Letter Sequence Other |
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Results
Other: 05000267/LER-1986-020, :on 860711,determined That FSAR Analyses for Safe Shutdown Cooling Following 90-minute Loss of Forced Cooling May Be Invalid.Caused by Design Omission.Three Options Presently Being Investigated, 05000267/LER-1986-026, :on 860917,FSAR Analysis for Safe Shutdown Cooling W/Firewater Invalid.Caused by Incomplete Analysis/ Inadequate Review.Review & Reanalysis Will Be Performed on Various Accidents Described in FSAR, ML19306G340, ML20137H372, ML20197B076, ML20204G924, ML20205T170, ML20206B329, ML20206B459, ML20206F887, ML20207K386, ML20207K441, ML20207K446, ML20207K506, ML20207K512, ML20207P779, ML20207P991, ML20207P993, ML20209E329, ML20209F187, ML20209G043, ML20210A740, ML20210A748, ML20210A757, ML20210T436, ML20210T655, ML20210T686, ML20211D992, ML20211E058, ML20211E084, ML20211E110, ML20211G583, ML20211N368, ML20214Q988, ML20214Q998, ML20214S836, ML20215H964, ML20215H973, ML20215J855, ML20215J871, ML20234C109, ML20235E520, ML20235F508, ML20245C018
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MONTHYEARML20137H3721985-11-26026 November 1985 Memorandum & Order Granting Extension of 851130 Deadline for Environ Qualification of Electrical Equipment to 860531 & Approving Proposal to Allow Operation w/35% Reactor Power Limit During Interim.Served on 851127 Project stage: Other ML20211E0841986-02-20020 February 1986 Issue a to Fort St Vrain:Delayed Firewater Cooldown;Effect of Liner Cooling on Orifice Valve Temps Project stage: Other ML20209F1871986-03-18018 March 1986 Fort St Vrain Steam Generator Temps During Interruption of Forced Cooling from 105% Power Project stage: Other 05000267/LER-1986-020, :on 860711,determined That FSAR Analyses for Safe Shutdown Cooling Following 90-minute Loss of Forced Cooling May Be Invalid.Caused by Design Omission.Three Options Presently Being Investigated1986-08-10010 August 1986
- on 860711,determined That FSAR Analyses for Safe Shutdown Cooling Following 90-minute Loss of Forced Cooling May Be Invalid.Caused by Design Omission.Three Options Presently Being Investigated
Project stage: Other ML20211E0581986-09-30030 September 1986 Effect of Delayed Firewater Cooldown W/Loss of Liner Cooling on Pcrv Temps Project stage: Other 05000267/LER-1986-026, :on 860917,FSAR Analysis for Safe Shutdown Cooling W/Firewater Invalid.Caused by Incomplete Analysis/ Inadequate Review.Review & Reanalysis Will Be Performed on Various Accidents Described in FSAR1986-10-17017 October 1986
- on 860917,FSAR Analysis for Safe Shutdown Cooling W/Firewater Invalid.Caused by Incomplete Analysis/ Inadequate Review.Review & Reanalysis Will Be Performed on Various Accidents Described in FSAR
Project stage: Other ML20211G5831986-10-22022 October 1986 Anticipates Completion of Steam Generator Analysis & App R Modeling Reanalysis Work by Feb 1987,per 860918 Telcon W/Nrc Re Steam Generator Cool Down Studies for App R Project stage: Other ML20197B0761986-10-22022 October 1986 Informs That Util Will Update & Submit Rept on Chernobyl Accident by 861126.Update Will Ctr on Graphite Related Concerns,Including Analysis of Worst Case Explosive Gas Mixtures & Comparison of Reactor Kinetics Behavior Project stage: Other ML20207K5121986-11-13013 November 1986 Fort St Vrain Calculations for Circulator Temp-Related Operating Limits Project stage: Other ML20207K5011986-12-0404 December 1986 Effect of Firewater Cooldown Using Economizer-Evaporator- Superheater (EES) Bundle on Steam Generator Structural Integrity. Draft Rept of Steam Generator Ability to Withstand post-App R Firewater Cooldown Transient Encl Project stage: Draft Other ML20207K4461986-12-12012 December 1986 Issue a to Effect of Firewater Cooldown Using Reheater on Steam Generator Structural Integrity Project stage: Other ML20211N3681986-12-12012 December 1986 Forwards Restart Interaction Schedule,Per 861205 Request Project stage: Other ML20207K5061986-12-22022 December 1986 Issue a to Effect of Intentional Depressurization on Cooldown from 39% Power Using One Reheater Module (1-1/2 H Delay) Project stage: Other ML20207K4411986-12-23023 December 1986 Issue a to Economizer-Evaporator-Superheater (EES) Cooldown from 39% & 78% Power Using Condensate or Firewater (1.5 H Delay) Project stage: Other ML20207K3861986-12-30030 December 1986 Forwards Analyses Supporting Power Operation Up to 39% Power Based on Safe Shutdown Cooling Following 90 Min Interruption of Forced Circulation.Conclusions of Repts Listed.Corrective Actions for LERs 86-020 & 86-026 Also Listed Project stage: Other ML20207P7791987-01-0707 January 1987 Forwards Current Integrated Schedule for Restart & Power Ascension Activities.Schedule Incorporates Consolidated Schedular Info on Both Interaction Activities.Updates Will Be Provided Twice Per Month.W/One Oversize Graph Project stage: Other ML20207P9931987-01-13013 January 1987 SAR for Tech Spec Limiting Condition for Operation 4.3.1 Change Permitting Safe Shutdown Cooling W/Evaporator- Economizer-Superheater Project stage: Other ML20207P9871987-01-15015 January 1987 Forwards Application for Amend to License DPR-34,changing Tech Specs to Require Both evaporator-economizer Superheater Sections & Both Reheater Sections to Be Available During Operation at Power.Fee Paid Project stage: Request ML20207P9911987-01-15015 January 1987 Proposed Tech Specs,Requiring Both evaporator-economizer Superheater Sections & Both Reheater Sections to Be Available During Operation at Power as Min Number of HXs Project stage: Other ML20207P9891987-01-15015 January 1987 Application for Amend to License DPR-34,requiring Both evaporator-economizer Superheater Sections & Both Reheater Sections to Be Available During Operation at Power as Min Number of Operable HXs Project stage: Request ML20211E1101987-01-26026 January 1987 Rev a to Engineering Evaluation of Procedure to Recover from Actuation of Steam Line Rupture Detection/Isolation Sys for Power Levels Through P2 Project stage: Other ML20210A7571987-01-30030 January 1987 Fort St Vrain 1987 Power Ascension Plan Project stage: Other ML20210A7481987-01-30030 January 1987 Requests Concurrence to Start Up & Operate Facility Through Graduated Rise to Power Up to 100% of Rated Power,Subj to Listed Constraints. Fort St Vrain 1987 Power Ascension Plan Encl Project stage: Other IR 05000267/19870021987-01-30030 January 1987 Partially Withheld Insp Rept 50-267/87-02 on 870106-09 (Ref 10CFR73.21).No Violations or Deviations Noted.Major Areas Inspected:Matl Control & Accounting Project stage: Request ML20210A7401987-02-0202 February 1987 Forwards Updated Nrc/Public Svc Co of Colorado Restart Interaction Schedule, Reflecting Current Target Dates & Recently Completed Items Project stage: Other ML20209G0431987-02-0202 February 1987 Forwards Current Integrated Schedule for Plant Restart & Power Ascension Activities.W/One Oversize Encl Project stage: Other ML20210N8831987-02-0303 February 1987 Forwards Request for Addl Info on 861230 & 870115 Submittals Re Analysis of Firewater Cooldown from 82% of Full Power Project stage: RAI ML20210P0191987-02-0505 February 1987 Summary of 870113 Meeting W/Util Re Completion of Equipment Qualification Program & Program & Approvals Required for Plant Restart Project stage: Meeting ML20210T6861987-02-0505 February 1987 Rev a to Engineering Evaluation of Reanalysis of FSAR Accidents/Transients Relying on EES Cooling. W/Four Oversize Drawings Project stage: Other ML20211D9921987-02-0505 February 1987 Issue a to Economizer-Evaporator-Superheater Cooldowns for Equipment Qualification & App R Events W/Vent Lines (1.5 H Delay) Project stage: Other ML20210T6551987-02-0606 February 1987 Provides Results of Confirmatory Analyses for FSAR Accidents Which Utilize Either EES or Reheater Section of Steam Generator for DHR Project stage: Other ML20210T4361987-02-11011 February 1987 Requests Publication of Fr Notice of Consideration of Issuance of Amend to License DPR-34 & Proposed NSHC Determination & Opportunity for Hearing on 870115 Request Re Operation of evaporator-economizer-superheater Sections Project stage: Other ML20211E9791987-02-12012 February 1987 Forwards Proposed Agenda & Slides for 870226 Meeting W/ Commission & Staff to Secure Commission Approval for Full Power Operation of Facility Project stage: Meeting ML20211D8901987-02-17017 February 1987 Forwards Response to NRC 870203 Request for Addl Info Re Firewater Cooldown from 82% of Full Power,Per Util 861230 & s Project stage: Request ML20207Q7941987-03-0303 March 1987 Forwards Second Request for Addl Info Re Util Analysis of Firewater Cooldown from 82% of Full Power Operation,Based on Review of 861230,870115 & 0217 Submittals Project stage: Approval ML20204G9241987-03-20020 March 1987 Forwards Restart & Power Ascension Schedule,Incorporating Consolidated Schedular Info on NRC-util Interaction Activities.Brief Narrative Description of Scope of Each Line Item Activity Also Encl.W/One Oversize Encl Project stage: Other ML20205B3441987-03-20020 March 1987 Forwards Response to NRC 870303 Second Request for Addl Info Re Firewater Cooldown from 82% of Full Power (Safe Shutdown Cooling) Project stage: Request ML20205M8901987-03-30030 March 1987 Forwards Third Request for Addl Info Re Util 861230,870115 & 0217 Submittals Concerning Analysis of Firewater Cooldown from 82% of Full Power.Major Concerns Re Effects of Transient Loading Due to Seismic Motion or Flow Project stage: RAI ML20205T1701987-04-0101 April 1987 Forwards Oversize Current Integrated Schedule for Facility Restart & Power Ascension Activities Required for Equipment Qualification Completion Certification,Startup/Plant Criticality & Power Ascension to 82%.Related Info Encl Project stage: Other ML20206B6031987-04-0101 April 1987 Forwards Comments Re Implication of Chernobyl Reactor Accident.Design Differences Between Fort St Vrain & Chernobyl Preclude Accident Similar to Chernobyl from Occurring at Fort St Vrain Project stage: Approval ML20206B4591987-04-0303 April 1987 Forwards Summary of Equipment Qualification (EQ) Insp Conducted by NRR & IE on 870126-30.EQ Program Approved. Detailed Results of Insp Will Be Provided Project stage: Other ML20206B3291987-04-0707 April 1987 Submits Daily Highlight.Public Svc Co of Colorado Authorized to Restart & Operate Facility HTGR at Level of Up to 35% Full Power.Facility Out of Operation Since 860531,when Shut Down for Equipment Qualification Mods Project stage: Other ML20206F8871987-04-10010 April 1987 Submits Requested Addl Info for Analysis of Firewater Cooldown for 82% Power Operation,Per Project stage: Other ML20209E3291987-04-27027 April 1987 Provides Written Authorization to Operate Reactor at Up to 35% Full Power,Per Section IV of 870406 Confirmatory Order Modifying License DPR-34 Project stage: Other ML20215H9641987-04-30030 April 1987 Forwards Updated Ga Technologies Procedure 909410, Buckle Users Manual, Per 870330 Request.Manual Updated to Include Revs to Computer Code Required by High Temps & Short Times Assumed for Steam Generator Tube Stress Analysis Project stage: Other ML20215H9731987-04-30030 April 1987 Revised Buckle Users Manual:Creep Collapse of Thin-Walled Circular Cylindrical Shells Subj to Radial Pressure & Thermal Gradients Project stage: Other ML20215J8711987-05-0404 May 1987 Rev a to Evaluation of Test Data for Confirmation of Fire Water Flow Rate to Circulator Water Turbine During EES Cooldown for Safe Shutdown Cooling Project stage: Other ML20215J8551987-05-0404 May 1987 Forwards Rev a to EE-EQ-0057, Evaluation of Test Data for Confirmation of Fire Water Flow Rate to Circulator Water Turbine During EES Cooldown for Safe Shutdown Cooling Project stage: Other ML20214S8361987-05-27027 May 1987 Requests Insp & Audit Per 10CFR50,App B of Licensee Activities Supporting Request for 82% Power Operation. Requests That Insp Be Conducted & Completed within 180 Days Project stage: Other ML20214Q9881987-05-29029 May 1987 Forwards Rept GA909438,Issue Nc, Verification Rept for Buckle Computer Program. Edition of Buckle Code Covered by User Manual Validated & Independently Verified by Rept Project stage: Other 1987-02-11
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Text
i h Public Service-lch
=_
2420 W. 26th Avenue, Suite 1000, Denver, Colorado 'iO211 R.O. WILUAMS, JR.
Et$Nk"bTioNS January 30, 1987 Fort St. Vrain Unit No. 1 P-87038 U. S. Nuclear Regulatory Commission ATTN:
Document Control Desk Washington, D.C.
20555 Attention: Mr. H. N. Berkow, Director Standardization and Special Projects Directorate Docket No.
50-267
SUBJECT:
Request for Authorization to Operate FSV with Specified Power Restrictions
REFERENCES:
- 1) PSC Letter, Williams to Berkow, dated January 15, 1987 (P-87002)
- 2) PSC Letter, Warembourg to Berkow, dated December 30, 1986 (P-86683)
- 3) PSC Letter, Walker to Berkow, dated December 10, 1985 (P-85460)
- 4) NRC Letter, Denton to Walker, dated February 7, 1986 (G-86062)
Dear Mr. Berkow:
The Public Service Company of Colorado (PSC) hereby requests that the Nuclear Regulatory Commission (NRC) provide concurrence to start up and operate Fort St. Vrain (FSV) through a graduated rise to power up to 100% of rated power, subject to the constraints as delineated in this letter.
Acci I 10 8702090005 870130 PDR ADOCK 0500 7
P
P-87038 Page 2 January 30, 1987 Power Ascension Plan Attached for NRC information and review is a copy of the " Fort St.
Vrain 1987 Power Ascension Plan,"
including a
pictorial representation of plant startup activities as a function of power level.
In brief, upon-receipt of permission from the NRC to restart, and upon completion of pre-critical testing including testing of the Steam Line Rupture Detection / Isolation System (SLRDIS), criticality would be achieved.
Startup and testing activities in the startup range (0-2% power) would then proceed as described in the Power Ascension Plan.
The reactor power would then be raised above 2%
into the Low-Power range to less than 10% reactor power for nuclear dryout, training, testing, and other activities as described in the Power Ascension Plan. Ten percent (10%)
rated reactor power is considered to be an appropriate hold point for assessment of PSC's startup activities by NRC Region IV.
Upon receipt of authorization from NRC Region IV to exceed 10%, PSC would continue to raise the power level in an orderly manner through the Low-Power range into the Power range up to, but not to exceed, 35% of rated reactor power.
As justified below, 35% power is considered to be an appropriate restriction level for FSV operation under provision of the existing Technical Specifications while awaiting NRR approval and issuance of the Technical Specification change proposed by Reference 1.
Upon receipt of NRR approval, PSC would continue in accordance with the Power Ascension Plan up to, but not to exceed, 82% of rated reactor power.
Shutdown cooling has been analyzed to be safe and adequate from power levels above 82% as summarized in the justification below and detailed in References 1 and 2.
The alternatives for supporting a power level above 82% have not been evaluated at this time.
Additional analyses will certainly be required and further plant modification may be required to justify power operation up to 100% power. At the present time, PSC considers the 100% operation goal to be a longer term goal (beyond the next refueling). Therefore, when operation at a power level above 82% is pursued, PSC will provide the NRC with the necessary supporting analysis and justification.
Justification for 35% Power Operation PSC has previously requested permission for interim operation with a 35% power restriction during 1986 (Reference 3).
This previous request conservatively assumed that in the event of an Environmental Qualification Design Basis Event, all electrical equipment exposed to the resulting harsh environment would fail.
Shutdown cooling of the reactor would be accomplished using only electrical equipment located in a mild environment supplying firewater to the PCRV liner cooling system. As a result of this previous request, the NRC authorized interim operation of FSV at 35% of full reactor power through May 31, 1986 (Reference 4).
The NRC's Safety Evaluation Report (Enclosure to Reference 4) found that following a High Energy Line Break (HELB) with the firewater system utilized for cooling the
P-87038 Pag: 3 January 30, 1987 PCRV liner from power levels of 35% or less, a permanent Loss of Forced Circulation (LOFC) accident can be experienced without significant damage to any of the fission product barriers, including the fuel particle coatings. This evaluation also concluded that re-establishing liner cooling in the 35% power case after it had been shut off for a prolonged period of time was acceptable.
(
PSC affirms that there have been no adverse changes to the basic assumptions and analyses transmitted by Reference 4.
The most significant change enhances safety.
It is that two redundant trains of Safe Shutdown equipment necessary for forced circulation Safe Shutdown Cooling will have been environmentally qualified to the requirements of 10CFR50.49.
Two other related improvements will have been implemented before criticality is achieved. One improvement is installation of the Steam Line Rupture Detection / Isolation System (SLRDIS). SLRDIS has the capability to automatically and quickly shut off escaping steam or hot water in the event of a HELB within the Turbine or Reactor Building.
This would result in substantially lower building temperatures than those presented in Reference 3, thus permitting much earlier operator access to the affected building to perform any f
required manual actions. The other beneficial modification pertinent L
to this discussion is the environmental qualification of the helium
~
circulator brake and shaft seal system controls.
This will essentially eliminate primary coolant leakage along the shaft of a stopped circulator following a HELB, resulting in a considerable 3 (which were already extremely low)previously presented in Reference reduction in the radiological doses For the purpose of analysis of the above mentioned permanent LOFC accident, no credit is taken for any of the multiple and redundant methods of removing core decay heat utilizing forced circulation of the helium.
If all forced circulation is arbitrarily assumed to be permanently unavailable, the previously reviewed permanent LOFC accident analysis described above is considered to be bounding for reactor power levels up to 35%. This analysis was approved by the NRC in Reference 4.
For this reason 35% power is considered to be an appropriate rc:triction level for FSV while awaiting NRC's Office of Nuclear Reactor Regulation (NRR) approval and issuance of the Technical Specification change proposed by Reference 1,
PSC completion of the modification to install a new six-inch vent line on each main steam loop header, and finalization of identified EQ related issues.
Justification for 82% Power Operation NRR approval of the Technical Specification change request submitted with Reference 1 will be required prior to exceeding the 35%
restriction level, since the existing Technical Specifications require that at least one reheater section be available to support shutdown heat removal, which includes Safe Shutdown Cooling. As discussed in Reference 1, the reheaters have limited capability to support Safe Shutdown Cooling (i.e. supplied with firewater from one firewater pump after a 1-1/2 hour Interruption of Forced
P-87038
. Pag? 4 January 30, 1987 Circulation). PSC must also complete the plant modification to add a six-inch vent pipe to atmosphere from the outlet of each of the two economizer-evaporator-superheater (EES) sections of the steam generator. These vents (one per loop) provide a discharge path to atmosphere for the.once-through cooling mode (Reference 2) and prevent the redundant EES sections from being incapacitated simultaneously by a postulated HELB located in the common discharge piping. While the six-inch vents are required before exceeding 35%
i
- power, the modification is currently expected to be completed prior to criticality.
As described in References 1 and 2, Safe Shutdown Cooling can be satisfactorily performed with one firewater pump supplying one of the two redundant EES sections after a 1-1/2 hour Interruption of Forced Circulation from reactor power levels up to 87.5%.
Safe Shutdown Cooling utilizes only equipment on the Safe Shutdown list, all of which are seismically qualified to withstand a Design Basis Earthquake (DBE), and where required, are environmentally qualified to withstand a HELB inside the Turbine or Reactor Building.
The analyses performed in regards to fire protection (i.e.,
in conformance to 10CFR50, Appendix R) confirm the adequacy of the
" Appendix R"
shutdown cooling water flow paths from reactor power levels up to 83.2% (Attachment 1 to Reference 2).
Some of the recent concerns regarding the capability of an EES section or a reheater section to adequately support Safe Shutdown Cooling were also raised regarding use of these heat exchangers for cooldown from certain other accidents previously identified in the FSAR.
These other accidents (i.e., other than those that result in Safe Shutdown Cooling) have now been reevaluated to determine the effects of the revised secondary coolant analytical models on the accident consequences. Results of these reanalyses assure that the steam generator heat transfer sections are capable of supporting decay heat removal and do not require power level limitations more restrictive than the 83.2% analyzed in the Appendix R case in to Reference 2.
The results of these reanalyses are being submitted separately to the NRC in the immediate future.
Justification for 100% Power Operation As mentioned above, the alternatives for supporting a power level above 82% have not been evaluated at this time.
Further analyses will certainly be required and additional plant modification may be required to justify power operation up to 100% power. At the present time, PSC considers the 100% operation goal to be a longer term goal (beyond the next refueling). Therefore, when operation at a power level above 82% is pursued, PSC will provide the NRC with the necessary supporting analysis and justification.
PSC Restart Reauest Summary PSC formally requests that NRC grant permission for FSV to be operated at reactor power levels up to 82% of rated power, subject to the 10% hold point and 35% power restriction level as discussed in this letter.
i
P-87038 Page 5 January 30, 1987 PSC hereby comits to an 82% power restriction until such time as NRC Staff approval is secured for operation at a power level above 82%.
PSC understands that the NRC has the option of confirming by order that the 35% power restriction and the 82% power restriction are not to be exceeded without prior NRC approval.
If you have any qtiestions or comments, please call Mr. M. H. Holmes at (303) 480-6960.
Very truly yours, R. O. Williams, Jr.
Vice President, Nuclear Operations R0W/TRM:jmt Attachments cc:
J. E. Gagliardo Region IV, NRC R. E. Farrell NRC Senior Resident Inspector, FSV