20006B4121990-01-26026 January 1990 Informs That Photographic Surveys Discontinued,Per Basemat Monitoring Program.Monitoring Program Implementing Procedure Will Be Revised to Reflect Change ML20006A7091990-01-22022 January 1990 Forwards List of Individuals That No Longer Require Reactor Operator Licenses at Plant 1990-09-06
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I l OUISIANA ,42 OctAnONOe srnur MiOO;.E SOU TH POWE R & LiG H T P O DOX 6000
- NEW OnLE ANS LOUISIANA 70174 . (504) 366 2345 UTIUT:ES SYSTE M L. V. MAURIN Vice President Nuclear Operations W3P82-2630 September 9, 1982 3-A1.01.04 3-A20.20 Mr. T. 11. Novak Assistant Director for Licensing U.S. Nuclear Regulatory Commission Washington, D.C. 20555
SUBJECT:
Waterford SES 3 Depressurization and Decay Heat Removal
References:
(1) R. L. Tedesco to L. V. Maurin dated 3/27/82 (2) L. V. Maurin to R. L. Tedesco, W3P82-2309, dated 8/27/82
Dear Mr. Novak:
Reference (1) transmitted questions regarding the rapid depressurization and decay heat removal capability of the Waterford 3 design. By reference (2) we indicated that the questions were being addressed by the CE Owners Group and LP&L would respond by August 15, 1983.
Reference (1) also asked that LP&L provide a justification for safe operation should our response not be complete one month prior to fuel load. Consequently, enclosed please find a justification report entitled "A Review of Depressurization and Decay Heat Removal Capabilities of Waterford 3".
Should you have any questions or comments please let me know.
Sincerely, L. V. Maurin LVM/>UM/pco Enclosure Q[
cc: W. M. Stevenson, E. L. Blake, S. Black 8209130027 820909 PDR A
ADOCK 05000302 PDR
. A REVIEW OF DEPRESSURIZATION AND DECAY HEAT REMOVAL CAPABILITIES OF WATERFORD 3
1.0 INTRODUCTION
The NRC has requested that Louisiana Power and Light (LP&L) provide an evaluation of the rapid depressurization and decay heat removal capabilities of the Waterford 3 design. LP&L is participating with the CE Owners Group (CEOG) in developing responses to the NRC's questions. The NRC has also requested that LP&L provide a justification for safe operation of the plant at full power during the period of this evaluation. This report provides justification for safe full power operation of Waterford 3 based on the following considerations, which are amplified later in this report:
- 1. The Waterford 3 NSSS is coupled with a highly reliable, safety grade Emergency Feedwater System (EFWS). The EFWS design for Waterford 3 exhibits a higher level of reliability than most EFWS designs.
- 2. Waterford 3 is capable of achieving cold shutdown conditions using only safety grade systems, even without offsite power and with an additional single failure.
- 3. The Waterford 3 steam generator design includes many features which will enhance tube integrity, minimizing concerns associated with operating reactors. Additionally, careful attention to the plant water chemistry program will ensure that the magnitude of the impurity ingress into the steam generators is maintained at a low level. Because of the steam generator water chemistry program and design features which minimize steam generator tube corrosion and stress, LP&L considers that steam generator tube degradation should not be a concern during the period the NRC questions are being addressed.
- 4. Even if all auxiliary feedwater supply were somehow lost, heat removal could still be achieved by depressurizing the steam generators to allow the use of the low head condensate pumps.
- 5. Review of probabilistic analyses conducted by the NRC do not show any justification for the addition of Reactor Coolant System (RCS) valves for decay heat removal purposes.
2.0 BACKGROUND
The early CE NSSS designs used Power Operated Relief Valves (PORVs) as nonsafety grade equipment to limit overpressure transients to pressures below the ASME Code safety valve setpoint. This function was intended to reduce challenges to the safety valves, thereby minimizing weepage and avoiding potential leakage following actuation. The PORVs were not intended to prevent a high pressure reactor trip, but rather, were to be used in conjunction with the trip to mitigate the pressure transient.
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l As each of the early plants became operational, the effectiveness of the '
pressurizer spray system to limit pressure transients was demonstrated.
Consequently, CE was unable to substantiate any advantages to opening PORVs during transients to protect the safety valves from leakage. PORVs were also considered to be counterproductive in light of the PORV leakage problems that had been experienced. Furthermore, system analysis has demonstrated the pressure overshoot above the high pressure trip to be so minimal that, when PORV operation was not credited, the safety valves were still not challenged.
, Accordingly, the PORV function during power operation was not considered necessary, and was eliminated from subsequent CE designs.
Recently, a contingency method of core cooling employing once-through flow in the RCS has been advanced as an alternate decay heat removal system. This method would use PORVs in conjunction with the High Pressure Safety Injection (HPSI) pumps and has been referred to as " feed and bleed". In this regard, the Advisory Committee on Reactor Safeguards (ACRS), following its review of CE's System 80, (which is similar to Waterford 3 in this regard) stated:
"In recent years, the availability of reliable shutdown heat removal capability for a wide range of transients has been recognized to be of great importance to safety. The System 80 design does not include capability for rapid, direct depressurization of the primary system or for any method of heat removal immediately after shutdown which does not require use of the steam generators. In the present design, the steam generators must be operated for heat removal after shutdown when the primary system is at high pressure and tempera-ture. This places extra importance on the reliability of the auxiliary feedwater system used in connection with System 80 steam generators and extra requirements on the integrity of the steam generators. The ACRS believes that special attention should be given to these matters in connection with l any plant employing the System 80 design. The Committee also believes that it may be useful to give consideration to the potential for adding valves of a size to facilitate rapid depressurization of the System 80 primary coolant system to allow more direct methods of decay heat removal. The Committee wishes to review this matter further with the cooperation of Combustion Engineering and the NRC Staff."
In meetings with the ACRS and NRC Staff, CE has presented its position and the bases for its design. The NRC has raised a series of concerns regarding this issue and provided a list of questions to CE and applicant utilities. In recognition of the scope of these questions the NRC has requested justification for operation during the period of time the questions are being addressed. The ACRS has agreed with this approach stating that:
"....while this evaluation should be conducted expeditiously its resolution should not now be a condition for operation of
< System 80 plants at full power or of plants having similar features."
2
The CEOG has agreed to sponsor preparation of generic (and some plant specific) responses for affected CE utilities. This submittal provides justification for full power operation of Waterford 3 during the period of time that thcae questions are being addressed.
3.0 EMERGENCY FEEDWATER SYSTEM RELIABILITY The Waterford 3 NSSS design is coupled with a safety grade Emergency Feedwater System which has been subjected to extensive development oy LP&L, CE, and EBASCO. This sytem in conjunction with the safety grade atmospheric dump valves provides an assured method of RCS heat removal.
The EFW system, which is documented in the Waterford 3 FSAR, is a three train system with one train independent of ac power. It is seismic category 1, electrical class IE and designed to ASME code class 2 and
- 3. The EFWS design for Waterford 3 exhibits a higher level of reliability than most other EFWS designs. In its Safety Evaluation Report the NRC concluded that the Waterford 3 design satisfied all applicable Commission requirements. Additionally, the staff review of modifications initiated since the accident at Three Mile Island Unit 2 showed an increase in Waterford's EFWS reliability due to the modifications.
Although no quantitative requirement for expected system availability was explicitly imposed, the Waterford 3 EFWS design reflects the high reliability needed to meet the current SRP criteria of unavailabilities in the range of 10-4 to 10-5 per demand. This conclusion is supported by analyses presented in both the Waterford 3 FSAR and NRC staff analyses referenced on Waterford's Docket No. 50-382 in the "NRC Staff's Answer in Support of Applicant's Motion for Reconsideration of March 18, 1982 Memorandum and Order Raising Sua Sponte Issue", dated April 12, 1982.
In this document the staff concludes "that a feed and bleed capability is not necessary as a back-up system to the Waterford Unit 3 EFWS".
4.0 CAPABILITY TO ACHIEVE COLD SHUTDOWN There are numerous systems available, both within the NSSS design and BOP design for Waterford 3, to perform the various functions necessary to bring the plant to a cold shutdown condition. As a group, these systems provide the operator with the flexibility necessary to cool down and depressurize the plant in a variety of possible situations.
The design meets Branch Technical Position RSB 5-1 as documented in Waterford's Safety Evaluation Report, Supplement 2, pg. 5-1. Some of the more significant features of the Waterford 3 design related to shutdown, cooldown, and depressurization capabilities are discussed below.
Normal Shutdown:
Under the vast majority of situations, the same systems used for power generation will be employed for plant cooldown. In these cases primary coolant is circulated through the RCS using the reactor coolant pumps.
Steam is drawn from the steam generators, bypasses the turbine and is rejected to the main condenser. The main feedwater and condensate systems are used to return the condenser inventory to the steam generators.
RCS heat removal is maintained with the steam generators. RCS pressure is maintained with the pressurizer, using the normal heater and spray control i systems.
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Shutdown with Heat Rejection to Atmosphere:
In the event that the main condenser or associated systems are unavailable, steam may be rejected directly to atmosphere. Either of two safety grade steam generator atmospheric dump valves located upstream of the MSlVs may be operated manually to bleed steam. Makeup water to the steam generator is supplied from either the bbin Feedwater System or the safety grade EFWS.
This system provides sufficient inventory to allow for plant cooldown (i.e.
sensible heat removal) and decay heat removal for a period of time in excess of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Additional makeup from other site sources allows for extended operations.
Natural Circulation:
Central to the accomplishment of the basic safety function of Core Heat Removal is the ability to transport reactor coolant to a heat sink where RCS Heat Removal can be accomplished. Reactor coolant pump forced circulation and heat transfer to the steam generators is the preferred mode of operation for residual heat removal whenever plant temperatures and pressures are above the shutdown cooling system (SDCS) entry conditions. Subcooled natural circulation provides an effective alternate means for controlled core cooling, using the steam generators, for extended periods of time if the reactor coolant pumps are unavailable. Two-phase natural circulation and reflux cooling will also occur to provide adequate core cooling following transients which result in loss of RCS inventory and/or subcooling.
Component elevations of Waterford 3 are such that satisfactory natural circulation for decay heat removal is obtained as a result of density differences between the bottom of the core and the top of the steam generator tube sheet, an elevation head of approximately 25 feet. An additional small contribution to natural circulation flow rate is the density difference obtained as the coolant passes throught the steam generator U-tubes.
Additionally, several systems design features have been incorporated to assure the maintenance of natural circulation flow. A redundant pressurizer heater capacity of 150 KW from each diesel generator is available to maintain system subcooling. A reactor coolant gas vent system is provided to allow the purging of noncondensible gases should they form. Additionally, natural circulation plant performance will be extensively tested during the startup period of San Onofre Unit 2 and Waterford Unit 3.
When in natural circulation, the main pressurizer spray system is unavailable.
The safety grade auxiliary spray from the charging system provides for system depressurization under these conditions. This system has been modified to provide an independent manual bypass. Thermal shock considera-tions are addressed by the use of a thermal sleeve in the spray nozzle. CE recommends use of the auxiliary spray system for primary depressurization whenever the main pressurizer spray system is unavailable.
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In summary, the Waterford 3 design meets Branch Technical Position RSB 5-1,
, " Design Requirements of the Residual Heat Removal System" as described above. Waterford 3 can be brought to SDCS initiation in less than 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />
- using only seismic category I equipment, assuming the most limiting single failure, and with only onsite or only offsite power available.
5.0 STEAM GENERATOR INTEGRITY The 3410 MWt steam generators are of an improved design selected to mitigate or resolve operating problems which have been experienced with U-tube steam generators of the recirculation type. The general arrangement is similar to currently operating 2570 MWt CE systems including a number of design l improvements and retained features to assure improved operational reliability and maintenance of integrity for decay heat removal after reactor shutdown.
! The 3410 MWt steam generator is of the vertical U-tube, natural recirculation, noneconomizer type and is somewhat larger than the earlier 2570 MWt steam generator and contains approximately 9,350 tubes instead of 8,400 tubes.
The design as it affects secondary side hydraulics has been improved to i remove areas of possible localized dryout. This has been accomplished by a number of modifications in the tube bend region:
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- 1. The vertical tube spacer strips have been separated from the diagonal
" bat wing" tube supports.
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- 2. The " bat wing" supports have been lowered to avoid intersecting the tube bends.
- 3. The tube supports in the small radius bend region have been located below the bends.
- 4. The vertical tube spacer strips are now provided with large "punchouts" to
- enhance cross flow freedom.
! 5. The former drilled upper tube support plates have been replaced with
- partial "eggerate" type supports.
i' Thus all tube supports are of the "eggerate" or lattice type to promote j freedom of vertical as well as cross flow.
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The elimination of the drilled upper tube support plates will mitigate the denting problems previously experienced in this region.
! The Inconel 600 mil annealed tubing is specified, controlled and tested in a
! manner to preclude sensitivity to stress corrosion cracking or intergranular j attack. Subsequent CE shop tube fabrication practices utilize carefully controlled and proven techniques to minimize residual tube stress, a contributor to stress corrosion cracking. These include:
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- 1. The bending techniques used are selected to minimize residual tube stresc. CE has historically used a relatively large tube bending radius for the inner tube rows.
- 2. CE uses the explosive technique for placing the tube in contact with the tubesheet for the full tubesheet thickness. This eliminates the tube-to-tubesheet crevice which has caused corrosion problems in this region, such as stress cracking and intergranular attack.
The steam generator design allows for sludge lancing to periodically remove accumulations of solids from the upper tubesheet face. These sludge accumulations have been the site of tube pitting type attack.
CE utilizes a mechanical joint between the primary head divider plate and its juncture with the tubesheet and primary head. This eliminates the possibility of the differential growth and deflection between these members causing tubesheet clad separation and tube damage which has occurred in nonce units.
The 3410 MWt design utilizes large top discharge elbows for the main /
auxiliary feedwater inlet sparger. In addition the drain time of this sparger ring has been increased by a sealing device located between the sparger and the feedwater inlet nozzle. Thus water hammer potential with possibic feed-water line damage is reduced.
The integrity of the steam generator tubing is also protected through the use of strict controls on the steam generator water chemistry. The chemical environment of the steam generator secondary side is monitored and controlled during all phases of plant operations including power operation, startup, shutdown, and maintenance outages.
Steam gcnerator chemistry is maintained through a combination of control of impurities delivered to the steam generator, monitoring and controlling the chemical environment within the steam generator, and removal-of any materials which may be introduced. Through feedtrain features and procedures, including a high integrity condenser, startup recirculation, and chemical addition, the magnitude of impurity ingress into the steam generator is maintained at a low level. In addition, the Waterford 3 design has provisions for prestartup cleanup of the main feedwater system by flushing to the steam generator blowdown system. A chemistry control program is employed to assure that secondary water chemistry is maintained within appropriate control bounds during operation and that timely corrective actions are taken in the event abnormal chemistry occurs. An all volatile treatment water chemistry is utilized for the secondary systems. This method of secondary chemistry control precludes tube corrosion and related problems due to the chemical additives, and it minimizes the amount of sludge deposited within the steam generator. Routine corrective actions for abnormal chemistry include increasing the steam generator blowdown rate, adjustment of chemical addition rates, and more extensive monitoring of steam generator chemistry. For severe upset conditions, power reduction and/or 6
plant shutdown is specified. Continuous sampling of and chemical addition to the steam generator monitors the effectiveness of feedtrain impurity controls and maintains a chemical environment conducive to low corrosion rates within the steam generator. Finally, steam generator blowdown, supplemented by fill and drain when required, serves to remove those impurities which are introduced. By minimizing contaminant ingress, monitoring system performance, and taking corrective action when necessary, chemistry related challenges to the integrity of the steam generator tubes are minimized.
During accident response conditions, water supplied to the steam generator by the Emergency Feedwater System originates in the condensate storage pool.
This makeup quality water is chemically treated and its use will not challenge the steam generator tube integrity. In the quite unlikely event that water must be supplied from alternate sources during the accident (auxiliary Component Cooling Water System) it is not anticipated that even this impure water will cause tube failure in the time frame of the accident and subsequent plant cooldown.
In summary it is considered that the design, material and manufacturing features discussed above, along with appropriate chemistry control, will assure improved steam generator tube integrity. LP&L further considers that steam generator tube degradation should not be a concern during the period the NRC questions are being addressed.
6.0 CONTINGENCY DECAY HEAT REMOVAL (DHR)
The Waterford 3 design meets current licensing criteria with regard to DHR capabilities. The consideration of additional RCS valves for DHR essentially addressed contingency (or "last resort") capabilities that go beyond existing design bases. In this regard it is significant to note that a potential already exists for contingency heat removal by depressurizing the steam generators.
The potential mode of plant operation considered is as follows: Following reactor trip and the very unlikely event of a total loss of all feedwater, the plant could be brought to hot standby using either the secondary safety valves of the atmospheric dunp valves. The safety grade steam generator atmospheric dump valves then provide the contingency capability te blowdown and depressurize the steam generator secondary system. At the reduced steam generator pressure the low head condensate pumps could be aligned to deliver feed to the steam generator. Then, with sufficient feedwater and steam flow, continuous decay heat removal could be established at those "off design" conditions.
There appear to be several advantages to steam generator depressurization in preference to primary feed and bleed. These are:
- 1. The reactor coolant pressure boundary is maintained intact.
Therefore the potential radiological release to the containment and possibly to the environment is avoided. Any necessary containment entry 7
for repairs would not be impeded. Additionally the large clean-up cost that would be associated with the use of primary feed and bleed is avoided.
- 2. There is time available for operator action.
Delivery of secondary makeup to a depressurized steam generator can be accomplished anytime prior to core uncovery, which is estimated to be approximately 90 minutes, to ensure adequate core cooling.
- 3. Equipment involved is accessible.
The atmospheric dump valves and various low head pumps are located outside containment where access for maintenance and repair is possible.
PORVs on the other hand would be inside containment and virtually inaccessible.
- 4. Procedures are consistent with normal DHR procedures.
Normal procedural efforts focus upon restoration of feedwater.
Initiation of primary feed and bleed would represent a dramatic departure from this strategy.
The final reason noted above is worthy of elaboration in that it was strongly supported by plant operators during procedure workshops conducted at CE.
Plant operators feel that it is highly preferable to continue operation with the steam generators performing the function of RCS Heat Removal, while the functions of RCS Inventory and Pressure Control are being controlled separately. With the initiation of RCS feed and bleed all three safety functions would now rely on a single process with no degree of independent control. The extreme difficulty in dealing with the competing demands of RCS Heat Removal, Pressure and Inventory Control by regulating a single process has been clearly demonstrated at TMI-2 and Ginna.
7.0 PROBABILISTIC JUSTIFICATION (REVIEW OF DRAFT PRA)
The January 29, 1982 memorandum from F. Rowsome and J. Murphy entitled
" Feed and Bleed Issue for CE Applicants" included a draft PRA by the NRC Division of Risk Analysis (DRA) attempting to demonstrate that the CE plants which lack a capability for core cooling via feed and bleed operation will not meet the NRC's proposed plant performance guidelines. This guideline is that "the likelihood of a nuclear reactor accident that results in a large-scale core melt should normally be less than one in 10,000 per year of reactor operation". Additionally, the DRA study made a case for incorporating feed and bleed capability to partially alleviate the perceived problea, and presented analysis to show that such a change is cost beneficial to the utilities.
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Review of the draf t PRA (which has since been characterized as " overstated" by the author) indicates that the recommendations are not well supported by the analyses. This is most succinctly presented in the Staff's " Affidavit of Richard Lobel, Brian Sheron and Ashok Thadani Concerning Feed and Bleed and Emergency Feedwater System Reliability" filed with the Waterford Licensing Board on April 12, 1982:
"The probability of complete losses of the EFWS in the Rowsome and Murphy memorandum was based on past operating experience as reported in an ORNL report (CR-2497). The staff is aware of ten events in which there was a loss of all emergency feedwater (two more events than are listed in ORNL report CR-2497). An analysis of this past experience as it relates to the Waterford Unit 3 EFWS design results in the following conclusions.
First, post-TMI recommendations should greatly lower the probabil-ity of occurrence for several of these events. For example, in several events, the EFWS pumps did not start on the automatic initiation signal; safety-related EFWS flow indication must now be provided, and an indicator such as that available at Waterford Unit 3 would alert the operator immediately that the EFWS was inoperable so that he could initiate a timely manual actuation.
In addition, human error resulting in a closure of valves in the pump discharge path, such as occurred during the TMI-2 accident, should be less probable now as a result of the required increased surveillance of the EFWS flow path after system testing or extended shutdown.
" Secondly, some of these events were recoverable in less time than the time calculated for loss of the secondary heat sink (i.e. steam generator dryout time). The Waterford Unit 3 steam generators have a relatively large water inventory, which provides the operator with a greater period of time to attempt a manual start in the event that the system does not start automatically.
A human error resulting in a closure of valves in the pump discharge path, such as occurred during the TMI-2 accident, should have a high probability of being correctcd in the Waterford Unit 3 design before the heat sink is lost.
" Thirdly, some of these events involved a type of failure that could not occur in an EFWS of the Waterford Unit 3 design. For example, several of these events resulted from clogged strainers in the EFWS piping; the strainers will be removed from the Water-ford Unit 3 EFWS after startup testing. In addition, one of these events resulted from the interference of a reactor control system with the function of the EFWS. This event was peculiar to reactors designed by Babcock & Wilcox and the problem was fixed following the Crystal River Unit 3 event of February 1980; accordingly, it is not applicable to the Waterford Unit 3 design.
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4 "In conclusion, the Staff's reanalysis cf these data, taking into 1 account (1) the post-TM1 modifications and corrective actions, (2) the high probability of recovery of some of these events, (3) the limited applicability of some of these events to the Waterford Unit 3 EFWS design leads the Staff to conclude that the Waterford Unit 3 EFWS is subject to a demand failure probability of less than 10-4 per demand."
i Based on the above comments it is considered that if a corrected analysis was to be performed there would be no apparent justification for plant modifica-
- tion.
8.3 CONCLUSION
S As requested, a review of the Waterford 3 design has been completed and the following determined:
- 1. The Waterford 3 NSSS is coupled with a highly reliable emergency
. feedwater system, with an unavailability in the range of 10-4 to 10-5 l per demand.
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- 2. Waterford 3 is capable of achieving cold shutdown conditions using only safety grade systems, even without offsite power and with an added single failure, i 3. The Waterford 3 steam generator water chemistry program and design
! features will minimize steam generator tube corrosion and stress.
} Additionally, LP&L considers that steam generator tube degradation should not be a concern during the period the NRC questions are being addressed.
, 4. Even if all auxiliary feedwater supply were somehow lost, the potential exists for DHR by depressurizing the steam generators to allow use of l
low head pumps.
- 5. Contrary to the draft probability analysis developed by DRA, there is
! no reason to believe that installing PORVs will result in a significant I
improvement in safety.
Baned upon the considerations listed above, it is concluded that the
- current Waterford 3 design provides adequate protection for the health and l safety of the public and full power operation is fully justified while j responses are being prepared to the NRC request for additional information j associated with the rapid depressurization and decay heat removal capabilities for Waterford 3.
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