Insp Rept 50-255/98-07 on 980413-1023.One Apparent Violation Be Considered for Escalated Enforcement Action.Major Areas Inspected:Review of Events,Circumstances & Licensee Investigation of TS Surveillance Refueling TestML18066A324 |
Person / Time |
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Site: |
Palisades |
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Issue date: |
11/12/1998 |
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From: |
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
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To: |
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Shared Package |
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ML18066A323 |
List: |
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References |
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50-255-98-07, 50-255-98-7, NUDOCS 9811170210 |
Download: ML18066A324 (11) |
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Category:INSPECTION REPORT
MONTHYEARIR 05000255/20240122024-11-12012 November 2024 Restart Inspection Report 05000255/2024012 IR 05000255/20244022024-09-0606 September 2024 Public: Palisades Nuclear Plant - Decommissioning Security Inspection Report 05000255/2024402 IR 05000255/20240022024-08-0909 August 2024 NRC Inspection Report No. 05000255/2024002 IR 05000255/20240112024-07-15015 July 2024 Nuclear Plant - Restart Inspection Report 05000255/2024011 IR 05000255/20240012024-05-10010 May 2024 NRC Inspection Report No. 05000255/2024001 IR 05000255/20244012024-04-0909 April 2024 – Decommissioning Security Inspection Report 05000255/2024401 IR 05000255/20240102024-03-20020 March 2024 Plant Reference Simulator Inspection Report 05000255/2024010 IR 05000255/20230042024-02-20020 February 2024 NRC Inspection Report 05000255/2023004(DRSS) Holtec Decommissioning International, LLC, Palisades Nuclear Plant IR 05000255/20230032023-10-0404 October 2023 NRC Inspection Report No. 05000255/2023003(DRSS)-Holtec Decommissioning International, LLC, Palisades Nuclear Plant IR 05000255/20230022023-07-19019 July 2023 NRC Inspection Report 05000255/2023002 DRSS-Holtec Decommissioning International, LLC, Palisades Nuclear Plant IR 05000255/20220032022-12-28028 December 2022 NRC Inspection Report No. 05000255/2022003(DRSS); 07200007/2022001 (Drss) – Holtec Decommissioning International, LLC, Palisades Nuclear Plant IR 05000255/20224012022-11-0909 November 2022 Decommissioning Palisades Nuclear Plant - Decommissioning Security Inspection Report 05000255/2022401 IR 05000255/20220022022-08-0303 August 2022 Integrated Inspection Report 05000255/2022002 IR 05000255/20220012022-05-13013 May 2022 Integrated Inspection Report 05000255/2022001 IR 05000255/20220102022-04-0101 April 2022 Triennial Inspection of Evaluation of Changes, Tests and Experiments Baseline Inspection Report 05000255/2022010 IR 05000255/20210062022-03-0202 March 2022 Annual Assessment Letter for Palisades Nuclear Plant, Unit 1, (Report 05000255/2021006) IR 05000255/20210102022-02-24024 February 2022 Triennial Fire Protection Inspection Report 05000255/2021010 IR 05000255/20210042022-02-0808 February 2022 Integrated Inspection Report 05000255/2021004 and Exercise of Enforcement Discretion IR 05000255/20214042021-11-15015 November 2021 NRC Independent Spent Fuel Storage Installation Security Inspection Report 05000255/2021404 and 07200007/2021401 IR 05000255/20210032021-11-0303 November 2021 Integrated Inspection Report 05000255/2021003 IR 05000255/20214032021-10-21021 October 2021 Material Control and Accounting Program Inspection Report 05000255/2021403 IR 05000255/20214022021-10-0606 October 2021 Security Baseline Inspection Report 05000255/2021402 IR 05000255/20210052021-09-0101 September 2021 Updated Inspection Plan for Palisades Nuclear Plant (Report 05000255/2021005) IR 05000255/20210022021-08-10010 August 2021 Integrated Inspection Report 05000255/2021002 ML21197A0322021-07-21021 July 2021 Review of the Fall 2020 Steam Generator Tube Inspection Report IR 05000255/20210012021-05-12012 May 2021 Integrated Inspection Report 05000255/2021001 IR 05000255/20214012021-04-14014 April 2021 Security Baseline Inspection Report 05000255/2021401 IR 05000255/20200062021-03-0404 March 2021 Annual Assessment Letter for Palisades Nuclear Plant (Report 05000255/2020006) IR 05000255/20200042021-02-11011 February 2021 Integrated Inspection Report 05000255/2020004 IR 05000255/20204012021-01-0606 January 2021 Security Baseline Inspection Report 05000255/2020401 IR 05000255/20204202020-12-10010 December 2020 Security Inspection Report 05000255/2020420 ML20342A1812020-12-10010 December 2020 Security Inspection Report Cover Letter 05000255/2020420 IR 05000255/20204022020-11-30030 November 2020 Cyber Security Inspection Report 05000255/2020402 IR 05000255/20205012020-11-20020 November 2020 Emergency Preparedness Inspection Report 05000255/2020501 IR 05000255/20200032020-11-13013 November 2020 Integrated Inspection Report 05000255/2020003 IR 05000255/20200052020-09-0101 September 2020 Updated Inspection Plan for Palisades Nuclear Plant (Report 05000255/2020005) IR 05000255/20200102020-08-24024 August 2020 Biennial Problem Identification and Resolution Inspection Report 05000255/2020010 IR 05000255/20203012020-08-13013 August 2020 NRC Initial License Examination Report 05000255/2020301 IR 05000255/20200022020-08-11011 August 2020 Integrated Inspection Report 05000255/2020002 and Exercise of Enforcement Discretion IR 05000255/20200012020-05-12012 May 2020 Integrated Inspection Report 05000255/2020001 IR 05000255/20010082020-05-12012 May 2020 Final ASP Analysis - Palisades (IR 050002552001008) IR 05000255/20200112020-04-21021 April 2020 Design Basis Assurance Inspection (Teams) Inspection Report 05000255/2020011 IR 05000254/20204012020-03-23023 March 2020 Security Baseline Inspection Report 05000254/2020401 and 05000265/2020401 IR 05000255/20190062020-03-0303 March 2020 Annual Assessment Letter Palisades Nuclear Plant (Report 05000255/2019006) IR 05000255/20190042020-01-28028 January 2020 Integrated Inspection Report 05000255/2019004 and 07200007/2019001 ML19357A2752019-12-23023 December 2019 Request for Information for an NRC Triennial Baseline Design Bases Assurance Inspection (Team); Inspection Report 05000255/2020011 IR 05000255/20194112019-11-25025 November 2019 Security Baseline Inspection Report 05000255/2019411 and Independent Spent Fuel Storage Security Inspection Report 07200007/2019401 (Cover Letter Only) (DRS-M.Ziolkowski) IR 05000255/20190032019-11-14014 November 2019 Integrated Inspection Report 05000255/2019003 ML19294A2872019-10-21021 October 2019 Design Basis Assurance Inspection (Programs) Inspection Report 05000255/2019010 IR 05000255/20190052019-08-28028 August 2019 Updated Inspection Plan for Palisades Nuclear Plant, Unit 1 (Report 05000255/2019005) 2024-09-06
[Table view] Category:NRC-GENERATED
MONTHYEARIR 05000255/19990101999-10-13013 October 1999 Insp Rept 50-255/99-10 on 990812-0921.One Violation Noted & Being Treated as Ncv.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000255/19990141999-09-23023 September 1999 Insp Rept 50-255/99-14 on 990831-0901.No Violations Noted. Major Areas Inspected:Review of Chemical & Radiological Services Dept on-line Planning & Scheduling Program IR 05000255/19990091999-09-0303 September 1999 Insp Rept 50-255/99-09 on 990522-0811.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000255/19990081999-07-13013 July 1999 Insp Rept 50-255/99-08 on 990522-0630.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000255/19990041999-06-0404 June 1999 Insp Rept 50-255/99-04 on 990410-0521.No Violations Noted. Major Areas Inspected:Operations,Maint Engineering & Plant Support IR 05000255/19990061999-06-0303 June 1999 Insp Rept 50-255/99-06 on 990506-12.Three Violations Noted & Being Treated as non-cited Violations.Major Areas Inspected: Effectiveness of Radiation Protection Program IR 05000255/19990051999-05-19019 May 1999 Insp Rept 50-255/99-05 on 990503-06.Violations Noted.Major Areas Inspected:Activities Associated with GL 96-05, Periodic Verification of Design-Basis Capability of Safety- Related Movs IR 05000255/19990031999-04-23023 April 1999 Insp Rept 50-255/99-03 on 990226-0409.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000255/19990011999-03-0505 March 1999 Insp Rept 50-255/99-01 on 990112-0225.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML18066A4101999-02-0505 February 1999 Insp Rept 50-255/98-22 on 981126-990112.Violations Noted. Major Areas Inspected:Licensee Operations,Engineering & Plant Support IR 05000255/19990021999-02-0505 February 1999 Partially Withheld Insp Rept 50-255/99-02 on 990119-22. Violations Noted.Major Areas Inspected:Status of Security Facilities & Equipment,Testing & Maintenance,Protected Area Detection & Assessment Aids IR 05000255/19980211998-12-29029 December 1998 Insp Rept 50-255/98-21 on 981130-1204.No Violations Noted. Major Areas Inspected:Licensee Performance During Plant Biennial Exercise of Emergency Plan IR 05000255/19980191998-12-14014 December 1998 Insp Rept 50-255/98-19 on 981008-1125.No Violations Noted. Major Areas Inspected:Licensee Operations,Engineering & Plant Support IR 05000255/19980201998-11-24024 November 1998 Insp Rept 50-255/98-20 on 981026-30.No Violations Noted. Major Areas Inspected:Review Evaluation of Shipping Cask Used in Transportation Incident Wherein Class 7 Radioactive Matl Shipment,Exceeded NRC & DOT Limits for Radiation IR 05000255/19980071998-11-12012 November 1998 Insp Rept 50-255/98-07 on 980413-1023.One Apparent Violation Be Considered for Escalated Enforcement Action.Major Areas Inspected:Review of Events,Circumstances & Licensee Investigation of TS Surveillance Refueling Test IR 05000255/19980171998-11-0505 November 1998 Insp Rept 50-255/98-17 on 980821-1007.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000255/19980181998-10-0101 October 1998 Insp Rept 50-255/98-18 on 980824-0902.One Violation Being Considered for Escalated Enforcement Action.Major Areas Inspected:Review Transportation Incident in Which Class 7 Radioactive Package,Shipped on Open Transport Vehicle ML18068A4741998-09-18018 September 1998 Insp Rept 50-255/98-15 on 980702-0821.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support Re Fire Brigade Response to Minor Electrical Fire Wearing Appropriate Safety Gear in Timely Manner IR 05000255/19980121998-09-0202 September 1998 Insp Rept 50-255/98-12 on 980706-24.No Violations Noted. Major Areas Inspected:Engineering IR 05000255/19980161998-08-28028 August 1998 Insp Rept 50-255/98-16 on 980810-14.No Violations Noted. Major Areas Inspected:Review of Emergency Preparedness Program,As Aspect of Plant Support IR 05000255/19980131998-08-0707 August 1998 Insp Rept 50-255/98-13 on 980720-22 & 27-29.No Violations Noted.Major Areas Inspected:Reviewed Fire Protection Program,Aspect of Plant Support ML18066A2601998-07-30030 July 1998 Insp Rept 50-255/98-10 on 980507-0701.Violation Noted,Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000255/19980141998-07-29029 July 1998 Insp Rept 50-255/98-14 on 980707-10.No Violations Noted. Major Areas Inspected:Review of Planning & Radiological Controls for Resin Sluice,Calibration of Personal Contamination Monitors & Mgt & Operation of Area IR 05000255/19980111998-07-0202 July 1998 Insp Rept 50-255/98-11 on 980518-0604.No Violations Noted. Major Areas Inspected:Licensee C/As & Engineering Involvement in C/A Process ML18066A1951998-06-15015 June 1998 Insp Rept 50-255/98-09 on 980504-0601.Violations Noted.Major Areas Inspected:Control of Plant Radiological Conditions, Development of RWP & Planning to Ensure That Radiation Exposure During Recent Refueling Outage Was ALARA IR 05000255/19980061998-06-12012 June 1998 Insp Rept 50-255/98-06 on 980504-08 & 11-14.No Violations Noted.Major Areas Inspected:Maint & Engineering ML18066A1911998-06-11011 June 1998 Insp Rept 50-255/98-05 on 980314-0506.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000255/19980081998-05-28028 May 1998 Partially Withheld Insp Rept 50-255/98-08 on 980504-08 (Ref 10CFR73.71).No Violations Noted.Major Areas Inspected: Effectiveness of Access Control Functions & Testing & Maint Activities Related to Security Equipment ML18066A2131998-05-18018 May 1998 Insp Rept 50-255/98-03 on 980325-0410.Violations Noted.Major Areas Inspected:Engineering ML18065B2491998-05-18018 May 1998 Insp Rept 50-255/98-04 on 980325-0401.Violations Noted.Major Areas Inspected:Review of Training Procedures,Written & Operating Exam Matl & Observation & Evaluation of Operator Performance & Licensee Evaluators During Exam ML18065B2161998-04-16016 April 1998 Insp Rept 50-255/98-02 on 980128-0313.Violation Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML18065B1681998-02-26026 February 1998 Insp Rept 50-255/97-18 on 971206-980127.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000255/19970161998-02-0202 February 1998 Insp Rept 50-255/97-16 on 971212-19 & 980114-16.Violation Noted.Major Areas Inspected:Control Room Habitability Sys, Respiratory Protection Program,Plant Water Quality,Chemistry Program,Fuel Monitoring,Post Accident Sample Monitoring Sys ML18065B1481998-01-21021 January 1998 Insp Rept 50-255/97-13 on 971018-1205.Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Maint, Engineering & Plant Support IR 05000255/19970171998-01-12012 January 1998 Insp Rept 50-255/97-17 on 971210-11.No Violations Noted. Major Areas Inspected:Maint & Matl Condition of Facilities & Equipment,Miscellaneous Maint Issues & Mgt Meetings IR 05000255/19972011997-12-30030 December 1997 Insp Rept 50-255/97-201 on 970916-1114.Deficiencies Identified in Control & Performance of Calculations.Purpose of Insp Was to Evaluate Capability of Selected Sys to Perform Safety Functions Required by Design Bases ML18065B1281997-12-19019 December 1997 Insp Rept 50-255/97-11 on 970828-1017.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML18065B1241997-12-13013 December 1997 Insp Rept 50-255/97-15 on 971105-07.Violations Noted.Major Areas Inspected:High Radiation Area Posting Incident, Radiation Protection Training,Corrective Action Program & Communication of Radiation Protection Expectations of Staff IR 05000255/19970141997-12-12012 December 1997 Insp Rept 50-255/97-14 on 971028-1119.Apparent Violations Being Considered for Escalated Enforcement Action.Major Areas Inspected:Operations & Maint IR 05000255/19970121997-10-25025 October 1997 Insp Rept 50-255/97-12 on 970922-26.No Violations Noted. Major Areas Inspected:Implementation of Radiological Effluents & Radiological Environ Monitoring Programs IR 05000255/19970091997-10-14014 October 1997 Insp Rept 50-255/97-09 on 970708-0827.No Violations Noted. Major Areas Inspected:Operations,Maint & Engineering ML18067A6891997-09-0505 September 1997 Insp Rept 50-255/97-08 on 970524-0707.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000255/19970101997-09-0101 September 1997 Insp Rept 50-255/97-10 on 970804-08.No Violations Noted. Major Areas Inspected:Review of Implementation of Solid Radioactive Waste Mgt & Shipping Program IR 05000255/19970061997-07-0909 July 1997 Insp Rept 50-255/97-06 on 970412-0523.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML18067A5951997-06-17017 June 1997 Insp Rept 50-255/97-05 on 970301-0411.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000255/19970021997-04-22022 April 1997 Insp Rept 50-255/97-02 on 970111-0303.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000255/19960171997-02-20020 February 1997 Insp Rept 50-255/96-17 on 961124-970110.Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000255/19960141997-01-22022 January 1997 Insp Rept 50-255/96-14 on 961019-1123.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000255/19960181997-01-17017 January 1997 Insp Rept 50-255/96-18 on 961118-970106.No Violations Noted. Major Areas Inspected:Engineering IR 05000255/19960161997-01-0303 January 1997 Insp Rept 50-255/96-16 on 961119-21 & 1216.No Violations Noted.Major Areas Inspected:Maintenance Procedures, Documentation & Engineering Support of Facilities 1999-09-03
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARPNO-II-99-043, on 991013,Palisades Nuclear Plant Located Near South Haven,Mi Notified NRC That Package Received from Licensee Exceeded External Radiation Limits of 200 Mrem Per H Authorized by Regulations.Shipper & Carrier Notified1999-10-14014 October 1999 PNO-II-99-043:on 991013,Palisades Nuclear Plant Located Near South Haven,Mi Notified NRC That Package Received from Licensee Exceeded External Radiation Limits of 200 Mrem Per H Authorized by Regulations.Shipper & Carrier Notified IR 05000255/19990101999-10-13013 October 1999 Insp Rept 50-255/99-10 on 990812-0921.One Violation Noted & Being Treated as Ncv.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000255/19993011999-10-0404 October 1999 NRC Operator Licensing Exam Rept 50-255/99-301OL (Including Completed & Graded Tests) for Tests Administered on 990607- 14 IR 05000255/19990141999-09-23023 September 1999 Insp Rept 50-255/99-14 on 990831-0901.No Violations Noted. Major Areas Inspected:Review of Chemical & Radiological Services Dept on-line Planning & Scheduling Program IR 05000255/19990091999-09-0303 September 1999 Insp Rept 50-255/99-09 on 990522-0811.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000255/19990081999-07-13013 July 1999 Insp Rept 50-255/99-08 on 990522-0630.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support PNO-III-99-032, on 990617,fire Discovered in Trailer Complex Containing Offices for Licensee Dry Cask Storage Project Staff.Fire Caused Extensive Damage to Main Portion of complex,triple-wide Trailer.Fire Extinguished1999-06-18018 June 1999 PNO-III-99-032:on 990617,fire Discovered in Trailer Complex Containing Offices for Licensee Dry Cask Storage Project Staff.Fire Caused Extensive Damage to Main Portion of complex,triple-wide Trailer.Fire Extinguished PNO-III-99-031, on 990609,minor Hydrogen Burns Occurred During Welding of Structural Lid on Spent Fuel Storage Cask Following Loading Earlier in Wk.Nrc Resident Inspector Will Follow Licensee Response to Incident & Observe1999-06-10010 June 1999 PNO-III-99-031:on 990609,minor Hydrogen Burns Occurred During Welding of Structural Lid on Spent Fuel Storage Cask Following Loading Earlier in Wk.Nrc Resident Inspector Will Follow Licensee Response to Incident & Observe IR 05000255/19990041999-06-0404 June 1999 Insp Rept 50-255/99-04 on 990410-0521.No Violations Noted. Major Areas Inspected:Operations,Maint Engineering & Plant Support IR 05000255/19990061999-06-0303 June 1999 Insp Rept 50-255/99-06 on 990506-12.Three Violations Noted & Being Treated as non-cited Violations.Major Areas Inspected: Effectiveness of Radiation Protection Program IR 05000255/19990051999-05-19019 May 1999 Insp Rept 50-255/99-05 on 990503-06.Violations Noted.Major Areas Inspected:Activities Associated with GL 96-05, Periodic Verification of Design-Basis Capability of Safety- Related Movs IR 05000255/19990031999-04-23023 April 1999 Insp Rept 50-255/99-03 on 990226-0409.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000255/19990011999-03-0505 March 1999 Insp Rept 50-255/99-01 on 990112-0225.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML18066A4091999-02-10010 February 1999 Notice of Violation from Insp on 981126-990112.Violation Noted:As of 981218,util Had Not Submitted Evaluation of Exam Results Completed on 980523 on Acceptability of Continued Svc with 2 Degraded Pressure Retaining Code Class 1 Studs ML18066A4101999-02-0505 February 1999 Insp Rept 50-255/98-22 on 981126-990112.Violations Noted. Major Areas Inspected:Licensee Operations,Engineering & Plant Support IR 05000255/19990021999-02-0505 February 1999 Partially Withheld Insp Rept 50-255/99-02 on 990119-22. Violations Noted.Major Areas Inspected:Status of Security Facilities & Equipment,Testing & Maintenance,Protected Area Detection & Assessment Aids IR 05000255/19980211998-12-29029 December 1998 Insp Rept 50-255/98-21 on 981130-1204.No Violations Noted. Major Areas Inspected:Licensee Performance During Plant Biennial Exercise of Emergency Plan IR 05000255/19980191998-12-14014 December 1998 Insp Rept 50-255/98-19 on 981008-1125.No Violations Noted. Major Areas Inspected:Licensee Operations,Engineering & Plant Support IR 05000255/19980201998-11-24024 November 1998 Insp Rept 50-255/98-20 on 981026-30.No Violations Noted. Major Areas Inspected:Review Evaluation of Shipping Cask Used in Transportation Incident Wherein Class 7 Radioactive Matl Shipment,Exceeded NRC & DOT Limits for Radiation IR 05000255/19980071998-11-12012 November 1998 Insp Rept 50-255/98-07 on 980413-1023.One Apparent Violation Be Considered for Escalated Enforcement Action.Major Areas Inspected:Review of Events,Circumstances & Licensee Investigation of TS Surveillance Refueling Test IR 05000255/19980171998-11-0505 November 1998 Insp Rept 50-255/98-17 on 980821-1007.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000255/19980181998-10-0101 October 1998 Insp Rept 50-255/98-18 on 980824-0902.One Violation Being Considered for Escalated Enforcement Action.Major Areas Inspected:Review Transportation Incident in Which Class 7 Radioactive Package,Shipped on Open Transport Vehicle ML18068A4741998-09-18018 September 1998 Insp Rept 50-255/98-15 on 980702-0821.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support Re Fire Brigade Response to Minor Electrical Fire Wearing Appropriate Safety Gear in Timely Manner IR 05000255/19980121998-09-0202 September 1998 Insp Rept 50-255/98-12 on 980706-24.No Violations Noted. Major Areas Inspected:Engineering ML18068A4281998-09-0202 September 1998 Notice of Violation from Insp on 980706-24.Violation Noted: Testing Program Not Developed Until 971201,after 44 of 72 Molded Case Circuit Breakers Failed to Trip During Testing IR 05000255/19980161998-08-28028 August 1998 Insp Rept 50-255/98-16 on 980810-14.No Violations Noted. Major Areas Inspected:Review of Emergency Preparedness Program,As Aspect of Plant Support IR 05000255/19980131998-08-0707 August 1998 Insp Rept 50-255/98-13 on 980720-22 & 27-29.No Violations Noted.Major Areas Inspected:Reviewed Fire Protection Program,Aspect of Plant Support ML18066A2581998-07-30030 July 1998 Notice of Violation from Insp on 980507-0701.Violation Noted:Shift Supervisor Failed to Maintain Proper Procedure Configuration in That Safety Injection Tank Pressure Control Valves Manual Isolation Valves ES-3038 & ES3042 Not Closed ML18066A2601998-07-30030 July 1998 Insp Rept 50-255/98-10 on 980507-0701.Violation Noted,Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000255/19980141998-07-29029 July 1998 Insp Rept 50-255/98-14 on 980707-10.No Violations Noted. Major Areas Inspected:Review of Planning & Radiological Controls for Resin Sluice,Calibration of Personal Contamination Monitors & Mgt & Operation of Area IR 05000255/19980111998-07-0202 July 1998 Insp Rept 50-255/98-11 on 980518-0604.No Violations Noted. Major Areas Inspected:Licensee C/As & Engineering Involvement in C/A Process ML18066A1951998-06-15015 June 1998 Insp Rept 50-255/98-09 on 980504-0601.Violations Noted.Major Areas Inspected:Control of Plant Radiological Conditions, Development of RWP & Planning to Ensure That Radiation Exposure During Recent Refueling Outage Was ALARA ML18066A1941998-06-15015 June 1998 Notice of Violation from Insp on 980504-0601.Violation Noted:On 980429,Radiation Controlled Door to 607 Mainsteam Room in Containment,W/Radiation Levels Ranging Up to 5,000 Mrem/H Was Not Locked & Guarded IR 05000255/19980061998-06-12012 June 1998 Insp Rept 50-255/98-06 on 980504-08 & 11-14.No Violations Noted.Major Areas Inspected:Maint & Engineering ML18066A1901998-06-11011 June 1998 Notice of Violation from Insp on 980314-0506.Violation Noted:On 980426,inspectors Identified That Palisades Administrative Procedure 5.09 Failed to Prescribe Foreign Matl Exclusion Controls for Electrical Safety Equipment ML18066A1911998-06-11011 June 1998 Insp Rept 50-255/98-05 on 980314-0506.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000255/19980081998-05-28028 May 1998 Partially Withheld Insp Rept 50-255/98-08 on 980504-08 (Ref 10CFR73.71).No Violations Noted.Major Areas Inspected: Effectiveness of Access Control Functions & Testing & Maint Activities Related to Security Equipment ML18066A2121998-05-18018 May 1998 Notice of Deviation from Insp on 980325-0410.Deviation noted:FC-854 Moved Backup Power Source from MCC 3 to MCC 2, Redundant Power Source,Which Resulted in Bus Y-01 Being Able to Automatically Transfer Between Two safety-related Busses ML18066A2111998-05-18018 May 1998 Notice of Violation from Insp on 980325-0410.Violation Noted:As of 971114,listed Analyses Were Not Revised When Analytical Inputs Were Changed or Found to Be in Error ML18065B2491998-05-18018 May 1998 Insp Rept 50-255/98-04 on 980325-0401.Violations Noted.Major Areas Inspected:Review of Training Procedures,Written & Operating Exam Matl & Observation & Evaluation of Operator Performance & Licensee Evaluators During Exam ML18065B2481998-05-18018 May 1998 Notice of Violation from Insp on 980325-0401.Violation Noted:On 980121 & 980128,licensee Annual Licensed Operator Category B Written Exam Constructed w/look-up Questions & 10 of 23 Questions Considered Simple Knowledge Level Questions ML18066A2131998-05-18018 May 1998 Insp Rept 50-255/98-03 on 980325-0410.Violations Noted.Major Areas Inspected:Engineering ML18065B2161998-04-16016 April 1998 Insp Rept 50-255/98-02 on 980128-0313.Violation Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML18065B2151998-04-16016 April 1998 Notice of Violation from Insp on 980128-0313.Violation Noted:On 980113,activity Affecting Quality Was Not Accomplished in Accordance W/Procedure 4.02 & Associated Checklist Cl 3.4 in That Watertight Door 59 Found W/O Dogs ML20217K5821998-04-0202 April 1998 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $55,000.Violation Noted:On 971017,shift Supervisor Failed to Ensure That Equipment Could Be Removed from Svc,By Failing to Ensure That TS Requirements Were Met ML18066A1561998-03-30030 March 1998 EN-98-019:on 980402,notice of Proposed Imposition of Civil Penalty in Amount of $55,000 Issued to Licensee.Action Based on Six Violations,That Represent Severity Level III Problem ML18065B1681998-02-26026 February 1998 Insp Rept 50-255/97-18 on 971206-980127.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML18067A8191998-02-0606 February 1998 Notice of Violation from Insp on 971212-19 & 980114-16. Violation Noted:Licensee Failed to Post High Radiation Area W/Conspicuous Signs Bearing Radiation Symbol & Words Caution High Radiation Area on 980107 ML18067A8241998-02-0505 February 1998 Errata to NOV from Insp on 971213.NRC Agree That NOV Should Refer Only to Failure to Perform Contamination Survey on 970910,based on Further Review of Radiological Survey Sheets & Conversation W/Staff IR 05000255/19970161998-02-0202 February 1998 Insp Rept 50-255/97-16 on 971212-19 & 980114-16.Violation Noted.Major Areas Inspected:Control Room Habitability Sys, Respiratory Protection Program,Plant Water Quality,Chemistry Program,Fuel Monitoring,Post Accident Sample Monitoring Sys 1999-09-03
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U.S. NUCLEAR REGULATORY COMMISSION Docket No:
License No:
Report No:
Licensee:
Facility:
Location:
Dates:
Inspectors:
Approved by:
9811170210 981112 PDR ADOCK 05000255 G
PDR REGION 111 50-255 DPR-20 50-255/98007 (DRP)
Consumers Energy Company 212 West Michigan Avenue Jackson, Ml 49201 Palisades Nuclear Generating Plant 27780 Blue Star Memorial Highway Covert, Ml 49043-9530 April 13, 1998, through October 23, 1998 J. Lennartz, Senior Resident Inspector P. Prescott, Resident Inspector Bruce L. Burgess, Chief Reactor Projects Branch 6
EXECUTIVE SUMMARY Palisades Nuclear Generating Plant NRC Inspection Report 50-255/98007 This special inspection was conducted to review the events, circumstances, and the licensee's investigation of the Technical Specification surveillance refueling test that rendered both trains of high pressure safety injection inoperable. The inspectors reviewed selective procedures and representative records, observed management review boards, and interviewed personne Operations
The inspectors concluded that licensee personnel aggressively pursued and identified the appropriate root causes for this incident. The licensee's incidence response team rigorously evaluated the incident and the identified corr~ctive actions were thoroug Multiple barriers to preclude performing an inadequate procedure failed for several years which contributed to the incident. Regulatory significance was high regarding the failure to perform safety reviews for procedure revisions that affected the high pressure safety injection system's safety analysis. The failure to perform adequate safety reviews for the procedure revisions resulted in the development of inadequate Procedure RT-71 Also, the failure to recognize Technical Specification implications contributed to the incident in that it allowed the inadequate procedure to be performed. The incident wa non-risk significant and had no actual safety consequences. Safety significance was high regarding the potential consequences in that emergency core cooling criteria regarding peak clad temperature would have been exceeded for a design based small break loss of coolant accident assuming no operator action. The inspectors noted that the required operator actions were not complex and could have been accomplished in a timely manner which would mitigate the potential consequences. (Section 01)
The crew's knowledge regarding the Technical Specification requirements associated with the high pressure safety injection system surveillance test was poor. Also, the crew demonstrated a poor questioning attitude regarding the test lineup and a lack of awareness regarding the relationship between the high pressure safety injection system manipulations_ that were performed and the purpose of the test. (Section 04)
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Report Details Summary of Test Performance The following summarizes Technical Specification (TS) surveillance Refueling Test (RT) -71 B,
"High pressure safety injection (HPSI) Train 1 and 2 and safety injection tank (SIT) System, Class 2 System Functional/lnservice Test," that was performed on April 10, 1998:
The test's purpose was to verify HPSI system and SIT operability by demonstrating leak tightnes *
The test was divided into two parts. Part 1 tested system components outside containment and was allowed to be performed with the plant at power. Part 2 tested system components inside containment and was only allowed to be performed with the planf shutdow *
With the plant at 96 percent power, the "A" shift (nights) control room crew authorized performance of RT-718, Part 1 only, at time 0010 hour1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> *
The system was aligned per the procedure and both HPSI pumps were started to supply a pressure source of approximately 1200 psia for the leak tes *
A pressure surge in the system after the HPSI pumps were started resulted in all four SIT pressure control valves (PCVs) opening momentarily which was not expected. The.
valves opened below their set pressure of 1300 psig due to a known problem with the control valve actuator springs. (The valve actuator springs had been previously *
scheduled and were subsequently replaced during the 1998 refueling outage).
Opening of the SIT PCVs established a momentary flowpath of the 1200 psi a water to the SIT drain relief valve (RV) - 3161 which had a setpoint of 500 psig. Valve RV-3161 momentarily opened and relieved water to the quench tank, as designed, where it was *
containe *
Valve RV-3161 and all SIT PCVs subsequently reseated appropriatel *
The test was logged in the Shift Supervisors log at time 0415 hours0.0048 days <br />0.115 hours <br />6.861772e-4 weeks <br />1.579075e-4 months <br /> as being completed satisfactoril I. Operations
Conduct of Operations 01.1 _General Comments Operations management questioned the adequacy of Procedure RT-71 B because'of the HPSI system transient that resulted during the test. Operations management requested that the procedure sponsor, Engineering Programs, review the procedure. Engineering
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personnel identified, on April 13, 1998, that both trains of HPSI were rendered inoperable for approximately 90 minutes during the test. The licensee appropriately reported the incident to the NRC as a 4-hour non-emergency report in accordance with 10 CFR 50.72(b)(2)(iii)(B), accident mitigation. Subsequently, the licensee appropriately reported the incident to the NRC in Licensee Event Report (LER) 98-00 Condition Report (CR) C-PAL-98-0578, "Valve Alignment During.RT-71 B Results in Both Trains of HPSI Being Inoperable," was generated and classified as "level one" because of the incident's high significance. The level one condition report required multi disciplinary evaluations. In addition, plant management formed an incident response team (IRT) to investigate the even.2 Investigation of Event By Licensee's Incident Response Team Inspection Scope (92701. 71707)
The inspectors conducted personnel interviews, observed management review boards, and reviewed selective portions of the following procedures and representative records: Technical Specification surveillance refueling test (RT) procedure, RT-71B, "HPSI Train 1 and 2 and SIT System, Class 2 System Functional/lnservice Test,"
Revision 3, dated 8/5/97, and the associated basis document, Revision 1 Condition Report C-PAL-98-0578, "Valve Alignment During RT-71 B Results in Both Trains of HPSI Being Inoperable" Design Basis Document - 2.02, "High Pressure Safety Injection System," Rev. 3 The licensee's investigation team's documented evaluation of C-PAL-98-0578 Palisades' Operating Requirements Manual, Standing Order 62, Revision 39, Section * Palisades' TSs 3.0.3, "Applicability," and 3.3, "Emergency Core Cooling System" Technical Specification surveillance inservice test procedure, Quarterly Operating (Q0)-19, "HPSI Pumps and ESS Check Valve Operability Test'.'
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Palisade*s LER 98-007, "High Pressure Safety Injection System lnoperability During TS Surveillance Test" Control room shift supervisor logs
_j Engineering analysis determination of risk signifi_cance, EA-PSA-RT-71 B 1 Final Safety Analysis Report Chapters 6, 7, and 14
Observations and Findings Regulatory Significance.
The licensee identified on April 13, 1998, during post implementation review of TS Surveillance Test RT-718, that both trains of HPSI had been rendered inoperable on April 10, 1998, for approximately 90 minutes. Plant management immediately formed an IRT to investigate the incident and aggressively pursued causes of the even Surveillance test procedure, RT-718, directed the operators to close the normally open HPSI cold leg injection orifice bypass valves (M0-3080 and M0-3081) and open the normally closed hot leg injection valves (M0-3082 and M0-3083). This aligned both
- trains of HPSI cold leg injection through the orifices in all four cold legs. The normal at power HPSI cold leg injection lineup bypassed the orifices. Consequently, the test lineup rendered both trains of HPSI inoperable due to the reduced flow through the cold leg In addition, both trains of HPSI were aligned to the single hot leg injection line simultaneously and therefore, were vulnerable to a single failure of the hot leg injection line. A hot leg injection line piping failure could divert enough flow out the break to prevent both trains of HPSI from performing their intended safety functio The IRT determined that Procedure RT-718 had been revised three times. In 1988, the.*
procedure (RT-74 at the time) was revised to manipulate the hot leg injection valves within the test. This was when the inappropriate HPSI system line-up was first introduced into the procedure. That revision was completed in accordance with the temporary change process as described in TSs that were in effect at the time. In 1991, the 1988 temporary change was incorporated as a permanent revision. In 1997, the procedure was revised to allow the test to be performed with the plant at power. The IRT identified that the 10 CFR 50.59 requirements were not met for each of the three revisions to RT-718. The 10 CFR 50.59 screening criteria failed to identify that the procedure revisions affected TSs and the final safety analysis report (FSAR).
Consequently, a 10 CFR 50.59 safety evaluation was not performed and re,sulted in the development of Procedure RT-718 that was inadequat The licensee determined that emergency core cooling peak cladding temperature performance criterion would have been exceeded, with no operator action, for the previously analyzed small break loss of coolant accident while in the test lineup. Also, the test lineup rendered both trains of HPSI vulnerable to a single failure in the hot leg injection piping. 1 O CFR Part 50, Appendix 8, Criterion V, requires that activities affecting quality be prescribed by procedures of a type appropriate to the circumstance CFR Part 50, Appendix 8, Criterion V, applies to Surveillance Procedure RT-71 Surveillance *Procedure RT-718 prescribed inservice testing, an activity affecting quality, for the HPSI system.. Procedure RT-718 was not appropriate for the circumstance in that it rendered both trains of HPSI inoperable and therefore is an apparent violation of 10
.CfR Part SQ, App_e_odix 8, Criterionv.___
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(EEi 50-255/98007-01)
The IRT determined that the current 50.59 process would require a safety evaluation when a system alignment similar to this was included in a procedure revision. The
current process had improved computer search tools and therefore, the licensee concluded that it was unlikely that the errors made in 1988 and 1991 would be repeate The IRT attributed the failure to perform a safety review in 1997 to individual knowledge and performance weakne.sses when the procedure was revised to allow test performance while the plant was onlin Procedure RT-718 had been completed on six separate occasions between 1988 and 1998. From 1988 through 1996, the procedure was completed five times with the plant in hot shutdown. Technical Specifications required at least one HPSI train available while in hot shutdown. Consequently, both trains of HPSI may have been inoperable when required. The IRT concluded that it was unlikely that the HPSI trains were inoperable during the test while in hot shutdown due to the reduced decay heat requirements; however, the licensee did not perform any analysis fo validate that assumptio On April 10, 1998, the test was performed with the plant at power and rendered both HPSI trains inoperable. Technical Specification 3.3.4, required two operable HPSI pumps when the primary coolant system was greater than 325°F. One HPSI pump could be inoperable provided TS 3.3.2.c requirements were met. Technical Specification *
3.3.2.c allowed one inoperable HPSI pump for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> while at power. Therefore, the HPSI system configuration utilized during the test did not comply with TS requirement Technical Specification 3.0.3 applied and should have been entered. Technical Specification 3.0.3 required that action be initiated within one hour to place the plant in a
. condition that the applicable specification did not apply. With both trains of HPSI inoperable, TSs required that the plant be placed in cold shutdown within 36 hour4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> On April 10, 1998, both HPSI trains were inoperable for 90 minutes and therefore a plant shutdown to cold shutdown should have been initiated within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. However, licensee personnel involveo failed to recognize that the test aligned the HPSI system such that TS requirements were not complied with. Consequently, the inadequate procedure was performed and the required action to commence shutdown to cold shutdown within one hour did not occur. The system line-up was restored to normal following the test, and.
therefore the TS requirement to place the plant in cold shutdown within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> was fortuitously satisfie Risk Significance The IRT requested a probabilistic safety assessment (PSA) using the system configuration established during the surveillance test with the plant at 100 percent power. The licensee's safety assessment was documented in EA-PSA-RT71 B. The current PSA model and plant risk software were utilized along with EPRI PSA Application Guidelines. The licensee's PSA group calculated the core damage probability (CDP)
increase while HPSI was in the test lineup which was then compared to the PSA
Applications Guideline, Figure 4.3, "Quantitative Screening Criteria For Temporary Ch.ange..". Figure 4.3 indicated that a CDP increase of 1 E-5 was the threshold for potentially risk significant changes and changes below 1 E-6 were considered non-risk significant. Licensee PSA personnel determined that the CDP increase during the test was 1.94E-6 assuming no operator action which was just above the non-risk significant threshold.
The licensee's PSA gro"up also calculated an increase in CDP using a nominal human *
error probability of 1 E-02 for operator action. In this instance, the CDP increase during the test was 2.00E-8 which was well below the non-risk significant threshold. In addition, due to the uncertainty of human error probability, the licensee's PSA group calculated the CDP increase using a human error probability of 0.5. A human error probability of meant that there was a 50 percent chance that the operators would not restore the lineup. The resultant CDP increase during the test using a human error probability of was 9.69E-7, just below the non-risk significant threshold. The crew had discussed the necessary contingency actions to secure the surveillance test for a plant transient and *
the licensee concluded that it would be reasonable to assume that the operator action would be performed. Therefore, the licensee considered the human error probability of 0.5 as very conservative. The inspectors noted that the required operator actions were not extensive and agreed with the licensee's assumptio The IRT concluded that performance of RT-718 at power on April 10, 1998, was a non-risk significant event according to the PSA and the guidance provided by the EPRI PSA Applications Guideline. The inspectors and an NRC Senior Reactor Analyst reviewed the licensee's risk analysis and agreed with the licensee's conclusions. Also, the NRC Senior Reactor Analyst noted that the licensee's PSA was conservative in that a sensitivity calculation using a human error probability of 0.5 was also performe Safety Significance The IRT identified that the potential safety significance from a design basis accident perspective was much higher. Flow models of the HPSI system were run for two
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situations. The first situation modeled the HPSI flow that would be seen for a short time during the "transition" from the normal HPSI lineup to the.test lineup. This "transition" required the cold leg injection orifice bypass valves (M0-3080, M0:-3081) to be closed prior to opening the hot leg injection valves (M0-3082, M0-3083). Consequently, there would be. reduced flow to the cold leg injection lines. This condition would have existed only for a couple of minutes. The second situation modeled the HPSI flow while in the--
test lineup with the hot leg injection valves open. This condition existed for the test duration of approximately 90 minutes. The IRT identified that 10 CFR 50.46, emergency core cooling peak cladding temperature criteria would have been exceeded if the previously analyzed design basis small break loss of coolant accident occurred during either situatio A break in the hot leg injection line was also modeled which was approximately 22 percent smaller than the design basis small break. A hot leg injection line break, while in the test lineup, would have also resulted in exceeding 10 CFR 50.46 peak cladding temperature criteria. Operator action to realign the system was not credited in any of the models. The IRT determined that emergency core cooling criteria would not have been exceeded, while in the test lineup, for other design basis accidents such as
- __. large break loss of coolant, main steam line break, and steam generator tube ruptur While the potential safety consequences were high, the IRT determined that there were no actual safety consequences from the event. There were no plant or system transients that required the HPSI system to perform its intended safety function during test
performance. Also, the operators were not challenged by any transients during the tes Root Cause and Corrective Actions The IRT determined that the root cause was a knowledge weakness in that engineering and operations personnel failed to recognize how the hot leg injection valve manipulations affected HPSI system operability. This knowledge weakness allowed the inadequate procedure to be performed. Several barriers associated with the procedure development, review, approval, scheduling, and implementation process failed. Also, an inadequate "questioning attitude" by all licensee personnel involved with the test demonstrated the need for further improvement in this area. Planned corrective actions to address the root cause included:
Training for licensed operators and engineers to improve operational decision makin *
Strengthen the surveillance procedure preparation proces *
Clarify and communicate performance standards to operations staff regarding understanding of integrated plant operations and decision makin In addition to the planned corrective actions, the inspectors noted that several immediate actions, as documented in C-PAL-98-578, were completed. Some examples included:
Surveillance Procedure RT-71 B was revise *
The HPSI system line-up was verified to be correc *
Additional surveillance procedures that were scheduled in subsequent weeks were reviewed to verify that the appropriate TS implications were identifie Performance of all safety related surveillances and special tests were stoppe until this review was complete *
An expert panel reviewed the surveillance procedures associated with the Auxiliary Feedwater and Emergency Diesel Generator systems to ensure that all.
- applicable TSs were appropriately addressed. No similar deficiencies were identifie *
Safety and Design Review personnel qualified to review 10 CFR 50.59 evaluations were trained in the performance failures that led to this even Conclusions The inspectors concluded that licensee personnel aggressively pursued and identified the appropriate root causes for this incident. The licensee's IRT rigorously evaluated the
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incident and the identified corrective actions were thorough. Multiple barriers to preclude performing an inadequate procedure failed for several years which contributed to the incident. *Regulatory significance was high regarding the failure to perform safety reviews for procedure revisions that affected the HPSI system's safety analysis. The failure to perform adequate safety reviews resulted in the development of Procedure RT-71 B that was inadequat Also, the failure to recognize TS implications contributed to the incident in that it allowed the inadequate procedure to be performed. The incident was non-risk significant and had no actual safety consequences. Safety significance was high regarding the potential consequences in that emergency core cooling criteria regarding peak clad temperature would have been exceeded for a design based small break loss of coolant accident assuming no operator action. The inspectors noted that the required operator actions were not complex and could have been accomplished in a timely manner which would mitigate the potential consequence Operator Knowledge and Performance a. *
Inspection Scope The inspectors conducted personnel interviews and reviewed control room log books.
. Observations and Findings
Prior to performing the test, the on-shift crew identified that the test could not be performed as planned. It was originally schedule to be performed in parallel with a related surveillance. The on-shift crew noted that the test required both trains of HPSI to be started while the related surveillance required only one train to be started and therefore, the tests could not be performed in parallel. The test was rescheduled for a later date; however, neither the crew nor operations planning and scheduling personnel recognized the test inadequacies regarding TS and HPSI design basis implication The valves manipulated during the test were located inside of containment. However, only piping outside of containment was to be leak tested and the crew failed to question why valves inside of containment were manipulated for the. test. Also, the inspectors noted that the on-shift crew submitted a procedure change request following the test due to the system transient that was observed during the test. The procedure change request was to open the HPSI loop isolation valves slowly after the HPSI pumps were started to avoid the pressure surge that was experienced. This demonstrated that the crew failed to recognize that valves inside of containment were being manipulated unnecessarily to complete the test. The crew demonstrated a lack of awareness regarding the relationship between the system manipulations that were performed and the purpose of the tes The on-shift Control Room Supervisor and Shift Engineer did question why entry into TSs was not required during performance of the test. Based on these questions, they referenced TSs and a related HPSI system surveillance test. However, both crew members incorrectly concluded that the test lineup did not require entry into any TSs.
- Misinterpreting TSs and the related surveillance's failure to reference the appropriate TS contributed to the incorrect conclusions. Consequently, neither the Control Room Supervisor nor the Shift Engineer communicated their questions to the Shift Superviso This precluded the senior licensed crew member from providing any insights. The inspectors determined, based on interviews, that the Shift Supervisor had the same knowledge weakness regarding the TSs and therefore, may not have prevented the incident if consulte The crew's failure to recognize that both trains of HPSI were inoperable and in non-compliance with TSs during the test precluded a required entry into TS 3.0.3. Also, the crew failed to recognize that the HPSI system was vulnerable to a single failure in the hot leg injection piping during the test. This demonstrated poor knowledge of the TS implications and poor recognition of a single failure vulnerability for the HPSI system configuration utilized during the tes * Conclusions The crew's knowledge regarding the TS requirements associated with the HPSI surveillance test was poor. Also, the crew demonstrated a poor questioning attitude regarding the HPSI system surveillance test lineup and a lack of awareness regarding the relationship between the HPSI system manipulations that were performed and the purpose of the tes V. Management Meetings X1 Exit Meeting Summary The inspectors presented the inspection results to licensee management representatives during an exit meeting on August 21, 1998. On October 23, a re-exit was conducted to discuss a change in the inspection results and to convey to the licensee the details and circumstances regarding the apparent violation. The licensee acknowledged the findings and did not indicate that any material examined during the inspection should be considered proprietar.
PARTIAL LIST OF PERSONS CONTACTED Licensee R. A Fenech, Senior Vice President, Nuclear, Fossil, and Hydro Operations.
T. J. Palmisano, Site Vice President - Palisades G. R. Boss, Operations Manager B. M. Dusterhoft, Operations Condition Review Team Leader J. K. Ford, ~ngineering Programs Manager N. L. Haskell, Director, Licensing P. Harden, Safety/Design Review Supervisor C. S. Kozup, Licensing D. G. Malone, Licensing D.W. Rogers, General Manager, Plant Operations T. C. Watson, Training R. G. Schaaf, Palisades Project Manager, NRR IP 71707:
IP 92701:
OPENED INSPECTION PROCEDURES USED Plant Operations Followup ITEMS OPENED, CLOSED, AND DISCUSSED 50-255/98007-01 EE Inadequate Surveillance Test Procedl,!re CLOSED None Discussed None 11