IR 05000255/2019003
ML19318F463 | |
Person / Time | |
---|---|
Site: | Palisades |
Issue date: | 11/14/2019 |
From: | Billy Dickson NRC/RGN-III/DRP/B2 |
To: | Corbin D Entergy Nuclear Operations |
References | |
IR 2019003 | |
Download: ML19318F463 (21) | |
Text
ber 14, 2019
SUBJECT:
PALISADES NUCLEAR PLANT - INTEGRATED INSPECTION REPORT 05000255/2019003
Dear Mr. Corbin:
On September 30, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Palisades Nuclear Plant. On October 15, 2019, the NRC inspectors discussed the results of this inspection with Mr. O. Gustafson, Director, Regulatory Assurance & Performance Improvement and other members of your staff. The results of this inspection are documented in the enclosed report.
No NRC-identified or self-revealing findings were identified during this inspection.
A licensee-identified violation which was determined to be of very low safety significance is documented in this report. We are treating this violation as a non-cited violation (NCV)
consistent with Section 2.3.2 of the Enforcement Policy.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Billy C. Dickson, Jr., Chief Branch 2 Division of Reactor Projects Docket No. 05000255 License No. DPR-20
Enclosure:
As stated
Inspection Report
Docket Number: 05000255 License Number: DPR-20 Report Number: 05000255/2019003 Enterprise Identifier: I-2019-003-0055 Licensee: Entergy Nuclear Operations, Inc.
Facility: Palisades Nuclear Plant Location: Covert, MI Inspection Dates: July 01, 2019 to September 30, 2019 Inspectors: B. Bartlett, Senior Operations Engineer E. Fernandez, Reactor Inspector G. Hansen, Sr. Emergency Preparedness Inspector M. Holmberg, Senior Reactor Inspector P. Laflamme, Senior Resident Inspector T. Ospino, Reactor Engineer J. Rutkowski, Project Engineer J. Winslow, Resident Inspector M. Ziolkowski, Sr Physical Security Inspector Approved By: Billy C. Dickson, Jr., Chief Branch 2 Division of Reactor Projects Enclosure
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Palisades Nuclear Plant in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. A licensee-identified non-cited violation is documented in report section: 71111.15.
List of Findings and Violations No findings or violations of more than minor significance were identified.
Additional Tracking Items None.
PLANT STATUS
The plant began the inspection period at rated thermal power and remained at or near rated thermal power until July 27, 2019. On July 27, 2019, plant operators down powered the plant and took the unit offline to conduct a planned maintenance outage. During the planned maintenance outage, the licensee completed repairs on control rod drive (CRD) mechanism 14 and 23 seals and the digital electro-hydraulic turbine control system. The plant operators restarted the plant on July 31, 2019 and the reactor reached rated thermal power on August 2, 2019. The plant remained at or near rated thermal power for the rest of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.04Q - Equipment Alignment Partial Walkdown Sample (IP Section 03.01)
- (1) Right Train Service Water after QO-14 testing and strainer cleaning on August 29, 2019
- (2) Left Train Component Cooling Water (CCW) after valve maintenance and testing on September 13 through 16, 2019
- (3) 12 Battery System on September 18, 2019
71111.04S - Equipment Alignment Complete Walkdown Sample (IP Section 03.02)
- (1) The inspectors evaluated system configurations during a complete walkdown of the 2400V 1C electrical system from September 23 through September 26, 2019
==71111.05A - Fire Protection (Annual)
Annual Inspection (IP Section 03.02) (1 Partial)
(1) (Partial)
The inspectors evaluated fire brigade performance during a drill on September 18, 2019. The inspectors were not able to observe and evaluate all of the important drill activities as part of this drill and will assess additional drill activities in 2019 in order to evaluate fire brigade performance.
71111.05Q - Fire Protection Quarterly Inspection (IP Section 03.01)
==
- (1) Fire Area 15: Auxiliary Building Stairway and Engineering Safeguards Panel Room on August 23, 2019
- (2) Fire Area 13B: Charging Pump Rooms on September 5, 2019
- (3) Fire Area 28: West Engineered Safeguards Room on September 5, 2019
- (4) Fire Areas 11 & 12: Battery Rooms on September 18, 2019
- (5) Fire Area 2: Cable Spreading Room on September 24, 2019
==71111.06 - Flood Protection Measures Inspection Activities - Internal Flooding (IP Section 02.02a.) (1 Partial)
(1) (Partial)1D Switchgear room, Cable Spreading Room, and Battery Rooms. The licensee is evaluating the as found conditions of a drain line in the Cable Spreading Room as documented in CR-PLP-2019-03874. The inspectors are assessing the extent of condition and the licensee's actions associated with this CAP.
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)==
- (1) The inspectors observed and evaluated licensed operator performance in the Control Room during a shutdown for a maintenance outage due to elevated CRD leakage on July 27, 2019
- (2) The inspectors observed and evaluated licensed operator performance in the Control Room during reactor start-up and power ascension following CRD maintenance repairs on July 31, 2019 Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
- (1) The inspectors observed and evaluated a simulator scenario on September 10, 2019
71111.12 - Maintenance Effectiveness Routine Maintenance Effectiveness Inspection (IP Section 02.01)
(1) Ultimate Heat Sink during the week of July 15, 2019 Quality Control (IP Section 02.02)
The inspectors evaluated maintenance and quality control activities associated with the following equipment performance activities:
- (1) 1-2 EDG Ventilation System during the week of September 23, 2019
71111.13 - Maintenance Risk Assessments and Emergent Work Control Risk Assessment and Management Sample (IP Section 03.01)
- (1) Elevated risk during CRD maintenance outage on July 29, 2019
- (2) Scheduled 1-2 Emergency Diesel Generator (EDG) testing and maintenance, emergent troubleshooting of Pressurizer Heater Breakers, and NI-7 dropped rod card replacement during the week of August 19, 2019
- (3) Emergent troubleshooting and repairs following Thermal Margin Monitor (TMM)
Channel D failure on September 10 and 11, 2019
- (4) Emergent troubleshooting following TMM Channel C inoperability, elevated K-7B Main Feedwater (MFW) Pump turbine thrust bearing vibrations, and diving activities during the week of September 16, 2019
71111.15 - Operability Determinations and Functionality Assessments Operability Determination or Functionality Assessment (IP Section 02.02)
- (1) CR-PLP-2019-02906, Evaluation of Containment Area Monitors on August 5, 2019
- (2) CR-PLP-2019-03099, Evaluation of Missed Main Steam Isolation Valve (MSIV) Surveillance Requirement 3.7.2.1 discovered on August 6, 2019
- (3) CR-PLP-2019-02941, Evaluation of B Steam Generator MSIV solenoid valve SV-0505A on August 7, 2019
71111.18 - Plant Modifications Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02)
- (1) Engineering Change (EC) 56669, Alternate Design to Trip Charging Pumps to Implement NFPA 805 during the weeks of September 2 and September 9, 2019
71111.19 - Post-Maintenance Testing Post-Maintenance Test Sample (IP Section 03.01)
- (1) Digital Electro-hydraulic power supply replacement on July 29, 2019
- (2) Pressurizer Spray Valve CV-1057 repack and diagnostic valve test on July 30, 2019
- (3) Visual examination results following CRD-14 and CRD-23 seal replacement on July 30, 2019
- (4) Standard Operating Procedure 22 after replacement of P-209A, 1-1 EDG Fuel Oil Booster Pump on August 13, 2019
- (5) Special Operating Procedure CVCO-4 after P-55A Charging Pump maintenance on August 28, 2019
- (6) QI-25 after replacement of C TMM Display Screen on September 19, 2019
71111.20 - Refueling and Other Outage Activities Refueling/Other Outage Sample (IP Section 03.01)
- (1) The inspectors evaluated maintenance outage activities to repair CRD-14 and CRD-23 seals from July 27, 2019 to July 31, 2019
71111.22 - Surveillance Testing Surveillance Tests (other) (IP Section 03.01)
- (1) RI-3A, High Pressurizer Pressure Channel Calibration on July 15, 2019
- (2) QO-37, Main Steam Isolation and Bypass Valve testing on July 28, 2019
Inservice Testing (IP Section 03.01) (1 Sample)
- (1) RO-146, CCW Pump Compressive Test on July 2, 2019
RCS Leakage Detection Testing (IP Section 03.01) (1 Sample)
- (1) DWO-1, Primary Coolant System Daily Leak Rate Surveillance Test on July 10, 2019
71114.02 - Alert and Notification System Testing Alert and Notification System Testing
- (1) The inspectors evaluated the following maintenance and testing of the alert and notification system:
- Annual siren inspection and maintenance records for the period from July 2017 to June 2019
- Monthly alert notification system (siren) tests for the period from July 2017 to June 2019
71114.03 - Emergency Response Organization Staffing and Augmentation System Emergency Response Organization Staffing and Augmentation System
- (1) The inspectors evaluated the readiness of the Emergency Preparedness Organization.
71114.05 - Maintenance of Emergency Preparedness Maintenance of Emergency Preparedness
- (1) The inspectors evaluated the maintenance of the emergency preparedness program.
71114.06 - Drill Evaluation Drill/Training Evolution Observation (IP Section 03.02)
- (1) A full scale Emergency Planning Drill on August 7,
OTHER ACTIVITIES - BASELINE
71151 - Performance Indicator Verification 02.12 Drill/Exercise Performance
- (1) Unit 1 (January 1, 2018 - March 31, 2019)02.13 ERO Drill Participation (1 Sample)
- (1) Unit 1 (January 1, 2018 - March 31, 2019)02.14 Alert & Notification System Reliability (1 Sample)
- (1) Unit 1 (January 1, 2018 - March 31, 2019)
MS07: High Pressure Injection Systems (IP Section 02.06) (1 Sample)
- (1) Unit 1 (July 1, 2018 - June 30, 2019)
MS09: Residual Heat Removal Systems (IP Section 02.08) (1 Sample)
- (1) Unit 1 (July 1, 2018 - June 30, 2019)
BI02: RCS Leak Rate Sample (IP Section 02.11) (1 Sample)
- (1) Unit 1 (July 1, 2018 - June 30, 2019)
71152 - Problem Identification and Resolution Annual Follow-up of Selected Issues (IP Section 02.03)
- (1) Security Excellence Plan in-depth review during the week of August 5,
INSPECTION RESULTS
Licensee-Identified Non-Cited Violation 71111.15 This violation of very low safety significance was identified by the licensee and has been entered into the licensee corrective action program and is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.
Violation: Technical Specification (TS) Surveillance Requirement 3.7.2.1 requires that the licensee verify at least every 18 months that the closure time of each Main Steam Isolation Valve (MSIV) is less than or equal to 5 seconds on an actual or simulated signal from each train under no flow conditions.
Contrary to the above, on August 6, 2019, licensee personnel identified that the MSIV closure time surveillance test only tested the valves from their individual train hand switches and failed to stroke time test the MSIVs from the opposite train hand switches. The missed surveillance had been occurring since January 23, 1996.
Significance/Severity: Green. The inspectors answered No to all the questions in IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, because the licensee complied with TS Surveillance Requirement 3.0.3 for a missed TS Surveillance. In addition, the MSIVs had been timed from one hand switch but not the other train which supplied evidence that the valves were capable of performing their intended function. Therefore, the finding screened as Green.
Corrective Action References: The licensee entered this issue into their CAP as CR-PLP-2019-03099.
Observation: Security Excellence Plan In-depth Review 71152 In October 2018, the licensee identified a slow decline in attention to detail, engagement with direct reports, and standard adherence that led to multiple human performance and safety errors. The licensee implemented an improvement plan to reinforce standards, increase accountability for first line supervisors, and establish security officer expectations. In order to assess the licensees actions, the inspectors performed a selected issue follow-up inspection sample. The inspectors conducted a limited assessment of the security force. The assessment consisted of interviews with security officers from all shifts and various members of security supervision. The inspectors determined the licensee's improvement plan to be effective as implemented. No significant issues were identified.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On October 15, 2019, the inspectors presented the integrated inspection results to Mr. O. Gustafson, Director, Regulatory Assurance & Performance Improvement and other members of the licensee staff.
- On July 12, 2019, the inspectors presented the Emergency Preparedness Baseline Inspection inspection results to Mr. D. Corbin, Vice President, Operations and other members of the licensee staff.
THIRD PARTY REVIEWS The inspectors reviewed an Institute on Nuclear Power Operations report that was issued during the inspection period.
DOCUMENTS REVIEWED
Inspection Type Designation Description or Title Revision or
Procedure Date
71111.04Q Corrective Action CR-PLP-2016- ED-02 Battery Hair Line Cracks on the Jar Lids of the 07/30/2016
Documents 03412 Battery Cells
CR-PLP-2016- Visual Inspection on ED-01 Station Battery Identified 3 Cells 07/25/2016
03426 with Hairline Cracks on the Jar Lids
CR-PLP-2016- All Cells on ED-01 Showed Signs of Cracking from the Post 07/27/2016
03454 Seals Toward the Outer Edge of the Lid
Drawings M-208, Sheet 1A Piping & Instrument Diagram, Service Water System 67
M-208, Sheet 1B Piping & Instrument Diagram, Service Water System 43
M-209, Sheet 2 Piping & Instrument Diagram, Component Cooling System 33
M-209, Sheet 3 Piping & Instrument Diagram, Component Cooling System 60
M-213 Piping & Instrument Diagram, Service Water, Screen 96
Structure, and Chlorinator
Procedures SOP-15 Service Water System 69
SOP-16 Component Cooling Water System 48
71111.04S Corrective Action CR-PLP-2019- Discovered Water Dripping from the Bottom of V-96, Control 07/22/2019
Documents 00283 Room Ventilation Main Supply Fan Housing
CR-PLP-2019- Replace Bumper Stop Assemblies on Select 2400V Bus 1C 03/07/2019
00959 Breakers
CR-PLP-2019- Received PPC Alarms 2400V AC Bus 1D Voltage and 03/09/2019
00996 2400V AC to 1C Voltage Alarms for High Voltage
CR-PLP-2019- While Performing WO 52796691, PM Breaker with Starter 09/23/2019
03812 52-2413, Found a Bad Contact
Drawings E-11, Sheet 1 Schematic Meter and Relay Diagram 2.4 KV System 37
Miscellaneous DBD-3.04 Design Basis Document: 2400V AC System 8
Procedures SOP-30 Station Power 91
71111.05A Miscellaneous Fire Drill Scenario 09/18/2019
71111.05Q Corrective Action CR-PLP-2019- NRC Identified that FZ-0032 on the East Wall of the 1-1 09/20/2019
Documents 03785 Diesel Generator Room to the Old Baler Room, has Mastic
Resulting from that has Cracked Due to Movement of the 3 Inch Pipe
Inspection
Fire Plans Pre Fire Plan Fire Area 15 - Stairway & Engineering Safeguards Panel 5
Room
Inspection Type Designation Description or Title Revision or
Procedure Date
Pre Fire Plan Fire Areas 2, 11 & 12, 13 B, and 28 5
Miscellaneous DBD-7.10 NFPA 805 Fire Protection Program 3
E-90 (Q) Technical Specification for Furnishing and Installation of 8
Cables, Raceways, Terminations, Panel Modifications, and
Associated Work
71111.06 Corrective Action CR-PLP-2019- As Found Conditions of Drain Line Associated with the 9/26/2019
Documents 03874 Cable Spreading Room Floor Drain Cleaning
Miscellaneous DBD-7.08 Plant Protection Against Flooding 6
Procedures AOP-38 Acts of Nature 17
AOP-39 Internal Plant Flooding 1
71111.11Q Miscellaneous SES-400 Dynamic Simulator Evaluation 0
Procedures GOP-4 Mode 2 to Mode 1 24
GOP-8 Power Reduction and Plant Shutdown to Mode 2 or Mode 3 40
Greater than or Equal to 525 Degrees
71111.12 Corrective Action CR-PLP-2013- Damage to Intake Crib Top Plate Discovered by Diver 07/29/2013
Documents 03273
CR-PLP-2016- Functional Failure of the DGV System 02/18/2016
294
CR-PLP-2016- AS-DGV System has Exceeded its Performance Criteria of 03/03/2016
01095 Less than 2 Functional Failures in 24 Months
CR-PLP-2016- Need to Generate a Work Order to Repair the Intake 07/12/2016
03189 Structure Rack
CR-PLP-2016- V-24B, Diesel Generator Room Supply Fan, in Standby 11/20/2016
05680 Started Prior to the V-24A, Diesel Generator Room Supply
Fan
CR-PLP-2018- Diesel Generator Ventilation System 07/02/2018
03085
CR-PLP-2019- Spring Dive Inspection Identified Holes in the Velocity Cap of 05/31/2019
209 the Intake Structure
CR-PLP-2019- Emergency Diesel Generator 1-2 Room was Indicating 87.5 07/03/2019
2606 Degrees F but Neither V-24C Diesel Generator Room
Supply Fan nor V-24D Diesel Generator Room Supply Fan
were Running
CR-PLP-2019- Received Alarm EK-0557, Diesel Generator 1-2 Trouble 08/07/2019
Inspection Type Designation Description or Title Revision or
Procedure Date
03116 Unexpectedly
CR-PLP-2019- Maintenance Rule Functional Failure Determination for CV- 09/04/2019
03467 2099, PCP Controlled Bleed Off Containment Isolation,
Position Indication
CR-PLP-2019- Noted on EDG 1-2 that the Temperature Probe Conduit for 09/25/2019
03868 TE-1479-LR has Come Loose from the LB Box
Engineering EC 63643 Monitor V-24A Fan Control Circuit Operation and Motor 03/28/2016
Changes Current
EC 6402 EDG RM Vent Fan Temp Switch Replacement 0
Miscellaneous DBD-1.07 Design Basis Document: Auxiliary Building HVAC System 6
PLP-RPT-12- EGAD-EP-10 Palisades Maintenance Rule Scoping 3
00026 Document
System Health DGV - Diesel Generator Room HVAC Q1-2019
Report
Work Orders WO 438690 03 TS-1828; Bench Prep New Switch 12/14/2016
WO 438690 05 52-2535 Install/Remove Monitoring Device 12/14/2016
WO 462441 01 TS-1828 (V24A); Check Calibration 01/30/2017
71111.13 Calibration CR-PLP-2019- VOP-0754, AFW to Steam Generator E-50A Isolation, has 09/25/2019
Records 03865 Grease Separation and a Small Amount of Oil is Seeping
Out of the Actuator
Corrective Action CR-PLP-2019- Fuel Oil Leaking Past the Seal on Fuel Oil Booster Pump 08/08/2019
Documents 03118 Mounted on the North End of the EDG 1-1 at a Rate of
Approximately 16 Drops per Minute
CR-PLP-2019- NI-7 Rod Drop; Card did not Work as Desired 08/21/2019
285
CR-PLP-2019- Ops Could not Reset and Close Breaker 52-1510 08/21/2019
287
CR-PLP-2019- Cubicle Heaters were On 08/22/2019
03321
CR-PLP-2019- On PY-0102D, Thermal Margin Monitor Channel 'D' was 09/09/2019
03549 Blank/Dark
Miscellaneous Operator's Risk Reports Various
Procedures Admin 4.02 Control of Equipment 81
DWO-1 Operator's Daily/Weekly Items Modes 1, 2, 3, and 4 109
Inspection Type Designation Description or Title Revision or
Procedure Date
EN-FAP-WM-002 Critical Evolutions 5
EN-WM-104 On-Line Risk Assessment 20
GOP-14 Shutdown Cooling Operations 53
SOP-35 Neutron Monitoring System 17
Work Orders WO 477934 PY-0102D, CRT Monitor is Failing 09/11/2019
WO 531075 PY-0102D; Replace Components & Reset Error Code 75 09/11/2019
WO 531075 01 'D' TMM Failure Troubleshooting 09/09/2019
WO 531611 TH-056S K-7B Thrust Trip 09/20/2019
71111.15 Corrective Action CR-PLP-2019- SV-0505A, Solenoid for 'B' S/G MSIV (CV-0501), was 07/28/2019
Documents 02941 Sluggish While Closing in Step 5.2.15
CR-PLP-2019- Steam Generator B Main Steam Isolation Sluggish 07/29/2019
2964 Operation While Closing
CR-PLP-2019- Missed TS Surveillance Requirement for Main Steam 08/06/2019
03099 Isolation Valves in RI-17
CR-PLP-2019- Suction Pressure for VC-10 (Control Room HVAC Refrig 08/07/2019
03105 Condensing Unit) was Observed to Cycle Between 48-54
psig
Engineering EC 83836 Risk Assessment for Missed Surveillance Requirement 0
Changes SR 3.7.2.1
Miscellaneous QO-37 Basis Main Steam Isolation and Bypass Valve Testing 7
Procedures MI-6 Area Monitor Operational Check 15
QO-37 Main Steam Isolation and Bypass Valve Testing 13
RI-17 Main Steam Isolation Valve Circuits Test and Valve Closure 23
Testing
Work Orders WO 528713 01 RIA-1806/1807 Perform Partial MI-6 07/27/2019
71111.18 Engineering EC 56669 Alternate Design to Trip Charging Pumps to Implement 0
Changes Requirements of NFPA 805
Procedures EN-DC-115 Engineering Change Process 25
Work Orders WO 431058 805A, EC 56669, Alternate Design to Trip Charging Pumps 10/10/2018
71111.19 Corrective Action CR-PLP-2019- Refurbished 13V DEH Power Supply Maintained 13 VDC up 07/20/2019
Documents 02815 to 3.8 A then Output Dropped to 10 VDC Above 4 A Load
CR-PLP-2019- EC-06-03 SPI Cabinet Cooling Fan is Making an Intermittent 07/20/2019
2817 Squeaking Noise
Inspection Type Designation Description or Title Revision or
Procedure Date
CR-PLP-2019- Control Room EDH Output Changed from 815 MW to 840 07/20/2019
2818 MW and then back to 815 MW
CR-PLP-2019- Power Supply DC Output Steadily Declined from 12.520 07/29/2019
2966 VDC to 12.441 VDC Between 7/10/2019 and 7/27/2019
CR-PLP-2019- While Performing PMT for CV-1057, PZR Spray Valve, 07/30/2019
03007 Noted CV-2057 Controls Pressure Properly @ NOP/NOT,
However, the Red (Open) Light does not Illuminate
Miscellaneous System Health Ultimate Heat Sink Q1-2019
Report
Procedures EN-DC-196 Pressurizer Spray Valve from Loop 1B Stroke Test 08/05/2019
QI-25 Thermal Margin Monitor Constant Checks 23
SOP-22 Emergency Diesel Generators 77
Work Orders WO 524133 04 CRD-23 CRD Seal Housing: PMT 07/30/2019
WO 527780 04 CRD-14 CRD Seal Housing: PMT 07/30/2019
WO 527870 03 EC-23; Drop 2/52, I/O Power Supplies - Return to Service 07/28/2019
WO 527941 01 EC-23; Backup Power Supply to DPY-2 & 52 Failed 08/15/2019
WO 52869306 CVCO-4 for P-55A 08/28/2019
WO 52886264 P-55A (T-105A) Accumulator Pressure Test 08/28/2019
WO 52890320 P-55A (T-106A) Accumulator PM 08/28/2019
WO 529518 P-209A (K-6A) Fuel Oil Leaking Past Seal on Booster Pump 08/13/2019
WO 5300855 PY-0102C; Display is Very Dim - Adjust Brightness on 09/19/2019
Display
71111.20 Corrective Action CR-PLP-2019- CRD-23, Control Rod Drive Mechanism Took a Step Change 07/24/2019
Documents 02860 to 190-192 Degrees Fahrenheit
CR-PLP-2019- CRD-14, Control Rod Drive Mechanism Spiked to 07/24/2019
2861 Approximately 175 Degrees Fahrenheit
CR-PLP-2019- Following Manual Trip of the Reactor for the Planned 07/27/2019
2908 Outage, TA-0305B, Loss of Load Channel B RPS Aux Trip
Unit, Light did not Illuminate
CR-PLP-2019- During the CRD-40 Forced Outage Mode 3 Walkdown, Boric 07/28/2019
2910 Acid Buildup was Identified on CV-1059, Pressurizer Spray
Valve from Loop 2A
CR-PLP-2019- During the CRD-23 Forced Outage Mode 3 Walkdown, Boric 07/28/2019
2912 Acid Buildup and Identified on MO-3049, Safety Injection
Inspection Type Designation Description or Title Revision or
Procedure Date
Tank 82C Outlet
CR-PLP-2019- During CRD-40 Forced Outage Mode 3 Walkdown a Packing 07/28/2019
2918 Leak was Discovered on CV-1057, Pressurizer Spray Valve
from Loop 1B
CR-PLP-2019- Mode 4 to Mode 3 Hole, CV-0501, Main Steam Isolation 07/28/2019
2941 Valve (MSIV)
CR-PLP-2019- Engineering Identified that Boric Acid Residue is Still Present 07/30/2019
2992 at CRD Leak-Off Connections for CRDs 15 and 18
CR-PLP-2019- Received Alarm EK-0954 Rod Drive Seal Leak Off High 07/31/2019
03024 Temperature, Unexpectedly on 2 Occasions Within a Few
Minutes
CR-PLP-2019- Received Alarm EK-0954, Rod Drive Seal Leak Off High 08/01/2019
03039 Temperature Unexpectedly
CR-PLP-2019- PIA-1066, Primary Coolant System Reactor Head Vent, Prior 08/05/2019
03065 to the Forced Outage was Reading 2050 PSIG
Corrective Action CR-PLP-2019- NRC Identifed a Cable for Control Rod Drive 33 has its 07/30/2019
Documents 02989 Raychem Pulled out of the Junction Box such that Cables
Resulting from Inside are Exposed
Inspection CR-PLP-2019- NRC Identified that the Thermocouple for Control Rod Drive 07/30/2019
2990 40 has its Conduit Pulled out of a Fitting such that the 2
Wires are Visible
CR-PLP-2019- NRC Identified the Conduit for the Thermocouple for Control 07/30/2019
2991 Rod Drive 8 was not Secured in the Support Bracket
Procedures GOP-14 Shutdown Cooling Operations 53
GOP-5 Power Escalation in Mode 1 45
Work Orders WO 528903 01 RSPT-33 Raychem Pulled Out of Junction Box 07/30/2019
71111.22 Corrective Action CR-PLP-2019- Rod Drive Seal Leak Off High Temperature During RO-146A 07/02/2019
Documents 02596 CCW Pump In-Service Testing
CR-PLP-2019- SV-0505A, Solenoid for 'B' S/G MSIV (CV-0501), was 07/28/2019
2941 Sluggish
CR-PLP-2019- CV-0736A, P-8C Flow Control to E-50B and CV-0737A P-8C 09/06/2019
03507 Flow Control to E-50A not Being Stroked Timed During the
Performance of QO-5 on 8/29/19
Procedures DWO-1 Operator's Daily/Weekly Items Modes 1,2,3, and 4 108
Inspection Type Designation Description or Title Revision or
Procedure Date
QO-37 Basis Main Steam Isolation and Bypass Valve Testing 7
RI-3A High Pressurizer Pressure Channel Calibration 9A
RO-146 Comprehensive Pump Test Procedure - Component Cooling 12
Water Pumps P-52A, P-52B and P-52C
SEP-PLP-IST- Inservice Testing of Plant Valves 6
101
Work Orders WO 480329 01 RO-146, P-52A, IST CCW Pump Comprehensive 06/17/2019
WO 52853233 QO-37 - Main Steam Isolation an Bypass Valve Testing 07/28/2019
WO 52868659 01 DWO-1 - OPS IST Line Supervisor Review DWO-1 06/17/2019
71114.02 Corrective Action CR-PLP-2017- Siren 45 Intermittent Communication Failures 07/07/2017
Documents 03258
CR-PLP-2017- Siren 22 Test Failure 09/09/2017
04162
CR-PLP-2018- Siren 55 Test Failure 06/09/2018
2778
CR-PLP-2018- Sirens 57 and 61 on DC Power Since 10/22/2018 10/25/2018
04978
CR-PLP-2019- Siren 62 Battery Failure 02/07/2019
00582
Miscellaneous Federal Emergency Management Agency Letter - Subject: 12/20/2002
Palisades Nuclear Plant Public ANS Approval
Federal Emergency Management Agency Letter; Provisions 12/10/2012
for Backup Alert and Notification (ANS) for the Palisades
Nuclear Power Plant Emergency Planning Zone (EPZ)
Palisade Nuclear Plant Public Warning System Replacement 10/01/2002
Project Design Report
2019 Emergency Preparedness Public Information Calendar
Operability Documentation of Public Warning System (PWS) Monthly 07/2017 -
Evaluations Tests 06/2019
Procedures PAL PWS Palisades Nuclear Plant Public Warning System Operating 22
Procedure
71114.03 Corrective Action CR-PLP-2018- Off Hours Mobilization Drill - Gold Team Ops Coordinator 06/05/2018
Documents 02713 Response
CR-PLP-2018- Off Hours Mobilization Drill - Gold Team Mechanical 06/05/2018
Inspection Type Designation Description or Title Revision or
Procedure Date
2715 Coordinator Response
CR-PLP-2018- ERO Red Team - TSC Manager Expired Qualification 07/02/2018
03136
CR-PLP-2018- ERO Performance Negative Trend 07/11/2018
236
CR-PLP-2018- ERO Member Response Failure - 8/16/18 ERO Test 08/20/2018
03797
Miscellaneous Current ERO Team Staffing Roster 05/31/2019
Palisades Nuclear Station On-Shift Staffing Analysis Final 4
Report
Emergency Response Organization Off-hours, 07/2017 -
Unannounced, Augmentation Response Test Records 06/2019
Procedures EI-2.2 Emergency Staff Augmentation 21
EN-EP 310 Emergency Response Organization Notification System 8
EN-TQ-110 Emergency Response Organization Training 13
71114.05 Corrective Action CR-PLP-2017- Controller/Evaluators did not Complete Required CBT 08/22/2017
Documents 03900
CR-PLP-2017- Drill Objective E.1 Graded as Needs Improvement 11/07/2017
05122
CR-PLP-2017- Potassium Iodide Briefing Inefficiently Performed During 12/13/2017
05691 ERO Drill
CR-PLP-2018- Event Notification Form Errors During April 24, 2018 EP 04/26/2018
2031 Exercise
CR-PLP-2019- Control Room Operators Failed to Fulfill KI Issuance 04/16/2019
01531 Procedures
CR-PLP-2019- Exercise SAE Notification Failure 04/16/2019
01533
CR-PLP-2019- EP Exercise - ERO Failure to Determine Status of Rad 04/16/2019
01534 Release
CR-PLP-2019- EP Exercise - Insufficient Command and Control Hindered 04/16/2019
01538 Performance
Corrective Action CR-HQN-2019- NRC Inspection - Electronic Notification System Issue 07/11/2019
Documents 01499 Identified
Resulting from
Inspection Type Designation Description or Title Revision or
Procedure Date
Inspection
Miscellaneous Quarterly Emergency Communications Test Records 07/2018 -
06/2019
Monthly Communications Test Records 07/2018 -
06/2019
After Action Drill Report/Improvement Plan - April 11, 2018 05/10/2018
ERO Blue Team Drill
After Action Drill Report/Improvement Plan - April 24, 2018 05/23/2018
ERO Blue Team Drill
After Action Drill Report/Improvement Plan - June 6, 2018 06/29/2018
After Action Drill Report/Improvement Plan - September 5, 01/15/2019
2018 ERO Red Team Drill
After Action Drill Report/Improvement Plan - April 10, 2019 05/08/2019
ERO Blue Team Drill
KLD TR - 1020 Palisades Power Plant 2018 Population Update Analysis 09/19/2018
Procedures EN-LI-102 Corrective Action Process 36
SEP Palisades Nuclear Plant Site Emergency Plan 31
SEP Supplement EAL Wall Chart 4
SEP Supplement Evacuation Time Estimate 0
Self-Assessments QA-7-2018-PLP-1 Quality Assurance Audit Report - Emergency Preparedness 05/31/2018
[10CFR50.54(t)]
QA-7-2019-PLP-1 Quality Assurance Audit - Emergency Preparedness 05/29/2019
[10CFR50.54(t)]
71114.06 Corrective Action CR-PLP-2019- Discovered During EP Exercise that Cellular Phone is Non- 08/07/2019
Documents 03107 Operational, Phone Battery Leaking
CR-PLP-2019- While Performing Kit #5 Inventory for Emergency Vehicle 08/07/2019
03114 (GMC Van) if was Discovered that the Portable Batter
Charger was not Operational
Miscellaneous Emergency Preparedness Full Scale Drill 08/07/2019
71151 Miscellaneous Emergency Response Organization Drill Participation 01/01/2018 -
Inspection Type Designation Description or Title Revision or
Procedure Date
Performance Indicator Records 03/31/2019
Drill and Exercise Performance (DEP) Performance Indicator 01/01/2018 -
Records 03/31/2019
Alert Notification System Performance Indicator Records 01/01/2018 -
03/31/19
MSPI Derivation MSPI Derivation Documents 07/01/2018 -
Documents for 06/30/2019
July 1, 2018
through June 30,
2019
71152 Corrective Action WT-WTPLP- Develop a Plan to Address the Identified Issues 10/09/2018
Documents 2018-00403
Self-Assessments Palisades Security April 2019 Performance Summary 25
Palisades Security July 2019 Performance Summary 25
19