IR 05000255/2020010

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Biennial Problem Identification and Resolution Inspection Report 05000255/2020010
ML20237F480
Person / Time
Site: Palisades 
Issue date: 08/24/2020
From: April Nguyen
NRC/RGN-III/DRP/B2
To: Corbin D
Entergy Nuclear Operations
References
IR 2020010
Download: ML20237F480 (17)


Text

August 24, 2020

SUBJECT:

PALISADES NUCLEAR PLANT - BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000255/2020010

Dear Mr. Corbin:

On July 10, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at your Palisades Nuclear Plant and discussed the results of this inspection with yourself and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspection team reviewed the stations corrective action program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

The team also evaluated the stations processes for use of industry and NRC operating experience information and the effectiveness of the stations audits and self-assessments.

Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

Finally, the team reviewed the stations programs to establish and maintain a safety-conscious work environment, and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews the team found no evidence of challenges to your organizations safety-conscious work environment. Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

No findings or violations of more than minor significance were identified during this inspection. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA by Hironori Peterson for/

April M. Nguyen, Acting Chief Branch 2 Division of Reactor Projects

Docket No. 05000255 License No. DPR-20

Enclosure:

As stated

Inspection Report

Docket Number:

05000255

License Number:

DPR-20

Report Number:

05000255/2020010

Enterprise Identifier: I-2020-010-0036

Licensee:

Entergy Nuclear Operations, Inc.

Facility:

Palisades Nuclear Plant

Location:

Covert, Michigan

Inspection Dates:

June 22, 2020 to July 10, 2020

Inspectors:

P. Laflamme, Senior Resident Inspector

V. Meghani, Reactor Inspector

J. Neurauter, Senior Reactor Inspector

R. Ruiz, Project Engineer

C. St. Peters, Resident Inspector

Approved By:

April M. Nguyen, Acting Chief

Branch 2

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at Palisades Nuclear Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the coronavirus (COVID-19), regional inspectors were directed to begin telework. The inspection documented below was determined that the objectives and requirements stated in the IP, in part, could be performed remotely.

OTHER ACTIVITIES - BASELINE

71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 02.04)

(1) The inspectors performed a biennial assessment of the licensees corrective action program, use of operating experience, self-assessments and audits, and safety conscious work environment.
  • Corrective Action Program Effectiveness: The inspectors assessed the corrective action programs effectiveness in identifying, prioritizing, evaluating, and correcting problems. The inspectors also conducted a five-year review of the component cooling water system.
  • Operating Experience, Self-Assessments and Audits: The inspectors assessed the effectiveness of the stations processes for use of operating experience, audits and self-assessments.
  • Safety Conscious Work Environment: The inspectors assessed the effectiveness of the stations programs to establish and maintain a safety-conscious work environment.

INSPECTION RESULTS

Assessment 71152B Assessment of the Corrective Action Program

Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

Effectiveness of Problem Identification

Overall, the station was effective at identifying issues at a low threshold and was properly entering them into the corrective action program (CAP) as required by station procedures.

The team determined that the station was generally effective at identifying negative trends that could potentially impact nuclear safety. The team walked down the emergency diesel generators and various security-related areas. For the areas reviewed, the team did not identify any issues in the area of problem identification.

Effectiveness of Prioritization and Evaluation of Issues

In-depth reviews of a risk-informed sampling of condition reports (CRs), work orders (WOs),and cause evaluations were completed, including a 5-year time period for the component cooling water (CCW) system. The team determined that the licensee had established a low threshold for entering deficiencies into the CAP, that the issues were generally being appropriately prioritized and evaluated for resolution, and that corrective actions (CAs) were implemented to mitigate the future risk of issues occurring that could affect overall system operability and/or reliability.

The team identified one example of a CR categorized as N (non-adverse) where the team considered the issue to be a condition adverse to quality (CAQ). Specifically, CR-PLP-2018-03582 documented microbiologically induced corrosion (MIC) of the safety-related train B CCW system heat exchanger, E54B, with a loss of pressure boundary material of more than 1/3rd of the nominal wall thickness at the south end-bell of the heat exchanger.

Although the condition was bounded by a previously evaluated condition on the E54A heat exchanger, the team considered this to be a deviation or deficiency, i.e., a departure from the normal standard, because the wall thickness was reduced below the specified thickness by more than the standard allowable-tolerances and therefore met the definition of a CAQ in procedure EN-LI-102. The plant staff determined that the condition of the E54B heat exchanger was acceptable for at least 52 months because it was bounded by an evaluation of E54A heat exchanger. The bounding structural integrity evaluation was documented in CR-PLP-2018-01375, which concluded that E54A condition was acceptable for an interval of 52 months and that a follow-on examination would be required no later than 26 months. The team noted that although the E54A evaluation was used as the basis for acceptance of the E54B condition, no actions were identified for subsequent examination of the E54B. The team concluded that the licensee's "non-adverse" CR classification was incorrect, but did not have any safety concerns or issues with the licensee's operability determination, so the issue was considered minor in nature.

Effectiveness of Corrective Actions

The team concluded that the licensee was generally effective in developing CAs that were appropriately focused to correct the identified problem and to address the root and contributing causes for significant conditions adverse to quality to preclude repetition. The licensee generally completed CAs in a timely manner and in accordance with procedural requirements commensurate with the safety significance of the issue. For NRC-identified issues, the team determined that the licensee generally assigned CAs that were effective and timely.

Assessment 71152B Assessment of Operating Experience and Self-Assessments and Audits

Based on the samples reviewed, the team determined that licensee performance in the use of Operating Experience (OE) and Self-Assessments and Audits adequately supported nuclear safety.

Use of Operating Experience

The licensee routinely screened industry and NRC OE information for station applicability.

Based on these initial screenings, the licensee initiated actions in the CAP to fully evaluate the impact, if any, to the station. When applicable, actions were developed and implemented in a timely manner to prevent similar issues from occurring. Operating Experience lessons-learned were communicated and incorporated into plant operations.

Self-Assessments and Audits

The inspectors reviewed several audits and self-assessments and deemed those sampled as thorough and intrusive with regards to following up with the issues that were identified through previous NRC inspections and in the self-assessments and fleet oversight audits.

Reviewed corrective actions for the identified issues were deemed reasonable and completed commensurate with their safety significance. The inspectors regarded licensee performance as adequately self-critical of their own performance and that performance-related issues were being identified through their self-assessment process.

Assessment 71152B Assessment of Safety Conscious Work Environment

The team reviewed the stations programs to establish and maintain a safety-conscious work environment and interviewed over 30 station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews, workers at the station expressed freedom to raise and enter safety concerns through any one of the various avenues available to them, and the team encountered no indications of chilling or retaliation. Finally, all plant personnel interviewed were aware of the Employee Concerns Program and expressed a willingness to use it as an avenue to raise concerns, if desired.

In addition, the team included questions on the topic of the permanent plant shutdown (scheduled for 2022) to assess for any negative impacts on safety performance or overall safety culture both for the individuals and the organization. Employees consistently communicated the belief that sufficient competency, engagement, resources, and commitment exist at the station to maintain high performance standards at the site.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On July 10, 2020, the inspectors presented the biennial problem identification and resolution inspection results to Mr. D. Corbin, Vice President, Operations and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71152B

Corrective Action

Documents

CR-PLP-2019-

03474 NCA

Line of Sight for CR-PLP-2019-03474

11/04/2019

OE-NOE-2018-

00012

NRC-RIS-2005-31 - R1 Control of Security Related Sensitive

Unclassified Non-safeguards

01/04/2018

CR-PLP-2015-

00180

P-52C CCW Pump Oil Leak

01/12/2015

CR-PLP-2016-

03486

p-52B CCW Pump Oil Leak

07/28/2016

CR-PLP-2017-

2568

P-52C CCW Pump Leaking Oil

05/16/2017

CR-PLP-2017-

05551

CV-2008 PMU TANK T-81 M/U Not Able to Be Manually

Stroked

2/07/2017

CR-PLP-2018-

00405

Various Attachments in (3) Three Radiation Work Permit

Packages Found with Incomplete Information

01/23/2018

CR-PLP-2018-

00469

Approved and Routed Preventative Maintenance Change

Request 251063 Not Implemented

01/26/2018

CR-PLP-2018-

01126

Some of Posting Formats (Colors, Specific Wording, Etc.) in

Fleet Procedure EN-RP-108, "Radiation Protection Posting,

Differ from Postings Currently Used and at Palisades

03/07/2018

CR-PLP-2018-

01523

Equipment Failure Evaluation: PS-0139A did not Respond to

Flow

05/22/2018

CR-PLP-2018-

01691

T-105C, Charging Pump P-55C Suction Stabilizer "As

Found" Bladder Pressure at ZERO PSI

04/05/2018

CR-PLP-2018-

01961

RAS Pump Air Sampler Number 233 Not in Sentinel

Database with Current Calibration

04/23/2018

CR-PLP-2018-

2110

During QO-1 "Safety Injection System," Right Channel Safety

Injection Actuated Red Light on Control Room Panel C-13

Failed to Illuminate

05/02/2018

CR-PLP-2018-

2129

No Station or Fleet Level Procedural Guidance Exists that

Directs Site Emergency Planning (EP) Staff to Submit Annual

Letter Regarding Interface Adequacy (as required by 10 CFR

50.54(t)(2)) into Records

05/03/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CR-PLP-2018-

2143

During Trouble Shooting for CR-PLP-2018-02110

Discovered Wire #13 Not Landed on SIS-2

05/03/2018

CR-PLP-2018-

2143

Right Channel Safety Injection System Wire Not Landed on

SIS-2 Relay

05/03/2018

CR-PLP-2018-

2143 CA-3

Root Cause Evaluation: Wire Not Landed on the Maintained

Safety Injection Initiation Relay Circuit

06/18/2018

CR-PLP-2018-

2518

NIOS Identified - Emergency Preparedness Job Aids

05/24/2018

CR-PLP-2018-

2568

Regulatory Assurance - NRC Compliance Closure Review of

CR-PLP-2017-5551

05/29/2018

CR-PLP-2018-

2571

Maintenance and Technical Training Comprehensive

Assessment Negative Observation

05/29/2018

CR-PLP-2018-

2578

Concurrent Verification May Not Be Appropriate for Technical

Specification Surveillance Procedure RO-12, Containment

High Pressure (CHP) and Spray System Tests, Step 5.8.27

05/29/2018

CR-PLP-2018-

2794

Some Fire Extinguishers at the Emergency Operations

Facility (EOF) have not been Serviced or Inspected Since

2015

06/11/2018

CR-PLP-2018-

2980

Multiple Leaks Detected during PMT of P-52C CCW Pump

06/21/2018

CR-PLP-2018-

03393

Simulator Evaluation Guide Issues

CR-PLP-2018-

03582

E-54B CCW Heat Exchanger Wall Thickness Below

Minimum

08/02/2018

CR-PLP-2018-

03989

Error in Record "COG-0118" - Monthly Condenser Off-gas

Effluent Calculation

08/30/2018

CR-PLP-2018-

04632

Palisades SRC 2018-02 Noteworthy Observation

10/10/2018

CR-PLP-2018-

04917

Piece of Metal Found Near P-52A CCW Pump

10/20/2018

CR-PLP-2018-

05329

VT-3 Examination of Piping Support H-19 Identified Contact

between Spring can Support and Adjacent Metal Plate

11/01/2018

CR-PLP-2018-

Regulatory Assurance - NRC Compliance Closure Review of

11/02/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

05405

CR-PLP-2018-02143

CR-PLP-2018-

05830

Erratic indications CV-0944A during RT-8D

11/10/2018

CR-PLP-2018-

06329

ICS 3000 Out of Service for Sulfate Analysis

11/26/2018

CR-PLP-2019-

00063

CRDM Housing #37 & #28 Cooling Lines

01/04/2019

CR-PLP-2019-

222

Failed Power Supply for P/S-0712 Not Sent Out for Timely

Failure Evaluation

03/25/2019

CR-PLP-2019-

00314

P-52B CCW Pump Degraded Trend

01/21/2019

CR-PLP-2019-

00327

Recurring Equipment Failures on Control Room Ventilation

System, Maintenance Rule Functional Failures

01/22/2019

CR-PLP-2019-

00327 CA-1

Non-adverse Condition Analysis: Recurring Equipment

Failures on Control Room Ventilation System

03/06/2019

CR-PLP-2019-

00655

Search of Adverse CRs using Trend Code EX11 for the Last

Months

2/11/2019

CR-PLP-2019-

00918

Current Calibration Record for WP2-1050 Protean Serial

Number 1171115 and PM-7 Serial Number 688 Could Not

Be Located in Records

03/05/2019

CR-PLP-2019-

01400

Annual Radiological Effluent Release Reports (ARERR)

Misidentified Reactor Type

04/05/2019

CR-PLP-2019-

01534

ERO Team Failed to Correctly Determine the Status of a

Radiological Release

04/16/2019

CR-PLP-2019-

01537

During the Performance of the Palisades Emergency

Planning Full Scale Drill, April 10th, 2019, the EOF Dose

Assessment Team made Several Errors that could have

Impacted the Performance of the ERO

04/16/2019

CR-PLP-2019-

01543

Drill and Exercise Performance (DEP) Data Indicates

Presence of an Aggregate Performance Issue

04/17/2019

CR-PLP-2019-

2089

OSC & TSC Players Showed up to the Facility without DLR.

ERO Players Needs to Validate they have DLR Assigned

05/22/2019

CR-PLP-2019-

2118

During the Performance of the Palisades Emergency

Planning Full Scale Drill, May 22, 2019, the Dispatch of

05/23/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Damage Control Teams in a Timely Manner Needs to be

Improved

CR-PLP-2019-

22 CA-1

Adverse Condition Analysis: Delay in Obtaining Auxiliary

Feedwater Actuation System (AFAS) Power Supply Failure

Evaluation

05/09/2019

CR-PLP-2019-

2855

Evaluation for CR-PLP-2018-2699 was too Narrowly

Focused

09/10/2019

CR-PLP-2019-

03005

CV-1057 Rework Due to Step 5.2.30 of Section 5.2, VALVE

REPACK, of Procedure PCS-M-8 Not Revised

07/30/2019

CR-PLP-2019-

273

Monthly Groundwater Sampling Results Contain Unexpected

Tritium Indications in Monitoring Well Sample

08/20/2019

CR-PLP-2019-

03609

Viper 20 Valve Diagnostic Testing System) Found to Be Non-

Conforming during Calibration Services

09/11/2019

CR-PLP-2019-

03692

NRC EQ DBAI: Evaluation of Effects of pre-RAS Borated

Containment Spray on Specific Materials in EQ Qualified

Equipment Exposed to Spray is not Provided in EQ Program

Documentation as Required by 10 CFR 50.49(e)(3)

09/16/2019

CR-PLP-2019-

03806

Spare Cathode Ray Tube Chassis Serial/Number-013 for

TMM's Failed on Bench

09/23/2019

CR-PLP-2019-

03819

TMM Stock Monitor Circuit Board Installed 180 Degrees Out

of Position

09/23/2019

CR-PLP-2019-

03819

TMM Stock Monitor Circuit Board Installed 180 Degrees Out

of Position

09/23/2019

CR-PLP-2019-

03829

Foreign Material Exclusion (FME) Requirements Contained

in Chemistry and Maintenance Procedures Not Consistently

Followed

09/24/2019

CR-PLP-2019-

03829 CA-1

Adverse Condition Analysis: Foreign Material Exclusion

(FME) Requirements Contained in Chemistry and

Maintenance Procedures Not Consistently Followed

10/24/2019

CR-PLP-2019-

228

The licensee Failed to Base the Qualification of Electric

Equipment Inside Containment on a Chemical Composition

that was at Least as Severe as that Resulting from the most

10/22/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Limiting Mode of Plant Operation

CR-PLP-2019-

04558

Nuclear Independent Oversight (NIOS) identified - Problem

Identified during the Performance of Observation O2C-PLP-

2019111448

11/14/2019

CR-PLP-2019-

04605

Mechanics during the EP Drill Conducted on November 13,

2019, Simulated Working (coupling assembly) on

Containment Spray Pump P-54B without Simulating being

Signed onto a Tagout or using EN-OP-200

11/19/2019

CR-PLP-2020-

238

Cyclic Status Control Performance

03/16/2020

CR-PLP-2020-

00338

As-Found PS-1482 and PS-1498 (K-6A Jacket Water

Pressure Switches) Out of Tolerance in Conservative

Direction

2/04/2020

CR-PLP-2020-

00402

Department Aggregate Performance Issue (API) Identified

2/07/2020

CR-PLP-2020-

00510

CV-0944A, CCW to SFP HXS failed to close during QO-1

2/17/2020

CR-PLP-2020-

00513

Sample Point for Service Water Grab for MR-36, when

Service Water Compositor Is Out of Service

2/18/2020

CR-PLP-2020-

00596

Two Additional Deficiencies were Identified in the Inform

Program Related to the Generation of Technical Data Sheets

2/24/2020

CR-PLP-2020-

00618

Procedure FPS-E-1 Incorporated Non "AS-BUILT" /

"PENDING" DRN 16-P460

2/25/2020

CR-PLP-2020-

00884

Issue Related to Sensitivity Test of Gamma Portal Monitors

to Detect Intakes of Contamination

03/18/2020

CR-PLP-2020-

00981

Boric Acid Leak - P-66B High Pressure Safety Injection

Pump

03/25/2020

CR-PLP-2020-

00988

CV-0944A not Fully Closed on Manual Operation

03/26/2020

CR-PLP-2020-

01053

Document Errors Found during EC-86037

04/02/2020

CR-PLP-2020-

01167

Administrative Limit for Service Water Total Residual Oxide

Exceeded

04/14/2020

CR-PLP-2020-

Condition Report Documents Request for Release and

04/14/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

01174

Installation of Non-conformant Material

CR-PLP-2020-

01184

Suspected Bad Female End Connection Point to Mettler

ToledoT-90 Boron Auto Titrator pH Probe

05/19/2020

CR-PLP-2020-

01195

AMS4 Did Not Have Filter Paper in Detector

04/16/2020

CR-PLP-2020-

212

Radiation Work Permit (RWP) Packages with Attention to

Detail Errors

04/17/2020

CR-PLP-2020-

220

RP Supervisor Does Not Have Required Training to Meet

Requirements in EN-OM-123, Fatigue Management Program

04/17/2020

CR-PLP-2020-

01305

ICP-OES Tripping on High Temperature Reading

05/20/2020

CR-PLP-2020-

01392

Measuring &Testing Equipment ID# 006428 (OD

MICROMETER) Found Non-conforming during Calibration

Services

05/01/2020

CR-PLP-2020-

01446

Inadequate or Untimely Response to C-42 Secondary Panel

Slarms and Deficient Chemistry Parameters Does Not Meet

Management Expectations

05/05/2020

CR-PLP-2020-

01448

PCS Lithium Under Target at 2.06 ppm Post Delithiation

05/06/2020

CR-PLP-2020-

01457

Area of Concern Associated Rigorous Use of HU/THINK 3

Tools

05/06/2020

CR-PLP-2020-

01460

Radiation Protection Department Aggregate Performance

Issue

06/22/2020

CR-PLP-2020-

01468

Measuring &Testing Equipment ID#014993 (Dynamometer)

Found Non-conforming during Calibration Services

05/07/2020

CR-PLP-2020-

01517

Dosimetry Investigation Reports (DIRs) May Not Accurately

Characterize Impact of Silver-110m on Dosimetry Results

05/12/2020

CR-PLP-2020-

01521

Contrary to EN-EV-112, Unlabeled, Unattended, Open

Five-Gallon Bucket Containing Approximately Two Gallons of

Apparent Aluminum Sulfate

05/12/2020

CR-PLP-2020-

01533

PMT of Newly Installed Mag Traps on Secondary Sample

Panel, Noted Operation of Mag Traps Causes EC-42

Dissolved Oxygen Alarms

05/13/2020

CR-PLP-2020-

Measuring &Testing Equipment ID#012344 (15-75 Inch Dial

05/15/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

01572

Torque Wrench) Found Out of Tolerance during Calibration

Services

OE-NOE-2018-

00012

NRC-RIS-2005-31 - R1

01/04/2018

OE-NOE-2018-

00042

T.S. 3.0.4 - MODE CHANGES MADE WITH INOPERABLE

EQUIPMENT TS LCO 3 0 4 June 2015 to September 2017

01/17/2018

OE-NOE-2019-

00142

INPO-IER-L3-19-5 - Crew Leadership Shortfalls Result in

Nonadherence to Procedure-required Reactor Scram and

Reactivity Transient

05/08/2019

OE-NOE-2020-

00068

IRIS-470127 - Emergency Diesel Generators Autostarted as

Designed Due to Loss of Power To 6.9kV Shutdown Board

03/16/2020

Miscellaneous

Q4-2019 CCS

System Health

report

Q4-2019 CCS System Health report

05/26/2020

QA-7-2018-PLP-1 QA Audit - Emergency Preparedness [10CFR50.54 (t)]

06/11/2018

QA-8-2019-PLP-1 Engineering Programs (Engineering, License Renewal, and

Operational Information Technology) 2019 Audit Report

05/14/2019

Procedures

EN-LI-102

Corrective Action Program

EN-LI-104

Self-Assessment and Benchmark Process

EN-LI-118

Cause Analysis Process

EN-WM-101

On-line Work Management Process

Self-Assessments LO-PLPLO-2018-

00001

Chemistry Human Performance Assessment

4/25/2018

LO-PLPLO-2018-

00017

Maintenance - Adherence to Electrical Safety Practices

10/17/2018

LO-PLPLO-2018-

00023

Chemistry 4th Quarter 2018 Chemistry Tracking

03/14/2019

LO-PLPLO-2018-

00053

Failed Fuel Airborne Radioactivity Controls Formal

Benchmark

06/05/2018

LO-PLPLO-2018-

00067

Effectiveness Review for RCE, CR-PLP-2018-02143

05/07/2018

LO-PLPLO-2019-

00014

Pre-NRC Design Basis Assurance Inspection (DBAI)

Self-Assessment

09/05/2019

LO-PLPLO-2019-

2019 Pre-NRC Emergency Planning Program Inspection

2/11/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

00026

Assessment

LO-PLPLO-2019-

00049

20 PI&R Readiness Assessment

03/24/2020

QA-10-2018-PLP-

Quality Assurance Audit Report: Maintenance

08/07/2018

QA-14-15-2019-

PLP-1

Quality Assurance Audit Report: Combined Radiation

Protection (RP) and Radwaste (RW)

10/29/2019

QA-2-6-2019-

PLP-1

Quality Assurance Audit Report: Combined Chemistry,

Effluents and Environmental Monitoring

09/30/2019

Work Orders

00528935-01

LT-0146B (PCP-50D) Upper Oil Level Indicates High Off

Scale

00541047-01

CV-0605; Heater E-6B Drain Valve Not Controlling Level

2924271-01

Manual Stroke of Valve CV-2008/2010

0