LER-1979-011, Forwards LER 79-011/01T-0 |
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PHILADELPHIA ELECTRIC COMPAMY 2301 MARKET STREET PHILADELPHI A. PA.19101 215:841-400o March 29, 1979 Mr. Boyce H.
Grier, Director Office of Inspection and Enforcement hu31on I United States Nuclear Regulatory Commission 631 Park Avenue King of Prussia, Pennsylvania 19406 Dear Mr. Griez.
SUBJECT:
Licensee Event Repo r,t_,Na r r a t iv e Description The following occurrence was reported to Mr. Greenman, Region I, Office of Inspection and Enforcement initially on March 2, 1979 with supplemental notification on March 15, 1979.
Reference?
Docket Numbers 50-277 & 50-278 Report No:
LER 2-79-11/IT Report Da:e March 29, 1979 Occurrence Date:
March 2, 1979 Facility:
Peach Bottom Atomic Power Station Units 2 and 3 R.D.
1, Delta, PA 17314 Te_chnical Specification Reference'.
Technical Specification 6.9.2.a.(9) requires reporting "perforaance of structures, systems, or components that requires remedial action or corrective measures to prevent operation in a manner less conservative than assumed in the accident analyses in the safety analysis report..."
Description of the Event'.
An engineering review of the containment ventilation system isolation valves determined that the valves (butterfly valves) would not close from the fully open (90 degree) position when subjected to post-LOCA conditions.
Post-LOCA conditions are defined in the FSAR in Figure 14.6-10.
Valve manufacturer preliminary calculations indicated that the valves would close o
Mr. Boyce II. Grier Page 2 March 29, 1979 LER 79-11/1T under post-LOCA conditions if restricted to a maximum of 35 to 40 degrees open.
Subsequent analysis confirmed this valve to be 37 degrees open.
The valve mangfacturer confirmed that the valve body, disc and operator meet heismic requirements.
Further investigation, in;1uding inspection of the valve installation by a re p re s e n t a t ive of PECo Mechanical Engineering Division and members of the :ite Engineering Group (3/3/79), analysis by our Architect Engineer, and subsequent installation inspection by a seismic expert employed by our Architect Engineer, indicated that in some areas the valve control system could not be certified as seismically qualified.
Specifically, one component of the contro) system, a booster relay, could not be certified.
Also the analyses and inspections indicated that soue of the piping and components required additional strapping.
As a result of the initial inspection on 3/3/79, th re e valves A0 2519 (Unit 2 6 inch nitrogen inlet to drywell or torus), A0 3519 (Unit 3 6 inch nitrogen inlet to drywell or torus) and A0 3507 (Unit 3 18 inch exhaust from drywell to standby gas treatment outboard isolation valve) were found with their inflatable seal not inflated.
In each case redundant valves in the respective lines were closed with seals pressurized.
Adjustments were immediately made to the actuating bolt which operates the 2-way seal chamber p ressurizing valve.
This energized the inflatable seal and returned the valve to a fully operational closed position.
Consequences of E v e n t.'
The containment ventilation isolation valves are normally maintained in a closed position during power operation.
The only time both valves are normally opened is during inertment and de-inertment of the containment during startup and just prior to shutdown.
The probability of a LOCA occurring during these short time intervals is considered minimal.
The Technical Specifications provide for these valves to be open (aring the inerting and de-inerting op e ra t i on.
Failure of the accumulator or control components in the valve control system during a seismic event can result in depressurizing the inflatable. seal on the valve disc.
This would cause significant leakage.
I.f the control system on both the inner and outer valve f ailed 'du ring a seismic event, a containnent leak would result.
In order for this occu rre nce to have significant safety implication, a LOCA coupled with a low probability seismic event and failure of the control air system for both isolation valves in a flow path nust occur.
2233 041
M r.
Boyce H.
Grier Page 3 March 29, 1979 LER 79-ll/lT
Cause of Event
In the orig:.nal design of the plant the containment isolation valves were assumed to be in the closed position during reactor operation.
The valves were designed and built to remain closed against post-Loca p re s s u re s.
However, subsequent licensing activities resulted in the requirement for inertment of the containment and the need ts use the isolation valves during reactor operation both for inertment, and maintenance of tne Tech Spec requirement of less than 4% oxygen.
The lack of seismic certification of the cont rol air system was due to a design oversight.
The valves do not require air pressure to close (i.e.,
they are spring to close).
However, the fact that air pressure is required to maintain a leak tight pressure boundary during a seismic event was apparently overlooked during the design of the cont rol air system.
The three uninflated seals were caused by misadjustment of the linkage between the valve stem and the 2-way seal chamber p re s s u riz ing valve.
Correcti_ve Action:
Upon discovery of the inability of the valves to close from a full open position against post-LOCA conditions the valves were blocked in a closed position.
Authorization by the Station Superintendent or his alternate was, and still is, required for opening of these valves during operating conditions when primary containment is required.
Openings of these valves under such conditions are restricted to 30 degrees.
The supply pressure to the valves has been adjusted so that the valves will only open to 30 degrees.
These operations 'are addressed in a System Procedure.
Upon discovery of the seismic concern regarding the valve seal air supply a seismically designed system was installed on the containment ventilation isolation valves.
An ar.ound-the-clock effort resulted in the modification being completed by midnight March 16, 1979 on Unit 2 and by March 19, 1979 on Unit 3 (Unit 3 being shutdown for maintenance at this time).
This modification included installation of a ni t ro ge n supply bottle and related piping and valves to supply air to each valve seal.
While the system as presently modified will provide containment isolation as required, it does hamper operational flexibility.
Further modifications, designed to restore the operational flexibility are being implemented expeditiously and are expected to be completed by May 31, 1979.
The system presently includes an alarm which annunciates the valve open (i.e.
valve not fully closed position).
The modification will include revision of this alarm circuit to include a pressure switch monitoring inflatable 2233 042
Mr. Boyce H.
Grier Page 4
- March 29, 1979 LER 79-11/1T seal pressure so that the alarm will annunciate both the valve not fully closed position and improper seal pressure.
In addition a positive mechanical stop will be installed to further insure limiting the valves to 37 degrees open.
Yours truly,
/ bb 1.
( Cooney S 2erintende t Generation Division-Nuclear Attachment cc:
Director, NRC - Office of Inspection and Enforcement Mr. Norman M.
Haller, NRC - Office of >lanagement &
Program Analysis 2233 043
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| 05000277/LER-1979-001, Forwards LER 79-001/01T-0 | Forwards LER 79-001/01T-0 | | | 05000277/LER-1979-001-01, /01T-0 on 790104:design Errors in Cable Designations Were Identified.Ten Cables Found to Be Designated Nonsafeguard.Caused by Improper Designation of Cables During Design Phase.New Cable Routing Completed | /01T-0 on 790104:design Errors in Cable Designations Were Identified.Ten Cables Found to Be Designated Nonsafeguard.Caused by Improper Designation of Cables During Design Phase.New Cable Routing Completed | | | 05000278/LER-1979-001-03, /03L-0 on 790111:discovered That Recorded hi-hi Trip Valve for Steam Line Radiation Monitor Was 50 man-rem/h Greater than Tech Spec Limit & No Corrective Action Taken. Caused by Procedural Deficiency | /03L-0 on 790111:discovered That Recorded hi-hi Trip Valve for Steam Line Radiation Monitor Was 50 man-rem/h Greater than Tech Spec Limit & No Corrective Action Taken. Caused by Procedural Deficiency | | | 05000277/LER-1979-002-01, /01T-0 on 790108:cable Spreading Room Cardox Sys Disabled W/O Firewatch Present.Absence Due to Failure of Personnel to Notify Shift Supervisor Upon Work Completion | /01T-0 on 790108:cable Spreading Room Cardox Sys Disabled W/O Firewatch Present.Absence Due to Failure of Personnel to Notify Shift Supervisor Upon Work Completion | | | 05000277/LER-1979-002, Forwards LER 79-002/01T-0 | Forwards LER 79-002/01T-0 | | | 05000278/LER-1979-002-01, /01T-0 on 790108:roof Vent Stack Instantaneous Gas Release Rate Above Tech Spec Limit Due to Valve Operator Failure,Causing Loss of Inservice RHR Loop,Rise in Coolant Temp & Gaseous Release Via Core Isolation Cooling Valves | /01T-0 on 790108:roof Vent Stack Instantaneous Gas Release Rate Above Tech Spec Limit Due to Valve Operator Failure,Causing Loss of Inservice RHR Loop,Rise in Coolant Temp & Gaseous Release Via Core Isolation Cooling Valves | | | 05000278/LER-1979-002, Forwards LER 79-002/01T-0 | Forwards LER 79-002/01T-0 | | | 05000277/LER-1979-003-03, /03L-0 on 790109:2A Offgas Radiation Monitor Failed Downscale.Dirt on Contacts of Trip Test/Zero Calibr Switch Caused Input Key to Remain Deenergized Upon Release of Switch.Contacts Were Cleaned & Monitor Returned to Svc | /03L-0 on 790109:2A Offgas Radiation Monitor Failed Downscale.Dirt on Contacts of Trip Test/Zero Calibr Switch Caused Input Key to Remain Deenergized Upon Release of Switch.Contacts Were Cleaned & Monitor Returned to Svc | | | 05000278/LER-1979-003-03, /03L-0 on 790111:during Unit Shutdown for Maint an Instrument Shutoff Valve to Pressure Switch Found Closed Due to Personnel Error.Unit Operated 9 Days W/Instrument Out of Svc.Appropriate Disciplinary Action Taken | /03L-0 on 790111:during Unit Shutdown for Maint an Instrument Shutoff Valve to Pressure Switch Found Closed Due to Personnel Error.Unit Operated 9 Days W/Instrument Out of Svc.Appropriate Disciplinary Action Taken | | | 05000277/LER-1979-004-03, /04L-0 on 790112:during Surveillance Test of Cable Spreading Room Smoke Detector,Annunciator Could Not Be Reset Because It Was Not Properly Reset Previously.Detector Lead Disconnected to Reset Annunciator | /04L-0 on 790112:during Surveillance Test of Cable Spreading Room Smoke Detector,Annunciator Could Not Be Reset Because It Was Not Properly Reset Previously.Detector Lead Disconnected to Reset Annunciator | | | 05000278/LER-1979-004-03, /03L-0 on 790117:during Surveillance Test,Setpoint of PS-3-14-44D Found to Be Greater than Tech Spec Max.Caused by Setpoint Drift on static-o-ring Model 5N-AA3 Pressure Switch.Instrument Recalibrated | /03L-0 on 790117:during Surveillance Test,Setpoint of PS-3-14-44D Found to Be Greater than Tech Spec Max.Caused by Setpoint Drift on static-o-ring Model 5N-AA3 Pressure Switch.Instrument Recalibrated | | | 05000277/LER-1979-005-03, /03L-0 on 790118:at Power,Routine Surveillance Test Revealed Setpoint of DPIS-2-14-43B Was Below Tech Spec Min.Caused by Instrument DPIS-2-14-43B Being Out of Calibr Due to Setpoint Drift | /03L-0 on 790118:at Power,Routine Surveillance Test Revealed Setpoint of DPIS-2-14-43B Was Below Tech Spec Min.Caused by Instrument DPIS-2-14-43B Being Out of Calibr Due to Setpoint Drift | | | 05000278/LER-1979-005-03, /03L-0 on 790208:setpoint of Reactor Core Isolation Cooling Turbine Steam Supply Flow Sensor Was Above Tech Specs Max.Caused by Setpoint Drift on Barton Model 288 Differential Pressure Switch.Switch Recalibrated | /03L-0 on 790208:setpoint of Reactor Core Isolation Cooling Turbine Steam Supply Flow Sensor Was Above Tech Specs Max.Caused by Setpoint Drift on Barton Model 288 Differential Pressure Switch.Switch Recalibrated | | | 05000277/LER-1979-006-01, /01T-0 on 790130:recirculation Motor Generator Set Room Fire Detection Sys (Smoke Detectors) Disabled for Mod Work & Not Restored When Work Completed.Caused by Personnel Error.Sys Restored to Svc Upon Discovery | /01T-0 on 790130:recirculation Motor Generator Set Room Fire Detection Sys (Smoke Detectors) Disabled for Mod Work & Not Restored When Work Completed.Caused by Personnel Error.Sys Restored to Svc Upon Discovery | | | 05000277/LER-1979-006, Forwards LER 79-006/01T-0 | Forwards LER 79-006/01T-0 | | | 05000278/LER-1979-006-03, /03L-1 on 790212:at Power & During Surveillance Test,Setpoint of B Core Spray Pump Start Timer Was Less than Tech Spec Min.Caused by Setpoint Drift on GE Model CR-2820 Time Delay Relay.Relay Readjusted & Tested | /03L-1 on 790212:at Power & During Surveillance Test,Setpoint of B Core Spray Pump Start Timer Was Less than Tech Spec Min.Caused by Setpoint Drift on GE Model CR-2820 Time Delay Relay.Relay Readjusted & Tested | | | 05000278/LER-1979-007-03, /03L-0 on 790212:during Surveillance,Setpoint of a Logic Automatic Depressurization Sys Time Delay Relay Was Greater than Tech Spec Limit.Caused by Setpoint Drift on GE Model CR-2820 Time Delay.Relay Readjusted & Tested | /03L-0 on 790212:during Surveillance,Setpoint of a Logic Automatic Depressurization Sys Time Delay Relay Was Greater than Tech Spec Limit.Caused by Setpoint Drift on GE Model CR-2820 Time Delay.Relay Readjusted & Tested | | | 05000277/LER-1979-008-03, /03L-0 on 790225:fuses Were Blown in Control Circuit of Main Steam Relief Valve RV-71L.Replacements Blew Immediately.Caused by Failed Solenoid & Short Circuit.Leads to Solenoid Lifted;Fuses & Solenoid Replaced | /03L-0 on 790225:fuses Were Blown in Control Circuit of Main Steam Relief Valve RV-71L.Replacements Blew Immediately.Caused by Failed Solenoid & Short Circuit.Leads to Solenoid Lifted;Fuses & Solenoid Replaced | | | 05000277/LER-1979-008, Forwards LER 79-008/01T-0 | Forwards LER 79-008/01T-0 | | | 05000277/LER-1979-008-01, /01T-0 on 790219:steady State Power Level Exceeded License Limit by Less than 2% for About 6-h.Caused by Error Calculating Scanned Feedwater Flow.Power Reduced to License Limit | /01T-0 on 790219:steady State Power Level Exceeded License Limit by Less than 2% for About 6-h.Caused by Error Calculating Scanned Feedwater Flow.Power Reduced to License Limit | | | 05000277/LER-1979-009-03, /03L-0 on 790213:fire Alarm Sys Malfunctioned, Causing Audible Signal to Alarm W/O Coding.Caused by Mechanical Binding of Cam in Alarm Box.Binding Problem Corrected & Sys Returned to Svc | /03L-0 on 790213:fire Alarm Sys Malfunctioned, Causing Audible Signal to Alarm W/O Coding.Caused by Mechanical Binding of Cam in Alarm Box.Binding Problem Corrected & Sys Returned to Svc | | | 05000278/LER-1979-009-03, /03L-0 on 790307:calculated Torus Water Level Did Not Provide Proper Torus Water Vol Per Tech Spec.Caused by Failure to See Pressure Differential Between Drywell & Torus Holds Level in Downcomers Was Below Torus Level | /03L-0 on 790307:calculated Torus Water Level Did Not Provide Proper Torus Water Vol Per Tech Spec.Caused by Failure to See Pressure Differential Between Drywell & Torus Holds Level in Downcomers Was Below Torus Level | | | 05000277/LER-1979-010-01, /01T-0 on 790226:power & Control Cables Associated W/Recirculation Pump Discharge Valves & Bypass Valves Were Found Routed in non-safeguard Cable Trays.Caused by Improperly Designated Cables During Design Phase | /01T-0 on 790226:power & Control Cables Associated W/Recirculation Pump Discharge Valves & Bypass Valves Were Found Routed in non-safeguard Cable Trays.Caused by Improperly Designated Cables During Design Phase | | | 05000277/LER-1979-010, Forwards LER 79-010/01T-0 | Forwards LER 79-010/01T-0 | | | 05000278/LER-1979-011-01, /01T-0 on 790323:during Routine Insp of Drywell & Torus Ventilation Valves,Inflatable Disc Seals Were Found Depressurized.Caused by Procedural Deficiency Following Mod to Drywell & Torus Vent Valves.Procedures Revised | /01T-0 on 790323:during Routine Insp of Drywell & Torus Ventilation Valves,Inflatable Disc Seals Were Found Depressurized.Caused by Procedural Deficiency Following Mod to Drywell & Torus Vent Valves.Procedures Revised | | | 05000278/LER-1979-011, Forwards LER 79-011/01T-0 | Forwards LER 79-011/01T-0 | | | 05000277/LER-1979-011-01, /01T-0 on 790302:engineering Review Determined Certain Containment Isolation Valves Incapable of Closing Against LOCA Pressure.Caused by Design Oversight.Future Mod to Expand Valve Open Alarm to Include Seal Low Pressure | /01T-0 on 790302:engineering Review Determined Certain Containment Isolation Valves Incapable of Closing Against LOCA Pressure.Caused by Design Oversight.Future Mod to Expand Valve Open Alarm to Include Seal Low Pressure | | | 05000277/LER-1979-011, Forwards LER 79-011/01T-0 | Forwards LER 79-011/01T-0 | | | 05000278/LER-1979-013-01, /01T-0 on 790613:main Steam Relief Valve RV3-2-71L Lifted,Causing Torus Water Vol to Exceed Tech Spec Limit by 2.6%.Reactor Manually Scrammed.Valve Replaced & Sent to Wiley Lab to Determine Cause for Failure | /01T-0 on 790613:main Steam Relief Valve RV3-2-71L Lifted,Causing Torus Water Vol to Exceed Tech Spec Limit by 2.6%.Reactor Manually Scrammed.Valve Replaced & Sent to Wiley Lab to Determine Cause for Failure | | | 05000278/LER-1979-013, Forwards LER 79-013/01T-0 | Forwards LER 79-013/01T-0 | | | 05000278/LER-1979-014, /O3L-0 on 790522:offsite Source Breaker SU25 Tripped on Low Air Pressure.Caused by Short Circuit in Light Socket & Dirty Contacts on Voltage Relay.Relay Contacts Cleaned & Socket Removed Pending Replacement | /O3L-0 on 790522:offsite Source Breaker SU25 Tripped on Low Air Pressure.Caused by Short Circuit in Light Socket & Dirty Contacts on Voltage Relay.Relay Contacts Cleaned & Socket Removed Pending Replacement | | | 05000277/LER-1979-014-03, /03L-0 on 790327:trip Setpoint Drift of Drywell High Pressure Switch Was Beyond Tech Spec Limit.Caused by Static-O-Ring Model 12N-AA4 Being Out of Calibr Due to Setpoint Drift.It Was Recalibrated & Returned to Svc | /03L-0 on 790327:trip Setpoint Drift of Drywell High Pressure Switch Was Beyond Tech Spec Limit.Caused by Static-O-Ring Model 12N-AA4 Being Out of Calibr Due to Setpoint Drift.It Was Recalibrated & Returned to Svc | | | 05000278/LER-1979-015, /O3L-0 on 790523:automatic Depressurization Sys a Auto Blowdown Timer Trip Setting Found 13-s Less than Tech Spec Min.Caused by Setpoint Drift of Time Delay Relay.Relay Readjusted,Tested & Returned to Svc | /O3L-0 on 790523:automatic Depressurization Sys a Auto Blowdown Timer Trip Setting Found 13-s Less than Tech Spec Min.Caused by Setpoint Drift of Time Delay Relay.Relay Readjusted,Tested & Returned to Svc | | | 05000278/LER-1979-016-03, /03L-0 on 790628:while at Power,Routine Surveillance Test Revealed Setpoint of Switch 2 Was Below Tech Spec Min.Caused by Barton Model 288 Instrument Out of Calibr from Drift.Instrument Recalibr | /03L-0 on 790628:while at Power,Routine Surveillance Test Revealed Setpoint of Switch 2 Was Below Tech Spec Min.Caused by Barton Model 288 Instrument Out of Calibr from Drift.Instrument Recalibr | | | 05000278/LER-1979-017-31, /03L-0 on 790615:while Reactor Subcritical,D Main Steam Line Radiation Monitor Hi-Hi Trip Failed.Caused by Dirty Trip Relay or Dirty Test Switch Contacts. Condition Corrected by Repeated Testing | /03L-0 on 790615:while Reactor Subcritical,D Main Steam Line Radiation Monitor Hi-Hi Trip Failed.Caused by Dirty Trip Relay or Dirty Test Switch Contacts. Condition Corrected by Repeated Testing | | | 05000278/LER-1979-017, Discusses LER 79-017/03L-0.While Reactor Subcritical & Less than 212 F,Main Steam Line D Radiation Monitor Hi-Hi Trip Failed.Caused by Dirty Trip Relay or Dirty Test Switch Contacts.Repeated Testing Corrected Condition | Discusses LER 79-017/03L-0.While Reactor Subcritical & Less than 212 F,Main Steam Line D Radiation Monitor Hi-Hi Trip Failed.Caused by Dirty Trip Relay or Dirty Test Switch Contacts.Repeated Testing Corrected Condition | | | 05000278/LER-1979-018-03, /03L-0 on 790630:during Surveillance Testing, Reactor Water Sample Line Isolation Valve Failed to Close. Caused by Lack of Valve Operator Spring Tension.Valve Operator Spring Tension Was Increased | /03L-0 on 790630:during Surveillance Testing, Reactor Water Sample Line Isolation Valve Failed to Close. Caused by Lack of Valve Operator Spring Tension.Valve Operator Spring Tension Was Increased | | | 05000277/LER-1979-019-03, /03L-0 on 790501:during Surveillance Testing of Normally Open Primary Containment Isolation Valves,Four Oxygen Analyzer Sys Isolation Valves Failed to Close.Caused by Binding of Pistons in Valve Bodies.Valve Parts Rebuilt | /03L-0 on 790501:during Surveillance Testing of Normally Open Primary Containment Isolation Valves,Four Oxygen Analyzer Sys Isolation Valves Failed to Close.Caused by Binding of Pistons in Valve Bodies.Valve Parts Rebuilt | | | 05000278/LER-1979-019-01, /01T-0 on 790621:during Seismic Support Insp Program, Reactor Core Isolation Cooling Piping Anchor Discovered to Have Two Bolts That Could Not Be Torqued. Caused by Improper Installation of Bolt Shells | /01T-0 on 790621:during Seismic Support Insp Program, Reactor Core Isolation Cooling Piping Anchor Discovered to Have Two Bolts That Could Not Be Torqued. Caused by Improper Installation of Bolt Shells | | | 05000278/LER-1979-019, Forwards LER 79-019/01T-0 | Forwards LER 79-019/01T-0 | | | 05000277/LER-1979-020-03, /03L-0 on 790503:solution Temp in Standby Liquid Control Sys Found to Be 2 F Less than Tech Spec Requirement for Existing Boron Concentration.Caused by Incorrect Acceptable Temp Controller Setpoint Range | /03L-0 on 790503:solution Temp in Standby Liquid Control Sys Found to Be 2 F Less than Tech Spec Requirement for Existing Boron Concentration.Caused by Incorrect Acceptable Temp Controller Setpoint Range | | | 05000278/LER-1979-020-01, /01T-0 on 790621:radioactive Release Rate at Main Stack During Plant Startup Exceeded Tech Specs.Caused by Deficiency in Procedure for Depressurization Following Shutdown.Investigation Underway to Improve Procedure | /01T-0 on 790621:radioactive Release Rate at Main Stack During Plant Startup Exceeded Tech Specs.Caused by Deficiency in Procedure for Depressurization Following Shutdown.Investigation Underway to Improve Procedure | | | 05000278/LER-1979-020, Forwards LER 79-020/01T-0 | Forwards LER 79-020/01T-0 | | | 05000278/LER-1979-021-03, /03X-1:on 790630,during Surveillance Testing,Main Steam Sample Line Inboard Isolation Valve Failed to Close. Probably Caused by Valve Packing Binding or Solenoid Valve Sticking While Valve Was at High Temp | /03X-1:on 790630,during Surveillance Testing,Main Steam Sample Line Inboard Isolation Valve Failed to Close. Probably Caused by Valve Packing Binding or Solenoid Valve Sticking While Valve Was at High Temp | | | 05000277/LER-1979-022-03, /03L-0 on 790513:fire Hose Nozzles Were Missing from Two Hose Stations in Turbine Bldg.Cause Not Noted. Nozzles Replaced & Wrench Tightened to Inhibit Removal | /03L-0 on 790513:fire Hose Nozzles Were Missing from Two Hose Stations in Turbine Bldg.Cause Not Noted. Nozzles Replaced & Wrench Tightened to Inhibit Removal | | | 05000278/LER-1979-022-03, /03L-0 on 790719:annunciator Sys II Drywell Pressure Permits Containment Spray Alarmed During Routine Startup.Caused by Failure of Diaphragm on PS-3-10-119D. Switch Repaired,Tested & Returned to Svc within Five Days | /03L-0 on 790719:annunciator Sys II Drywell Pressure Permits Containment Spray Alarmed During Routine Startup.Caused by Failure of Diaphragm on PS-3-10-119D. Switch Repaired,Tested & Returned to Svc within Five Days | | | 05000277/LER-1979-023-01, /01T-0 on 790724:insp Program Performed in Response to IE Bulletin 79-02 Identified Two Anchors in One Support Which Failed to Torque Test Properly.Caused by Improper Installation.Anchors Replaced | /01T-0 on 790724:insp Program Performed in Response to IE Bulletin 79-02 Identified Two Anchors in One Support Which Failed to Torque Test Properly.Caused by Improper Installation.Anchors Replaced | | | 05000277/LER-1979-023, Forwards LER 79-023/01T-0 | Forwards LER 79-023/01T-0 | | | 05000277/LER-1979-023-04, /04T-0 on 790515:routine Ph Analysis of Sewage Plant Effluent Identified Ph of 5.8 Which Exceeded Tech Specs.Caused by Air Blower Failure Which Allowed Dissolved Oxygen to Drop to 0 & Aeration Tank to Become Anaerobic | /04T-0 on 790515:routine Ph Analysis of Sewage Plant Effluent Identified Ph of 5.8 Which Exceeded Tech Specs.Caused by Air Blower Failure Which Allowed Dissolved Oxygen to Drop to 0 & Aeration Tank to Become Anaerobic | | | 05000277/LER-1979-024, Forwards LER 79-024/01T-0 | Forwards LER 79-024/01T-0 | |
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