ML18065B168

From kanterella
Jump to navigation Jump to search
Insp Rept 50-255/97-18 on 971206-980127.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML18065B168
Person / Time
Site: Palisades Entergy icon.png
Issue date: 02/26/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML18065B166 List:
References
50-255-97-18, NUDOCS 9803030376
Download: ML18065B168 (21)


See also: IR 05000255/1997018

Text

U.S. NUCLEAR REGULATORY COMMISSION

Docket No:

License No:

Report No:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved by:

9803030376 980226

PDR

ADOCK 05000255

G

PDR

REGION Ill

50-255

DPR-20

50-255/9701 B(DRP)

Consumers Power Company

212 West Michigan Avenue

Jackson, Ml 49201

Palisades Nuclear Generating Plant

27780 Blue Star Memorial Highway

Covert, Ml 49043-9530

December 6, 1997, through January 27, 1998_

P. Prescott, Resident Inspector .

E. Schweibinz, Regional Inspector

Bruce L. Burgess, Chief

Reactor Projects Branch 6

EXECUTIVE SUMMARY

Palisades Nuclear Generating Plant

NRC Inspection Report No. 50-255/97018

This inspection reviewed aspects of licensee operations, maintenance, engineering and plant

support. The report covers a seven-week period of resident inspection,

Operations

The operators responded appropriatelyJo a loss of component cooling water event that

occurred on January 1, 1998. The licensee established an incident response team (IRT)

to investigate the circumstances surrounding the event, and the inspectors concluded

that the IRT's findings and proposed corrective actions were thorough. However, the

inspectors identified several IRT weaknesses, most significantly, the team's lack of

understanding of Generic Letter 91-18 regarding degraded conditions. The inspectors

discussed the weaknesses with licensee management and concluded that the corrective

actions taken or planned were adequate (Section 01.2).

Following the discovery of a mispositioned valve at a nitrogen station, the li.censee

instituted an equipment status control record to enhance the operations department's

control of equipment. To date, no discrepancies have been identified (Section 01.3).

Maintenance

The inspectors concludE;id that the spent fuel pool maintenance activity to repair body to

bonnetleaks on two valves, MV-SFP131 and MV-SFP132, was well planned and

executed. However, the inspectors noted one deficiency in that the nuts and bolts on the

valves were heat treated steel instead of stainless steel. An unresolved item was opened

pending a review of the licensee's evaluation of the nuts and bolts (Section M1 .2).

Engineering

During follow up to a March 1997 failure of CV-3018 to reposition, the inspectors

concluded that the corrective action for air line filter placement for pressure control valves

(PCVs) was inadequate in that the licensee fail~d to correct a previously identified

condition adverse to quality. The inspectors further concluded that placement of low

point drains in the air lines leading to the PCVs was inadequate. The low point drain

problem and the lack of corrective action for the air filter placement problem led to failure

  • of CV-3018's air regulator. A violation of NRC requirements was identified (Section E1 .1).

The inspectors concluded that the system engineer had adequately prepared to perform

leak checks on the radwaste evaporator component cooling water supply and return

valves. However, the inspectors noted that the system engineer did not communicate to

the control room supervisor all of the activities performed in preparation of valve testing

(Section E1 .2).

2

Three 10 CFR 50, Appendix R, issues were of concern because of the safety significance

associated with plant equipment con*figuring that did not meet 10 CFR Part 50,

Appendix R, safe shutdown requirements for a design basis fire. These issues would

normally be designated as a Severity Level Ill problem in accordance with the NRC's

  • NUREG-1600, "General Statement of Policy and Procedures for NRC Enforcement

Actions," (Enforcement Policy). However, enforcement discretion will be used in

accordanc.e with Section Vll.8.3, "Violations Involving Old Design Issues," of the

Enforcement Policy and a Notice of Violation will not be issued. The decision to apply

enforcement discretion was based on consideration of the following: 1) significant NRC

enforcement action (EA 96-131) was taken against the Consumers Energy Company for

several examples of a failure to take prompt corrective actions related to Appendix R

deficiencies. Palisades identified the issues detailed above and promptly notified the

NRC; 2) corrective actions were immediate and encompassed the root causes for these

issues; 3) some of the issues were related to activities that were in progress before the

enforcement action was issued; 4) the issues would not be classified at a severity level

higher than Severity Level Ill; and 5) Consumers Energy Company met with the NRC to

explain their efforts to resolve these issues, which were outlined in their reply dated

September 12, 1996.

During a closeout of a licensee event report, the inspectors identified a non-cited violation

for failure to meet Technical Specifications testing requirements of the emergency escape

air lock (Section EB.3).

  • Plant Support .

The inspectors concluded that radiological practices observed during the maintenance

activities and plant daily walkdowns were adequate.

3

Report Details

Summary of Plant Status

The plant operated at full power for the entire inspection period.

I. Operations

01

Conduct of Operations

01.1

General Comments (71707)

The inspectors conducted frequent reviews of ongoing plant operations. The conduct of

operations was considered by the inspectors to be good; specific events and noteworthy

observations are detailed below.

01.2

Component Cooling Water Leak

a.

Inspection Scope (71707 and 40500)

On January 1, 1998, a loss of component cooling water (CCW) inventory occurred which

was greater than the CCW surge tank makeup capacity. The inspectors followed up on

the circumstances surrounding the event, the licensee's investigation, and the corrective

actions for the loss of CCW.

b.

Observations and Findings

Event Description:

On December 24, 1997, plant operators identified a leaking air solenoid on the radwaste

evaporator CCW return valve, CV-09778. After discussing the leak with system

engineering and management, the operators decided to place CV-09778 in its safety

function position by closing the valve. Closing CV-09778 resulted in isolating CCW flow

and pressurizing the cooler to full CCW system pressure. Because there was no

immediate need to process radioactive waste, the licensee planned to repair the valve

two weeks later.

On December 28, 1997, the operators identified a CCW leak on the "A" radwaste

evaporator distillate cooler head gasket flange. The leak was approximately 100 milliliters

per minute. On the following day, the fix-it-now team determined that tightening the

flange could cause the leakage to increase.

On January 1, 1998, the leak rapidly increased to 200 gallons per minute (gpm),

exceeding the CCW surge tank makeup capability of 135 gpm. The operators first

became aware of the problem when a remote panel annunciator alarmed for high level in

the auxiliary building sump. While the operators were taking actions to isolate the "A"

4

evaporator distillate cooler, the CCW surge tank alarm annunciated in the control room.

The operators entered Off Normal Procedure (ONP) 6.2, "Loss of CCW," and isolated the

CCW leak. After the leak was isolated, the CCW system was refilled; however, the

system required several venting evolutions over the following two days.

Operator Response:

After the CCW surge tank alarm annunciated in the control room, the operators entered

Off Normal Procedure (ONP) 6.2, "Loss of CCW." The shift supervisor directed that the

reactor be tripped and primary coolant pumps (PCPs) secured if abnormal CCW pump

operating conditions were noted. These actions were more conservative than the ONP

guidance. Also, the shift supervisor determined that starting a standby CCW pump would

have worsened the low CCW inventory problem and resulted in the air-binding of the

CCW pumps. Therefore, contrary to the ONP, the operators did not start another CCW

pump. The operators recovered surge tank level before CCW flow was disrupted to the

PCPs.

The inspectors concluded that operator response to the event was appropriate and

timely. The operators avoided a reactor trip and potential damage to the PCP seals. The

inspectors also noted that the shift supervisor conservatively decided to trip the reactor

should any significant operational problem occur with the CCW system or PCP seals.

The licensee's incident response team (IRT) noted a weakness in the event response in

that the shift supervisor did not announce the decision not ~o start the standby CCW

pumps to the shift crew.

Also, the licensee failed to recognize the potential for degradation to the CCW system.

Based on the number of venting evolutions, air entrapment in the CCW system was

significant; however, the licensee determined that the system was operable because it

had met system performance requirements. The inspectors concluded that the licensee's

operability determination was weak in that it did not account for the significant inventory

loss and air entrapment.

Incident Response Team Performance:

As documented in Inspection Report No: 50-255/97014, the NRC had identified a

weakness in the licensee's response to the failure to recognize all control rods out of

service while at power. Following the loss of CCW on January 1, 1998, the licensee

established an incident response team (IRT) to investigate the circumstances

surrounding the event. The IRT appropriately prioritized significant corrective actions and

ensured that the actions were completed in a timely manner. Overall, the licensee's IRT

evaluation resulted in a thorough understanding of the event. However, the inspectors

noted several IRT weaknesses. The most significant weakness was that the IRT

personnel did not have a thorough understanding of Generic Letter 91-18 as it applied to

the loss of CCW event. Generic Letter 91-18 addressed operability of systems,

structures and components and the resolution of degraded and nonconforming

conditions. The initial condition report for the loss of CCW surge tank did not recognize

that the CCW system was degraded but operable. Declaring the system inoperable or

degraded would have required an operability evaluation to be documented .

5

Also, IRT personnel did not request an analysis of the loss of CCW event in terms of its

effect on core damage frequency. The inspectors discussed a loss of CCW with the

primary coolant pump system engineer: The in.spectors were concerned that the

licensee's engineering staff did not have an understanding of what would happen to the

PCP seals after a 1 O minute loss of CCW. The licensee is presently discussing thi~

matter with the seal vendor. Another weakness noted by the inspectors was that the IRT

process was not formalized in that it had not been proceduralized. The licensee originally

planned to complete this action item by the end of January 1998. The inspectors

discussed these weaknesses with licensee management and concluded that the

corrective actions taken or planned would adequately address the problems.

c.

Conclusions

The operators responded appropriately to a loss of component cooling water event that

occurred on January 1, 1998. The licensee established an incident response team (IRT)

to investigate the circumstances surrounding the event, and the inspectors concluded

that the IRT's findings and proposed corrective actions were thorough. However, the

inspectors identified several IRT weaknesses, most significantly, the team's lack of

understanding of Generic Letter 91-18 regarding degraded conditions. The inspectors

discussed these weaknesses with licensee management and concluded that the

corrective actions taken or planned were adequate.

01.3 . Nitrogen Station Valve Mispositioned

a .

b.

Inspection Scope (71707)

During performance of surveillance M0-29, "Engineered Safety System Alignment,"

nitrogen bottle isolation Valve MV-N2-126 was found closed. The inspectors reviewed

corrective actions taken for the mispositioning of a nitrogen station bottle isolation valve.

Observations and Findings

The purpose of surveillance M0-29 was to determine by inspection that Technical

Specification (TS) limiting conditions for operations are not being violated by

misalignment of valves, breakers, or controls contained within or affecting engineered

safety systems. Valve MV-N2-126, an isolation valve to a nitrogen bottle associated with

nitrogen station 38, was checked as part of the surveillance and found closed contrary to

its normally open position. The licensee investigated the mispositioned valve. While

performing maintenance on nitrogen station 38, an auxiliary operator closed the supply

valves on the nitrogen header to provide added personnel protection due to a leaking cap

on a test connection. This action was logged in the secondary plant log. However, when

the auxiliary operator went to restore the nitrogen bottle isolation valves,

Valve MV-N2-126 was missed. The inspectors concluded that the safety significance of

this event was minor because the instrument air system was available.

Corrective action for this event was the development of an equipment status control

record. Equipment operated in t.he plant not covered by any controlling document was to

be listed on this record. The inspectors questioned se.veral operators to ascertain

whether or not sufficient controls were in place to review and store completed valve

record sheets. The inspectors found that the record sheets were not being reviewed or

6

saved. The issue was discussed with the operations superintendent, and the operations

superintendent agreed it would be prudent to retain and periodically review the record

sheets.

c.

Conclusions

Following the discovery of a mispositioned valve at a nitrogen station, the licensee

instituted an equipment status control record to enhance the operations department's

. control of equipment. To date, no discrepancies have been identified.

08

Miscellaneous Operations Issues (92701 and 92901)

08.1

(Closed) IFI 50-255/94014-06: Control room ventilation noise was considered a

distraction in the control room. The licensee evaluated this concern from the Diagnostic

Evaluation Team inspection and performed modifications to quiet the airflow. Silencers

were installed by temporary modification TM-95-107 and made permanent by the

engineering specification change SC-95-073. Main control room silencers and a balance

damper were installed under specification change SC-97-027. The inspectors and

operating personnel interviewed have noticed a significant reduction in control room

ventilation noise. This item is closed.

08.2

(Closed) Violation 50-255/96008-01: F'ailure to have a senior reactor operator in the

control room at all times. On August 9, 1996, the control room supervisor left the control

room with no other senior reactor operator (SRO) present. The control room supervisor

entered the viewing gallery, which is adjacent to the control room. The control room

supervisor was out of the control room less than one minute. On August 13, 1996, a

similar occurrence resulted when the shift engineer, who temporarily relieved the control

room supervisor as the SRO in the control room, briefly left to file a work order in the

adjacent technical support center. The shift engineer was out of the control room

approximately one minute. Extensive remodeling of the control room was ongoing in both

instances. In each case, the SRO went to an area that was normally part of the control

room envelope but had been temporarily relocated outside the control room.

Immediate corr~ctive actions for the first event included a reminder in the Daily Orders

regarding control room staffing, and operations management discussed the event with

the involved SRO. Also, the door between the control room and the temporary shift

engineer's desk was closed in an attempt to make it less convenient for an SRO to leave

the control room inadvertently. Operations management discussed with the available

SROs their responsibility to maintain an SRO in the control room at all times. An entry

was also made on the SRO turnover sheet as a reminder for SROs that had not

participated in the discussion.

In addition, the control room remodeling project has been completed. The shift

supervisor, shift engineer and control room supervisor work areas have now been

restored to their normal locations. This item is closed .

7

-*

II. Maintenance

M1

Conduct of Maintenance

M1 .1

General Comments

a.

Inspection Scope (62707 ~nd 61726)

The inspectors observed all or portions of the following work activities:

Work Order No:

24713751

24713416

24710557

24714900

24510530

24002261

2410939

Surveillance Activities

SOP-3

Q0-23

M1-39

M1-3

M1-3

Q0-21C

PCV-0522A, Alternate steam Sl,lpply to AFW pump P-88:

Calibrate Controller. Steam pressure setting has drifted

below setpoint

P-7C Service water pump: Perform preventive

maintenance on Breaker 152-205

Nitrogen station 1 A: Replacement of check valve and

manifold valves on

SV-09778, CCW return from radwaste evap.: Removal,

replacement and testing of leaking solenoid valve

MV-SFP 131, sperit fuel pool supply valve to shutdown

cooling heat exchanger: Repair body to .bonnet leak

MV-SFP 132, spent fuel pool return valve from shutdown

cooling heat exchanger: Repair body to bonnet leak

MV-SFP 512, instrument isolation valve to spent fuel pool

heat exchanger E-538: Lap valve seat and repair body to

bonnet leak

Safety Injection and Shutdown Cooling System (Safety

injection tank sampling)

Auxiliary Hot Shutdown Panel Instrumentation Checks

Auxiliary Feedwater Actuation System Logic Test

Reactor Protection Matrix Logic Tests

Venting of the CCW System

lnservice Test Procedure - Auxiliary Feedwater Pump P-8C

8

b.

Observations and Findings

The inspectors noted that the work was conducted in a professional and thorough

manner. All work observed was done with the work package present and in active use.

Work packages were comprehensive for the task and post maintenance testing

requirements were adequate. The inspectors frequently observed supervisors and

system engineers monitoring work. When applicable, work was done with the appropriate

radiation control measures in place. Specific events and noteworthy observations are

noted below.

The inspectors noted that the spent fuel pool maintenance activity was well planned and

. executed; however, one deficiency was noted. The nuts and bolts on the valves and at

the job site for contingency use were heat treated steel instead of stainless steel. This

issue is discussed in detail in Section M1 .2.

The inspectors observed the auxiliary operators at the hot shutdown panel. The

inspectors noted that the off-normal procedure and emergency operating procedures

were stored inside the cabinet. The inspectors were concerned that the manuals could

move around during a seismic event and damage control wiring in the panel. A condition

report was generated, and the manuals were removed from the panel. The inspectors

reviewed the operability determination, which was found adequate.

During replacement of two manifold valves on Nitrogen Station 1A, the inspectors noted

that maintenance technicians demonstrated a proper questioning attitude by notifying

their supervisor of a tagout deficiency before starting work on the* nitrogen station.

Operations personnel had removed the hoses from the.nitrogen bottles and tagged the

hoses. This meant that the maintenance technicians would have had to remove the

tagged isolation boundary from the manifold valves, which posed no personnel safety

risk, but was contrary to procedural requirements of Administrative Procedure AP 4.10,

"Personnel Protective Tagging." Operations edited the switching .and tagging order; and

removed the tag.s. Reinstallation of the hoses was covered in the restoration activities.

c.

Conclusions

Overall, the inspectors observed good procedure adherence and maintenance and

radiation work practices. Two identified deficiencies were promptly corrected; however,

the inspectors identified a concern regarding the use of heat treated steel nuts and bolts

on two spent fuel poof valves.

M1 .2

Spent Fuel Pool System Maintenance Outage

a.

Inspection Scope

The inspectors reviewed the licensee's preparatory activities and observed portions of the

spent fuel pool valve maintenance. Discussions were held with the maintenance planner

C!l'1~L~ystem engineer. Observations of the prejob brief, the spent fuel poof draindown

evolution, portions of the valve maintenance activities, and the post-maintenance critique

were conducted .

9

b.

Observations and Findings

The purpose of the spent fuel pool maintenance outage was to repair body to bonnet

leaks on two valves, MV-SFP131 and MV-SFP132. Performance of the repairs required

lowering the spent fuel pool approximately three feet.* This would bring the level below

the suction for the spent fuel pool pumps. Portions of the spent fuel pool system piping

above the valves also had to be drained. The risk of this maintenance activity was

potential loss of positive control over fuel pool level and water temperature.

The inspectors discussed the activity with the system engineer and planner. It was

evident from the procedure and schedule that the activity was well planned. Adequate

controls were in place to monitor spent fuel pool level and temperature. Also, planned

radiological precautions were adequate to account for potential airborne contamination

when the uncovered portion of the spent fuel pool walls dried out and when the spent fuel

pool system integrity was breeched during maintenance activities on the valve bonnets.

The schedule allowed for a sufficient margin to avoid exceeding administrative limits for

fuel pool temperature. Blank flanges were made as a contingency if the system integrity

had to be restored once the valves were apart.

The inspectors observed the tagout and draining of the spent fuel pool and piping. The

activity by the operations shift was well executed and controlled. The inspectors noted

good oversight of the evolution by the shift supervisor. The maintenance activity went'

well; no deficiencies were noted. However, the inspectors noted that the extra nuts and

bolts at the job site for contingency use were heat treated steel. Also, nuts and bolts on

the valves body to bonnet connections were heat treated steel. These should have been

stainless steel, because the spent fuel pool has borated water. The inspectors brought

this to the system engineer's attention. Generic Letter 88-05, "Boric Acid Co.rrosion of

Carbon Steel Reactor Pressure Boundary Components in PWR Plants," and several

information notices have addressed this issue. Also, the inspectors had discussed with

licensee management this concern pertaining to the spent fuel pool system. The

  • inspectors considered this issue to be an unresolved item (50-255/97018-02) pending a

review of the licensee's evaluation of the heat treated steel nuts and bolts.

The licensee was reviewing purchase order requirements as to why the steel nuts and

bolts were considered acceptable. The maintenance outage was completed ahead of

schedule. Operations restored the fuel pool system integrity and refilled the spent fuel

pool.

c.

Conclusions

The inspectors concluded that the spent fuel pool maintenance activity to repair body to

bonnet leaks on two valves, MV-SFP131 and MV-SFP132, was well planned and

executed. However, one deficiency was noted in that the nuts and bolts on the valves

were heat treated steel instead of stainless steel. An unresolved item was opened

pending a review of the licensee's evaluation of the nuts and bolts.

10

Ill. Engineering

E1

Conduct of Engineering

E1 .1

Review of Engineering Corrective Actions and Evaluations of Air Systems

a.

Inspection Scope (37551)

On March 18, 1997, CV-3018, Safety Injection Tank Test Line Redundant High Pressure

Injection Isolation Valve, failed to change position during a surveillance test because its

air regulator was plugged with rust. The inspectors reviewed NUREG-1275 Volume 2,

"Operating Experience Feedback Report - Air System Problems.,.. and the.licensee's

corrective actions and evaluation of Generic Letter 88-14. The inspectors also inspected

improvements made to the instrument air system and high pressure air system.

b.

Observations and Findings

One of the licensee's evaluations supporting the response to Generic Letter 88-14,

ATRN-88-55, dated February 15, 1989, stated, in part:

"Another issue to be resolved is the placement of satellite filters in the airlines.

Most of the filters are installed downstream of pressure regulating valves ....

However, the regulators then go unprotected from larger airline particles which

could cause regulator failure."

Inspection Report No. 50-255/97005 discussed the failure of CV-3018 to reposition in

March 1997. In addition to discussing safeguards high pressure air system drawing

discrepancies, the inspection report documented the inspectors' concern about the

placement of the air filters:

"The inspectors reviewed the safeguards high pressure air system drawings and

noted that not all pressure control valves (PCVs) were configured the same ..

Some PCVs had the air filters upstream of the valve, as would be expected.

However, the majority of the filters were located downstream of the PCVs and

system engineering was aware of the discrepancy. However, the inspectors were

concerned that this was a longstanding issue which had not been resolved."

The safety function of CV-3018, a fail-close valve, is to close or remain closed. However,

CV-3018 is opened in Emergency Operating Procedure Supplement 20 for alternate hot

leg injection, and it is also used in Off Normal Procedure (ONP) 25.2 as an optional

  • makeup path if all charging pumps have been lost. The filter for CV-3018 was

downstream of the valve; therefore, it was one of the valves previously identified as

susceptible to regulator failure. 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective

Action," requires, in part, that measures shall be established to assure that conditions

adverse to quality are promptly identified and corrected. In 1989, the licensee identified

that filter placement downstream of the valve could lead to regulator failure due to airline

particulate, a condition adverse to quality. In March 1997, CV-3018 failed to reposition as

expected during a surveillance due to airline particulate (rust). The failure to correct an

identified condition adverse to quality is considered a violation of 10 CFR Part 50,

Appendix B, Criterion XVI (50-255/9~018-01 ).

Inspection Report No. 50-255/97005 concluded the discussion of the failure of CV-3018

with the following:

"System engineering has since scheduled PM activities to inspect and clean

selected PCVs; specifically, those that have filters downstream of the PCVs.

These have been determined most susceptible to plugging. System engineering

was reviewing the feasibility of modifications to improve system reportability. One

of the corrective actions instituted to help remove moisture from the high pressure

air system in the west safeguards room was the practice of blowing down the low

point drains on a monthly basis."

On December 2, 1997, the inspectors identified a low point section of the air supply line,

48 feet long, which had no drains, resulting in approximately 6 cubic feet of air line which

could not be drained. CV-3018 was on a downstream section of line which taps off the

48-foot low point section of the air supply line. Therefore, the practice of blowing down

the air.line did not remove moisture from the lines leading to CV-3018, and rust

accumulated to the point where the regulator became plugged. The inspectors

concluded that the low point drain problem and the lack of corrective action for an air filter

placement problem led to failure of the air regulator.

Work request No. 251837 was written on December 3, 1997, to install two new low point

drains in the west safeguards room high pressure air system per engineering assistance

request (EAR) 97-0729. EAR 97-0729 also requested a change to the surveillance

requiring weekly air system blow downs to include these two new locations.

c.

Conclusions

During follow up to a March 1997, failure of CV-3018 to reposition, the inspectors

concluded that the corrective action for air line filter placement for pressure control valves

(PCVs) was inadequate in that the licensee failed to correct a previously identified

condition adverse to quality. The inspectors further concluded that placement of low

point drains in the air lines leading to the PCVs was inadequate. The low point drain.

problem and the la.ck of corrective action for the air filter placement problem led to failure

of CV-3018's air regulator. A violation of NRC requirements was identified.

E1 .2

Radwaste Evaporator Isolation Valve Testing (37551)

a.

Inspection Scope

During recovery from the loss of component cooling water inventory discussed above in

Section 01.2, the licensee noted that some of the radwaste evaporator isolation valves

were leaking by. The inspectors reviewed the licensee's preparations for troubleshooting

the affected valves, CV-0944, component cooling water (CCW) supply isolation valve to

the radwaste evaporators and CV-0977, CCW return isolation valve to the radwaste

evaporators.

b.

Observations and Findings

The inspectors observed the cognizant system engineer brief the control room supervisor

prior to conducting testing of both CCW valves. The system engineer planned to use an

informal guideline to perform the test rather than a procedure. When the control room

12

-*

C.

supervisor questioned the system engineer as to the implications of unisolating the

affected portion of the CCW system, the system engineer did not have a response.

Therefore, the control room supervisor determined that he did not have enough

information to conduct the test.

The inspectors have also identified past weaknesses with informal testing by the

licensee. Examples included the turbine vibration testing that failed to set limits on the

amount of vibration allowed before stopping testing (IR 50-255/97009) and spent fuel pool

rate of temperature rise that had no set temperature limits (IR 50-255/96007). However,

testing performed in accordance with a procedure required a safety evaluation and

management approval.

The inspectors reviewed the activities completed in preparation for valve testing. Design

engineering had prepared an evaluation in the event that one or both of the valves failed

to close during the test. The inspectors reviewed the document and found that various

potential design basis accidents had been addressed. Also, system engineering had

completed an evaluation of all gasketed joints in the radwaste evaporator system. The

remaining gasketed joints had flexitallic gaskets, and the distillate cooler joint had been

properly repaired. System engineering had revised the operability evaluation on the

supply and return valves to include the leakage noted by the valve seats after the loss of

CCW inventory had occurred.

The system engineer held another brief with the control room supervisor and discussed

the completed evaluations. The control room supervisor approved the test and the

testing was completed with no unexpected results .

Conclusions

The inspectors concluded that the system engineer had adequately prepared to perform

leak checks on the radwaste evaporator component cooling water supply and return

valves. However, the inspectors noted that the system engineer did not communicate to

the control room supervisor all of the activities performed in preparation of valve testing.

E1 .3

Motor Operated Valve T-Drain Issue

a.

Inspection Scope (37551)

The inspectors reviewed the licensee's response to a significant events report issued by

another utility that concerned defective T-drains on environmentally qualified motor

operated valves (MOVs). Discussions were held with the component engineering

supervisor, who is responsible for MOVs. The applicable condition report and preventive

maintenance documents were also reviewed to ensure an adequate response to this

concern by the licensee.

b.

Observations and Findings

Recently, two separate utilities discovered vendor supplied T-drains installed on safety-

related MOVs without drilled drain holes. The purpose of the T-drain on the MOV motor

housing is to relieve moisture buildup in a harsh environment following a major accident.

13

c.

EB

E8.1

a.

The vendor supplied T-drains were not drilled and would act as a pipe plug rather than as

a drain. The vendor and other utilities were not able to i.dentify a particular batch or

manufacturing time frame for the defective parts.

This condition was identified at Palisades on November 6, 1996, during inspection of a

new motor. However, the potential generic industry implications were missed. Following

the identification of this problem (C-Pal-96-1338), several corrective actions were

implemented. Spare T-drains and environmentally qualified motors were examined to

ensure a proper drain path had been drilled; all T-drains and motors were found

acceptable. Additionally, the procurement engineering check list (PEC-93-001-0010) was

revised to require receipt inspection of T-drains and the T-drains on motors. Following

the recent identification of a similar problem at other utilities, the licensee revised the

preventive maintenance procedures to ensure a more thorough inspection of the

T-drains.

The licensee reviewed the test data for the 15 environmentally qualified MOVs installed

inside containment which have T-drains. Based on a review of the original test procedure

and engineering judgement, the licensee declared the potentially affected MOVs

operable. The licensee's engineering staff also concluded that the environmental

parameters from the original test procedure were acceptable for qualification at Palisades

for new motors. The inspectors reviewed the licensee's operability evaluation and

associated documentation and had no concerns.

Conclusions

The inspectors concluded that the licensee's response to a generic issue regarding motor

operated valve T-drains was adequate. The inspectors had no concerns with the

licensee's operability determination.

Miscellaneous Engineering Issues (92700 and 92903)

Enforcement Panel Review of Appendix R Issues

Inspection Scope

A NRC enforcement panel reviewed the licensee's corrective actions taken in response to

three reportable Appendix R 50. 72 events involving conditions outside the design basis.

The three Appendix R design issues pertained to: 1) improper evaluation for the effects

caused by spurious operation of component cooling water/service water interface valves;

2) alternate shutdown procedures that did not incorporate the Appendix R assumption

that all reactor c_oolant pumps would be tripped if a fire caus.ed an evacuation of the

control room; and 3) inadequate evaluation for the effects caused by spurious openfng of

the atmospheric steam dump valves. Details of the first two issues were outlined in

Inspection Report No. 50-255/97011. Details of the atmospheric dump valves were

outlined in licensee event report (LER)97-010.

b.

Observations and Findings

The three Appendix R issues were reviewed by an NRC enforcement panel on

October 30, 1997, including the licensee's corrective actions.

14

Design Issue One

On September 12, 1997, the licensee made a one hour nonemergency 10 CFR 50.72

notification for being in a condition outside of design bases. The Appendix R event

involved a control room fire, which generated a hot short condition of a control valve

solenoid resulting in a spurious actuation of a service water (SW) system interface valve.

The part of the SW system involved was the seal cooling water for the essential safety

system (ESS) pumps. The most limiting scenario calculated that only 25 seconds would

be available to close engineering safeguards pump cooling service water return valve,

CV-0951. This valve is *normally closed. An open item of this Appendix R analysis

acknowledged the 25 second requirement, but concluded since the ESS pumps are not

running during normal operation and the component cooling water (CCW) supply and

return Valves (CV-0913 and CV-0950, respectively) to the ESS pumps' sealing cooling

piping are normally closed, then the spurious opening of any one CCW/SW interface

valve could not result in the loss of CCW inventory. Based on this information, another

analysis did not consider actions for the required time period. This reasoning is in error

because CV-0913 and CV-0950 are normally open and fail open on loss of air or loss of

electric power. A single spurious operation of CV-0951 would require a 25 second

operator response to mitigate the consequences, which is not possible.

On September 24, 1997, permanent placards were placed in the control room to indicate

that the air supply valves were permanently closed. The valves were also placed on the

system checklist with the normal position indicated as "closed."

Design Issue Two

On September 23, 1997, the licensee reported the second issue to NRC via a

10 CFR 50.72. It involved the Appendix R analysis assuming all four primary coolant

pumps being tripped if the fire causes an evacuation of the control room. The Off Normal

Procedure (ONP) for Alternate Shutdown did not reflect the analysis and only directed the

operators t6 trip two of the four primary coolant pumps.

Procedure ONP-25.2, "Alternate Safe Shutdown Procedure," did not specifically address

securing all the primary coolant pumps when the operators lose the ability to monitor the

pumps, such as during a control room evacuation or a damage to the instruments.

Procedure ONP 25.2 provided guidance for fires where a control room evacuation was to

take place and fires where the control room is still manned. The procedure assumes that

monitoring of the primary coolant pumps is a condition of their continued operation.

Several fire scenarios could result in a loss of component cooling water (CCW) to the

primary coolant pump seals and bearing coolers. Upon leaving the control room,

operators do not have primary coolant pump monitoring capability or instrumentation to

monitor the CCW system. The licensee's design basis for the primary coolant pumps

indicated they are designed to operate without seal cooling for periods of up to ten

minutes. Immediate corrective action was to initiate a. procedure revision to direct

operators to trip all four primary coolant pumps prior to control room evacuation.

Operator training includes the necessity of CCW for primary coolant pump for operation,

therefore the operators may secure primary coolant pumps when CCW could no longer

be monitored .

15

Design Issue Three

On September 30, 1997, the inspectors were notified of a design vulnerability involving

the inadvertent simultaneous opening of all four atmospheric steam dump valves

discovered during a review of Appendix R documents. The event which may trigger this*

response is a smart hot short in any one of. three cable segments not previously

identified. The three cable/wire segments are in the atmospheric dump control circuitry,

and are physically located in two main control room panels and in a section of cable

routed in a raceway in the cable spreading room.

The event involves a fire that causes a single hot short iil the control room panels or a

single hot short in the cab.le spreading room that could potentially result in all four

atmospheric dump valves (ADVs) spuriously opening. An engineering analysis was

conducted for a plant response with only two stuck open ADVs under Appendix R

conditions. The analysis concluded that spurious operation of the control circuit during a

fire scenario would only affect two ADVs because the review was limited to only the

circuits identified on the circuit and raceway schedule. A cable routed between the cable

spreading room and the control room where a hot short could exist and cause the

deficient condition is not identified on the circuit and raceway schedule, contrary to what

is normally expected. Additionally, original plant design and construction practice

excluded wire and cable within the various panels in the plant from inclusion in the circuit

and raceway schedule. Rather, such* wire/cables are described in vendor prints for the

specific panels, not in the original architect engineering's cable and raceway schedule.

Thus, the scope of review of cable and raceway schedules excluded cables located

internally to specific panels.

The level of plant knowledge of those involved in the analysis also contributed to the

condition. Had they been aware .that a single controller operated the four ADVs, it is

expected the decision to only evaluate a condition with two AOVs opening would have

been questioned. A lack of adequate rigor in the analysis of the control circuits led to not

identifying this single common control feature.

The licensee performed an analysis and provided evidence that operators could close the

AOVs within six minutes. Procedure ONP 25.2 was revised to ensure the actions are

completed within the required time. Engineering is completing a new plant analysis

response to address the opening of all four ADVs during the postulated fire scenarios.

The Appendix R group is continuing to perform an in-depth review of Appendix R. This

effort is expected to conclude in early August 1998.

c.

Conclusions

These issues are of concern* because of the safety significance associated* with plant

equipment configuring that did not meet 10 CFR Part 50, Appendix R, safe shutdown

requirements for a design basis fire. These issues would normally be designated as a

Severity Level Ill problem in accordance with the NRC's NUREG-1600, "General

Statement of Policy and Procedures for NRC Enforcement Actions," (Enforcement

Policy). However, enforcement discretion will be used in accordance with Section Vll.B.3,

"Violations Involving Old Design Issues," of the Enforcement Policy and a Notice of

Violation will not be issued. The decision to apply enforcement discretion was based on

consideration of the following: 1) significant NRC enforcement action (EA 96-131) was

16

"

taken against the Consumers Energy Company for several examples of a failure to take

prompt corrective actions related to Appendix R deficiencies. Palisades identified the

issues detailed above and promptly notified the NRC; 2) corrective actions were

immediate and encompassed the root causes for these issues; 3) some of the issues

were related to activities that were in progress before the enforcement action was issued;

4) the issues would not be classified at a severity level higher than Severity Level Ill; and

5) Consumers Energy Company met with the NRC to explain their efforts to resolve these

issues, which were outlined in their reply dated September 12, 1996.

EB.2

(Closed) Unresolved Item No. 50-255/91014-01: Failure to perform a between-the-seals

test of the escape air lock. The inspectors found that the same issues of

LER 50-255/97-002 discussed in Section EB.3 of this inspection report, were pertinent to

the closeout of this unresolved item. This item is closed.

EB.3

(Closed) Licensee Event Report No. 50-255/97002-00: Failure to perform a between-the-

seals test of the escape air lock after each use of the air lock. 10 CFR, Appendix J,

requires that air locks opened during periods when containment integrity is required shall

be tested within three days after being opened. Also, testing did not meet TSs, which

required testing subsequent to the air lock door being opened.

Past TS surveillance testing of the escape air lock at containment design pressure with

strongbacks in place caused the seals to deform due to the door design. After

completion of the full pressure test, the doors must be opened to remove the strongbacks

and verify seal contact with the door seating surface to ensure th~t the seals have

rebounded to their pre-test condition. However, past test performance has shown that

after the strongbacks are removed, the seals may not fully rebound, leaving gaps in the

contact surface. After full pressure testing, a seal check was performed as part of the

surveillance test. If the seal contact check revealed gaps, a seal adjustment was

performed to ensure that the seal material rebounded to its pre-test condition. The

licensee considered seal adjustment a normal part of restoration from testing that was

controlled by procedure.

The licensee proposed a TS change and exemption to revise the test requirements. The

change allowed performance of a seal contact check instead of an unrestrained between-

the-seals test for the emergency escape air lock doors. The licensee also proposed

changes to clarify the pressure requirements for the personnel airlock doors between-the-

seals test. The test would be performed at less than or equal to 1 O psig instead of

55 psig.

In a letter dated September 30, 1997, the NRC granted the TS change and exemption

from the requirements of 10 CFR Appendix J relating to the testing of the emergency

escape lock. The exemption provided relief from the requirement to perform additional air

lock leakage rate testing after opening the doors for post-test restoration of seal

adjustment following air lock leakage rate testing. This item is closed.

EB.4

(Closed) Violation No. 50-255/96010-03: Failure to initiate a condition report upon

discovery that Palisades was potentially susceptible to the problems noted in NRC

Information Notice 96-45, "Potential Common-Mode Post Accident Failure of Containment

Coolers." The reason for the violation was due to weaknesses the inspectors identified in

the industry event review program and Administrative Procedure AP 3.03, "Corrective

Action Process." Administrative Procedure AP 3.16 lacked guidance about what types of

17

..

-*

information would warrant transferring an issue out of the industry experience review

program and into the corrective action system. It was also weak in the guidance provided

regarding processes of conditions discovered during the evaluation of industry experience

information that could potentially be a safety concern for the plant. In addition, the

guidelines provided in AP 3.03 as examples of when a condition report should be written

were vague in their treatment of issues being processed.

Procedure AP 3.16 was revised to include guidance for reporting conditions that could

potentially be a safety concern for the.plant which are discovered during the review of

industry experience events. The guidance included elevation to higher management

levels when industry experience information is reported as applicable by multiple facilities.

Procedure AP 3.03 was also revised to clarify when a condition repqr:t, should be written

for items being processed within the industry experience program. These procedure

revisions strengthened the interrelationship between the industry experience review

program and the corrective action program.

The licensee also improved the industry experience review organization and program. An

individual with a technical background was assigned as coordinator of the program. The

new coordinator visited several sites to review other licensees' programs. The

coordinator held briefings with engineering to discuss the purpose and changes being

made to the industry event review program. The industry event program was

incorporated into the program health assessment process for closer management

oversight. This item is closed.

IV. Plant Support

R1

Radiological Protection and Chemistry Controls (71750)

During the resident inspection activities, routine observations were conducted in the

areas of radiological protection and chemistry controls using Inspection Procedure 71750.

no discrepancies were noted.

S1

Conduct of Security and Safeguards Activities (71750)

During normal resident inspection activities, routine observations were conducted in the

areas of security and safeguards activities using Inspection Procedure 71750. No

discrepancies were noted.

F1

Control of Fire Protection Activities (71750)

During normal resident inspection activities, routine observations were conducted in the

area of fire protection activities using Inspection Procedure 71750. No discrepancies .

were noted.

X1

Exit Meeting

The inspectors presented the inspection results to members of the licensee management

at the concl1,1sion of the inspection on January 27, 1998. No proprietary information was

identified by the licensee.

18

"

PARTIAL LIST OF PERSONS CONTACTED

Licensee

R. A. Fenech, Senior Vice President, Nuclear, Fossil, and Hydro Operations

T. J. Palmisano, Site Vice President - Palisades

G. 8. Szczotka, Manager, Nuclear Performance Assessment Department

D. W. Rogers, General Manager, Plant Operations

K. M. Haas, Acting Director, Engineering

S. Y. Wawro, Director, Maintenance and Planning

R. J. Gerling, Manager, Design Engineering

P. D. Fitton, Manager, System Engineering

T. C. Sardine, Manager, Licensing

J. P. Pomeranski, Manager, Maintenance

D. G. Malone, Shift Operations Supervisor

M. P. Banks, Manager, Chemical & Radiation Services

E. Chatfield, Acting Manager, Training

19

" -

IP 37551:

IP 61726:

IP 62707:

IP 71707:

IP 71750:

IP 83750:

IP 92700:

IP 92701:

IP92702:

IP 92901:

IP 92902:

IP 92903:

INSPECTION PROCEDURES USED

Onsite Engineering

. Surveillance Observations

Maintenance Observation

Plant Operations

Plant Support Activities

Occupational Radiation Exposure

Licensee Event Reports

Followup

Followup on Corrective Action for Violations And Deviations

Followup - Operations

Followup - Maintenance

Followup - Engineering

ITEMS OPEN

50-255/97018-01

VIO

Inadequate corrective action for safeguards high pressure

air system filter placement

50-255/97018-03

URI

50-255/91014-01

URI

50-255/94014-06

IFI

50-255/96008-01

VIO

50-255/96010-03

VIO

50-255/97002-00

LER

Use of heat treated steel nuts and bolts on spent fuel pool

valves

ITEMS CLOSED

Failure to perform a between the seals test

Control room ventilation noise considered distraction in

control room

Failure to have a senior reactor operation in the control

room at all times

Failure to initiate a condition report

Failure to perform a between the seals test of the escape

air lock after each use of the air lock

20

A LARA

AFW

AP

ccw

CFR

CR

CV

DRP

GL

GPM

IP

IRT

LCO

LER

MO

MOV

MV

NRC

NCO

ONP

oos

PCP

PCV

PWR

QO

SOP

SRO

TM*

TS

URI

VIO

LIST OF ACRONYMS USED

As Low As Reasonably Achievable

Auxiliary Feedwater

Administrative Procedure

Component Cooling Water

Code of Federal Regulations

Condition Report

Control Valve

Division of Reactor Projects

Generic Letter

Gallons Per Minute

Inspection Procedure

Incident Response Team

Limiting Condition for Operation

Licensee Event Report

Monthly Operating (procedure)

Motor Operated Valve

Manual Valve

Nuclear Regulatory Commission

Nuclear Control Operator

Off Normal Procedure

Out Of Service

Primary Coolant Pump

Pressure Control Valve

Pressurized Water Reactor

Quarterly Operations (procedure)

System Operating procedure

Senior Reactor Operator

Temporary Modification

Technical Specification

Unresolved Item

Violation

21