IR 05000255/2020001

From kanterella
Jump to navigation Jump to search
Integrated Inspection Report 05000255/2020001
ML20133K066
Person / Time
Site: Palisades 
Issue date: 05/12/2020
From: Billy Dickson
NRC/RGN-III/DRP/B2
To: Corbin D
Entergy Nuclear Operations
References
IR 2020001
Download: ML20133K066 (21)


Text

May 12, 2020

SUBJECT:

PALISADES NUCLEAR PLANT - INTEGRATED INSPECTION REPORT 05000255/2020001

Dear Mr. Corbin:

On March 31, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Palisades Nuclear Plant. On April 14, 2020, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Billy C. Dickson, Jr., Chief Branch 2 Division of Reactor Projects

Docket No. 05000255 License No. DPR-20

Enclosure:

As stated

Inspection Report

Docket Number:

05000255

License Number:

DPR-20

Report Number:

05000255/2020001

Enterprise Identifier: I-2020-001-0032

Licensee:

Entergy Nuclear Operations, Inc.

Facility:

Palisades Nuclear Plant

Location:

Covert, MI

Inspection Dates:

January 01, 2020 to March 31, 2020

Inspectors:

R. Baker, Senior Operations Engineer

B. Bergeon, Operations Engineer

A. Childs, Reactor Engineer

P. Laflamme, Senior Resident Inspector

J. Mancuso, Resident Inspector

T. Ospino, Reactor Engineer

J. Winslow, Reactor Systems Engineer

Approved By:

Billy C. Dickson, Jr., Chief

Branch 2

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Palisades Nuclear Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

PLANT STATUS

The plant began the inspection period at rated thermal power, and remained at or near rated thermal power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/readingrm/doc-collections/insp-manual/inspection-procedure/index.html.

Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. From January 1 - March 19, 2020, the inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the coronavirus (COVID-19), resident inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time the resident inspectors performed periodic site visits each week and during that time conducted plant status activities as described in IMC 2515, Appendix D; and observed risk significant activities when warranted. In addition, resident and regional baseline inspections were evaluated to determine if all or portion of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In the cases where it was determined the objectives and requirements could not be performed remotely, management elected to postpone and reschedule the inspection to a later date.

REACTOR SAFETY

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1)1-2 Emergency Diesel Generator (EDG) starting air system on January 27, 2020

(2) Station Battery Number 2 system on March 16, 2020 (3)7A Service Water system on March 18, 2020

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Fire Area 13A: Auxiliary Building main corridor, 590' elevation on January 6, 2020
(2) Fire Area 9: Screen House/Intake Structure during P-7A support intallation on January 14, 2020
(3) Fire Area 28: West Engineered Safeguards Room; 570' elevation on January 15, 2020
(4) Fire Area 10: East Engineered Safeguards Room on March 12, 2020

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (1 Sample)

(1) The inspectors reviewed and evaluated the licensed operator examination failure rates for the requalification annual operating exam administered from January 8, 2020 through February 6, 2020.

71111.11B - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Requalification Program (IP Section 03.04) (1 Sample)

(1) Biennial Requalification Written Examinations

The inspectors evaluated the quality of the licensed operator biennial requalification written examinations administered between February 15, 2019 and March 22, 2019.

Annual Requalification Operating Tests

The inspectors evaluated the adequacy of the facility licensees annual requalification operating test.

Administration of an Annual Requalification Operating Test

The inspectors evaluated the effectiveness of the facility licensee in administering requalification operating tests required by 10 CFR 55.59(a)(2) and that the facility licensee is effectively evaluating their licensed operators for mastery of training objectives.

Requalification Examination Security

The inspectors evaluated the ability of the facility licensee to safeguard examination material, such that the examination is not compromised.

Remedial Training and Re-examinations

The inspectors evaluated the effectiveness of remedial training conducted by the licensee and reviewed the adequacy of re-examinations for licensed operators who did not pass a required requalification examination.

Operator License Conditions

The inspectors evaluated the licensees program for ensuring that licensed operators meet the conditions of their licenses.

Control Room Simulator

The inspectors evaluated the adequacy of the facility licensees control room simulator in modeling the actual plant, and for meeting the requirements contained in 10 CFR 55.46.

Problem Identification and Resolution

The inspectors evaluated the licensees ability to identify and resolve problems associated with licensed operator performance.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the Control Room during letdown isolation and restoration activities during relief valve replacement inside containment on March 10, 2020

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated PLSEG-LOR-19G-03 on March 12, 2020

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (2 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1) Turbine building sump system on March 16, 2020
(2) Neutron monitoring system on March 30, 2020

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Risk associated with installing support brackets on P-7A, service water pump and repack of P-7B, service water pump during the week of January 13, 2020
(2) Elevated risk for planned maintenance on component cooling water pump P-52B on January 27, 2020
(3) Risk associated with emergent repair activities on CV-944A, Component Cooling Water (CCW) to Spent Fuel Pool (SFP) cooling, air operated valve on February 18, 2020
(4) Risk associated with unexpected letdown system isolation on February 25, 2020
(5) Elevated risk for unanticipated loss of one source of offsite power on March 2, 2020
(6) Elevated risk for shutdown cooling system maintenance, letdown safety valve replacement, and safety injection system testing on March 2, 2020

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (4 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) ED-02 Station Battery Number 2 Operability Evaluation as documented in CR-PLP-2020-00253 on February 13, 2020
(2) CCW Operability Evalution on February 21, 2020
(3) Containment Spray System Operability Evalution on March 4, 2020
(4) Right Train Service Water System Operability Evaluation on March 23, 2020

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1) Engineering Change: P-7A Service Water Pump Column Brace Bracket Replacement Modification on February 19, 2020

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (7 Samples)

The inspectors evaluated the following post maintenance test activities to verify system operability and functionality:

(1) P-8A Auxiliary Feedwater (AFW) breaker test and pump start following planned maintenance on January 6, 2020 (2)1-1 EDG turbo charger support non-destructive testing following planned maintenance on January 8, 2020
(3) QO-14, Inservice Test Procedure - service water pumps after repack of P-7B service water pump on January 15, 2020
(4) P-7A service water pump testing following seismic support installation on January 21, 2020
(5) NI-8 Power Range Safety Channel test following linear amplifier card replacement on January 22, 2020 (6)1-1 EDG load reject testing following governor replacement on February 6, 2020
(7) VT-2 inspection following letdown safety relief valve replacement on March 11, 2020

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01)

(1) Containment Spray System Pump P-54 Quarterly Surveillance Test on February 10, 2020
(2) Safety Injection System Right Train Test on March 11, 2020

Inservice Testing (IP Section 03.01) (1 Sample)

(1) AFW P-8C Quarterly Inservice Test (IST) Surveillance Test on January 30, 2020

RCS Leakage Detection Testing (IP Section 03.01) (1 Sample)

(1) Primary Coolant System Leak Rate Surveillance Test on January 22, 2020

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated:

(1) An Emergency Preparedness drill on February 19,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01)===

(1) Unit 1 (January 1, 2019 - December 31, 2019)

IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (1 Sample)

(1) Unit 1 (January 1, 2019 - December 31, 2019)

MS08: Heat Removal Systems (IP Section 02.07) (1 Sample)

(1) Unit 1 (January 1, 2019 - December 31, 2019)

71152 - Problem Identification and Resolution

Annual Follow-up of Selected Issues (IP Section 02.03) (1 Sample)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Elevated Unidentified Primary Coolant System (PCS) Leakage Condition Evaluation as documented in CR-PLP-2019-5037 during the week of February 24,

INSPECTION RESULTS

Observation: PCS Unidentified Leakage Evaluation 71152 The inspectors reviewed the events, circumstances, and causal evaluation associated with elevated Primary Coolant System (PCS) unidentified leakage rates that occurred in December of 2019, and January and February of 2020. Their efforts included assessing the licensee's Emergent Issues Team (EIT) level 3 troubleshooting, trending, and aggregate review activities. Additionally, the inspectors reviewed leakage trends, equipment condition assessments for the letdown system, Primary Coolant Pump (PCP)seal leak-off system, and control rod drive mechanism leakage collection manifold, monthly containment tour results, and containment sump level monitoring. The inspectors also interviewed operators, maintenance workers, and engineering personnel to complete their assessment efforts. In their review, the inspectors noted that most of the elevated unidentified leakage was accounted for by known leakage from the PCP seal leak off system (hard piped) to Primary System Drain Tank (in containment) and the letdown system to Vacuum Degassifier Tank (in auxiliary building) via the VCT divergent valve bypass (3-way flow valve). Since the above sources cannot be quantitatively measured individually on a routine basis, the collective measurements must administratively be quantified as unidentified combined leakage as required by station procedures. As a corrective action, the licensee performed adjustments on the VCT divergent valve and adjusted VCT system pressure to reduce flow across the divergent valve, which resulted in lowering unidentified leakage to normal and expected levels. Therefore, since the licensee confirmed the sources of elevated leakage in both measure and location, and associated corrective actions addressed the condition, the inspectors concluded the licensee actions taken were timely and effective commensurate with safety significance.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On April 14, 2020, the inspectors presented the integrated inspection results to Mr. D. Corbin, Vice President Operations, and other members of the licensee staff.
  • On January 24, 2020, the inspectors presented the licensed operator requalification program biennial inspection results to Mr. D. Lucy, General Manager Plant Operations, and other members of the licensee staff.
  • On February 25, 2020, the inspectors presented the licensed operator requalification program annual operating test results, inspection results to Mr. D. Karnes, Operations Training Instructor, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.04

Corrective Action

Documents

CR-PLP-2020-

00188

Threads for One 151-213 Alarm Relay Retention Screw and

Clip Found Stripped

01/21/2020

CR-PLP-2020-

214

Small Air Leak Coming from Diaphragm on PVC-1490, EDG

1-2 K-6B Starting Air Pressure Control

01/23/2020

CR-PLP-2020-

219

Flexible Conduit Separated from Junction Box in the

Overhead in Emergency Diesel Generator 1-2 Room

01/23/2020

CR-PLP-2020-

239

Air Leak Between the Bonnet and Body of PCV-1490, K-6B

Starting Air

01/25/2020

CR-PLP-2020-

248

Two Pressure Control Valves for PCV-1490 did not Regulate

Output Pressure as Designed

01/27/2020

CR-PLP-2020-

297

Bus 1D Relay Testing (Cubicle 152-208) Y-Phase Relay for

P-52B Protection Found to have High Dropout Moving

Contact Cutting into Resting Shelf

01/30/2020

CR-PLP-2020-

00301

Valve Seat Threaded into Valve Body not Securely Attached

on PCV-1490, EDG 1-2 Air Start Pressure

01/30/2020

CR-PLP-2020-

00899

P-7A Service Water Pump Packing Leak

03/19/2020

CR-PLP-2020-

00904

Repack Service Water Pump P-7C

03/19/2020

DR-PLP-2020-

00501

During Testing, Floor Drain in the Auxiliary Feedwater Room

was Very Slow to Drain Causing Back Up Around the P-8A

and P-8B Auxiliary Feedwater Pumps.

2/15/2020

Procedures

DBD-1.03

Auxiliary Feedwater System

SOP-12

Feedwater System

71111.05

Calculations

EA-FPP-03-001

Analysis of Combustible Loading at Palisades Nuclear Plant

Corrective Action

Documents

Resulting from

Inspection

CR-PLP-2020-

00019

NRC Identified: Left Sample on the Frisking Station in a

Level 1 Transient Combustible Area

01/06/2020

Fire Plans

Pre Fire Plan 13A

Main Corridor - North / Elevation 590'

Miscellaneous

DBD-7.10

NFPA 805 Fire Protection Program

71111.11A Miscellaneous

Palisades Licensed Operator Requalification Annual

2/25/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Examination Summary Results for 2020

71111.11B Corrective Action

Documents

CR-PLP-2019-

00652

Two SROs Failed DEP (Drill and Exercise Performance)

during CPE Simulator Scenario on 02/11/2019

2/11/2019

CR-PLP-2019-

00937

Licensed Operator Qualification were Removed from Two

Operators due to Failing the DEP Portion of the Annual

Operating Exam during Simulator Scenarios

03/06/2019

CR-PLP-2019-

04436

During the LOR As Found Simulator Exam a student

accessed ESOMS Narrative Logs in order to utilize the

Equipment Database portion. This is a forbidden program to

use during an exam.

11/05/2019

Corrective Action

Documents

Resulting from

Inspection

CR-PLP-2020-

229

EN-TQ-210, Conduct of Simulator Training, Procedure

Requires Clarification for the Scenario Grading Process

01/24/2020

Miscellaneous

Job Performance

Measure

PLJPM-LOR-CVCS-08

Job Performance

Measure

PLJPM-LOR-AOP-45

Job Performance

Measure

PLJPM-LOR-RO Admin-08

Job Performance

Measure

PLJPM-LOR-SRO Admin-08

Job Performance

Measure

PLJPM-LOR-FPS-02

Job Performance

Measure

PLJPM-LOR-AOP-32

Job Performance

Measure

PLJPM-LOR-CSS-03

Job Performance

Measure

PLJPM-LOR-AOP-41

Job Performance

Measure

PLJPM-LOR-RO Admin-07

Job Performance

Measure

PLJPM-LOR-SRO Admin-07

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Scenario-Based

Testing Checklist

SES-245

Scenario-Based

Testing Checklist

SES-246

Scenario-Based

Testing Checklist

SES-278

Scenario-Based

Testing Checklist

SES-279

Simulator Exam

Scenario

SES-276

Simulator Exam

Scenario

SES-277

Simulator Exam

Scenario

SES-278

Simulator Exam

Scenario

SES-279

Simulator

Performance Test

Procedure

Real Time and Repeatability Test

04/25/2016

Simulator

Performance Test

Procedure

Steady State Test

08/26/2019

Simulator

Performance Test

Procedure

Simultaneous Closure of All Main Steam Isolation Valves

10/23/2019

Simulator

Performance Test

Procedure

Trip of any Single Reactor Coolant Pump

10/23/2019

71111.11B Miscellaneous

Simulator

Performance Test

Procedure

Maximum Size Reactor Coolant System Rupture Combined

with Loss of All Offsite Power

10/23/2019

Simulator

Performance Test

Procedure

Slow Primary System Depressurization to Saturated

Condition with Pressurizer Relief or Safety Valve Stuck Open

10/23/2019

Simulator

Performance Test

Procedure

Cycle 27 Core Performance Test

11/09/2018

Simulator Post-

Transient

Comparison Test

Post Event Simulator Testing for DR-19-002 Event - Manual

Plant Trip

01/03/2019

Simulator Post-

Transient

Comparison Test

Post Event Simulator Testing for DR-19-003 Event -

Automatic Plant Trip

01/09/2019

TQF-201-IM05,

Rev 11

Remedial Training Plan, PL-N0019 Annual JPM Evaluation

Failure (PLJPM-LOR-AOP-S1, Rev 0 and PLJPM-LOR-SRO

ADMIN1, Rev 0)

03/14/2019

Procedures

EN-TQ-114

Licensed Operator Requalification Training Program

Description

EN-TQ-202

Simulator Configuration Control

EN-TQ-210

Conduct of Simulator Training

EN-TQ-217

Examination Security

PNT 8.0

Palisades Simulator Configuration Management

Procedure No.

4.00, Attachment

Certification for Resuming Active License Status

05/08/2018

Procedure No.

4.00, Attachment

Certification for Resuming Active License Status

09/12/2018

Procedure No.

4.00, Attachment

Certification for Resuming Active License Status

2/02/2019

RT-191

Startup Physics Test

TQF-210-DD03-

Grade

LOR Crew Performance Evaluation Grading Criteria

TQF-210-DD04-

Grade

RO/SRO Performance Evaluation Grading Criteria

TQF-210-DD05-

Grade

STA/SE Performance Evaluation Grading Criteria

Self-Assessments LO-PLPLO-2018-

00054

Pre-71111.11 Inspection Self-Assessment (Part 1)

03/29/2019

LO-PLPLO-2018-

00086

Pre-71111.11 Inspection Self-Assessment (Part 2)

01/22/2020

Work Orders

Discrepancy

Report DR 12-

28

Add Generator Output Breaker Malfunction Request

Discrepancy

Report DR 16-

036

Aux Feedwater Controller Replacement (FIC-0736A & FIC-

0737A)

Discrepancy

Report DR 18-

047

Phase 2 Modification to the Switchyard

Discrepancy

Report DR 19-

031

Loss of Simulator Sounds During Simulator Scenario

Discrepancy

Report DR 19-

057

CRDM Fan Failure

71111.12

Corrective Action

Documents

CR-PLP-202-

00418

The Display Screen on PY-0102B (Thermal Margin Monitor

Channel 'B') is Dim and the Brightness Needs to be Adjusted

2/10/2020

CR-PLP-2020-

259

Exceeded Maintenance Rule Performance Criteria for

Primary Coolant and Pressurizer & Level Control Systems

01/28/2020

CR-PLP-2020-

00919

CV-0511, Turbine Bypass to Condenser, Actuator not

Maintaining Pressure for a Minimum of 5 Minutes.

03/20/2020

CR-PLP-2020-

00922

FPS Door #60 Located Near the Missile Door of the TSC

had Threshold Gasket Lifted up

03/20/2020

CR-PLP-2020-

00952

Tracking CR for Maintenance Rule Evaluations of Low

Safety Significant Equipment Performance Issues

03/24/2020

Miscellaneous

System Health

Report

Neutron Monitoring System

Q3 - 2019

71111.12

Miscellaneous

System Health

Report

Turbine Generator System

Q3 - 2019

71111.13

Corrective Action

Documents

CR-PLP-020-

231

P-39B Cooling Tower Pump Packing has a Large Leak

01/24/2020

CR-PLP-2020-

232

Water Bubbling Out of Inspection Cover Near Base of P-

39B, Cooling Tower Pump

01/24/2020

CR-PLP-2020-

00611

Received EK-0702 Relief Valve RV-2006 Discharge High

Temp Unexpectedly

2/25/2020

Drawings

M-202

System Diagram Chemical and Volume Control System

M-202

Piping & Instrument Diagram Chemical & Volume Control

System Sheet 1A

Engineering

Changes

34410

Heat Balance Calculation Using the Ultrasonic Flowmeter

Measurement Device

EC 85426

Use of Tree Stand on Service Water Pump P-7A

Procedures

Admin 4.02

Control of Equipment

AOP-23

Primary Coolant Leak

EN-WM-104

On-Line Risk Assessment

Work Orders

539281 01

HTR Drain Pump Subcooling Valve Fuse Block Loose

2/14/2020

71111.15

Corrective Action

Documents

CR-PLP-2020-

00126

White Crystalline Substance Found on Wire Termination on

Cable C51/J49C/2 in Junction Box J49C

01/15/2020

CR-PLP-2020-

253

Discovered Foreign Material/Debris Inside Numerous Cells

During Quarterly Battery Check of ED-02 Station Battery

01/27/2020

CR-PLP-2020-

00510

CCW Should be Considered Inoperable - DNC

2/20/2020

CR-PLP-2020-

00552

During Review of Diagnostic Test on CV-0944A an Anomoly

on the Trace was Suspected to be Easy-Torque-Thrust

Sensor Failure

2/20/2020

CR-PLP-2020-

00559

Determined that Technical Specifications Basis for Limiting

Condition of Operation (LCO) 3.7.7, Component Cooling

Water (CCW) System, Should be Clarified

2/20/2020

71111.15

Corrective Action

Documents

CR-PLP-2020-

00568

Information on Vendor Drawing M-240, Sheet 9 (Revision 5)

did not Appear to Have a Valid Model Number for the

Actuators Associated with the 18" Valves (722A-SR-51).

2/20/2020

CR-PLP-2020-

00722

Control Room Received EK-0702 Relief Valve RV-2006

Discharge High Temp Unexpectedly

03/04/2020

CR-PLP-2020-

00872

Commercial Grade Valve ASME Sect. III, Class 3 Application

Evaluation

03/17/2020

CR-PLP-2020-

00907

Low Pressure Safety Injection Stem Nut Transition Time

Evaluation

03/19/2020

CR-PLP-2020-

00948

Found 52-1501 Group 1 Proportional heaters, in the Tripped

Free Condition

03/24/2020

Corrective Action

Documents

Resulting from

Inspection

CR-PLP-2020-

00563

The NRC Identified a 15 Drop per Minute Leak (Severity

Level 3) from CV-0944A, CCW to SFP HXS, RW Evaps,

C-50's/54 & NSSS

2/20/2020

Drawings

M-209

Piping & Instrument Diagram, Component Cooling System,

Sheet 3

Engineering

Changes

27090

Palisades EDG Turbo Support Cracking Report by MPR

Associates

224

ED-02 Foreign Material Cell 26 Reasonable Assurance of

Operability

000

234

Engineering Assessment of MV-SW602B

Procedures

CEP-NDE-0640

Turbocharger Support Liquid Penetrant Examination

01/08/2020

EN-OP-104

Operability Determination Process

MO-29

Engineered Safety System Alignment

SPS-E-20

Maintenance for 2400 Volt Siemens Switchgear

Work Orders

2874649-01

K-6A Turbocharger Support Inspection

10/09/2019

2877399 03

Containment Spray Header Level/Pressurizer Gauge Cal

01/28/2020

2898504

MO-29 Engineering Safety System Alignment

01/26/2020

71111.18

Calculations

EA-EC82054-01

Equivalency Evaluation of SW PUmps P-7A, P-7B, and P-7C

Lower Column Brace Brackets

01/15/2020

Corrective Action

Documents

Resulting from

Inspection

CR-PLP-2020-

00583

The NRC Found a Numerical Error in the Computation

Section of Calculation "Equivalency Evaluation of SW Pumps

P-7A, P-7B, and P-7C Lower Column Brace Brackets:

2/21/2020

71111.18

Corrective Action

CR-PLP-2020-

The NRC Found a Computational Error in the Computation

2/21/2020

Documents

Resulting from

Inspection

00584

Section of Calculation "Equivalency Evaluation of SW Pumps

P-7A, P-7B, and P-7C Lower Column Brace Brackets"

Engineering

Changes

2054

Service Water Pumps P-7A, P-7B, and P7-C

Procedures

NMS-1-10

Dual Linear Power Current Measurements

Work Orders

00536528 01

2-104, AFW-P-8A Breaker, Adjust Bayonet per SPS-E-1

01/06/2020

71111.19

Corrective Action

Documents

CR-PLP-2019-

04896

NMS-I-7, Dual Linear Power Channel Tilt Adjustment and

NMS-I-10, Dual Linear Power Current Measurements,

Procedures Needed a DRN Initiated

2/13/2019

CR-PLP-2020-

00114

NI-1/3A (Source & Wide Range Neutron Monitor CH1/3) was

Found Out of Tolerance for the Upper End of the Source

Count Range

01/14/2020

CR-PLP-2020-

00169

Calibration of Excore Nuclear Instrumentation is Needed

01/20/2020

CR-PLP-2020-

00355

The Plan for Refilling T-25A, Diesel Generator Fuel Oiol Day

Tank was Changed to Utilize on Site Fuel

2/05/2020

CR-PLP-2020-

00356

During Maintenance on K-6A, Emergency Diesel Generator

1-1, it was Discovered that the 2R Fuel Pump Cover was

Loose when it's Wingnut was Bottomed Out

2/05/2020

CR-PLP-2020-

00369

The CK-DE412 Left Bank Valve Train Lube Oil Supply is

Leaking

2/05/2020

CR-PLP-2020-

00373

During Performance of MO-7A-1, FI-0890, Diesel Generator

1-1 Service Water Flow was 710 gpm

2/06/2020

CR-PLP-2020-

00483

FUZ/J015-1 was Found Ajar from it's Fuse Block Holder

2/13/2020

Engineering

Changes

EC 85426

Use of Tree Stand on Service Water Pump P-7A

Procedures

CEP-NDE-0902

ASME Section XI VT-2 Examination Record

03/11/2020

EN-MA-101-03

Maintenance Work Preparation Process

EN-MA-118

Foreign Material Exclusion

01/08/2020

MO-7A-1

Emergency Diesel Generator 1-1

101

NMS-I-7

Dual Linear Power Channel Tilt Adjustment

QO-14

Inservice Test Procedure - Service Water Pumps

RE-131

Diesel Generator 1-1 Load Reject

71111.19

Procedures

SPS-E-1

2400 Volt and 4160 Volt Allis Chalmers and Siemens

Vacuum Circuit Breaker Auxiliary Switch Adjustments

Work Orders

00532545 01

K06A; Turbocharge S. Vertical Support has 2 Cracks

01/08/2020

00536251 01

Power Range Excore Drawers / NMS-l-10

01/21/2020

00536591 01

NI-8; Replacement of Linear Amplifier Cards

01/21/2020

2907186

MO-7A-1X - D/G 1-1 Emergency Diesel Generator Fuel Oil

Trans Test

2/05/2020

539805 05

RV-2006, Valve Replacement PMT

03/11/2020

539805 11

PMT: Ops, Charging and Letdown System Checks

03/11/2020

E-605

Connection Diagram 2400V SWGR #1C Unit #104

WO 536382

P-7B; Studs on Packing Gland Follower are Difficult to Move

01/15/2020

71111.22

Corrective Action

Documents

CR-PLP-2020-

00191

The 5% and 10% Deviation Alarm Lights on the NI-7 Power

Range Drawer were not Illuminating During Calibration of the

NI-5 Power Range Drawer

01/21/2020

CR-PLP-2020-

00192

Power Range Encore Drawers / NMS-I-7 Upper and Lower

Meter Readings Out of Tolerance

01/21/2020

CR-PLP-2020-

221

NI-2/4A Source Range Found Out-Of-Tolerance During

Right Channel Instrumentation Calibration

01/23/2020

CR-PLP-2020-

240

The DWO-1PCS Unidentified Leak Rate Values Require

Entry to Action Level 2 per Admin 4.19

01/25/2020

CR-PLP-2020-

261

ESSO-1 Containment Spray Header Fill Required due to as

Left and as Found Pressures on PI-3002 During

Replacement of Pressure Gauges

01/28/2020

CR-PLP-2020-

264

ESSO-1 Containment Spray Header Fill Required due to as

Left and as Found Pressures on PI-3002 During

Replacement of Pressure Gauges

01/28/2020

CR-PLP-2020-

00373

During Performance of MO-7A-1, FI-0890, Diesel Generator

1-1 Service Water Flow was Reading 710gpm

2/06/2020

CR-PLP-2020-

00405

Results from Independent Lab Analysis of Diesel Fuel Oil

Delivery Received on 01/21/2020 List an UNSAT Result for

Heat Content of 19343 BTU/lb

2/07/2020

Procedures

4.10

PCS Leak Rate Monitoring Program

4.19

PCS Leak Rate Monitoring Program

DWO-1

Operator's Daily/Weekly Items Modes 1, 2, 3, and 4

109

QO-1

Safety Injection System

03/11/2020

QO-14

Inservice Test Procedure - Service Water Pumps

QO-16

Inservice Test Procedure - Containment Spray Pumps

QO-21

Inservice Test Proceudre - Auxiliary Feedwater Pumps

SOP-4

Containment Spray System

Work Orders

2905576

QO-21C, Auxiliary Feedwater System Valve Inservice Test

01/30/2020

2906177 01

QO-16B - 1st Procedure - Containment Spray Pump P-54B

2/10/2020

71114.06

Procedures

SOE-3

Entergy Palisades Nuclear Plant February 19, 2020

Emergency Planning Drill Scenario Narrative

71151

Corrective Action

Documents

CR-PLP-2020-

00724

The Monthly Performance Indicator (PI) for Maintenance

Execution Index Changed from Green to Red for the Month

of February 2020

03/04/2020

Miscellaneous

MSPI Derivation

Documents

MSPI Derivation Documents for January 1, 2019 through

December 31, 2019

01/01/2019 -

2/31/2019

Procedures

EN-FAP-OM-005

Nuclear Performance Indicator Program

09/01/2019

EN-LI-114

Regulatory Performance Indicator Process

08/28/2019

71152

Corrective Action

Documents

CR-PLP-2020-

00403

Pressure Control Valves for T-57 Vacuum Degasifier Tank

are not Controlling Pressure at their Designed 22.5 psig and

23.5 psig

2/07/2020

CR-PLP-2020-

00409

The DWO-1 PCS Unidentified Leak Rate Exceeded Action

Level 3

2/09/2020

CR-PLP-2020-

00414

Reach Rods for MV-CRW105, Vacuum Degasifier Tank T-57

Inlet and MV-CRW106, Vacuum Degasifier Tank T-57

Bypass Appeared Closed when the Associated Valves were

not Fully Closed

2/10/2020

Miscellaneous

January 2020 3-Hour UNID Leak Rate Averaged vs. RIA-

1817

Primary System Drain TAnk T-74 - Cycle 27

January 2020 3-Hour UNID Leak Rate Averaged vs Sump

Fill Rate (60 Min Sample)

Procedures

EN-MA-125

Troubleshooting Control of Maintenance Activities

EN-MA-125-

Troubleshooting Control Form - PCS Leakage Assessment

Determination

01/30/2020