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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M6631999-10-19019 October 1999 Forwards Insp Rept 50-277/99-07 & 50-278/99-07 on 990920.No Violations Noted ML20217K9241999-10-14014 October 1999 Forwards Amend 234 to License DPR-56 & Se.Amend Consists of Changes to TS in Response to Application & Suppls ,1001 & 06,which Will Support PBAPS Mod P00507,which Will Install Digital Pr Neutron Mining Sys ML20217F7391999-10-14014 October 1999 Requests Addl Info Re Peach Bottom Atomic Power Station Units 2 & 3 Appendix R Exemption Requests ML20217F6841999-10-13013 October 1999 Forwards Senior Reactor Operator Initial Exam Repts 50-277/99-302(OL) & 50-278/99-302(OL) Conducted on 990913- 16.All Applicants Passed All Portions of Exam ML20217F3021999-10-12012 October 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at PBAPS Have Been Completed.Ltr Also Confirms Completion of Actions Required by Confirmatory Order Modifying Licenses, ML20217E7451999-10-0808 October 1999 Forwards Response to NRC 990820 RAI Concerning Proposed Alternatives Associated with Third ten-yr Interval ISI Program for Pbaps,Units 2 & 3 ML20217B7701999-10-0606 October 1999 Submits Corrected Info to NRC 980528 RAI Re Util Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions ML20217B9151999-10-0606 October 1999 Provides Clarifying Info to Enable NRC to Complete Review of License Change Request ECR 98-01802,re Changes Necessary to Support Installation of Digital Pr Neutron Monitoring & Incorporate long-term T/H Stability Solution Hardware ML20217C4141999-10-0606 October 1999 Forwards Response to NRC 981109 RAI Re Resolution of USI A-46 for Pbaps.Proprietary Excerpts from GIP-2,Ref 25 Results of BWR Trial Plant Review Section 8 Also Encl. Proprietary Excerpts Withheld ML20217B3181999-10-0505 October 1999 Advises That Info Submitted in 990712 Application,Which Contained Attachment Entitled, Addl Info Re Cycle Spec SLMCPR for Peach Bottom 3 Cycle 13,dtd 990609, with Affidavit,Will Be Withheld from Public Disclosure ML20217B4051999-10-0505 October 1999 Forwards Amend 233 to License DPR-56 & Safety Evaluation. Amend Changes Minimum Critical Power Ratio Safety Limit & Approved Methodologies Referenced in Core Operating Limits Report 05000278/LER-1999-004, Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv)1999-10-0101 October 1999 Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv) ML20217B8891999-10-0101 October 1999 Forwards Response to RAI Re Request to Install Digital Power Range Neutron Monitoring Sys & Incorporate long-term,thermal-hydraulic Stability Solution Hardware. Revised TS Table 3.3.2.1-1 Encl ML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20212J6851999-09-29029 September 1999 Informs of Completion of mid-cycle PPR of Peach Bottom Atomic Power Station on 990913.No Areas Identified in Which Licensee Performance Warranted Addl New Insps Beyond Core Insp Program.Historical Listing of Plant Issues Encl ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212J5751999-09-28028 September 1999 Informs of Individual Exam Results for Applicants on Initial Exam Conducted on 990913-16 at Licensee Facility.Without Encls ML20216J0191999-09-27027 September 1999 Forwards Request for Addl Info Re Util 990301 Request to Support Installation of Digital Power Range Neutron Monitoring Sys & Incorporation of long-term thermal- Hydraulic Stability Solution Hardware,For Plant ML20212H6171999-09-24024 September 1999 Forwards Rev 2 to COLR for Pbaps,Unit 2,Reload 12,Cycle 13, IAW TS Section 5.6.5.d.Rept Incorporates Revised Single Loop Operation MAPLHGR Flow Multiplier ML20216H6451999-09-24024 September 1999 Forwards Notice of Withdrawal of Util 990806 Application for Amends to Fols DPR-44 & DPR-56.Proposed Change Would Have Involved Temporary Change to Increase Limit for Average Water Temp of Normal Heat Sink ML20212H5431999-09-24024 September 1999 Informs of Decision to Inspect H-3 & H-4 Shroud Welds During Upcoming 3R12 Outage Scheduled to Begin Late Sept 1999 ML20216H6751999-09-24024 September 1999 Forwards Amends 229 & 232 to Licenses DPR-44 & DPR-56, Respectively & Ser.Amends Will Delete SR Associated Only with Refueling Platform Fuel Grapple Fully Retracted Position Interlock Input,Currently Required by SR 3.9.1.1 ML20216F8811999-09-23023 September 1999 Withdraws 990806 Exigent License Change Application.Tech Spec Change to Allow Continued Power Operation with Elevated Cooling Water Temps During Potentially Extreme Weather Conditions No Longer Needed Due to Favorable Weather ML20212E8661999-09-22022 September 1999 Discusses GL 98-01 Y2K Readiness of Computer Sys at NPPs & Supplement 1 & PECO Response for PBAPS Dtd 990630. Understands That at Least One Sys or Component Listed May Have Potential to Cause Transient During Y2K Transition ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212D1191999-09-17017 September 1999 Forwards SE Re Proposed Alternatives to ASME Section XI Requirements for Containment Inservice Insp Program at Plant,Units 2 & 3 ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment ML20211P2961999-09-0707 September 1999 Provides Authorization to Administer NRC Approved Initial Written Exams to Listed Applicants on 990913 at Peach Bottom Npp,Delta,Pennsylvania ML20211K7031999-08-30030 August 1999 Forwards Response to NRC 990826 RAI Re License Change Application ECR 99-01255,revising TSs 2.1.1.2 & 5.6.5 ML20211E6941999-08-26026 August 1999 Forwards Request for Addl Info Re Min Critical Power Ratio. Response Should Be Submitted within 30 Days of Ltr Receipt ML20211Q4491999-08-25025 August 1999 Responds to Re Changes to PBAPS Physical Security Plan,Safeguards Contingency Plan & Guard Training & Qualification Plan Identified as Revs 13,11 & 9, Respectively.No NRC Approval Is Required,Per 10CFR50.54(p) ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211D5421999-08-23023 August 1999 Forwards Amends 228 & 231 to Licenses DPR-44 & DPR-56, Respectively & Se.Amends Revise TSs to Correct Typographical & Editorial Errors Introduced in TSs by Previous Amends ML20211A9721999-08-20020 August 1999 Forwards Request for Addl Info Re Third 10-year Interval Inservice (ISI) Insp Program Plan for Plant,Units 2 & 3 ML20210T5451999-08-12012 August 1999 Forwards Copy of Environ Assessment & Findings of No Significant Impact Re Licensee Request for Amends to Plant. Amends Consist of Changes to TS to Correct Typos & Editorial Errors Introduced in TS by Previous Amends ML20210P8321999-08-11011 August 1999 Responds to NRC 990715 Telcon Re Util 990217 Submittal of Proposed Alternatives to Requirements of 10CFR50.55a(g)(6)(ii)(B)(1) Re Containment Inservice Insp Program ML20210P8151999-08-11011 August 1999 Forwards Final Pages for Pbaps,Unit 2 & 3 OLs Re License Change Application ECR 99-01497,which Reflects Change in Corporate Structure at Pse&G ML20211B6521999-08-10010 August 1999 Informs That Dp Lewis,License SOP-11247,has Been Permanently Reassigned & No Longer Requires License,Per 10CFR50.74.Util Requests That Subject Individual Be Removed from List of License Holders ML20210P1561999-08-10010 August 1999 Submits Response to Requests for Addl Info Re GL 92-01,rev 1,Suppl 1, Rv Structural Integrity, for Pbap,Units 1 & 2. NRC Will Assume That Data Entered Into Rvid Are Acceptable for Plants,If Staff Does Not Receive Comments by 990901 ML20211B7881999-08-10010 August 1999 Transmits Summary of Two Meetings with Risk-Informed TS Task Force in Rockville,Md on 990514 & 0714 ML20210N7831999-08-0909 August 1999 Forwards Copy of Notice of Consideration of Issuance of Amends to Fols,Proposed NSHC Determination & Opportunity for Hearing, Re 990806 Request for License Amends.Amends Incorporate Note Into PBAPS TS to Permit One Time Exemption ML20210P0801999-08-0404 August 1999 Forwards Initial Exam Repts 50-277/99-301 & 50-278/99-301 on 990702-14 (Administration) & 990715-22 (Grading).Six of Limited SRO Applicants Passed All Portion of Exam ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response NUREG-1092, Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls1999-08-0303 August 1999 Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls ML20210J0161999-07-30030 July 1999 Forwards Copy of Notice of Consideration of Approval of Transfer of FOL & Issuance of Conforming Amends Re 990723 Application ML20210H5341999-07-27027 July 1999 Forwards Insp Repts 50-277/99-05 & 50-278/99-05 on 990518- 0628.NRC Determined That Two Severity Level IV Violations of NRC Requirements Occurred & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20210F3731999-07-23023 July 1999 Submits Confirmation That,Iaw 10CFR50.80,PSE&G Is Requesting NRC Approval of Transfer of Ownership Interests in PBAPS, Units to New Affiliated Nuclear Generating Company,Pseg Nuclear LLC ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20210E5811999-07-21021 July 1999 Forwards Final Tech Specs Pages for License Change Application.Proposed Change Will Revise Tech Specs to Delete Requirement for Refuel Platform Fuel Grapple Fully Retracted Position Interlock Currently Required by TS ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217F3021999-10-12012 October 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at PBAPS Have Been Completed.Ltr Also Confirms Completion of Actions Required by Confirmatory Order Modifying Licenses, ML20217E7451999-10-0808 October 1999 Forwards Response to NRC 990820 RAI Concerning Proposed Alternatives Associated with Third ten-yr Interval ISI Program for Pbaps,Units 2 & 3 ML20217C4141999-10-0606 October 1999 Forwards Response to NRC 981109 RAI Re Resolution of USI A-46 for Pbaps.Proprietary Excerpts from GIP-2,Ref 25 Results of BWR Trial Plant Review Section 8 Also Encl. Proprietary Excerpts Withheld ML20217B9151999-10-0606 October 1999 Provides Clarifying Info to Enable NRC to Complete Review of License Change Request ECR 98-01802,re Changes Necessary to Support Installation of Digital Pr Neutron Monitoring & Incorporate long-term T/H Stability Solution Hardware ML20217B7701999-10-0606 October 1999 Submits Corrected Info to NRC 980528 RAI Re Util Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions ML20217B8891999-10-0101 October 1999 Forwards Response to RAI Re Request to Install Digital Power Range Neutron Monitoring Sys & Incorporate long-term,thermal-hydraulic Stability Solution Hardware. Revised TS Table 3.3.2.1-1 Encl 05000278/LER-1999-004, Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv)1999-10-0101 October 1999 Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv) ML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212H6171999-09-24024 September 1999 Forwards Rev 2 to COLR for Pbaps,Unit 2,Reload 12,Cycle 13, IAW TS Section 5.6.5.d.Rept Incorporates Revised Single Loop Operation MAPLHGR Flow Multiplier ML20212H5431999-09-24024 September 1999 Informs of Decision to Inspect H-3 & H-4 Shroud Welds During Upcoming 3R12 Outage Scheduled to Begin Late Sept 1999 ML20216F8811999-09-23023 September 1999 Withdraws 990806 Exigent License Change Application.Tech Spec Change to Allow Continued Power Operation with Elevated Cooling Water Temps During Potentially Extreme Weather Conditions No Longer Needed Due to Favorable Weather ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment ML20211K7031999-08-30030 August 1999 Forwards Response to NRC 990826 RAI Re License Change Application ECR 99-01255,revising TSs 2.1.1.2 & 5.6.5 ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20210P8321999-08-11011 August 1999 Responds to NRC 990715 Telcon Re Util 990217 Submittal of Proposed Alternatives to Requirements of 10CFR50.55a(g)(6)(ii)(B)(1) Re Containment Inservice Insp Program ML20210P8151999-08-11011 August 1999 Forwards Final Pages for Pbaps,Unit 2 & 3 OLs Re License Change Application ECR 99-01497,which Reflects Change in Corporate Structure at Pse&G ML20211B6521999-08-10010 August 1999 Informs That Dp Lewis,License SOP-11247,has Been Permanently Reassigned & No Longer Requires License,Per 10CFR50.74.Util Requests That Subject Individual Be Removed from List of License Holders ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML20210F3731999-07-23023 July 1999 Submits Confirmation That,Iaw 10CFR50.80,PSE&G Is Requesting NRC Approval of Transfer of Ownership Interests in PBAPS, Units to New Affiliated Nuclear Generating Company,Pseg Nuclear LLC ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20210E5811999-07-21021 July 1999 Forwards Final Tech Specs Pages for License Change Application.Proposed Change Will Revise Tech Specs to Delete Requirement for Refuel Platform Fuel Grapple Fully Retracted Position Interlock Currently Required by TS ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 05000278/LER-1999-002, Forwards LER 99-002-01 to Correct Title Contained in Box (4) of LER Coversheet Form.Rev Does Not Change Reportability Requirements or Any Other Info Contained in Original Submittal of LER1999-07-12012 July 1999 Forwards LER 99-002-01 to Correct Title Contained in Box (4) of LER Coversheet Form.Rev Does Not Change Reportability Requirements or Any Other Info Contained in Original Submittal of LER ML20209G9121999-07-0909 July 1999 Informs That Ja Hutton Has Been Appointed Director,Licensing for PECO Nuclear,Effective 990715.Previous Correspondence Addressed to Gd Edwards Should Now Be Sent to Ja Hutton ML20209D9781999-07-0808 July 1999 Forwards Addl Info to Support EA of Proposed 990212 License Application ECR 98-01675,correcting Minor Administrative Errors in TS Figure Showing Site & Exclusion Areas Boundaries & Two TS SRs ML20209D8821999-07-0707 July 1999 Submits Estimate of Number of Licensing Actions Expected to Be Submitted in Years 2000 & 2001,as Requested by Administrative Ltr 99-02.Renewal Applications for PBAPS, Units 2 & 3,will Be Submitted in Second Half of 2001 ML20209D2671999-07-0202 July 1999 Responds to NRC 990322 & 0420 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20209E1131999-06-30030 June 1999 Forwards Proprietary NRC Form 398, Personal Qualification Statement-Licensee, for Renewal of RO Licenses for EP Angle,Md Lebrun,Jh Seitz & Zi Varga,Licenses OP-10646-1, OP-11081,OP-11082 & OP-11085,respectively.Encls Withheld ML20209B7001999-06-30030 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20209C1201999-06-30030 June 1999 Informs of Util Intent to Request Renewed License for PBAPS, Units 2 & 3,IAW 10CFR54.Licensee Anticipates That License Renewal Application Will Be Submitted in Second Half of 2001 05000277/LER-1999-004, Forwards LER 99-004-00 Re Unplanned ESF Actuations During Planned Electrical Bus Restoration Following Maint Activities1999-06-20020 June 1999 Forwards LER 99-004-00 Re Unplanned ESF Actuations During Planned Electrical Bus Restoration Following Maint Activities ML20196A5291999-06-14014 June 1999 Forwards Final Pbaps,Unit 3 TS Pages for License Change Request ECR 98-01802 Re Installation of Digital Power Range Neutron Monitoring (Prnm) Sys & Incorporation of long-term thermal-hydraulic Stability Solution Hardware ML20195E6051999-05-27027 May 1999 Requests Exemption from Requirements of 10CFR72.44(d)(3) Re Submittal Date for Annual Rept of Principal Radionuclides Released to Environ.Exemption from 10CFR72.72(d) Re Storage of Spent Fuel Records,Additionally Requested ML20195B8171999-05-25025 May 1999 Forwards Final TS Pages for License Change Application ECR 96-01511 Re Rev to Loss of Power Setpoints for 4 Kv Emergency Buses ML20195B6191999-05-19019 May 1999 Forwards PBAPS Units 2 & 3 Annual Radiological Environ Operating Rept 56 for 980101-1231, Per Section 6.9.2 of Ol. Trace Concentrations of Cs-137 Were Found in Sediment Consistent with Levels Observed in Previous Years ML20206P9171999-05-10010 May 1999 Updates Some of Transmitted Data Points Provided in Data Point Library ERDS for Pbaps,Units 2 & 3.Data Point Info Format Consistent with Guidance Specified in NUREG-1394 ML20206K6581999-05-0404 May 1999 Forwards PBAPS Bases Changes Through Unit 2 Bases Rev 25 & Units 3 Bases Rev 25.Bases Reflect Change Through Apr 1999, Thereby Satisfying Frequency Requirements of 10CFR50.71 ML20206D4651999-04-29029 April 1999 Forwards Rev 16 to UFSAR & Rev 11 to Fire Protection Program (Fpp), for Pbaps,Units 2 & 3.Page Replacement Instructions for Incorporating Rev 16 to UFSAR & Rev 11 to Fpp,Encl ML20207B8431999-04-23023 April 1999 Forwards Final Rept for 981117,plume Exposure Pathway Exercise of Offsite Radiological Emergency Response Plans site-specific for Peach Bottom Atomic Power Station.One Deficiency & 27 Areas Requiring C/A Identified ML20206C5461999-04-20020 April 1999 Forwards Radioactive Effluent Release Rept 41 for Jan-Dec 1998 for Pbaps,Units 1 & 2. Revs Made to ODCM & Station Process Control Program (PCP) During Rept Period,Encl 05000277/LER-1999-003, Forwards LER 99-003-00 Re 990318 Failure to Maintain Provisions of Fire Protection Program to Properly Address Effects of Flooding1999-04-16016 April 1999 Forwards LER 99-003-00 Re 990318 Failure to Maintain Provisions of Fire Protection Program to Properly Address Effects of Flooding ML20205K4541999-04-0808 April 1999 Forwards Revised Info Re 990330 NRC Nuclear Power Reactor Licensee Financial Qualifications & Decommissioning Funding Assurance Status Rept 05000278/LER-1999-001, Forwards LER 99-001-00 Re 990312 ESF Actuation of Rcics Due to High Steam Flow Signal During Sys Restoration.Rept Submitted Per 10CFR50.73(a)(2)(iv)1999-04-0808 April 1999 Forwards LER 99-001-00 Re 990312 ESF Actuation of Rcics Due to High Steam Flow Signal During Sys Restoration.Rept Submitted Per 10CFR50.73(a)(2)(iv) ML18106B1431999-03-31031 March 1999 Forwards Pse&G Rept on Financial Min Assurance for Period Ending 981231 for Hope Creek,Salem,Units 1 & 2 & Pbaps,Units 2 & 3,IAW 10CFR50.75 ML20205F8981999-03-31031 March 1999 Provides Info Re Status of Decommissioning Funding for LGS, Units 1 & 2,PBAPS,Units 1,2 & 3 & Sgs,Units 1 & 2,per Requirements of 10CFR50.75(f)(1) ML18106B1411999-03-30030 March 1999 Forwards Decommissioning Info on Behalf of Conectiv Nuclear Facility License Subsidiaries,Atlantic City Electric Co & Delmarva Power & Light Co,For Listed Nuclear Facilities ML20205J0831999-03-26026 March 1999 Requests Enforcement Discretion from Requirements of PBAPS, Units 2 & 3 Ts.Enforcement Discretion Pursued to Avoid Unneccessary Plant Transient Which Would Result from Compliance with TS ML20205B6421999-03-24024 March 1999 Submits 1998 Annual Decommission Rept for Pbaps,Unit 1. There Were No Reportable Events Involving Unit 1 for 1998 1999-09-09
[Table view] Category:UTILITY TO NRC
MONTHYEARML20064A7171990-09-18018 September 1990 Comments on SALP Board Repts 50-277/89-99 & 50-278/89-99. Author Pledges Continued Mgt Support of & Attention to Rate of Improvement,Achievement of Goals & Performance of Routine Activities ML20065D4421990-09-14014 September 1990 Responds to Generic Ltr 90-07, Operator Licensing Natl Exam Schedule. Proposed Schedules for Operator Licensing Exams, Requalification Exams & Generic Fundamental Exams Encl ML20064A7751990-09-13013 September 1990 Advises That Ba Stambauth No Longer Maintains Need to Hold Senior Operator License ML20065D3741990-09-11011 September 1990 Forwards Rev to Relief Request 10-VRR-2 Re RHR stay-fill Supply Check Valves,Per ML20059F0541990-08-31031 August 1990 Responds to NRC Re Violations Noted in Safety Insp Repts 50-277/90-13 & 50-278/90-13.Corrective Actions: Training Will Be Provided for Personnel Re Requirements of Drawing E1317 & Administrative Procedures A-2 & A-6 ML20028G8181990-08-27027 August 1990 Forwards Peach Bottom Atomic Power Station Semiannual Effluent Release Rept,Jan-June 1990. No Revs Made to ODCM During Rept Period ML20059A6461990-08-15015 August 1990 Responds to Violation Noted in Insp Repts 50-277/90-200, 50-278/90-200,50-277/90-06 & 50-278/90-06 & Payment of Civil Penalty in Amount of $75,000.Corrective Actions:Emergency Svc Water Sys Restored to Operable Status ML20058N1991990-08-0909 August 1990 Advises of Change of Address for Correspondence Re Util Operations.All Incoming Correspondence Must Be Directed to One of Listed Addresses ML20058Q4051990-08-0606 August 1990 Forwards Public Version of Revised Emergency Response Procedures,Including Rev 12 to ERP-140,App 2,Rev 13 to ERP-140,App 3,Rev 4 to ERP-230,Rev 3 to ERP-305 & Rev 3 to ERP-660 ML20058M6631990-08-0303 August 1990 Responds to NRC 890406 Integrated Assessment Team Insp Repts 50-277/89-81 & 50-278/89-81.Based on Encl Schedule,Overall Projected Implementation Date Will Be 901119 ML20056A9611990-08-0303 August 1990 Notifies That Be Saxman Terminated Employment & Operating Responsibilities W/Util on 900706 ML20081E1581990-07-30030 July 1990 Forwards List of 1990 QA Program Changes for Plant.List Identifies Page & Paragraph Number,Brief Description & Type of Change ML20056A0421990-07-27027 July 1990 Forwards Updated Human Resource Status Rept for Jan-Jul 1990 for Areas Identified in Integrated Assessment Team Insp Repts 50-277/89-81 & 50-278/89-81 ML18095A3761990-07-26026 July 1990 Forwards Decommissioning Repts & Certification of Financial Assurance for Plants ML18095A3661990-07-26026 July 1990 Forwards Decommissioning Repts for Hope Creek,Peach Bottom & Salem Nuclear Generating Stations ML18095A3721990-07-24024 July 1990 Forwards Rept & Certification of Financial Assurance for Decommissioning for Plants,Per 10CFR50.75 ML20055H8331990-07-20020 July 1990 Submits Change of Addresses for Correspondence Re Util Nuclear Operations ML20044B2621990-07-12012 July 1990 Forwards Annual Progress Rept on Implementation of Control Room Enhancements,Per NUREG-0737.Corrective Actions for All Priority 1 Human Engineering Discrepancies Completed for Unit.Remaining Priority 2 Discrepancies Under Reevaluation ML20055G5481990-07-11011 July 1990 Forwards Public Version of Revised Epips,Including Rev 12 to ERP-140,App 3 & Revs 3 to ERP-310 & ERP-317 ML20043H7041990-06-21021 June 1990 Forwards Endorsements 143-146 to Nelia Policy NF-140 & Endorsements 93-96 to Maelu Policy MF-67 ML20044A2961990-06-21021 June 1990 Submits Revised Response to NRC Bulletin 89-002 Re safety- Related Swing Check Valves to Be Installed on Emergency Diesel Generator.Bolts Will Not Be Replaced Because Valves W/Original Internal Bolts Meet Requirements of Bulletin ML20043H6081990-06-19019 June 1990 Corrects 900427 Response to Generic Ltr 87-07, Info Transmittal of Final Rulemaking for Revs to Operator Licensing - 10CFR55 & Conforming Amends. ML20055C7621990-06-18018 June 1990 Informs NRC of Plans Re Licensing of Senior Reactor Operators (Sros) Limited to Fuel Handling at Plants.Util in Process of Implementing New Program for Establishment & Maint of Licensed SROs Limited to Fuel Handling at Plants ML20043G8131990-06-13013 June 1990 Responds to NRC 900515 Ltr Re Violations Noted in Insp Repts 50-277/90-06 & 50-278/90-06.Corrective Actions:Surveillance Test 6.16, Motor Driven Fire Pump Operability Test, Will Be Revised ML20043H0111990-06-12012 June 1990 Advises That AR Wargo Reassigned from Operating Shift Responsibilities & Will Be Resigning License,Effective on 900514 ML20055D1141990-06-0808 June 1990 Forwards Public Version of Revs to Emergency Response Procedures,Including Rev 9 to ERP-140 & Rev 3 to ERP-315 ML20043D7351990-06-0404 June 1990 Responds to NRC 900504 Ltr Re Violations Noted in Insp Repts 50-277/90-04 & 50-278/90-04.Corrective Actions:Procedural Controls Strengthened to Preclude Licensed Operators from Performing Licensed Duties W/O Successfully Passing Exams ML20043E9261990-06-0404 June 1990 Forwards Response to 900327 Request for Addl Info Re Generic Ltr 88-01, NRC Position on IGSCC in BWR Austenitic Stainless Steel Piping. ML20043D2681990-05-31031 May 1990 Forwards Response to NRC Requests Re PECo-FMS-0006, Methods for Performing BWR Reload Safety Evaluations. Util Core Monitoring Activities Routinely Access Accuracy of steady-state Physics Models Used in Evaluation of Parameter ML20043D6451990-05-30030 May 1990 Responds to NRC 900503 Ltr Re Violations Noted in Insp Repts 50-277/90-08 & 50-278/90-08.Corrective Actions:Glaucoma Testing Program Initiated for Security Personnel & Necessary Equipment to Perform Glaucoma Testing Onsite Obtained ML20055C5491990-05-18018 May 1990 Forwards Response to Request for Addl Info on 900412 Tech Spec Change Request 89-20 Re Postponement of Next Snubber Visual Insp,Due 900526,until Scheduled mid-cycle Outage in Fourth Quarter 1990 ML20055C5121990-05-18018 May 1990 Provides Info Inadvertently Omitted in Re Property Insurance Coverage for Plants.Limerick Generating Station Unit 2 Should Have Been Ref as Being Included Under Insurance Coverage ML20055C4851990-05-15015 May 1990 Forwards Annual Financial Repts for 1989 for Philadelphia Electric Co,Pse&G,Atlantic Energy,Inc & Delmarva Power & Light Co ML20043A3341990-05-14014 May 1990 Advises of Util Proposal to Provide Response to NRC Request for Schedule for Compliance W/Reg Guide 1.97 Re Neutron Monitoring Instrumentation 3 Months After NRC Concurrence W/Bwr Owners Group Design Criteria ML20042E7651990-04-27027 April 1990 Informs That Mod 2285 Completed on Unit 3,but That Mod 2285 Will Not Be Completed on Unit 2 During 8th Refueling Outage ML20042E8931990-04-27027 April 1990 Responds to Violation Noted in Insp Rept 50-278/90-01. Corrective Actions:Automatic Depressurization Sys Logic Sys Functional Tests Will Be Revised to Include Guidance in Unique Application of Test Lights ML20042F3241990-04-27027 April 1990 Advises That Organizational Changes Made in Advance of Approval of Tech Spec Change Request 88-06.Changes Do Not Present Unreviewed Safety Question ML20042E8741990-04-27027 April 1990 Responds to Generic Ltr 87-07, Info Transmittal of Final Rulemaking for Revs to Operator Licensing. Certifies That Limerick Operator Requalification Training Program Renewed on 900125 & Peach Bottom Subj Program Renewed on 890622 ML20012F4801990-04-0202 April 1990 Forwards Errata to Unit Shutdowns and Power Reductions Monthly Operating Rept for Feb 1990 ML20012F0971990-03-22022 March 1990 Forwards Summary of ASME Repairs & Replacement Completed, Per Facility Second 10-yr Interval Inservice Insps Completed During 900331-891111 Extended Refueling Outage ML20012E2151990-03-20020 March 1990 Responds to Generic Ltr 89-19, Request for Action Re Resolution of USI A-47, 'Safety Implication of Control Sys in LWR Nuclear Power Plants,' for Peach Bottom.Response for Limerick Generating Station Will Be Provided by 900504 ML20012C2931990-03-12012 March 1990 Responds to Generic Ltr 90-01, Request for Voluntary Participation in NRC Regulatory Impact Survey, Per 900118 Request ML20012B6211990-03-0808 March 1990 Provides Actions Taken to Ensure & Verify Sys Design Basis Performance,Per 900205 SSFI at Facility ML20012B9011990-03-0606 March 1990 Forwards 870331-891111 Inservice Insp Program Final Rept for Peach Bottom Atomic Power Station Unit 3 1987-1989 Extended Refuel Outage. Several Indications Identified ML20012A2661990-02-26026 February 1990 Forwards Application for Amends to Licenses DPR-44 & DPR-56, Consisting of Tech Spec Change Requests 89-13 & 89-14, Revising Nuclear Review Board Membership & Meeting Frequency & Adding Independent Safety Engineering Group Requirements ML20011F2541990-02-23023 February 1990 Forwards Revs to Physical Security Plan.Encls Withheld (Ref 10CFR73.21 & 2.790) ML20011F3791990-02-21021 February 1990 Provides Revised Schedule for Installation of Hardened Wetwell Vent,Per Generic Ltr 89-16 & Explanation Why Jan 1993 Completion Date Cannot Be Met Due to Unavailability of Matls.Intallation Scheduled for Cycle 9 Outage ML20006F5491990-02-16016 February 1990 Certifies That 891122 Tech Spec Change Request (Tscr) 89-15, 891228 Tscr 88-18 & 900214 Tscr 90-04 Mailed to Commonwealth of Pa,Dept of Environ Resources ML20006F1621990-02-15015 February 1990 Forwards Progress Rept Re Implementation of Control Room Enhancements as of End of Seventh Refueling Outage,Per NUREG-0737.Rept Delayed to Allow for Independent Verification of Control Room Enhancement Status ML20012B1731990-02-15015 February 1990 Forwards Public Version of Revs to Epips,Including Rev 5 to ERP-101,App 1 to Rev 13 to ERP-110,App 2 to Rev 10 to ERP-110,App 1 to Rev 7 to ERP-140,App 2 to Rev 10 to ERP-140,App 3 to Rev 11 to ERP-140 1990-09-18
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PHILADELPHI A ELECTRIC COM PANY 2301 M ARKET STREET P.O. BOX 8699 i PHILADELPHIA. PA,19101 I SHIELDS L DALTROF F atacfneceno IQN i
August 26, 1982
! Docket Nos. 50-277 50-278 d
3 Mr. John F. Stolz, Chief U.S. Nuclear Regulatory Commission Operating Reactors Branch #4
, Division of Licensing j Washington, DC 20555
SUBJECT:
Peach Bottom Atomic Power Station, Unit 2 and 3, NRC Request for Additional Information on the Peach Bottom Containment Purge and Venting and Completion of NUREG-0737 Item II.E.4.2.
i Ref: Letter from J. F. Stolz (NRC) to E. G.
Bauer, Jr., (PECo.), dated July 7, 1982.
1
Dear Mr. Stolz:
i i In response to your reauest for additional information on the Containment Purge and Vent System and NUREG-0737 Item II.E.4.2. for the Peach Bottom Atomic Power Station review, Philadelphia Electric Company submits the attached summary report of our efforts and findings concerning this issue. This report i should provide the information required to complete the NRC review.
With respect to the specific request for information l identified in your letter:
1 i
Review Item 1 - Conformance to Standard Review Plan Section 6.2.4 Revision 1 and Branch Technical Position CSB 6-4 Revision 1; I
i 82083100 % 820826 PDR ADOCK 05000277
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P PDR ,_ _ _ . _ _ _ . _ _ _ _ _ , _ _ _ _ _ _ , _ , . . _ _ . _ , , _
Q~
Mr. John F. Stolz, Chief Page 2 Enclosure 2 of the referenced letter requested the following in order to complete your review:
- 1) Information concerning the provisions made to insure that isolation valve closure will not be prevented by debris which could potentially become entrained in the escaping air and i steam, i
- 2) An analysis which demonstrates the acceptability of the provisions made to protect structures and safety related equipment located beyond the purge isolation valves.
Response
The information presented as item 12 in the summary report describes the protective screens (Seismic Category 1) installed to prevent debris from disabling the valves. Item 16 of the summary report describes the efforts undertaken to demonstrate the acceptability of 3
the system design.
4 a
l Review Item 2 - Valve Operability: Requires further i cualification information to be forwarded for review.
Response
i The summary report identifies various analyses (Items 1 thru 11) on all phases of valve operability as described in the enclosure " Guidelines for Demonstration of Operability of Purge and Vent Valves" received with your letter of September 27, 1979.
l Review Item 3 - Safety Actuation Signal Override: Has been
{ reviewed by the NRC and no further information was requested in I
this letter.
l I Review Item 4 - Containment Leakage Due to Seal Deterioration:
Requests that we propose Technical Specification changes and
! provide details of a proposed test program.
Enclosure 1 of the referenced letter states "The purpose of the leakage integrity tests of the isolation valves in the ,
)
l l
a Mr. John F. Stolz, Chief Page 3 containment purge and vent lines is to identify excessive degradation of the resilient seats for these valves."
Response
The Peach Bottom ource and vent valves utilize an inflatable T-ring seal desian which has proven to be extremely reliable and leak tight over a ceriod of many years. This particular design is very forgiving with respect to seal dearadation, temperature changes, and leakaoe. By pressurizing the seal chamber, the elastomer seat is uniformiv pressed against the periphery of the closed butterfly disc, thereby assuring very low rates of leakage. Review of the surveillance test results have confirmed this as a superior design feature.
The possibility of excessive seal degradation is further neoated by the Peach Bottom preventive maintenance program wnich reauires that the seals be replaced approximately every four years (3 refueling outages maximum).
In view of the above, we conclude that the present testing frecuency of once per refueling cycle presently recuired by the Peach Bottom Technical Specifications is more than edecuate to identify seal degradation and assure proper operation of the valves.
We have reviewed the samole Technical Specification (Enclosure 3) of the referenced letter against the Peach Bottom Technical Soecification and have concluded that the existina specification orovides the essential operability and surveillance recuirements. For this reason we do not plan to reauest a Technical Specification chance for this issue.
If you have any cuestions or recuire further information l
on the subject, please do not hesitate to contact us.
I Very trulv yours,
~~
' j[G y f
Attacnment cc: NRC - Site Inspector
. o . .
Docket Nos. 50-277 50-278
SUMMARY
REPORT
SUBJECT:
Peach Bottom Atomic Power Station Operability of Purge and Vent Valves Introduction Since receiot of a letter from the NRC to Philadelohia Electric Comoany in November of 1978, purge and vent valve operability has been the subject of a continual dialog between PECo., the NRC, architect-engineer (Bechtel), and purge and vent valve manufacturers (Ficher & WKM). A partial listino of relevant external correscondence is attached. This report is intended to summarize the results of this activity and to outline a course of action to resolve remaining issues.
Desian of PBAPS Systems:
The Containment Atmospheric Control System (P&ID M-367, FSAR Figure 5.2.7) and Containment Atmospheric Dilution System (P&ID M-372, FSAR Figure Q14.6.5) are utilized to control the containment atmosphere durinq normal clant operations and post-LOCA, respectively. The portions of these systems used for
, containment venting are shared. All gases vented from the crimary containment are processed through the HEPA and charcoal filters of the Standby Gas Treatment System (FSAR Section 5.3.3) orior to release in accordance with the plant Technical Specifications.
The torus and drywell are each provided with large purge and vent lines for rapid deinerting during shutdowns, ventilation during outages, and rapid inerting during startuos. These lines are each provided with two, normally closed, system isolation valves. The 6" and 18" butterfly valves used for this service are designed to maintain a tight seal against design post-LOCA containment pressures. These isolation valves may be operated from the control room during normal plant operation and are automatically closed uoon receipt of a containment isolation signal. The containment isolation signal to these valves cannot be byoassed or over-ridden.
Docket Nos. 50-277 50-278 In addition to the above large vent lines, the torus and drywell are each provided with small makeup and vent lines for atmospheric control during plant operation and post-LOCA. These small lines are either 1" or 2" in diameter. Each is provided with 2-1" isolation valves (either 2 globe valves or a globe and a check). The valves used in this service are designed for rapid closure (less than 5 sec.), and a tight seal against design post-LOCA containment pressures. The globe isolation valves may be operated from the control room during normal operation and are automatically closed upon receipt of a containment isolation signal. For post-LOCA combustible gas control these small vent line isolation valves may be opened by taking the reactor mode switch out of the RUN position and utilizing keylocked bypass switches. This override of the isolation signal is alarmed in the control room.
Technical Soecifications:
The present Technical Specifications for PBAPS recuire that the containment atmosphere oxygen concentration be reduced to less than 4% within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of placina the ceactor in the RUN mode and maintained in this condition during operation.
Deinerting is oermitted 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> prior to a shutdown (see Tech.
Spec. 3.7.A.5). Purgina of the primary containment must be through the Standby Gas Treatment System whenever primary containment integrity is required (see Tech. Spec. 3.8.C.9).
In addition, all containment isolation valves are reauired to be operable, or in the isolated position during power operation (Tech. Spec. 3.7.D). Surveillance testing is reauired during each operating cycle to confirm operability, closure time, and leak rates for containment isolation valves (Tech. Spec.
4.7.A.2.f and 4.7.D.l.a). The specified maximum closure time for the purge and vent isolation valves is 5 seconds.
Ooerating Experience:
It has been necessary to periodically vent the PBAPS containments during normal plant power operation to control containment pressure, maintain a torus-to-drywell differential
Docket Nos. 50-277 50-278 oressure, and/or maintain an inert atmosohere. Torus-to-drywell differential pressure maintenance has been discontinued per agreement with the NRC (Safety Evaluation supporting Amendment Nos. 41 and 40). Presently, venting for pressure control and maintenance of an inert atmosonere is reauired only when the Instrument Nitrogen System (P&ID M-333, FSAR Fiqure 010.4.1) is out of service and olant Instrument Air is being utilized as a backup, or when other syster. leakage causes pressurization.
These conditions are encountered infrequently. In most cases, intermittent venting through'the small lines is sufficient. On some occasions, however, it has been necessary to cvcile the large butterfly valves to provide sufficient control. When this is done, the gas is released in batches by opening the inner, and then the outer valve. At least one of the 18" butterfly valves in each vent line remains closed at all times durino this operation.
Rapid purcing through the 18" lines for inerting or deinerting takes bet + 5 to 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> if the valves are fully open. Restriction < valves to less than 40' open, as described below, has aproximately trioled ource times. This ooeration is performed only for outages recuiring containment access.
Surveillance testing experience indicates that the assumed 5 second closure times are conservatively long. The 1" isolation valves actually close in less than 1 second. Tne 18" butterfly valves typically close in about 3 seconds.
i Operability Evaluation:
Normal Power Operation:
A December 1978 study by the Mechanical Engineering Division indicated that continued " unlimited ourging" was fully justified during all coerational modes except startuo and shutdown. Any limitation on controlled venting through the small lines, or through tha large lines when releases are " batched" was determined to be unwarranted. The above determination was based l
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l Docket Nos. 50-277 50-278 on a review of the existing design against Standard Review Plan r 6.2.4 and Branch Technical Position CSB 6-4.
Subsequent investigacions indicated that detailed seismic analyses of the small purge and vent valves manufactured by WKM had not been performed. The NRC was advised that analyses were beino performed to verify the adecuacy of the design.
In reference 5), we advised the Commission that additional operability analyses would not be performed on the 1" air-operated globe valves. These valves have been designed and tested for rapid closure against pressures significantly higher than they would see following a LOCA. The valves in the drywell purge lines have been demonstrated to close in less than 5 seconds against a differential oressure of 1135 osig, and those on the torus against 110 osiq. These are substantially greater i than the maximum post-LOCA pressures of 42 osig in the drywell and 26 psig in the torus (see FSAR Figure 14.6.10). It was further stated that a seismic analysis of these valves had recently been completed with satisfactory results and that the stainless steel seating surfaces of these valves would not be subject to degradation when exposed tu a post-accident environment.
Start-up and Shutdown:
! A review of the desian of the 6" and 18" butterfly valves with the manufacturer (Fisher) indicated that they might not close if subjected to DBA-LOCA differential pressures while in their full-open position. High stress levels would be experienced in the area of the stem-to-disc connection. In addition, it was determined that the air sucoly to the inflatable seals used in these valves was not safety-grade or seismic.
The NRC was immediately notified of these findings (reference 3), the valves were blocked closed, and a seismic air supply provided. Subsecuent efforts were directed at determining the maximum allowable valve opening, providing a permanent seismic air sucoly which would not hamper operational flexibility, providing mechanical stoos for positive valve cosition control,
e Docket Mos. 50-277 50-278 and further evaluations of operability. These considerations are discussed throuahout'the following text.
The following specific discussions correscond to issues in the NRC's " Guidelines'for Demonstration of Operability of Purge and Vent Valves" transmitted to PECo., with reference 4) and "Recuest for Additional Information" transmitted with reference
- 7) :
- 1. Valve Closure Rate Versus Time - The butterfly valves are designed to close from their full-open oosition in less,than 5 seconds. In accordance with the discussion in 2) , below, the valves have been limited to a maximum of 40' open. Fisher has advised us that test results indicate that an assumotion of a constant rate of closure from this oosition to the closed position is conservative. This assumption has been used in the determination of acceptable valve ooeninas.
- 2. Flow Direction Through Valve; A p Across Valve - Fisher has provided a tabulation of allowable 6 p for the 6" and 18" valves for flow into the flat and into the hub. In determining allowable pressure drops across a particular butterflv valve at various angles of the disc, Fisher used classical " mechanics of materials" type equations to calculate stress levels at various worst-case locations in the valve assembly (specifically, various locations along the valve shaf t) . Their analysis addressed all of the different states of shear and stress which are applicable to the loading conditions defined. Fisher has confirmed the dynamic torcue factors which are utilized in their analyses by testing.
- Code allowable stresses were assumed to be the limits of ooerability.
Since the valves are installed at random with regard to direction of flow, allowable values for the most limiting combination (18" valve, flow into hub) have been integrated with the DBA LOCA drywell pressurization curve to determine an acceotable valve onening limit.
This analysia indicates that the valves will close l
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Docket Mos. 50-277 50-278 acainst design pressures if they are limited to 40' open. All valves were initially limited to less than this openinq by adjustment of their air sucoly regulators. Mechanical stops have subsecuently been installed to provide a more oositive means of control.
- 3. Single Valve Closure - Two butterfly valves are provided in series in each ourge and vent line. Closure of a single valve has been assumed to be the limiting condition for analysis. Flow disruptions due to the simultaneous closure of an uostream valve could cor.ceivably cause undesirable stresses on the shaft-to-disc connection of the downstream valve. However, Fisher's evaluation has indicated that this condition is less severe as a result of sharing the pressure droo between the two valves.
- 4. Containment Back Pressure Effects - All PBAPS butterfly isolation valves are located outside of containment.
Thus, containment pressure on the valve operator can not exist and there will be no effect on the closing toraue margins of these air operated valves.
5 Adecuacy of Accumulator - An accumulator is not utilized to assure valve closure. These valves are spring loaded to close on loss of instrument air. A high pressure nitrogen cylinder is utilized as a source of safety-grade air for each inflatable seal. The controls are designed such that gas from this cylinder is utilized only when the instrument air line cressure drops below 75 osiq. Alarms are provided to indicate loss of seal pressure.
- 6. Toraue Limiting Devices - The PBAPS butterfly valves do not utilize torcue limiting devices since they are
! eouloped with air operators.
i
! 7. Pipina System Effects - The effects of oicing system l
discontinuities on flow distributions has been analyzed l by our architect-engineer (Bechtel). It has been I
j Docket Nos. 50-277 50-278 i
determined that all but two valves per unit will be subjected to even flow distributions. Velocity profiles for the valves with uneven flow distributions were provided to the valve manufacturer (Fisher).
Fisher has advised that valves AO-2520 and 3520 are oriented such that the non-uniform fluid profile will not produce an additional toraue on the valve disc since both " winos" of the disc (as split by the stem) will be subjected to the same flow. They have also advised that
- the non-uniform flow profile to which valves A02520 and 3505 will be subjected will assist valve closure.
- 8. Effect of Disc and Shaft Orientation - The effect of shaft orientation relative to the fluid mixture egressing from the containment was considered to be relevant only in those cases where the valves would see uneven flow distribution. This is discussed in 7.,
above. The effect of disc orientation was considered in the determination of allowable valve opening ner 2.,
above.
- 9. Seismic Design - A seismic analysis of the butterfly valve assemblies was performed by Fisher in 1974. This analysis considered normal operating loads plus loading due to seismic acceleration. In 1979 Bechtel was reauested to review their original piping seismic analysis for 2 of the 18 ourge and vent valves to confirm that allowable valve accelerations would not be exceeded. The results indicated that problems did not
! exist. A 100% check was subseauently reauested. This review indicated the need for several pipe suoport modifications to limit valve accelerations to acceotable levels. This condition was reported to the NRC and corrective actions taken immediately.
Fisher has provided confirmation that the addition of mechanical stops will not adverselv affect the seismic design of the valves. The seismic design of the safety grade air sucoly systems has been reviewed by Bechtel.
n._--,- , -- .- .. , _ _ _ . - _ - , _ _ - -,- - . - - _ - - - , - - , , , . , _ , , . - - , - . . , . . . - - - - . - - - - - . -
= ,o Docket Nos. 50-277 50-278 Seismic aualification documentation for components in the air suoply systems was sucolied by Fisher.
- 10. Seal Integrity - A tabulation of expected normal and post-LOCA environmental conditions was provided to Fisher for their evaluation of longterm seal integrity.
The seals in these butterfly valves are routinely reolaced approximately every 4 years in accordance with the manufacturer's recommendations. The ethylene prooylene seal material used in these valves has been cualified for use in numerous safgty-grade applications for radiation doses uo gom greater than the 2 x 10 5 x 10 Rads (7) which is Rads predicted for PBAPS. Test data furnished by a manufacturer of elastomeric seals indicates that this material yould experience between 28 and 47% compression set at 10 Rads (Y).
Tyoically, only gamma radiation has been considered a hazard to elastomeric seals since they are usually enclosed in metallic grooves. In this particular application, however, a cortion of the T-ring inflatable seal will be exposed to the containment atmosohere and thgreby subjected to substantial beta irradiation (a8 x 10 Rads). We have thus far been unable to find any work done on the effects of the exposure of elastomers to beta radiation. Because of the low energy level of beta radiation, it is felt that any effects will be shallow surface ohonomena that will not materially alter seal effectiveness.
The above described compression set phenomena may also occur due to temperature changes. As temperature increases the seal ring material attempts to expand but, due to the restrictive design, " thermal stresses" are develooed in the seal. Over a period of time, the seal retains some permanent set which is assumed to be caused by polymer crosslinking. Then as the temoeratuce is reduced, the seal material contracts resulting in less sealing compression, which tends to reduce its tight shut-off capability. This compression set phenomena will not be a problem for the Peach Bottom valves because the inflatable T-ring seal maintains a constant
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Docket Nos. 50-277 50-278 i ,
9-and uniform sealinq comoression. In addition, the seal has been designed for tight shutoff against a constant differential pressure of 62 osig. This is substantially higher and of much longer duration than the predicted containment pressure response.
The design of the T-ring inflatable seal makes it particularly forgiving with respect to seal degradation, temperature changes, and leakage. By oressurizing the seal chamber, the elastomer seal is uniformly pressed aaainst the oeriphery of the closed butterfly disc thereby assuring very low rates of leakage. It is therefore felt that continued seal replacement at aporoximately 4 year intervals (maximum 3 refueling outages) will provide sufficient assurance of seal integrity.
- 11. Design for Comoressible Flow - The butterfly valves used at Peach Bottom have been designed considering the effects of compressible flow. Fisher's philosoohy concerning the effects of compressible flow is presented in ISA Transaction Vol. 8, No. 4 entitled "Effect of Fluid Compressibility on Toraue in Butterfly Valves" written by Floyd P. Harthun. The method used by Fishet to determine dynamic toraue results in conservative
- loading conditions for stress and sizing calculations.
l 12. Debris Entrainment - Design features were originally not l provided at Peach Bottom to ensure that ourge and vent l
valve closure would not be orevented by debris which l
could potentially become entrained in the escaping air l and steam. Fisher has suggested that screen mesh with i 3/8" to 1/2" holes be provided. Accordingly, protective l screens have been installed on the inner end of each I containment purge and vent penetration. The screens are l of seismic Category I desian and located at a distance of at least several oice diameters from the inner side
, of each inboard isolation valve.
l
- 13. Leak Testing During Operation - Local leak rate tests of all the purge and vent valves are currently performed
Docket Nos. 50-277 50-278 during each refueling outage in accordance with the recuirements of 10 CPR 50, Appendix J and the Plant Technical Soecifications. The capability to leak rate test the purge and vent valves during reactor operation currently exists. Such testing would have to be performed by pressurizing between the inner and outer valves. Testing of the inner valve in its nonaccident direction will give conservative or eauivalent leak rates to testing in the accident direction for this type of valve.
- 14. Leak Rate vs.A o - The inflatable seal ring utilized in the Peach Bottom ourge and vent valves provides a design whose leakace is not sensitive to differential pressure across the valve but, rather, the relationship between seal sucolv and valve differential pressure. The seal supply pressure is maintained at a minimum of 75 osig which is more than 1.5 times greater than the maximum post-LOCA drywell pressure.
- 15. Limitation on Purge Time - In accordance with the recuirements of reference 1), the use of the large volume ourge oath durina operation has been limited to 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> per year. This limitation, in coniunction with the extended duration of ourging due to limited valve opening, has caused some operational difficulties and l
may cause more significant oroblems in the future, depending on the number of times drywell access is required during any given year. Leakage inspections are performed while the vessel is pressurized during shutdown and startuo operations. Once the current 90 hour0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> limit is reached, inerting and deinerting will have to be accomplished while the unit is shutdown, thus extending the duration of all subsecuent outages and precluding insoections. As a result, we have undertaken an evaluation of valve modifications which will allow greater opening cercentages. In addition, evaluations of the radiological consecuences of a range of LOCA's during purge operations are being comoleted in order to justify a less stringent limit.
1 l
Docket Mos. 50-277 50-278 16 Effects on Downstream Safety-Related Eauipment - Gases being vented from the Peach Bottom primary containment are transported through duct-work to the Standby Gas Treatment System (SGTS) for filtration prior to release.
Our Architect-Engineer (Bechtel) has completed an analysis of the pressure surge that the SGTS duct and filters could be exoosed to if a DBA-LOCA were to occur while the large diameter (18") vent valves were fully open. The pressure differential across the filters was determined to be limiting and was calculated to exceed the differential for which the filters were designed. A later analysis, assuming 40' open valves, has demonstrated that acceotable pressures are encountered.
However, filter effectiveness following such an event would be somewhat questionable due to the amount of moisture absorbed on the charcoal filters. We have thus undertaken a probabilistic assessment of the significance of potential damage. This effort has been comoleted to the point that we can conclude that there will be no increase in risk above WASH-1400 if duct failure does not occur. Further evaluations are continuing to support the same conclusion even with assumed duct and/or filter failure.
f . .
PEACH BOTTOM ATOMIC POWER STATION PURGE AND VENT VALVES REFERENCES
- 1) T. A. Ippolito (NRC) letter to E. G. Bauer (PECo) dated 11/29/78 - notice of problem, transmittal of SRP.
- 2) S. L. Daltroff (PECo) letter to T. A. Ipoolito (NRC) dated 1/2/79 - response to reference 1).
- 3) W. T. Ullrich (PECo) letter to B. H. Grier (NRC) dated 3/5/79
- LER on valve closure and seismic air supply.
- 4) D. G. Eisenhut (NRC) letter to all LWR's dated 9/27/79 -
transmittal of guidelines for demonstration of operability.
- 5) J. W. Gallagher (PECo) letter to D. G. Eisenhut (NRC) dated 10/25/79 - evaluation of large valves expected to be completed by about 4/30/80.
, 6) T. A. Icoolito (NRC) letter to E. G. Bauer (PECo) dated 10/22/79 - request for confirmation of operating limits and verification studies.
- 7) T. A. Ippolito (NRC) letter to E. G. Bauer (PECo) dated 1/2/80 - long term items (debris, leak testing, SGTS overpressure).
- 8) NEDO-24577, Mark I Containment Program - Plant Uniaue Load Definition Reports, April 1979.
- 9) NEDO-24708, Additional Information Recuired for NRC Staff Generic Report on Boiling Water Reactors, August 1979.
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