05000272/LER-1982-034, Forwards LER 82-034/03L-0.Detailed Event Analysis Encl

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Forwards LER 82-034/03L-0.Detailed Event Analysis Encl
ML20054G329
Person / Time
Site: Salem PSEG icon.png
Issue date: 06/07/1982
From: Midura H
Public Service Enterprise Group
To: Haynes R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20054G330 List:
References
NUDOCS 8206210444
Download: ML20054G329 (3)


LER-2082-034, Forwards LER 82-034/03L-0.Detailed Event Analysis Encl
Event date:
Report date:
2722082034R00 - NRC Website

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  • O >SEG Public Service Electric and Gas Company P.O. Box E Hancocks Bridge, New Jersey 08038 Salem Generating Station June 7, 1982 Mr. R. C. Haynes Regional Administrator USNRC Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406

Dear Mr. Haynes:

LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 82-034/03L Pursuant to the requirements of Salem Generating Station

. Unit No. 1, Technical Specifications, Section 6.9.1.9.b, we are submitting Licensee Event Report for Reportable Occurrence 82-034/03L. This report is required'within thirty (30) days of the occurrence.

Sincerely yours,..h{IA " H. J. Midura General Manager - Salem Operations RF:ks h CC: Distribution B206210444 820607 {DRADOCK 05000272 PnR The Energy People f[M l r m wonw

r-l Report Number: 82-034/03L Report Date: 06-07-82 Occurrence Date: '05-10-82

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Facility: Salem Generating Station, Unit 1 Public Service Electric & Gas Company Hancocks Bridge,.New Jersey 08038 IDENTIFICATION OF OCCURRENCE:. No. 14 Steam Generator Wide Range Level - Inoperable. This report was initiated by Incident Report 82-127. CONDITIONS PRIOR TO OCCURRENCE: Mode 1 - Rx Power 98% - Unit Load 1110 MWe. DESCRIPTION OF OCCURRENCE: On May 10, 1982 during routine operation, the Control Room Operator noticed the No. 14 Steam Generator Wide Range. Level indication had failed low. The channel was declared inoperable at 0415 hours, and Limiting Condition for Operation 3.3.3.7 Action 1 was entered. This occurrence constituted operation in a degraded mode in accordance with Technical-Specification 6.9.1.9.b. l DESIGNATION OF APPARENT CAUSE OF OCCURRENCE: l The failure of No. 14 Steam Generator Wide Range Level Instrument was due to a loose fuse in the power supply. ANALYSIS OF OCCURRENCE: Technical Specification 3.3.3.7 Action 1 requires: With the number of operable accident monitoring channels less than'the required number of channels, restore the inoperable channel (s) to operable status within 7 days, or be in hot shutdown within the next 12 hours. l l s

s LER 82-034/03L CORRECTIVE ACTION: The loose fuse was properly-tightened, and the instrument was satisfactorily tested. At 0450 hours, No. 14 Steam Generator Wide Range Level Instrument was declared operable, and Limiting Condition for-Operation 3.3.3.7 Action 1 was terminated. FAILURE DATA: Not Applicable Prepared By R. Frahm /!, ,

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General Manager - Salem Operations SORC Meeting No. 82-57 i l , }}