ML17348B333

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Monthly Operating Repts for Dec 1991 for Turkey Point Units 3 & 4.W/920115 Ltr
ML17348B333
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 12/31/1991
From: Knorr J, Plunkett T, Tierney R
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-92-009, L-92-9, NUDOCS 9201220222
Download: ML17348B333 (15)


Text

ACCELERATED DI< RIBUTION DEMONS 4.TION SYSTEM

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REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9201220222 DOC.DATE: 91/12/31 NOTARIZED: NO DOCKET g FACIL:50-250 Turkey Point Plant, Unit 3, Florida Power and Light C 05000250 50-251 Turkey Point Plant, Unit 4, Florida Power and Light C 05000251 AUTH. NAME AUTHOR AFFILIATION TIERNEY,R.A. Florida Power 6 Light Co.

PLUNKETTE,T.F. Florida Power & Light Co.

RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

Monthly operating repts for Dec 1991 for Turkey Point Units 3 6 4.W/920115 ltr. D DISTRIBUTION CODE: IE24D COPIES RECEIVED:LTR

/ ENCL 2 SIZE:

TITLE: Monthly Operating Report (per Tech Specs)

NOTES RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL D PD2-2 LA 3 3 PD2-2 PD 1 1 AULUCK,R 1 1 D INTERNAL'EOD/DOA 1 1 AEOD/DSP/TPAB 1 1 NRR/DLPQ LPEB10 1 1 NRR/DOEA/OEAB 1 1 REG . = 01 1 1 RGN2 1 1 EXTERNAL: E GG BRYCE,J.H 1 1 NRC PDR 1 1 NSI 1 1 D

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D NOTE TO ALI. "RIDS" RECIPIENTS: k S

PLEASE HELP US TO REDUCE WASfE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

TOTAL NUMBER OF COPIES REQUIRED: LTTR 14 ENCL 14 go<

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.0. Box 029100, Miami, FL, 33102-9100 JAN 15 l992 gi Ct L-92-009 10 CFR 50.36 U. S ~ Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Gentlemen:

RE: Turkey Point Units 3 and 4 Docket Nos. 50-250 and 50-251 Monthl 0 eratin Re ort In accordance with the requirements of Turkey Point Units 3 and 4 Technical Specification 6.9.1.5, and the guidance of NUREG 0020, attached are the December 1991 Operating Status and Summary of Operating Experience Reports for Turkey Point Units 3 and 4.

Very truly yours, T. F. Plunkett Vice President Turkey Point Nuclear TFP/DRP/RAT attachments cc: Stewart D. Ebneter, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant 9201220222 911231 PDR AGQCK 05000250 R

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AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-250 UNIT Turke Point 3 DATE Januaz 15 1992 COMPLETED BY R. A. Tierne TELEPHONE 305 246-6970 MONTH December 1991 AVERAGE DAILY POWER LEVEL (MWe-Net) 12/01/91 688 12/02/91 686 12/03/91 684 12/04/91 684 12/05/91 697 12/06/91 703 12/07/91 699 12/08/91 694 12/09/91 696 12/10/91 690 12/11/91 682 12/12/91 686 12/13/91 685 12/14/91 684 12/15/91 683 12/16/91 688 12/17/91 699 12/18/91 702 12/19/91 704 12/20/91 706 12/21/91 709 12/22/91 705 12/23/91 700 12/24/91 696 12/25/91 694 12/26/91 690 12/27/91 688 12/28/91 689 12/29/91 691 12/30/91 690 12/31/91 695

OPERATING DATA REPORT DOCKET NO 50 - 250 DATE 1/ 9/92 COMPLETED BY R.A. TIERNEY TELEPHONE 305/246/1300 OPERATING STATUS

1. UNIT NAME: TURKEY POINT UNIT 3
2. REPORTING PERIOD: DECEMBER 1991
3. LICENSED THERMAL POWER (MWT): 2200
4. NAMEPLATE RATING (GROSS MWE): 760
5. DESIGN ELECTRICAL RATING (NET MWE): 693
6. MAXIMUM DEPENDABLE CAPACITY (GROSS MWE): 699
7. MAXIMUM DEPENDABLE CAPACITY (NET MWE): 666
8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7)

SINCE LAST REPORT, GIVE REASONS:

9. POWER LEVEL TO WHICH RESTRICTED IF ANY (NET MWE)

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10. REASONS FOR RESTRICTIONS, IF ANY:

MONTHLY -YTD- CUMULATIVE

11. HOURS IN REPORT PERIOD: 744 8760 167193. 6
12. NUMBER OF HOURS REACTOR WAS CRITICAL 744.0 2252.1 106725.3
13. REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 844.4
14. HOURS GENERATOR ON-LINE 744.0 2155. 8 10521 1. 5
15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 121.8
16. GROSS THERMAL ENERGY GENERATED (MWH) 1639202 4338424 218570066
17. GROSS ELECTRICAL ENERGY GENERATED (MWH) 540325 1402395 70018386
18. NET ELECTRICAL ENERGY GENERATED (MWH) 515636 1314568 66193086
19. UNIT SERVICE FACTOR 100. 0 24.6 62.9
20. UNIT AVAILABIL'ITY FACTOR 100.0 24.6 63.0
21. CAPACITY FACTOR (USING MDC NET) 104. 1 22.5 60.6
22. CAPACITY FACTOR (USING DER NET) 100. 0 21.7 57. 1
23. UNIT FORCED OUTAGE RATE 0.0 1.2 12.3
24. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS
25. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:

UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50 -250 UNlT NAME Turke Point 3 DATE Januar 15 1992 COMPLETED BY J. E. Knorr REPORT MONTH December 1991 TELEPHONE 305 246-6757 Date Type Duration (Hours)

Reason'ethod ot Shutting Reactor'censee Down Event Report¹ System Code'ause Code'omponent 8 Conective Action to Prevent Recurrence Unit 3 operated at essentially full power and had no shutdowns or significant power reductions.

F Forced Reason Method Exhibit G - Instructions S Scheduled A - Equipment Failure (Exp) 1 - Manual for Preparation of Data B - Maintenance or Test 2- Manual Scram Entry Sheets Licensee C - Refueling 3 - Automatic Scram Event Report (LER) File D - Regulatory restriction 4 - Continued (NUREG-0161)

E - Operator Training 5- Load Reduction Examination 9 - Other (Explain) 5 fi'icense F - Administrative Exhibit 1 - Same Source G - Operational Error (Explain)

H - Other (Explain)

SUMMARY

OF OPERATING EXPERIENCE DOCKET NO. 50-250 UNIT Turke Point 3 DATE Janua 15 1992 COMPLETED BY R. A. Tierne TELEPHONE 305 246-6970 REPORT MONTH December 1991 Unit 3 operated during the month of December at essentially full power. The unit had no shutdowns or significant power reductions during the period.

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-251 UNIT Turke Point 4 DATE Janua 15 1992 COMPLETED BY R. A. Tierne TELEPHONE 305 246-6970 MONTH December 1991 AVERAGE DAILY POWER LEVEL (MWe-Net) 12/01/91 675 12/02/91 674 12/03/91 673 12/04/91 672 12/05/91 685 12/06/91 687 12/07/91 680 12/08/91 678 12/09/91 679 12/10/91 515 12/11/91 0 12/12/91 0 12/13/91 0 12/14/91 0 12/15/91 0 12/16/91 0 12/17/91 0 12/18/91 23 12/19/91 321 12/20/91 691 12/21/91 699 12/22/91 696 12/23/91 692 12/24/91 690 12/25/91 690 12/26/91 686 12/27/91 684 12/28/91 684 12/29/91 685 12/30/91 686 12/31/91 694

OPERATING DATA REPORT DOCKET NO 50 - 251 DATE 1/ 9/92 COMPLETED BY R.A. TIERNEY TELEPHONE 305/246/1300 OPERATING STATUS

1. UNIT NAME: TURKEY POINT UNIT 4
2. REPORTING PERIOD: DECEMBER 1991
3. LICENSED THERMAL POWER (MWT): 2200
4. NAMEPLATE RATING (GROSS MWE): 760
5. DESIGN ELECTRICAL RATING (NET MWE): 693
6. MAXIMUM DEPENDABLE CAPACITY (GROSS MWE): 699
7. MAXIMUM DEPENDABLE CAPACITY (NET MWE): 666
8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7)

SINCE LAST REPORT, GIVE REASONS:

9. POWER LEVEL TO WHICH RESTRICTED, IF ANY (NET MWE)
10. REASONS FOR RESTRICTIONS, IF ANY:

MONTHLY -YTD- CUMULATIVE

11. HOURS IN REPORT PERIOD: 744 8760 160925.0
12. NUMBER OF HOURS REACTOR WAS CRITICAL 561. 7 1426.3 102612. 6
13. REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 166.6
14. HOURS GENERATOR ON-LINE 553.5 1336.3 98903.4
15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 32. 1
16. GROSS THERMAL ENERGY GENERATED (MWH) 1182788 2684277 208314337
17. GROSS ELECTRICAL ENERGY GENERATED (MWH) 384300 859430 66472310
18. NET ELECTRICAL ENERGY GENERATED (MWH) 363283 798134 62851762
19. UNIT SERVICE FACTOR 74.4 15. 3 61.5
20. UNIT AVAILABILITYFACTOR 74.4 15.3 61.5
21. CAPACITY FACTOR (USING MDC NET) 73.3 13. 7 59.7
22. CAPACITY FACTOR (USING DER NET) 70.5 13. 1 56.4
23. UNIT FORCED OUTAGE RATE 4.2 1.8 11.8
24. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS
25. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:

UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50 251 UNIT NAME Turke Point 4 DATE Januar 15 1992 COMPLETED BY J. E. Knorr REPORT MONTH December 1991 TELEPHONE 305 246-6757 Date Type Duration Method or System Cause tt Corrective Shutting Code'omponent Codes (Hours) Event Action to Reactor'censee Down Report¹ Prevent Recurrence 06 911210 F 24.5 251-91-007 EK DG Unit 4 shutdown due to Load Sequencer Failure.

07 911211 S 164.6 B N/A IG PEN Unit 4 conoseal repair.

08 911219 S 1.4 B N/A TA TRB Unit 4 Turbine overspeed test.

F Forced Reason Method Exhibit G - Instructions S Scheduled A - Equipment Failure (Exp) 1 - Manual for Preparation of Data B - Maintenance or Test 2- Manual Scram Entry Sheets Licensee C - Refueling 3 - Automatic Scram Event Report (LER) File D - Regulatory restriction 4 - Continued (NUREG-0161)

E - Operator Training & 5 - Load Reduction License Examination 9 - Other (Explain) 5 F - Administrative Exhibit 1 - Same Source G - Operational Error (Explain)

H - Other (Explain)

SUMMARY

OF OPERATING EXPERIENCE DOCKET NO. 50-251 UNIT Turke Point 4 DATE Januar 15 1992 COMPLETED BY R. A. Tierne TELEPHONE 305 246-6970 REPORT MONTH December 1991 On December 10, 1991, after the failure of an output card on the 4A sequencer, the plant was shutdown due to the inoperability of the sequencer. This event is discussed in detail in LER 251 91-007.

During an inspection of the reactor vessel on December 11, a conoseal was found to have some evidence of leakage. The conoseal was repaired. On December 18, during the startup process, a hold at less than 30% power occurred due to secondary system water chemistry and a turbine overspeed test.

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