ML18067A595

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Insp Rept 50-255/97-05 on 970301-0411.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML18067A595
Person / Time
Site: Palisades Entergy icon.png
Issue date: 06/17/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML18067A592 List:
References
50-255-97-05, 50-255-97-5, NUDOCS 9707010168
Download: ML18067A595 (27)


See also: IR 05000255/1997005

Text

U.S. NUCLEAR REGULATORY COMMISSION

Docket No.:

License No.:

Report No.:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved by:

9707010168 970617

PDR

ADOCK 05000255

a

PDR

REGION Ill

50-255

DPR-20

50-255/97005(DRP)

Consumers Power Company

21 2 West Michigan Avenue

Jackson, Ml 49201

Palisades Nuclear Generating Plant

27780 Blue Star Memori~I Highway

Covert, Ml 49043-9530

March 1 through April 11, 1997

M. Parker, Senior Resident Inspector

P. Prescott, Resident Inspector

Bruce L Burgess, Chief

Reactor Projects Branch 6

EXECUTIVE SUMMARY

Palisades Nuclear Generating Plant

NRC Inspection Report 50-255/97005

This inspection reviewed aspects of licensee operations, maintenance, engineering and

plant support. The report covers a 6-week period of resident inspection.

Operations

The inspectors identified that a drawing discrepancy associated with the safeguards

high pressure air system was not dispositioned in a timely manner.

(Section 01 .2).

The inspectors concluded that, after identification by an operator, good followup

resulted in timely actions preventing further degradation of service water bay level

(Section 01.3).

Maintenance

The inspectors' review of the main steam isolation valve Code repair issue

determined that the licensee failed to provide adequate oversight resulting in an

improper code repair on these valves. The licensee understood the significance of

the event and the need to apply resources necessary to prevent recurrence.

Violations were identified for the failure to perform a proper Code repair, failure to

issue an LER within thirty days, and three examples of a failure to follow

procedures (Section M 1. 2). Corrective actions to date appeared to be thorough.

Engineering

The inspectors determined that the licensee initially did not aggressively pursue

resolution of the power cable ampacity issues. (Section E 1. 1).

The inspectors expressed concerns with timeliness of corrective actions. The

findings were discussed with the nuclear performance assessment department

(NPAD). NPAD agreed the data indicated a performance problem. Currently, NPAD

is trending these additional items to determine the significance and what future

actions may be necessary (Section E1 .2).

Due to the inspectors' concern with potential high pressure air system pressure

control valve degradation, the licensee developed a schedule to open and inspect

the valves in question. (Section E1 .3).

\\

Plant Support

The inspectors concluded that the licensee's placement of the criticality monitoring

devices was in accordance with 10 CFR 70.24 (a)(2). However, the inspectors

2

-

--.:.. __ _

-*-

were unable to determine the sensitivity of the monitors, as required by

10 CFR 70.24(a)(2), since the licensee was unable to produce any analysis to

support this conclusion. This was considered an Unresolved Item

(50-255/97005-04(DRP)) pending further evaluation by the licensee (Section R 1.2).

3

REPORT DETAILS

Summary of Plant Status

The plant operated at essentially 99.6 percent power for the entire inspection report

period. There was one power reduction commenced at 9:30 pm est on March 4, 1997, to

repack the P-1 OA heater drain pump. A return to full power began at 10:39 pm (EST) on

March 5, 1997. Full power was achieved at 5:59 am est on March 6, 1997. April 11,

1997, marked the 52nd day of the current power production run.

I. Operations

01

Conduct of Operations

01.1

General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations. The conduct of operations was considered by the

inspectors to be good; specific events and noteworthy observations are detailed

below.

01.2

High Pressure Air Drawing Discrepancies

a.

Inspection Scope (71707)

The inspectors observed portions of several plant activities.

b.

Observations and Findings

During a routine followup of the safeguards high pressure air system concerns with

plugging of Moore pressure control regulators, the inspectors identified concerns

with controlled drawings. The inspectors identified that a line had been mistakenly

dropped from the high pressure controlled air drawing, M-225, sheet 2, during the

revision process. The inspectors reviewed controlled drawings in the control room

and noted that the drawing had been modified by a penciled in correction. Also,

controlled drawings in the tagging center were observed to be addressed in a

similar manner. Discussions with system engineering noted that they were not

aware of the discrepancy as they were utilizing outdated laminated drawings.

Further followup did not identify that any drawing change had been initiated to

correct the discrepancy.

c.

Conclusions

The inspectors concluded that the drawing error was very minor in nature;

however, the inspectors were more concerned with the failure to properly address

this issue in a timely manner. This concern was discussed at the exit.

4

01.3

Service Water Pump Bay Debris Intrusion

a.

Inspection Scope (71707, 61726 and 62703)

The inspectors followed the licensee's actions in response to continuing fouling of

the service water bay traveling screens and service water pump basket strainers.

b.

Observations and Findings

As a result of a decrease in service water bay level on February 13, 1997, in which

level was observed to have decreased approximately two feet due to icing and

buildup of-.debris on the traveling screens, the inspectors have continued to closely

monitor the licensee's actions to address further service water fouling conditions.

Periodically, throughout the inspection period, the inspectors have observed an

increased frequency of debris intrusion into the service water bay. This condition

has been observed at the service water bay traveling screens, service water pump

basket strainers, and cooling tower pump seal coolers. Since initial identification,

the licensee has taken additional measures to address this concern, including

heightened awareness by both the operating shift and system engineering. The

increased monitoring has resulted in timely identification of debris intrusion by the

operating shift prior to encountering a significant buildup. The inspectors have

observed operations and system engineering involvement in the troubleshooting

efforts to understand the cause of debris intrusion. Initial evaluation of the debris

has indicated that it is not indigenous to Lake Michigan. System engineering has

noted that the debris is from runoff due to recent heavy rains, and its impact is

compounded by high lake levels and westerly wind conditions. The inspectors have

observed increased entry into limiting conditions for operation (LCO) due to

declaring the service water pumps inoperable for service water pump basket

strainer cleaning.

c.

Conclusions

The inspectors concluded that the licensee has provided the appropriate resources

to closely monitor service water bay debris intrusion and provided additional

oversight to monitor icing conditions. The inspectors concluded that continued

monitoring is warranted to ensure system performance is not impaired by further

intrusion of debris past the service water basket strainers into the service water

system.

08

Miscellaneous Operations Issues (92702)

- ---(Closed) Violation 50-255/95014-02: Failure to maintain low press_urizer_ PL~Ss_u_r~

function of safety injection system (SIS) operable. On January 18, 1996, the

reactor was being placed in cold shutdown due to faulted 2400 VAC cables that

supplied the 1 D bus. A work order for disabling the SIS was noted by an electrical

maintenance supervisor. After a discussion with the shift supervisor (SS), a review

of plant conditions, and a review of what were thought to be applicable

5

requirements, the SS released the work order. Primary coolant system (PCS)*

temperature was at approximately 364°F at the time the work order was released.

This work disabled the SIS actuation on low pressurizer pressure when PCS

temperature was approximately 364°F. This was a violation of Technical

Specifications (TS) section 3.17 .2, which required the SIS actuation signal to be

operable above 300°F.

Several program and process barriers were breached requiring corrective actions for

each. For the problems delineated below, the licensee's corrective action in

response to the item is also provided:

.,. __ The work order block marked "TS Involvement" referenced TS 3.17.

However, this section was not referred to and another section of TS was

thought to be the applicable requirement.

All maintenance supervisors were counselled on assuming any prerequisite is met

prior to commencing work. Also, operators, especially senior reactor operators,

were trained to verify information using available references when making decisions

affecting plant status or safety.

Procedure GOP-9, Attachment 1, section 4.4 stated, "When PCS is less than

210°F (ie, cold shutdown), then initiate work order to disable SIS actuation

circuits {refer to SOP-3, step 7. 7 .1 }. " These steps went unheeded in the

decision making process to disable SIS.*

TS 3.16 "Engineering Safety Features System Instrumentation Settings,"

was referenced as the controlling requirement.

Training was given to operators on the significance of adherence to both the TS

and the procedure in conjunction with disabling the SIS actuation signal.

Electrical maintenance procedure ESS~E-24, "Disable/Enable The SIS

Actuation On Low Pressurizer Pressure," section 3.3, specifies plant

condition to be "cold shutdown." Procedure step 5.1 requires the assigned

supervisor ensure all prerequisites are completed. The plant condition of

cold shutdown was not verified.

The procedure was revised in section 3.4 to state, "As controlled by the authorizing

work order." This is standard with other procedures. Section 3.3 still states "cold

shutdown."

SOP-3 section 7. 7 was revised to include reference to ESS-E-24. This procedure

performs the actual disabling/enabling of the SIS circuitry. This item is clQ~ed.

  • (Closed) LER 50-255/96-004: Safety injection disabled with primary coolant

system greater than 300°F. This event resulted in Violation 50-255/95014-02.

The inspectors reviewed the adequacy of the licensee's corrective actions

6

pertaining to the LER in response to the violation, as noted above. This item is

closed.

II. Maintenance

M 1

Conduct of Maintenance

M1 .1

General Comments

a.

Inspection Scope (62703 and 61726)

The inspectors observed all or portions of the foUowing work activities:

Work Order No:

  • *
  • *
  • *

24710994:

24511071:

24711073:

24611820:

FIN TEAM:

HSF97080:

24 710599N.2:

Surveillance Activities

Ml-2:

Ml-005A:

Ml-06:

Ml-27E:

Ml-39:

b.

Observations and Findings

Repack of P~1 OA heater drain pump

Repack, disassemble pump, and decontaminate P-55A

charging pump

DC circuit ground troubleshooting

Perform MSE-E-38 PM/EOPM of Safety Related

Limitorque Type SMB Actuators on VOP-307 2

(charging pump line to SI test line isol. valve)

Replacement of failed diaphragm on CV-5501, M-598

Evaporator Concentrator level control valve

Hot spots flu'sh on tilt pit drain line

Perform resin removal and flush line from tank T-80

equipment drain tank

Reactor Protective Trip Units

Containment High Pressure Test *

Area Monitor Operational Checks

Functional Check of PCS Low Temperature

Overpressure Protection (L TOP) System

Auxiliary Feedwater Actuation System Logic Test

The inspectors found the work performed under these activities to be professional

and thorough. All work observed was performed with the work package present

and in active use. Work packages were comprehensive for the task and post

maintenance testing .requirements were adequate. The inspector_s_fr_e_quently _______ .

observed supervisors and system engineers monitoring work practices. When

applicable, appropriate radiation control measures were in place.

7

c.

Conclusions

In general, the inspectors observed good procedure adherence and maintenance

practices. However, detailed below is the inspectors' follow up to the main steam

isolation valve issue that occurred during the 1996 refueling outage. The

inspectors' and licensee's review of this event identified several maintenance

process and human performance issues. See the specific observations detailed

below.

M1 .2 Main Steam Isolation Valves (MSIVs) Repair Issues

a.

Inspection Scope (62703)

In inspection report 50-255/96017, the inspectors reviewed the events that led to

potentially inadequate repairs to the stuffing box plugs in both main steam isolation

valve (MSIV) leakoff lines; identified as an unresolved item 50-255/96017-04. This

was a followup by the inspectors to the process weaknesses found and the

licensee's actions to prevent recurrence.

b.

Observations and Findings

On December 20, 1996, with the plant in hot shutdown, both MSIVs (CV-0501 and

CV-0510) were found leaking steam from the plugged west stuffing box leakoff

points. Initially, the valve contractor and the planning organization were requested

to evaluate appropriate repairs. The licensee decided a temporary leak repair was

. .

preferable; otherwise, the plant would have to return to cold shutdown to perform

permanent repairs.

Initial inspections identified that CV-0501 had a pinhole leak and CV-051 O had

several pin hole leaks at the threaded connection. The licensee's temporary leak

repair vendor, after an earlier initial review of the job, was brought onsite to initiate

repairs on January 6, 1997. The plant was at 20 percent power. The vendor

began drilling on CV-0510 first. However, drilling stopped when the vendor noted

leakage through what appeared to be fractures in the plug. Work was stopped on

CV-0510 and a decision was made to proceed on CV-0501. On CV-0501 , the

vendor began drilling into the pipe plug to prepare for threading in the leak injection

fitting. However, the vendor stopped because steam began leaking almost

immediately after the start of drilling, which would be indicative of an abnormal

configuration of the high pressure pipe plug. The inspectors noted that the licensee

did not evaluate problems with CV-0510 prior to starting work on CV-0501.

Licensee management was informed of the valves' condition and decided to bring

the plant to cold shutdown to make permanent repairs.

The inspectors reviewed past valve history. CV-0501 began leaking at the leakoff

plug in 1992. Leakage was minimal. System engineering trended leakage until the

1993 refueling outage. Although permanent repairs were performed, a work

history did not exist. A seal weld was requested but was not performed. In 1995,

another leak developed at the plug. The plug was drilled and pumped with a leak

8

sealant. It was subsequently pumped three more times prior to the 1996 refueling

outage. On CV-0510, there was no documented history of leakage of the stuffing

box leakoff pipe plugs.

During the refueling outage, extensive preventive maintenance (PMs) was

performed on CV-0501. As part of these activities, the stuffing box pipe plug was

to be replaced to restore system integrity after a temporary leak injection hole was

drilled into the plug body. Work order 24512907, step 6, required that the original

plug be replaced and seal welded. The original plug was not removed. Instead, on

November 16, 1996, a seal weld was placed over the leak injected plug and around*

the threads. To facilitate seal welding, the hex head of the plug was ground away.

The weld supervisor, after discussions with the valve team supervision approved

this repair even though the weld inspection checklist (WIC) sketch depicted the plug

hex head in place. Failure to adhere to the weld inspection checklist was

considered an example of a violation of 10 CFR 50, Appendix B, Criterion V

(50-255/97005-3A).

Preventive maintenance (PM) was also performed during the outage on CV~0510.

As part of the maintenance, the plug was to be seal welded. This action was taken

as a precaution to prevent leakage similar to CV-0501. Upon inspection, the

welder found the plug appeared to have a square versus hex head. The welder

discussed the condition with the contractor valve team manager instead of the

welding supervisor. Also, problems were encountered during welding, which were

indicative of welding dissimilar metals. The weld used to seal CV-0510 on

November 1 6, 1997, was not the weld specified by the weld inspection checklist.

This was another missed opportunity to identify a problem. The decision to accept

the condition was based on the premise that a non-destructive examination (NOE)

would be performed; therefore, any problems would be identified. A lab report

documenting a metal analysis of the plug indicated the plug material was 125 psig

cast iron versus the specified high pressure steel rated at 3000 psig. This also

explained \\IVhY welding proved difficult. The failure to adhere to the procedure

(weld inspection checklist) is another example of a violation of 1 O CFR 50,

Appendix 8, Criterion V (50-255/97005-038). *

The inspectors noted several maintenance work practice deficiencies during their

inspection. The licensee also identified similar concerns through a special

investigative team assigned to evaluate this condition. First, in the pre-job briefs

held for both MSIV PM activities, the welders were not included. Secondly, there

were design issues involving the grinding away of the hex head and seal welding

over the drilled hole in CV-0501. Both were accomplished without implementing

the required design change controls. Third, the inspectors review and the licensee

investigation identified a lack of questioning attitude on the part of welding

_____ QerSQDQ~I. . T_he as- left GOndition of the plug seal welds was different than

_

indicated on the WIC sketch. The welding supervisor approved the seal weld even

though the WIC sketch depicted the plug head in place. Work orders existed to

cover the general work activities on the valve. However, the WOs were not used

at the work site during the pipe plug activities. The failure to have the work orders

9

.. .........:~.

. c .

d.

at the work site is a third example of a violation of 1 O CFR 50, Appendix B,

Criterion V (50-255/97005-3C).

For CV-0510, the welder found the plug appeared to have a square head versus a

hex head. Also, the plug was degraded as there was a fracture in the head of the

plug. However, the weld supervisor was not made aware of these issues until after

the seal weld was completed, Also, for CV-0510, no records were found that

indicated the plug repairs or modifications were made. Finally, there was no single

point of contact during the maintenance activities performed on the valve for

problem resolution.

Both MSIVs are ASME Code Class 2 valves, which shall be repaired in accordance ....

with ASME Code Section XI. Failure to perform a proper ASME Code repair was

considered a Violation (50-255/97005-01 ).

The inspectors followed the licensee's root cause investigation and subsequent

corrective actions. Both leaking plugs were permanently repaired by installing

3,000 psi forged steel, one inch pipe plugs with high temperature sealant through

design change FES97-003. The issue was discussed with the various work

groups. The event was reviewed, weaknesses identified and corrective actions

discussed. Maintenance management developed action items, which were

incorporated into the department master action plan.

'

Reporta bility

On March 6, 1997, during a management review board (MRS) meeting for condition

report (C-PAL)97-007 the licensee questioned reportability for the unauthorized

repairs conducted to the stuffing box plugs on the MSIV's. Based upon this

discussion, the licensee determined that a 30 day licensee event report (LER) was

required to be submitted to the NRC based upon 10 CFR 50. 73. The inspectors

questioned the licensee's basis for start of the 30 day report, as It appeared that

the licensee had ample information on February 19, 1997, because the results of

the evaluation of the material composition for the stuffing box plug for MSIV

CV-0510 were 'Obtained, which was forwarded from the laboratory to the plant

site. The laboratory results confirmed that the installed stuffing box plug was cast

iron material and; therefore, a 125 psig plug was installed versus the required 3000

psig high pressure steel plug. In addition, on/or about January 10, 1997, adequate

information was available to determine that an unauthorized code repair had been

conducted to MSIV CV-0501, in that an unauthorized seal weld was performed on

the stuffing box plug on the MSIV. This condition was not identified until the plant

was started up on January 6, 1997. The failure to report a condition outside the

design basis of the plant within 30 days is considered a violation of 1 0 CFR 50. 73

. (50-255/97005-02).

- ----- ----- -- ---- -

Conclusions

The inspectors concluded the licensee failed to maintain adequate control over the

MSIV stuffing box valve pipe plug repairs, as evidenced by the procedural violation

10

with three examples. CV-0501 and CV-051 O should have been repaired in

accordance with ASME Section XI and this was considered a violation. Also, the

licensee failed to make a timely report to the NRC, a third violation.

However, the inspectors reviewed the licensee's extensive corrective actions to

date, which demonstrated an understanding of the potential significance of the

event. The inspectors' evaluation of the safety significance determined that had

the pipe plugs actually failed, the safety significance would have been minimal. The

leakage would have represented an additional potential radiological release,

coincident with a steam generator tube rupture. However, the leakage would be

small compared to the large secondary coolant mass released to atmosphere

through the atmospheric dump valves. Sufficient margin existed in the radiological

dose calculations to account for this minor leakage. The inspectors, through

observations of subsequent maintenance work did not identify additional examples

of inadequate procedural adherence or improper oversight of contractor and licensee

maintenance personnel.

MS

Miscellaneous Maintenance Issues (92902)

(Closed) LER 50-255/95-001: Malfunction of left channel design basis accident

(DBAl sequencer resulted in inadvertent actuation of left channel safeguards

equipment. The left channel sequencer, MC-34L, spuriously activated on March 2,

1995. All safeguards equipment responded as required. The licensee formed a

team to determine root cause. The team determined that a failure of the micro-

processor module of the electronic DBA sequencer caused the event. The

sequencer is a programmable logic controller (PLC) that consists of a main micro-

processor and various input/output (1/0) modules for each piece of equipment

actuated by the sequencer. The microprocessor was replaced and operability of the

sequencer verified. The microprocessor was sent to the vendor for testing. The

vendor could not simulate the problem, but agreed with the licensee's conclusion

that the problem was most likely a faulty component that caused an intermittent

  • memory or processor error. The inspectors reviewed the historical performance of

the DBA sequencer. A similar event occurred in 1989, to the right channel

sequencer. However, similarity was limited to the loss of active lights on the 1/0

cards and the inability to recreate the failure. In 1995, a polarity sensitive capacitor

was incorrectly installed during manufacture in the processor unit of MC-34L,

which caused its power supply to fail. During repair/diagnosis of the failure by the

vendor, it was determined that a capacitor had been installed backwards and was

the cause of the MC-34L failure. The inspecto.rs concluded that this did not appear

to be a generic reliability or maintenance issue. This item is closed.

{Closed) Violation 50-255/95002-01: Failure to perform the required independent

verifica_tiQIJ. A fieLc;I_ t!3chnician caused a false reactor trip indication while landing __

electrical leads to install a personal computer (PC) to record main generator output

data, per temporary modification (TM)94-017. The TM provided the steps for

installing the PC, but the field technician failed to follow these steps .

11

The inspectors had the following observations concerning the installation of the TM.

For each observation, the corrective action is outlined:

Contrary to TM Procedure 94-017, there was no independent verification

performed for each step of the TM.

Administrative procedure 9.31 was revised so that the independent verification

shall occur concurrent with the TM installation.

The proper method of independent verification was not understood by the

field technician.

The event was reviewed with all technicians. Also, written expectations for work

at Palisades was issued to all technicians.

The quality of the documentation of work performed was poor. Also, the

instructions in the TM were not clear.

The event was reviewed with planners and a memo sent to each planner stating

that relevant information from a temporary modification will be incorporated into

the work order. This event was also reviewed with all maintenance supervisors

sharing lessons learned from this event. The electrical and instrumentation and

control (I & C) supervisors were issued management expectations for work that

involves Consumers employees that are not permanently assigned to the Palisades

plant. A memo was issued to all engineering personnel to review this event. This

item is closed.

Ill. Engineering

E1

Conduct of Engineering

E1 .1

Power Cable Ampacity Review

a.

Inspection Scope (37551)

The inspectors reviewed engineering's progress on the issue of determining if plant

power cables are within Final Safety Analysis Report (FSAR) requirements for cable

ampacity and temperature limits. If a cable was identified outside of these limits,

then the inspectors reviewed the associated operability determination for adequacy.

b.

Observations and Findings

l~_Ln?_Pe!?ti_on report 50-255/96017, the inspectors reviewed the licensee's

development of a degraded equipment list in response to Ge-neric letter (GL). 91--18,-

"Resolution Of Degraded And Nonconforming Condition." This action was taken to

ensure that an appropriate overview of equipment/system operability had been

conducted prior to startup from the 1996 refueling outage. GL 91-18 provides

guidance on resolution of degraded and nonconforming conditions affecting safety-

12

related systems structures and components (SSCs). The inspectors reviewed the

list for thoroughness and potential conflicts with GL 91-18 guidance or

noncompliance with 10 CFR 50 Appendix B "Corrective Action." Specifically, the

inspectors looked for timely and adequate repair or engineering safety analyses of

the issues identified.

One of the issues that came out of the degraded equipment list was the

acceptability of the licensee's methodology for calculating cable ampacity. Since

1988, the licensee has been in the process of reviewing cables within the plant to

evaluate the impact of accelerated aging due to heat degradation of the insulation

caused while energized. The licensee had determined that 2700 of 2900 power

cables in 424 cable trays were routed in trays with greater than 30 percent fill. .. _

The licensee concluded that while certain analyzed cables exceeded Code ampacity

limits, the cable thermal limits were not exceeded and therefore, the FSAR design

basis was met. Section 8.5.2 of the FSAR states, in part, "Cables installed in

ventilated trays, conduit or underground ducts are thermally sized in accordance

with National Electrical Code (NEC) or the Insulated Power Cable Engineer

Association/Insulated Cable Engineer Association (IPCEA/ICEA) ampacity values.

Ampacities are adjusted based on actual field conditions when possible. These

adjustments may include, but not be limited to, conductor operating temperature,

ambient temperature, cable diameter, tray depth of fill, conduit percent fill, and

firestops."

Prior to startup from the 1996 refueling outage on December 25, 1996, the

licensee justified operability of 41 cables based upon a bounding Harshe-Black

analysis. Presently, the Harshe-Black methodology used to justify operability for

these cables has not been approved for use by the NRC. The Code assumes that

all cables are continuously energized and carrying rated current. The Harshe-Black

methodology considers only those cables that are energized for a design basis

accident (OBA). Harshe-Black also differs from the Code in that the code calculated

ampacity limit ensures the cable thermal limit will not be exceeded, while the

Harshe-Black method allows the ampacity limits to be exceeded because field

testing of ampacity (at Palisades) demonstrated that a cable could be above the

100 percent ampacity limit and the cable thermal limit will not be exceeded.

On March 31, 1997, the licensee determined that a number of cables might exceed

the ampacity of the non-refined Harshe-Black methodology; meaning direct readings

of environmental and operating conditions will be required for calculations.

During

this comprehensive review, the inspectors were notified by the licensee that 1 7

cables have been calculated to exceed the Harshe-Black methodology. The licensee

discussed with the inspectors the methods that would be used to determine

operability of the 17 cables. The licensee intends to provide direct temperature and

---cun:ent.measurements and perform a visual inspection to justify c_o!l~inued_ . ______ _

operability of the affected cables. The licensee provided an informal completion

date of the end of 1997 for this review. The inspectors expressed a concern to the .

licensee that this target date may not allow sufficient time to incorporate cable

13

--*-

c.

replacement, if determined necessary, by start of the May 1998 refueling outage.

The licensee has since reevaluated the time required to analyze the cables and

committed to complete evaluations of the remaining cables within a few months.

Conclusions

The inspectors determined the licensee's actions were adequate. The licensee did

not initially appear to be aggressively pursuing resolution of this issue. The NRC

intends to review the licensee's final engineering analysis to determine whether the

cables are within FSAR requirements, degraded but operable, or require

replacement. The licensee has also agreed to incorporate any necessary cable

replacements within the scope of the 1998 refueling outage.

E1 .2 Timely Resolution Of Issues

a.

Inspection Scope (37551)

In inspection report 50-255/97002, the inspectors reviewed the events surrounding

a February 1997, P-66A high pressure safety injection (HPSI) pump breaker trip.

The trip occurred while attempting to charge a safety injection tank (SIT). As part

of that review, the inspectors also looked at a similar event that occurred in July

1996. Specifically, the inspectors reviewed the licensee's timeliness of corrective

actions to address the events.

b.

Observations and Findings

The scenario for the two events was similar. While refilling a SIT following a

sampling collection, the HPSI pump tripped. Inspection of the HPSI pump breaker

revealed that the "Y" phase time overcurrent (TOC) relay had actuated, which

tripped the pump. Also, in October 1996, an auxiliary operator during rounds,

found the "Y" phase TOC relay target had dropped in. In each case, a different*

root cause was determined to have initiated the breaker trip or TOC relay flag to

drop in. The inspectors observed the licensee's actions for each event. Immediate

actions by the licensee were appropriate.

However, when the inspectors reviewed the assigned corrective actions of the

condition report (CR) from the July event, only two of the four corrective actions

had been completed. The procurement of spare relays had been extended from the

original November 1996, to March 1997 completion date. The action to revise

procedure SOP-3, "Safety Injection and Shutdown Cooling System," to permit the

use of the o.ther HPSI pump P-668, to fill the SITs at full primary coolant system

pressure, if justified by engineering analysis, was due to be completed in November

1996. This was also-given an-extension to-April 1997 .. Subsequentl¥., the liceosee_

had re-evaluated the issues. Spare parts have been procured and the procedure

revision completed.

Because of this example and other known instances of lack of a timely response to

issues, the inspectors reviewed the CR tracking system to verify how prevalent this

14

problem may be. The nuclear performance assessment department (NPAD) trended

the total number of CRs granted due date extensions and open CR corrective action

subdocuments for management review. NPAD also independently trended average

CR cycle time. The inspectors discussed with NPAD a concern that there may be

CRs that were given multiple extensions and CRs not meeting the original scheduled

completion period. Also, that system engineering may have the most significant

problem with extensions. From the discussion, NPAD performed a review of the

CR data base. For February 1997, out of the total 138 CRs granted extensions, 92

had one extension, 29 CRs had two extensions, and 10 CRs had 3 extensions.

There was one CR with 8 extensions. In February, only 57. 7 percent of the CRs

met the forecasted completion date. System engineering was granted the most due

date extensions (56) in the month of February.

c.

Conclusions .

The inspectors discussed the findings with NPAD and NPAD agreed the data

indicated a performance concern. Currently, NPAD is trending these additional*

items to determine the significance and what future actions may be necessary.

E 1 .3

Safeguards High Pressure Air System Reliability

a.

Inspection Scope (37551)

The inspectors reviewed the root cause analysis documenting the failure of a

pressure control valve (PCV) and an air regulator for the high pressure safety

injection (HPSI) .control valve. The inspector's review identified what could be

potentially viewed as a generic failure mechanism, the plugging of air regulator

controllers by rust accumulating on the debris screens. The inspectors reviewed

past work history on the PCVs and discussed the safeguards high pressure air

system performance with system engineering.

b:

Observations and Findings

On March 19, 1997, CV-3018, the HPSI discharge control valve cross-tie to train

two, was stroked. The valve was stroked closed and could not be stroked open.

The corresponding air regulator PCV was found to be plugged by rust that.

originated from the west engineering safeguards room high pressure air system

piping, which is carbon steel. The inspectors discussed with system engineering if

this had potential generic implications. From the discussions several longstanding

system deficiencies were noted. The present pressure control valves which were

installed in 1988, due to obsolescence of the previous valve. have a small orifice

with a screen that goes to a pilot chamber. That screen was found clogged with

rust,-which-disabled-the -PCV. The inspectors noted that .the piping-for-the. system- __ _

is carbon steel.

The inspectors reviewed the work history of PCVs and noted that the present PCVs

were installed in 1988, due to observed degradation of the original PCVs.

However, a review of the work history did not identify a reliability problem with the

15

valves. The inspectors, in discussions with system engineering, found that the

license's preventive maintenance program, known as Periodic Predetermined

Activities Control (PPAC), were stopped in 1991, due to concerns with taking the

valve out of service. System engineering had recently reinstituted the PPACs.

However, none of the PPACs have been performed to date. The inspectors

reviewed the safeguards high pressure air system drawings and noted that not all

PCVs were configured the same. Some PCVs had the air filters upstream of the

valve, as would be expected. However, the majority of the filters were located

downstream of the PCVs and system engineering was aware of the discrepancy.

However, the inspectors were concerned that this was a longstanding issue which

had not been resolved. Engineering followup on the issue was found to be minimal.

The inspectors noted nearly all valves have a backup system of either instrument air

or nitrogen. Further, system engineering noted that the pressure control valve

required a 10 psi differential pressure downstream before the PCV opens. The

inspectors identified that this could potentially mean the only time the PCV would

be operated is during the once a refueling outage high pressure air system

performance test. In normal system configuration the only air going through the

PCV is a nominal flow of bleed off air. The inspectors reviewed the refueling

outage performance test, T-205, "High Pressure Air System Performance

Verification." In the 1996 refueling outage the test was not performed. In the

1995 refueling outage, minimal testing was performed. The inspectors noted there

was questionable data from the test. The Final Safety Analysis Report (FSAR)

stated that there will be enough air to stroke required valves after 40 minutes. The

PCVs have a constant bleedoff port, yet the pressure did not dec;:ay after an hour.

Also, after stroking some valves, there was no system pressure loss noted. The

inspectors reviewed the FSAR and Technical Specifications for any testing

frequency requirements. None were found. The HP air system does not have a

design basis document (DBD). A DBD is under consideration for the near future.

In addition, the inspectors reviewed the licensee's probabilistic risk analysis (PRA)

which identified that the high pressure air compressors, C-6A and C-68, were fed

from the opposite train of power than the components they serve. This has led to

some PRA results that would not be expected if the compressor power feeds were

consistent with the served component power feeds. This becomes important in

scenarios where one train of power/components is failed and recirculation is

achieved more than one hour after accident initiation. Since it was demonstrated

that there is only enough air in the receiver tanks to last 40 minutes, the

containment sump valve would not open unless the compressors were available.

This type of scenario is most likely during fire events, especially in the west

safeguards room.

c.

Conclusions

The inspectors identified to the licensee the problems noted. System engineering

has since scheduled PM activiti.es to inspect and clean selected PCVs; specifically,

those that have filters downstream of the PCVs. These have been determined most

susceptible to plugging. System engineering was reviewing the feasibility of

modifications to improve system reportability .

16

ES

  • ---~-

Miscellaneous Engineering Issues (92700 and 92903)

(Closed) LER 50-255/95013: Circuit fuse coordination deficiency which affected

Appendix R safe shutdown equipment. Through the licensee's Appendix R

Enhancement Program, it was discovered that fuses in the potential transformer

(PT) circuit for the emergency diesel generator 1-1 were not properly _coordinated.

This could result in the PT primary side fuse blowing when Appendix R fire-related

faults appeared on a PT secondary side circuit. Blowing of the primary side fuse

should occur first to prevent fire-induced circuit faults from affecting diesel

generator operability. When the condition was discovered, compensatory measures

(hourly fire tours of the cable spreading room) were already in place. The lack of

fuse coordination in .the diesel generator PT circuit appeared to be an original design

deficiency.

The inspectors reviewed the Functional Equivalent Substitution (FES) that

documented the licensee's review to install properly sized fuses . .The circuit was

monitored for maximum inrush current and maximum steady state load. With this

information, a proper fuse size was determined .to coordinate with the upstream

fuse and still have acceptable margin for the expected load and available short

circuit current. The inspectors reviewed work order no. 24611 60, that installed the

fuses. This item is closed. *

IV. Plant Support

R 1

Radiological Protection

R 1.1

Maintenance Outages and Daily Radiological Work Practices

a.

Inspection Scope (71750 and 83750)

The inspectors observed radiological worker activities during various maintenance

activities detailed in this inspection report, and also monitored radiological practices

during daily plant tours.

b.

Observations and Findings

The inspectors observation of jobs in progress during the maintenance activities

detailed above revealed that radiation technicians were visible at the job sites. The

technicians took appropriate actions and surveys in accordance with good ALARA

practices.

c.

Conclusions

The inspectors concluded that radiological practices observed during the

maintenance activities and plant daily walkdowns were adequate. The inspectors

had no concerns. Specific observations are detailed below.

17

R 1 .2

Criticality Accident Monitoring

-*a.

Inspection Scope (71750 and 83750)

The inspectors reviewed the licensees conformance with the requirements of 1 0

CFR 70.24, "Criticality Accident Requirements."

b.

Observations and Findings

In reviewing the licensees compliance to 10 CFR 70.24, the inspectors identified

that the licensee had provided two criticality monitors in the spent fuel pool/new

fuel storage area. 10 CFR 70.24(a)(2) requires a monitoring system that is capable

of detecting a criticality which generates radiation levels of 300 rems per hour one

foot from the source of the radiation. It also required that monitoring devices in the

system have a preset alarm point of not less than 5 millirems per hour nor more

than 20 millirems per hour. The device shall be no further than 1 20 feet from the

special nuclear material. The licensee has two radiation monitors located in the

spent fuel pool/new fuel storage areas that are within 1 20 feet of the spent fuel

pool/new fuel storage areas. The area radiation monitors. RIA-2313 and RIA-5709,

Spent Fuel Pool Area Radiation Monitors, are set to alarm locally along with

illuminating an annunciator in the control room at a preset value of 1 5 millirems per

hour. The inspectors observed monthly surveillance testing which confirmed that

the alarm setpoints were properly established. In reviewing the instrument

sensitivity, the inspectors were unable to locate an*y analysis to support the

instruments ability to detect a criticality which generates radiation levels of 300

rems per hour at one foot. The licensee's review was unable to locate any

established documentation. The licensee had taken action, in response to the

inspectors concerns, to prohibit further receipt of new fuel in the new fuel vault

until adequate supporting instrument sensitivity analysis can be provided.

However, the licensee has provided a supporting analysis that concludes that the

reactivity will be less than 0.95 under worst case for the new fuel storage array.

In reviewing the licensee's procedures, the inspectors identified that the licensee

utilizes Alarm Response Procedure (ARP)- 8, "Safeguard Safety Injection and

Isolation Scheme EK-13 (EC-13)," upon initiation of a criticality alarm. After

confirmation of a valid alarm, Off Normal Procedure (ONP)-11.2, "Fuel Handling

Accident," is implemented to ensure that the appropriate steps are taken including

evacuation of personnel from the affected area. The licensee has identified that

evacuation drills have been conducted for simulated fuel handling accidents during

annual exercises and provided training on site specific alarms including area

radiation monitor alarms as part of the annual General Employee Training. This

training includes recognition of the specific alarm along with the required response

- -----to the alarm. Although the licensee has not conducted_ arw evac~at_ior:i __ q_rjll~;Jor_the _

specific area radiation monitor alarms, this action appears to meet the intent of

10 CFR 70.24(a)(3) .

18

c.

Conclusion

The inspectors concluded that the licensee's placement of the criticality monitoring

devices were in accordance with 10 CFR 70.24 (a)(2). However, the inspectors

were unable to determine the sensitivity of the monitors, as required by

10 CFR 70.24(a)(2), as the licensee was unable to produce any analysis to support

this conclusion. This was considered an Unresolved Item (50-255/97005-04(DRP)l

pending further evaluation by the licensee.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on April 16, 1997. No proprietary

information was identified .

19

PARTIAL LIST OF PERSONS CONTACTED

-Licensee

R. A. Fenech, Senior Vice President,

Nuclear, Fossil, and Hydro Operations

T. J. Palmisano, Site Vice President - Palisades

G. B. Szczotka,. Manager, Nuclear Performance Assessment Department

D. W. Rogers, General Manager, Plant Operations

D. P. Fadel, Director of Engineering

S. Y. Wawro, Director, Maintenance and Planning

J. L. Hanson, Director, Strategic Business Issues

R. J. Gerling, Design Engineering Manager

A. L. Williams, Acting Manager, System Engineering

T. C. Berdine, Manager, Licensing

J. P. Pomeranski, Manager, Maintenance

D. G. Malone, Shift Operations Supervisor

M. P. Banks, Manager, Chemical & Radiation Services

K. M. Haas, Manager, Training

M. E. Parker, Senior Resident Inspector. Palisades

P. F. Prescott, Resident Inspector. Palisades

20

  • -1p 37551:

IP 61726:

IP 62703:

IP 71707:

IP 71750:

IP 83750:

IP 92700:

IP 92903:

INSPECTION PROCEDURES USED

Onsite Engineering

Surveillance Observations

Maintenance Observation

Plant Operations

Plant Support Activities

Occupational Radiation Exposure

Onsite Followup of Written Reports of Nonroutine Events at Power Reactor

Facilities

Followup - Engineering

ITEMS OPENED

50-255/97005-01

VIO

Unauthorized Code repair performed on MSIVs

50-255/97005-02

VIO

Failure to submit a LER within 30 days as required by 10 CFR

50.73

50-255/97005-03

VIO

Failure to perform MSIV repairs in accordance with 10

CFR 50 Appendix B requirements

50-255/97005-04

URI

  • Unable to dete.rmine sensitivity of criticality monitors per 10

CFR 70.24

ITEMS CLOSED

50-255/96-017-04 URI

Inadequate repairs to stuffing box plugs in MSIVs

50-255/95014-02

VIO

Failure to maintain low pressurizer pressure function of safety

. injection system operable

50-255/96-004

LER

Safety injection disabled with PCS greater than 300 ° F

50-255/95-001

LER

Malfunction of left channel OBA sequencer resulted in

inadvertent actuation of left channel safeguards equipment

50-255/95002-01

VIO

Failure to perform the requireq independent verification

50-255/95-013

LER

Circuit fuse coordination deficiency which affected Appendix R

safe shutdown equipment

21

ff--AP

ALARA

ARP

ASME

CFR

CR

CRS

CV

DBA

DBD

DRP

EDG

FES

FSAR

GL

HPSI

ICEA

IFI

IPCEA

IR

LCO

LER

LTOP

MRB

MSIV

NCV

NDE

NOV

NPAD

NRC

NRR

ONP

oos

PCS

PCV

PLC

PDR

PM

PPAC

PRA

P-T--- --- -* . -

RFO

RIA

SI

SIS

SIT

LIST OF ACRONYMS USED

Administrative Procedure

As Low As Reasonably Achievable

Alarm Response Procedure

American Society of Mechanical Engineers

Code of Federal Regulations

Condition Report

Control Room Supervisor

Control Valve

Design Basis Accident

Design Basis Document

Division of Reactor Projects

Emergency Diesel Generator

Functional Equipment Substitution

Final Safety Analysis Report

Generic Letter

High Pressure Safety Injection

Insulated Cable Engineer Association

Inspection Followup Item

Insulated Power Cable Engineer Association

Inspection Report

Limiting Conditions for Operation

Licensee Event Report

Low Temperature Overpressure

Management Review Board

Main Steam Isolation Valve

Non-Cited Violation

Non-Destructive Examination

Notice of Violation

Nuclear Performance Assessment Department

Nuclear Regulatory Commission

Office of Nuclear Reactor Regulation

Off Normal Procedure

Out of Service

Primary Coolant System

Pressure Control Valve

Programmable Logic Controller

Public Document Room

Preventive Maintenance

Periodic & Predetermined Activity Control

Probabilistic Risk Assessment

Potential Transformer

Refueling Outage

Radiation Indication Alarm

Safety Injection

Safety Injection System

Safety Injection Tank

22

..

..

SRO

SS

--ssc

sv

SOP

TM

TOC

TS

VAC

WIC

WO

Senior Reactor Operator

Shift Supervisor

Systems, Structures and Components

Solenoid Valve

System Operating Procedure

Temporary Modification

Time Overcurrent

Technical Specification

Volts Alternating Current

Weld Inspection Checklist

Work Order 23

  • '

September 18, 1998

Mr. Thomas J. Palmisano

Site Vice President and General Manager

Palisades Nuclear Generating Plant

27780 Blue Star Memorial Highway

Covert, Ml 49043-9530

SUBJECT:

PALISADES INSPECTION REPORT 50-255/98015(DRP)

Dear Mr. Palmisano:

On August 21, 1998, the NRC completed an inspection conducted at your Palisades

Nuclear Generating Plant. The enclosed report presents the results of that inspection.

The inspection covered a 7-week period. Areas examined during the inspection are*

identified in the report. Within these areas, the inspection consisted of a selective *

examination of procedures and representative records, interviews with personnel, and

observation of activities in progress. The purpose of the inspection effort was to determine

whether activities authorized by the license were conducted safely and in accordance with

NRC requirements.

The operating crew demonstrated positive command and control while implementing the

emergency operating procedures in response to an inadvertent main feedwater pump trip

and resultant reactor trip. Your staff's root cause analysis for the main feedwater pump trip

  • was comprehensive and thorough.

No violations or deviations of NRC requirements were identified.

In accordance with 10 CFR 2. 790 of the NRC's "Rules of Practice," a copy of this letter and

the enclosure will be placed in the NRC Public Document Room.

Sincerely,

Original signed by ..

Geoffrey E. Grant, Director -

Division of Reactor Projects

Docket No.: 50-255

. License No.: DPR-20

Enclosure:

ln~pection Report 50-255/98015(DRP)

n {' r'I r o f\\

.

9810290171 980918

PDR

ADOCK 05000255

Cl

PDR

See Attached Distribution:

See Previous Concurrences

DOCUMENT NAME: C:\\WORK\\PAL98015.DRP

To receive a copy of this document, indicate in the box "C" =Copy w/o attach/encl

"E" = Copy w/attach encl "N" = No copy

OFFICE

Riii

Riii

Riii

Riii

NAME

Schweibinz/co

Burgess

Shear

Grant

DATE

09/ /98

09/ /98

09/ /98

09/ /98

T. Palmisano

-2-

\\

cc w/encl:

R. Fenech, Senior Vice President, Nuclear

Fossil and Hydro Operations

N. Haskell, Director, Licensing

R. Whale, Michigan, Public Service Commission

Michigan Department of Environmental Quality

Department of Attorney General (Ml)

Emergency Management Division, Ml Department

of State Police

T. Palmisano

-2-

cc w/encl:

R. Fenech, Senior Vice President, Nuclear

Distribution:

CAC (E-Mail)

Fossil and Hydro Operations

N. Haskell, Director, Licensing

R. Whale, Michigan, Public Service Commission*

Michigan Department of Environmental Quality

Department. of Attorney General (Ml)

Emergency Management Division, Ml Department

of State Police

Project Mgr., NRR w/encl

J. Caldwell, Riii w/encl

C. Pederson, Riii w/encl

B. Clayton, Riii w/encl

SRI Palisades w/encl

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