ML18065B216

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Insp Rept 50-255/98-02 on 980128-0313.Violation Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML18065B216
Person / Time
Site: Palisades Entergy icon.png
Issue date: 04/16/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML18065B214 List:
References
50-255-98-02, 50-255-98-2, NUDOCS 9804270158
Download: ML18065B216 (24)


See also: IR 05000255/1998002

Text

' -

U.S. NUCLEAR REGULATORY COMMISSION

Docket No:

License No:

Report No:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved by:

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9804270158 980416

PDR

ADOCK 05000255

G

PDR

REGION Ill

50-255

DPR-20

50-255/98002 (DR P)

Consumers Power Company

212 West Michigan Avenue

Jackson, Ml 49201

Palisades Nuclear Generating Plant

27780 Blue Star Memorial Highway

Covert, Ml 49043-9530

January 28 through March 13, 1998

J. Lennartz, Senior Resident Inspector

P. Prescott, Resident Inspector

Bruce L. Burgess, Chief

Reactor Projects Branch 6

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  • '

EXECUTIVE SUMMARY

Palisades Nuclear Generating Plant

NRC Inspection Report No. 50-255/98002

This inspection reviewed aspects of licensee operations, maintenance, engineering, and plant

support. The report covers a seven-week period of resident inspection.

Operations

Conservative decision making was noted by the inspectors during plant startup and

subsequent power escalation following emergent equipment problems. Plant response to

emergent issues was prompt and appropriate actions were implemented (Section 01.2).

The failure to properly secure a watertight door in accordance with procedural

requirements was a violation. Also, the inspectors identified several weaknesses in the

initial evaluation of.watertight door Number 59. The primary concern was a lack of safety

focus associated with the engineering department's review of the* undogged door. The

re-review and proposed corrective actions were more thorough (Section 02.1 ).

The inspectors noted that previously identified procedural weaknesses in the cold

weather checklist still existed. More significantly, the inspectors noted a large backlog of

outstanding procedure change requests. The inspectors were concerned that the long

delay of incorporating procedure ch~nges would have a negative impact in that licensee

personnel would be reluctant to submit additional needed procedure change requests.

Licensee management promptly allocated more personnel to the procedures group

(Section 03.1).

The licensee identified a condition outside the design basis involving inadequate

procedural guidance to ensure that high pressure air is restored during a loss of coolant

accident concurrent with a loss of power to the high pressure air compressors. Prompt

appropriate corrective actions were taken. This was considered a non-cited violation.

(Section 03.2).

The crew used procedures appropriately and completed the mitigative actions for the *

inadvertent containment high radiation in a timely manner. Crew communications, at

times, were weak (Section 04.3).

An independent team completed an audit in the area of operations. Overall, the audit

team concluded that the operations department at Palisades was functioning effectively.

The team reviewed individual procedure weaknesses and concluded they were minor.

However, the number of outstanding procedure changes was a concern. The audit

team's observations regarding procedures validated the inspectors concerns in this area

(Section 07.1)

2

Maintenance

Overall, good procedure adherence and maintenance work practices were noted ..

However, examples of weaknesses in post maintenance testing continued

(Section M1 .1 ).

Problems with control rod drive contactors continue. However, the problem associated

with Control Rod Drive 35 was caused by an error in reassembly of the contactor after

cleaning and inspection. Post maintenance testing for CRD 35 was considered

appropriate (Section M4.1).

Engineering

The redundant capability of the instrument air system was good. However, reliability of

the compressors appeared to be a problem due to service water silting problems, which

had not been addressed by the licensee (Section E2.1).

The licensee's review and root cause analysis of the circumstances surrounding the

inadvertent containment high radiation event were rigorous. This resulted in identification

of a condition outside design basis regarding the containment radiation monitoring

system. The proposed corrective actions were considered thorough. This was

considered a non-cited violation. (Section E7).

Plant Support

The inspectors identified a common misunderstanding among licens~e personnel for the

posted radiological requirements applicable to 2400 volt electrical Bus 1 C. Prompt and

thorough corrective actions were taken (Section R8.1 )~

  • ~,

Emergency Planning personnel effectively used an emergency drill to accomplish stated

objectives and to conduct training. The problems associated with an untimely response

of a search and rescue team identified last year was not evident during this drill

(Section PS) .

3

Report Details

Summary of Plant Status

The plant was at full power at the start of the inspection period. The plant was shutdown from

February 6 through 8, 1998, for a scheduled outage to refill the P-SOC primary coolant pump

motor oil reservoir and to inspect the pump for oil leakage. Operators completed the reactor

startup on February 8, 1998, and the generator was synchronized to the grid on February 9,

1998. The power escalation was put on hold at 22 percent power on February 10, 1998, due to

noted problems with the thermal margin monitors. Operations resumed the power escalation on

February 11, 1998, and the plant was at essentially full power on February 12, 1998.

I. Operations

01

Conduct of Operations

01.1

General Comments {71707)

The inspedors conducted frequent reviews of ongoing plant operations. The inspectors

considered that the conduct of operations was generally good; specific events and

noteworthy observations are detailed below.

01.2

Plant Maneuvering for Planned Outage

a.

Inspection Scope (71707)

The inspectors observed selected activities during a planned out~ge on February 6-8,

1998, including plant shutdown and startup. The inspectors also observed various

activities during the power escalation.

b.

Observations and Findings

The licensee determined, based on trending data, that a slight pre-existing oil leak on

Primary Coolant Pump (PCP) P-SOC would have resulted in a motor oil reservoir low level

prior to the start of the 1998 refueling outage scheduled in late April 1998. Therefore, a

short outage was scheduled to add oil to the PCP P-SOC motor oil reservoir. Observation

of PCP SOC during a containment entry did not identify new oil leaks and it was noted that

the leakage from existing oil leaks were contained within the pump's oil collection system.

Control rod drive (CRD) problems emerged while the plant was in hot standby during the

approach to criticality on February 8, 1998, following the outage. The plant was placed in

hot shutdown to investigate and conduct CRD repairs. Licensee management was

contacted and immediately responded to the plant. A management meeting was held to

discuss the circumstances surrounding the CRD problems. The discussions included

potential procedural adherence and maintenance practice deficiencies. No procedural--

adherence problems were noted; however, a deficiency regarding maintenance practices

(discussed further in Section M.4, "Maintenance Staff Knowledge and Performance," of

this report.) was identified. The plant startup was successfully completed later that same

day following the CRD maintenance.

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C.

During the power escalation on February 10, 1998, with reactor power at approximately

22 percent, problems with the Thermal Margin Monitor (TMM) emerged which potentially

affected equipment operability. The TMMs are part of the excore power distribution

monitoring system and provide the Thermal Margin/Low Pressure (TM/LP) reactor trip

signal to the reactor protection system as well as nuclear flux offset alarms. Operations

and plant management conservatively stopped the power escalation for approximately

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> due to the TMMs' questionable operability. An investigation revealed that the

TMMs were always operable. An escalation to full power was successfully accomplished

following the determination that the TMM's were operable.

Conclusions

Plant managements' decisions regarding the plant startup and subsequent power

escalation following emergent equipment problems were conservative. Management

response to emergent issues was prompt and appropriate actions were directed.

02

Operational Status of Facilities and Equipment

02.1

Safeguards Watertight Door Issue

a.

Inspection Scope (71707 and 37551)

The inspectors reviewed the investigation conducted by plant personnel into the

circumstances surrounding watertight door Number 59. This door is located between the

east and west safeguards rooms and was found undogged. The Final Safety Analysis

Report and design basis document (DBD) - 7.08, "Plant Protection Against Flooding,"

were reviewed. The inspectors also observed a management review board meeting on

this issue.

b.

Observations and Findings

On January 13, 1998, a maintenance worker found the watertight door between east and

west safeguards undogged. There was no one present, other than the maintenance

worker, in either room at the time. The licensee's investigation could not determine the

individual responsible for leaving the door undogged. The sign on the door delineating

the watertight door requirements was worn to the extent that the wording was not

discernable.

Administrative Procedure (AP) 4.02, "Control of Equipment," required that When the

watertight door was not in use then all dogs are engaged or, if someone is in the room,

only one dog is engaged. Failure to properly secure watertight door Number 59 in

accordance with AP 4.02 requirements was considered a violation of 10 CFR Part 50,

Appendix 8, Criterion V (50-255/98002-01 ).

The licensee initiated a Level II condition report and assigned a condition review team

leader (CRTL). The CRTL was responsible to ensure that the condition report was

investigated and analyzed to determine root cause(s) and that appropriate corrective

actions to prevent recurrence were identified.

5

The inspectors identified several weaknesses in the licensee's initial review. The internal

flooding analysis documented in DBD - 7.08 takes credit for operator action within

10 minutes to mitigate flooding caused by line ruptures and relies on remote detection by

operators in response to sump alarms in the control room. *However, the inspectors

noted that the alarm and response procedure (ARP) - 8 for an east or west safeguards

room sump high alarm was deficient in that Operator action was limited to verification of

sump pump operation indication in the control room. There was no requirement to have

an auxiliary operator inspect the cause for the alarm or the condition of the flooding in

either room. DBD - 7.08 also took credit for hourly fire tours by security as a means of

flood detection. However, the inspectors determined that hourly fire tours were not

occurring. The inspectors also noted that the flood door at one time was alarmed to

security's secondary alarm station by a micro-switch that actuated the alarm when the

door was opened. The inspectors were initially told by engineering that this was for a

high radiation alarm. The inspectors reviewed the high radiation alarm schematics and

found that the licensee's assumption was incorrect.

The inspectors noted that the micro-switch was referenced in security schematics. The

technician responsible for maintaining security equipment recalled during discussions

with the inspectors that the door was alarmed for watertight purposes. Included in

DBD - 7.08 was "NRC Guidelines for Protection from Flooding of Equipment Important to

Safety" which indicated that an alarm was a method to control watertight doors. This was

included as a reference to Safety Evaluation Plant (SEP) Topic V1-7.D. However,

Palisades was built prior to issuance ofthe SEP and was therefore not committed to its

requirements. The inspectors questioned why this would be included in the DBD.

However, neither the inspectors nor licensee personnel could find any documented

reference as to when and why. the micro-switch was disconnected.

The inspectors were concerned that the licensee's initial review did not focus on the

safety implications of the door being left open. The licensee's determination was that

flooding concurrent with the need for emergency core cooling systems to mitigate an

accident was not a valid assumption. However, the plant would find it difficult to ensure

safe plant operation after a flooding event that involved both trains of emergency core

cooling. The licensee conducted a second review of watertight door Number 59 following

discussions with the inspectors. A proposed corrective action from the second review

was to perform an engineering evaluation regarding a door 59 alarm because of the

potential for losing both trains of emergency core cooling systems due to flooding.

c.

Conclusions

The inspectors identified several weaknesses in the licensee's initial evaluation regarding

improper dogging of watertight door Number 59. The main concern was the licensee's

lack of safety focus during their review. The inspectors found the second review and the

proposed corrective actions more thorough.

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03

Operations Procedures and Documentation

03.1

Palisades' Cold Weather Preparations

a.

Inspection Scope (71714)

The inspectors reviewed the licensee's cold weather protective measures program to

ensure that safety-related systems were protected against cold weather. The inspectors

held discussions with the cold weather checklist procedure sponsor. The backlog of

procedure change requests were reviewed. Potential problem areas around the plant

were inspected for proper cold weather preparations. Past inspection report findings

were reviewed for possible recurring issues.

b.

Observations and Findings

The licensee's cold weather program consists of two operating checklists, CL-CWCL-1,

"Cold Weather Checklist," and CL-CWCL-2, "Cold Weather Checklist - Electrical." The

inspectors noted that the checklists had several pen and ink annotations to reference

various pieces of equipment that were tagged out or to note recommended changes to

the check lists. The inspectors observed this problem the previous year also. The

licensee had not developed a method for operators to track the status of various

equipment to ensure that proper cold weather preparations were implemented for

equipment returned to service. The licensee recently implemented a procedure change*

that required the checklist to be reperformed during operator rounds when the outside

temperature falls to less than 20° F. However, the inspectors identified that the operator

rounds did not note this requirement.

The inspectors reviewed the backlog of procedure change requests for the cold weather

checklist. There were several outstanding procedure change requests. One procedure

change request was over a year old and three comments from the 1996 checklists were

not yet incorporated. The inspectors expressed concern to operations management that

individuals recommending procedure change requests may get frustrated from the lack of

action taken to address concerns. The inspectors noted that the overall backlog of

procedure change requests was large. There were approximately 970 outstanding

operations procedure change requests. Further review found that a total of

1797 procedure change requests were outstanding for all departments. Recent NRC

examination of licensee events, such as the component cooling water inventory loss

(Report 50-255/97018), and the CRD Number 38 event (Report 50-255/97014), have

shown a weakness in the area of procedural adequacy. The inspectors were also aware

that recent operations attention in the area of procedural adherence may result in an

. increase in the existing backlog.

The inspectors identified that the list of open procedure change requests were not

prioritized. A review of the licensee's management report for tracking procedures did not

include, except for operations, the number of outstanding procedure change requests .

. The number reported to exist, however, was significantly less (600 vice 972) than the

backlog identified by the inspectors. Licensee management was aware that a large

backlog existed. However, the inspectors identified that the licensee was not sure how

large the backlog was and that the backlog had not been prioritized.

7

  • ,

Licensee management directed two Operation's Department personnel to independently

review and prioritize the backlog following discussions with the inspectors. The total

backlog was divided into three categories which included: (1) 221 significant requests of

which 220 were in progress; (2) 683 enhancement requests; and (3) 70 requests that

would not be required until after the upcoming refueling outage. A majority (150) of the

significant requests were related to Emergency Operating Procedures which are due to

be implemented later this year. Also, the licensee allocated additional resources to the

procedure group.

c.

Conclusions

03:2

a.

b.

The inspectors noted that previously identified procedural weaknesses in cold weather

checklists still existed. More significantly, the inspectors noted a large backlog of

outstanding procedure change requests. The inspectors were concerned that the long

delay of incorporating procedure changes would have a negative impact in that licensee

personnel would be reluctant to submit additional needed procedure change requests.

Licensee management promptly allocated more personnel to the procedures group.

Lack of Definitive Procedural Guidance to Ensure High Pressure Air Availability

Inspection Scope (71707)

The inspectors reviewed the condition report (C-PAL-98-03.69) and the event notification

regarding the required operator actions during accident conditions for the High Pressure

(HP) Air System which were not adequately addressed in operating procedures. Also, the

inspectors reviewed the interim contingency actions and training provided to the on-shift

  • crews as well as the permanent procedure revisions.

Observations and Findings

The licensee identified, during a review of HP air system operation, that the required

operator actions to restore HP air following a loss of coolant accident (LOCA) concurrent

with loss of power to the air compressors (i.e. loss of off-site power) were not adequately

defined in operating procedures. Some operator actions, which were permitted by plant

design basis, were required to ensure HP air availability for a range of small break

LOCAs. However, the operating procedures lacked definitive guidance and therefore,

there was the potential that the operators would fail to take the actions needed to ensure

HP air availability. The time to take the required actions was dependent on the break size

which would determine when recirculation cooling had to be established. This time. could

range from one hour, for large break LOCAs, to many hours as the break size decreased.

The licensee stated that the minimum time of one hour was very conservative.

Failure to take the necessary actions could jeopardize the emergency core cooling

system (ECCS) function to supply long term recirculation core cooling following a LOCA

with a loss of off-site power event. The HP air receivers' pressure would decrease during

the event due to the HP air compressors being deenergized following the designed load - -- - -*

shed. Therefore, HP air pressure may be insufficient when needed to open the ECCS

containment sump valves to establish ECCS recirculation cooling from the.containment

sump. The licensee reported this to the NRC via a 10 CFR 50. 72, one hour non-

emergency notification on March 5, 1998, as a condition outside design basis.

8

The licensee immediately provided interim guidance and training to the operating crews

regarding the required operator actions to ensure HP air availability following a LOCA with

loss of power to the HP air compressors. Permanent procedure revisions were

completed the next day. A step was added to Alarm and Response Procedure, (ARP)-7,

Annunciator Number 18, "High Pressure Control Air Compressors Hi-Lo Pressure," to

direct the operators to refer to the Standard Operating Procedure, (SOP)-20, to restore

HP air pressure if power was lost to the compressors with a LOCA in progress. Also,

Attachment 2, "To Restore HP Air In Emergency Conditions," was added to SOP-20 to

direct the specific actions. The licensee indicated that the appropriate Emergency

Operating Procedures (EOP) would also be revised. However, no specific date for

completing the EOP revisions was set at this time. The lack of definitive procedural*

guidance to accomplish required operator actions that were permitted by the design

bases to ensure HP air availability during a LOCA concurrent with a loss of power to the

HP air compressors is a Violation of 10 CFR 50, Appendix B, Criterion Ill, "Design

Control." However, this issue was identified by the licensee and prompt appropriate

corrective actions were taken. Therefore, this was a Non-Cited Violation consistent with

Section Vll.B.1 of the Enforcement Policy (50-255/98002-02).

c.

Conclusions

The licensee took prompt corrective actions after identifying a condition outside design

basis regarding inadequate procedural guidance to ensure HP air availability during a

LOCA concurrent with a.loss of power to the HP air compressors. The interim guidance

and training provided to the operating crews was considered appropriate.

04

Operator Knowledge and Performance

04.1

Plant Shutdown For Planned Outage

a.

Inspection Scope (71707)

On February 6 .. 1998, the inspectors observed activities in the control room during the*

plant shutdown for the planned outage.

b.

Observations and Findings

The Control Room Supervisor (CRS) provided oversight of the shutdown from the control

  • panels next to the Reactor Operator (RO) vice from the CRS station in the b~ck of the

control room. The Shift Supervisor (SS) maintained oversight from the CRS station. The

inspectors observed the following regarding crew performance during the shutdown:

The CRS, at times, did not display appropriate command and control of crew

actions which was especially evident during an evolution to switch from main

feedwater to auxiliary feedwater. The Balance of Plant (BOP) operator secured

Main Feedwater and started Auxiliary .feedwater after tripping the turbine. Th_e

BOP operator then commenced feeding the steam generators at a rate that was

inconsistent with plant conditions. The large increase in feed rate resulted in an

unnecessary rise in steam generator levels and a resultant drop in primary coolant

system average temperature from approximately 533°F to 525.6°F over about a

12 minute period with the reactor critical. Primary coolant system temperature

stopped decreasing and started to increase about the same time the reactor was

9

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subcritical. Therefore, the crew fortuitously did not exceed the Technical

Specification (TS) (3.1.3.a) minimum temperature for criticality of 525°F.

However, during this evolution, the CRS displayed poor command and control by

failing to provide timely direction to the BOP operator to decrease auxiliary

feedwater flow to the steam generators.

The RO communicated all planned changes in reactivity to the CRS before

performing the manipulations. The RO demonstrated good self-checking

techniques and performed all reactivity manipulations in a deliberate manner.

The crew referenced and used appropriate plant procedures during all evolutions.

c.

Conclusions

The CRS positioned next to the RO's control panel during the plant shutdown detracted

from the CRS's ability to maintain plant oversight and contributed to some informal and

softly spoken communications. The CRS displayed poor command and control during the

evolution to switch from main feedwater to auxiliary feedwater following the manual

turbine trip. Appropriate plant procedures were referenced and used during the

shutdown.

04.2

Plant Startup

a.

Inspection Scope (71707)

On February 8, 1998, the inspectors observed activities in the control room during the

plant startup following the planned outage.

b.

Observations and Findings

A reactor startup was commenced on "A" shift (midnights}, February 8, 1998, following

the planned outage. The startup had to be aborted due to CRD 35 problems. With the

reactor in hot standby, Group Ill control rod 35 moved inward from the 4.6" to the 2.6"

withdrawn position when the RO withdrew the control rods while in the "Manual

Sequential" mode on the CRD system. Annunciator EK-09, Window 11, "Rod Position 4

inches deviation," energized at this time. All other control rods moved appropriately. The

crew implemented the alarm response procedure and attempted to withdraw only rod 35

using "Manual Individual" on the CRD system as per the procedure. Control rod 35

moved inward during this withdrawal attempt from the 2.6" to the 2.1" position and*

annunciator EK-09, Window 48, "Dropped Rod" energized .. The crew referenced the

alarm response procedure which directed them to refer to Off N.ormal Procedure

(ONP) 5.1, "Control Rod Drop." .

ONP-5.1, Step 4.1.b, directed the operators to trip the reactor if one or more control rods

dropped with the reactor in hot standby. The crew referenced control rod traces and

control rod position indication available on the plant computer and diagnosed.that control-*

rod 35 had not dropped. Additionally, the crew determined that a control rod at the

2.1" position would energize the "Dropped Rod" annunciator. Further, the crew

diagnosed that the CRD brake was deenergizing but the CRD motor was not energizing

which allowed control rod 35 to "drift" inward during the outward signal from the CRD

system. The on-shift crew consulted with operation's management in the control room.

10

Due to the diagnosed rod "drift," the crew aborted the reactor startup and manually

inserted all the control rods. The crew's diagnosis of a "drifting" rod vice a dropped rod

was validated following the manual reactor trip signal that was inserted by the operators

to place the plant in hot shutdown. Following the reactor trip signal: control rod 35's trace

and rod position indicated that the rod had moved inward from the 2.1" position to the

core bottom.

Plant startup was recommenced on "C" (evenings) shift following the maintenance

activities concerning CRD 35. (CRD 35 is further discussed in Section M.4, "Maintenance

Staff Knowledge and Performance," of this report.) The startup was completed without

any additional plant equipment problems.

Two different control room crews were observed performing the reactor startups. The

inspectors noted the following regarding the crews' performance:

c.

Conclusions

The ROs performed all reactivity manipulations in a controlled and

deliberate manner, and displayed good self-checking techniques.

The CRS positioned next to the RO detracted from crew communications

in that the RO and* CRS often spoke only to each other. Other crew

members could not hear the communications and therefore were not

always kept cognizant of ongoing activities.

Appropriate plant and reactor startup oversight was provided by both

crews. However, the two crews conducted supervisory oversight

differently. One crew had the CRS positioned next to the RO during the

startup while the other crew's CRS maintained oversight from the CRS

normal work station. The CRS positioned at the CRS's normal work

station maintained plant oversight, and control room command and control

functions. The SS provided plant oversight on the crew that had the CRS

positioned by the RO. However, the CRS maintained command and

control functions regarding directing control room activities.

The crew's diagnosis of control rod 35 "drift" was accurate and timely. The RO's

displayed good self-checking techniques during the reactivity manipulations which were

performed in a deliberate and controlled.manner. Positioning of the CRS next to the RO

during the startup detracted from the CRS's ability to maintain.control room _oversight due

to*being narrowly focused on the startup. Communications between the CRS and RO

were very softly spoken due to close proximity of the two watchstanders which could

preclude an independent crew member from questioning and correcting incorrect

information; however, the inspectors did not observe any examples of this. Also, the soft

communications detracted from the authoritative demeanor that should be displayed by

the CRS. The SS's responsibility of maintaining the broadest perspective of operational

conditions affecting the plant was impacted on the crew that had the CRS positioned next

to the RO due to being more narrowly focused on control room oversight. .

11

04.3

Inadvertent Containment High Radiation Signal

The inspectors observed the control room crew on February 17, 1998, following an

inadvertent containment high radiation signal and resultant containment isolation signal.

The crew utilized appropriate procedures to mitigate the event. Crew communications, at

times, were informal and softly spoken between individual crew members. However, the

informal communications did not preclude any required actions from being completed.

The inspectors concluded that the crew used procedures appropriately and that the

mitigation actions were timely; however, crew communications, at times, were weak.

07

Quality Assurance in Operations

07.1

Licensee Self-Assessment Activities

a.

Inspection Scope (40500)

The licensee's Nuclear Performance Assessment Department (NPAD) performed an audit

(PA-98-03) of Operations during February 16 through 27, 1998. T.he inspectors attended

the exit meeting on February 27, 1998, and reviewed the audit team findings.

b.

Observations and Findings

Audit PA-98-03 was initiated by the licensee in response to issues identified regarding the

breakdown in the conduct of operations during CRD 38 maintenance activities (Inspection

Report No. 50-255/97014(DRS)). The audit team was composed of eight individuals.

Five audit team members were not associated with the licensee's NPAD or Operations

organizations. The audit team members all had at least 20 years nuclear experience in

areas which included Quality Assurance, Operations, and work control. "Four strengths

'

were identified which included professionalism in the Operations Department and the

morning meetings' effectiveness in providing plant status and coordination amongst work

groups. One weakness, which was viewed as a "significant problem," was identified

regarding operations department's procedural content and procedure revision backlog.

(The inspectors had also identified a concern regarding operations' procedures backlog

which is discussed further in Section 03, "Operations Procedures and Documentation," of

this report.) The audit team initiated condition report C-PAL-98-0311 regarding the

significant weakness.

c.

Conclusions

. An independent team completed an audit in the area of operations. Overall, the audit

team concluded that the operations department at Palisades was functioning effectively.

The team reviewed individual procedure weaknesses and concluded they were minor.

However, the number of outstanding procedure changes was a concern. The audit

team's observations regarding procedures validated the inspectors concerns in this area

12

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II. Maintenance

M1

Conduct of Maintenance

M1 .1

Observed Activities

a.

Inspection Scope (62707 and 61726)

The inspectors observed all or portions of the following work activities:

Work Order No:

24810347

24713876

24810451

24713836

24810476

24810556

24613645

24714775

"24810717

Surveillance Activities

R0-128

Q0-1

T-384

Level control valve (CV)-6001, Steam generator blowdown

level control valve: lncapsulate and inject sealant foi valve

body hole

Low pressure safety injection Pump P-678 breaker *

152-111 : Perform preventive maintenance on breaker

Solenoid valve (SV) - 0612 Bleeder trip valve: Solenoid

valve replacement for FW heater E-3A

VOP-3198, LPSI Pump P-67A Suction valve: Preventive

maintenance on valve operator and change out incorrect

operator

Motor operated valve (MOV)-3189, LPSI Pump P-678

suction valve: Replace valve to adaptor bolting

Temperature recorder and alarm (TRA)-0150, CRD leakoff

temperature recorder: Raise alarm setpoint from 200°F to

220°F for CRD mechanism 45

Feedwater purity air system to instrument air system

crosstie modification

Control valve (CV)-3070, HPSI pump P-668 Subcooling

valve: Static VOTES test

Emergency diesel generator 1-1: Repair leaks on fuel

injection pump for cylinders 9R, SR and 9L

Emergency Diesel Generator 1-1 24-Hour Load Run

Safety Injection System

CV-3018 Differential Pressure Test

13

Ml-39

Auxiliary Feedwater Actuation System Logic Test

SOP-8

Testing of Main Turbine Valves/Protective Trips

b.

Observations and Findings

A work order package to change the alarm setpoint on TRA-0150 was reviewed. This

temperature recorder was used in the control room to monitor CRO seal leakoff

temperatures. Control rod drive mechanism (CROM) 45 seal leakoff alarm setpoint was

changed from 200° F to 220° F by a temporary modification. This change was required

due to leakage by the seal into the CROM housing which resulted in the alarm for

CROM 45 seal leakoff being energized continuously. With the alarm energized, any

further degradation of the CROM would be masked. The inspectors noted that the post

maintenance test was to only verify that the alarm cleared after the setpoint was

changed. The inspectors questioned why the new alarm setpoint was not verified as

being properly set. The instrumentation and control supervisor for the job appropriately

revised the work order's post maintenance testing following discussions with the

inspectors.

The inspectors observed performance of surveillance Ql-25, Thermal Margin Monitor

Constants Check." The inspectors also reviewed the procedure and noted a wording

disparity in section 3.4, "System Conditions." The procedure stated that the TM/LP and

variable high power (VHP) trip functions shall all be operable prior to performing this test

unless below 70 percent power per TS 3.17. Based on discussions with the licensee, the

applicable TS was 3.17.1.3.b, which stated_, "If two power range nuclear instrument

channels are inoperable, limit power to less than 70 percent power within two hours."

The power range nuclear instruments were an input to TM/LP and VHP trips. The TM/LP

and VHP trips are required below 70 percent power. The state~ent implied that TM/LP

and VHP trips did not have to be operable if below 70 percent power. The licensee

reviewed the inspectors' concern and generated a procedure change request to remove

the statement. The inspectors viewed this as a procedure enhancement, which did not

impact performance of the surveillance or operability of the trips.

The inspectors observed portions of the preventive maintenance on the low pressure

safety injection pump P-67 A and 8 suction motor operated valves. * In preparation for the

task, a mechanical maintenance technician verified bolt size for application of proper

torque values as listed in maintenance procedure MSE-E-38, "PM/EQPM of Safety

Related Limitorque Type SMB Actuators." The valve actuator to valve yoke bolts were

checked for proper torque values.. The maintenance technician identified that the bolts in

place were a smaller size for the torque specifications given. This suggested that a

higher torque value for a larger bolt may have been incorrectly applied in the past. A

subsequent engineering inspection revealed that the actual bolt material was different

than that specified in the associated drawing. Heat treated 88 bolts were required;

however, Stainless Steel 87 bolts were in place. An operability determination performed

by engineering identified that the torque requirements for a 88 bolt did not exceed the bolt

material yield strength of the 87 bolts. The stainless steel 87 bolts were subsequently * **

replaced with heat treated 88 bolts and torqued to the proper specification. The

  • inspectors noted a good questioning attitude on the part of the mechanical maintenance

technician .

14

c.

Conclusions

The inspectqrs continued to note examples of weaknesses in post maintenance testing

and procedures. A mechanical maintenance technician displayed a good questioning

attitude which resulted in identification of incorrect bolts used in the low pressure safety

injection pumps motor operated suction valves' actuator to valve yoke. The deficiencies

did not affect equipment operability.

M4

Maintenance Staff Knowledge and Performance

M4.1

Control Rod Drive (CRO) 35

a.

Inspection Scope (62707)

b.

The inspectors observed the CRD 35 rod "drift" problems experienced during the plant

startup on February 8, 1998, and reviewed Work Order 24810449 and the applicable SS

logs. Also, the inspectors discussed CRD 35 problems with plant management and

control room operators.

Observations and Findings

Maintenance troubleshooting activities identified that one of the movable contacts in* the

"up" contractor for Control Rod 35 was off center and therefore would not allow the CRD

motor to energize. This contactor had been removed during the planned outage on

February 7, 1998, to clean the contacts. However, the maintenance technician

apparently bumped the moveable contact when reinstalling the contactor. This resulted

in the contact not being aligned with the center indent on the contact assembly. With the

contact misaligned, each time the rod got an outward signal the . .contact moved further

off-center and away from its associated fixed contact. After the contact moved far

enough off-center, it could not make-up with its associated fixed contact to allow the CRD

motor to energize. Therefore, during an outward demand signal, the CRD brake would

deenergize releasing the control rod. However, the CRD motor would not energize and

with the CRD brake deenergized, the rod would slowly "drift" into the core. In response to

Control Rod 35 problems, the licensee inspected all the CRD contactors that had been

removed for cleaning during the planned outage. No similar problems were identified.

The inspectors noted that post maintenance testing (PMT) had been performed following

CRD 35 contactor cleaning which required control rod 35 to be withdrawn five inches and

then inserted. Control rod 35 moved satisfactorily during the PMT. Also, the inspectors

noted that control rod 35 had successfully moved outward a total of three separate times

before the rod "drift" was experienced during the plant startup on February 8, 1998.

c.

Conclusions

CRO contactor problems have been a recurring problem. Past CRD problems were

associated with dirty contacts; however the CRD 35 problems experienced during this

startup were directly related to human error in maintenance practices. This delayed plant

startup for approximately 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />. Post maintenance testing for CRD 35 was

considered appropriate.

15

Ill. Engineering

E2

Engineering Support of Facilities and Equipment

E2.1

Emergent Work Support

During this inspection period, a number of emergent plant equipment problems required

engineering support. System and Design Engineering groups were consulted regarding

various emergent issues which included the containment radiation monitors and CRD 35

rod "drift." The containment radiation monitors' deficiency resulted in an inadvertent

containment high radiation signal and subsequent containment isolation. The inspectors

noted that the engineering review of the containment high radiation monitor's deficiency

(as discussed in Section E7, "Quality Assurance in Engineering Activities") was very

thorough. The inspectors noted that the engineering groups responded to requests for .

support iri a timely manner.

E2.2

Instrument Air System Reliability

a.

Inspection Scope (37551 and 62707)

The inspectors reviewed condition reports, work requests, quarterly system health reports

and observed portions of recent maintenance on the instrument air system. The

inspectors also discussed recent instrument air system performance with the system

engineer.

b.

.Observations and Findings

The inspectors were concerned with several recent material condition problems noted

with the instrument air system. On November 17, 1997, instrume-nt air compressor C-2A

was found not loading and C-2C was fully loaded, maintaining the plant air load. The

loader/unloader relay was found worn. The relay was original plant equipment and no

preventive maintenance had ever been performed. The relays were replaced for both

instrument air compressors. On December 9, 1997, instrument air compressor C-2A was

again not loading. The C-2A loader/unloader valve was found rusted closed, not allowing

the compressor to load. It was noted that service water was being supplied to the

compressor jacket cooler even though the compressor was not running. Sole.noid valve

(SV)-0801 was found leaking by due to debris on the valve seat. Continuous service

water flow caused condensation to form in the C-2A compressor h~ad which contributed

to rusting of the loader/unloader valve.

In January 1998, the jacket water cooler and aftercooler were found plugged with silt

following an inspection after the control room received a high temperature alarm. The

quality of the service water has been a concern of the system engineer. The licensee

instituted a periodic and predetermined activity control (PPAC), (CAS-098 and. CAS-099),

to change out the aftercoolers periodically, rather than fix the root cause of the plugging

caused by silt. The feedwater purity air compressors, which can supply the instrument air

system on a loss of the instrument air compressors, has also had silting problems with

the coolers.

On February 5, 1998, bearings for the C:2B air compressor motor were being greased .

The maintenance technicians noted the grease in the bearings was different from the

16

.*

grease being added. It was identified that.there were three different greases with the

same stock numbers from the same vendor. The bearings were replaced and the grease

identification problem was corrected. The inspectors examined the bearings and. found

them degraded.

The inspectors have noted some improvements with the instrument air system including a

significant reduction in. system leakage. This is evidenced. by the operation of either C-2A

or C-2C, which comprise one train of instrument air. Either compressor is now capable of

carrying system load individually. Another recent improvement included the ability to

adjust the feedwater purity air Compressors C-903A, B load/unload setpoint nearer to

instrument air system pressure. Also, the feedwater purity air system cross-tie pressure

control Valve (PCV)-1221 was adjusted to maintain feedwater purity pressure coincident

to the instrument air system pressure requirements. This addressed an operations

department concern.

c.

Conclusions

The inspectors noted that .the redundancy capability for the instrument air system was

good. However, reliability of the compressors appeared to be a problem due to service

water silting problems, which have not been directly addressed by the licensee.

E7

Quality Assurance in Engineering Activities

a.

Inspection Scope (37551)

The inspectors reviewed the condition report (C-PAL-98-0252) and observed the

management review board (March 5, 1998) regarding a deficiency associated with the

containment high radiation (CHR) monitors.

b.

Observations and Findings

An inadvertent CHR signal and resultant containment isolation occurred on February.17,

1998, during maintenance on the containment radiation monitoring system. The

containment radiation monitoring system, as described in FSAR Section 7.3.3, was to

include two separate actuation channels which are activated by four independent circuits. *

The containment isolation signal is initiated by a two out of four logic system. The left

channel consisted of RIAs 1805/1807 and the right channelconsisted of RIAs 1806/1808.

Maintenance personnel had scheduled the replacement of a power supply for monitor

RIA 1808. A maintenance technician removed the fuses for RIA 1808 and placed that

circuit in a "tripped" condition as designed. This allowed a containment isolation signal to

be generated if another radiation monitor trip signal were to occur from any one of the

three energized containment radiation monitors. The maintenance technician then

removed wires from terminals one thru six to further isolate RIA 1808 to accommodate

power supply replacement. No problems were noted when wires were lifted from

terminals two through six; however, RIA 1806 tripped when the wire was lifted from

terminal one. When RIA 1806 tripped the required two out of four logic was completed

and the i_nadvertent CHR signal and resultant containment isolation signals were

generated. All equipment actuated as designed which was verified by the operating crew

using the. appropriate procedure checklist.

17

The licensee initiated a level two condition report (C-PAL-98-0252) to determine the root

cause(s) for the event. Engineering and Instrument and Control Technician's review

determined that a common ground existed between RIA 1808 and RIA 1806, wh.ich

electrically tied the two circuits together at terminal one. The common ground caused

RIA 1806 to fail in a tripped condition when the wire from terminal one was lifted. Also,

the licensee determined that a similar common ground existed with the left channel

circuits, RIA 1805 and RIA 1807. Further investigation by the licensee determined that

there was no common electrical connection between the left channel (RIA 1805/1807)

and right channel (RIAs 1806/1808) circuits. However, the common ground that existed

between the left channel circuits and the right channel circuits respectively, failed to meet

the system's design requirements of four independent circuits as described in the FSAR.

The licensee reported this to the NRC via a 10 CFR 50.72, one hour non-emergency

notification on February 8, 1998, as a condition outside design basis.

The licensee's root cause analysis determined that this deficiency was introduced during

an unauthorized design change that was made while installing these containment

radiation monitors in the mid 1980's. It appears that the licensee's last opportunity to

identify this deficient design change was in the 1989 time frame during their configuration

control project (CCP). During their review of design drawings an inconsistency was

. noted. One drawing (E-623, Sheet 1 B, Revision 7) showed the wire that was removed

during the maintenance activity during the event as being connected to terminal one while

another drawing (E-227, Sheet 3, Revision 10) showed the wire disconnected. Further

review of historical drawings identified that E-227, Revision 3, was revised during the

CCP to reflect the radiation monitoring system's as built configuration which was different

than design configuration. However, no other documentation could be located that

approved the design change. Also, no other documentation could be found regarding

actions taken after the CCP found that the drawing did not accurately reflect the as built

configuration. The licensee stated that their current modification practices by the licensee

are designed to. prevent similar problems. The management revlew board concluded

that, based on no history of recurring design problems missed by CCP activities, the high

cost of reviewing other CCP documentation for similar problems was not appropriate for

the little benefit that was expected.

A contributing factor to the event was not installing a jumper to bypass RIA 1808 during

planned maintenance. The jumper would have prevented the inadvertent CHR since

RIA 1808's input to the logic would have been removed but would not have prevented

RIA 1806 from failing in the tripped condition. Use of jumpers had been a common

practice in the past (1989/1990 time frame). Licensee discussions with operations,

engineering, and maintenance personnel during their root cause analysis could not

definitively determine why that practice had been discontinued.

Eight corrective actions were developed which included: (1) review drawings and correct

inconsistencies associated with the containment RIA's (RIA 1805/1806/1807/1808);

(2) modify containment RIAs' circuit wiring to satisfy design requirements; (3) *develop a

permanent maintenance procedure to control a temporary modification to install and

remove a jumper to bypass the containment RIAs during maintenance; (4) evaluate* other.

plant systems without an installed bypass feature (i.e. safety injection system,

recirculation actuation system, contai.nment high pressure input to containment isolation)

for the need to develop similar controls for bypassing a channel during maintenance; and

(5) determine what action is needed to ensure the maintenance planners recognize *the

need to install a bypass during maintenance. The licensee stated that the target date to

18

  • '

complete all corrective actions wa*s September 1, 1998, with one exception. The

modification to the circuit wiring to satisfy design requirements was targeted for

completion during the 1999 refueling outage.

The failure of the containment radiation monitoring system to consist of four independent

circuits as described in the FSAR is a Violation of 10 CFR Part 50, Appendix B,

Criterion Ill, "Design Control." However, this issue was identified by the licensee and

prompt appropriate corrective actions were developed. Therefore, this was a Non-Cited

Violation consistent with Section Vll.B.1 of the Enforcement Policy

(NCV No. 50-255/98002-03).

c.

Conclusions

The licensee's review and root cause analysis of the circumstances surrounding the

inadvertent CHR event were rigorous. The proposed corrective actions were considered

thorough. This deficiency would cause the radiation monitors to fail in the tripped

condition which was considered conservative. The safety consequences related to this

deficiency would be an unnecessary challenge to a safety system due to the inadvertent

signal and resultant containment isolation.

IV. Plant Support

RS

Miscellaneous RP&C Issues

R8.1

Radiological Posting On 2400 volt electrical Bus 1 C

a.

Inspection Scope (71750 and 62707)

The inspectors observed electricians performing preventive maintenance on the low

pressure safety injection pump P-67B breaker, 152-111.

b.

Observations and Findings

Breaker 152-111 is located in 2400 volt electrical Bus* 1 C. In the early 1980s, the spent

fuel pool overflowed and contaminated the floor and cubicles of 2400 Volt electrical

Bus fC. **Two signs on the outside of 2400 volt electrical Bus 1 C stated that the inside

breaker cubicles were internally contaminated. The sign directed personnel to contact

health physics if entry into the bus cubicles was necessary.

The preventive maintenance was at the point where the breaker was to be put back into

the cubicle. The lead electrician was preparing to open the cubicle door and the

inspectors questioned if health physics should be notified. The lead electrician was

unsure if health physics had surveyed the cubicle when the breaker was removed the

previous shift. Therefore, the lead electrician decided to contact health physics prior to

installing the breaker back into the cubicle. The inspectors found that when

breaker 152-111 was removed, the cubicle was surveyed, but this was not discussed in

the electricians' turnover. Discussions following this incident revealed that expectations

for radiological requirements of working inside the bus were not clearly understood. The

inspectors discussed this with licensee management .

19

Health physics management took prompt action to clarify the radiological requirements for

maintenance personnel working inside the cubicle. The individuals involved were

counseled by health physics on the radiological requirements for 2400 volt electrical Bus

1 C. Guidance was issued to all supervisors to discuss this issue with their personnel.

New placards have been made which were to be posted on the front and rear door of

each cubicle. Placards were also made to post inside the cubicles. In addition, health

physics, in discussions with engineering, have developed a plan to survey the cubicles in

the upcoming outage for possible release of th.e cubicles from the current radiological

requirements.

c.

Conclusions

The inspectors identified a common misunderstanding among licensee personnel for the

posted radiological requirements applicable to 2400 volt electrical Bus 1 C. However, the

licensee responded promptly to correct the problem. The inspectors noted that the

corrective actions taken were thorough.

PS

Staff Training and Qualification in Emergency Planning (EP)

a.

Inspection Scope (71750)

The licensee conducted an emergency plan drill on the morning of February 27, 1998.

The inspectors monitored activities in the Technical Support Center (TSC) and the

simulated Control Room. The subsequent drill critique was also observed in the TSC.

b.

Observations and Findings

Licensee Emergency Planning personnel simulated a security drill which involved a bomb

.

'

explosion in track alley, an injured contaminated individual, and no radioactive releases.

The drill was designated as "practice," had well defined objectives, and was not

considered an evaluated drill. The drill scenario was the same one that was run on a

different team of licensee emergency response personnel last year in order to determine

if corrective actions for an identified weakness (Report 50-255/97013) regarding timely

search and rescue efforts were effective.

The inspectors noted that the operators in the simulated control room referred to

appropriate emergency plan implementing procedures and that the TSC was manned in a

timely manner. The Site Emergency Director (SEO) conducted briefs regarding pl~nt and

emergency status on a regular frequency and displayed sound command and control.

Other TSC emergency response personnel provided requested information to the SEO in

a timely manner, were knowledgeable of applicable procedures, and conducted

themselves in a professional manner. A search and rescue team was dispatched and

located the contaminated injured individual in a timely manner. This allowed transfer of

the contaminated injured individual to offsite medical facilities without unnecessary delay.

Some minor problems concerning communication equipment were noted. The TSC

communications team was delayed in assuming notifications to state and county officials

due to problems associated with utilizing the TSC phone that had the same extension as

the control room phone. The phone line for communications between the control room

and offsite authorities would be busy when the TSC communications team attempted to

monitor notifications that were being made by the control room communications team .

20

This unnecessarily delayed some of the required offsite notifications to state and local

officials. However, none of the required notifications were missed. Also, the inspectors

noted that the SEO declared that the TSC was activated prior to receiving a turnover from

the Control Room. The inspectors observed the TSC post drill self-critique and noted that

the critique was thorough in identification of numerous minor problems as well as drill

positives. All deficiencies in the TSC that were noted by the inspectors were identified

during the licensee's post drill self-critique.

c.

Conclusions

EP personnel effectively used a drill to accomplish the stated objectives and to conduct

training. The problems associated with timely response of a search and rescue team

identified last year was not evident during this drill.

51

Conduct of Security and Safeguards Activities (71750)

During normal resident inspection activities, routine observations were conducted in the *

areas of security and safeguards activities using Inspection Procedure 71750. No

discrepancies were noted.

F1

Control of Fire Protection Activities (71750)

During normal resident inspection activities, routine observations were conducted in the

area of fire protection activities using Inspection Procedure 71750. No discrepancies

were noted.

X1

Exit Meeting

The inspectors presented the inspection results to members of the licensee management

at the conclusion of the inspection on March 13, 1998. No proprietary information was

identified by the licensee.

21

  • '

PARTIAL LIST OF PERSONS CONTACTED

Licensee

R. A. Fenech, Senior Vice President, Nuclear, Fossil, and Hydro Operations

T. J. Palmisano, Site Vice President - Palisades

M. P. Banks, Manager, Chemical & Radiation Services

E. Chatfield, Acting Manager, Training

P. D. Fitton, Manager, System Engineering

R. J. Gerling, Manager, Design Engineering

K. M. Haas, Director, Engineering

N. L. Haskell, Manager, Licensing

D. G. Malone, Shift Operations Supervisor

J. P. Pomeranski, Manager, Maintenance

D. W. Rogers, General Manager, Plant Operations

G. B. Szczotka, Manager, Nuclear Performance Assessment Department

  • S. Y. Wawro, Director, Maintenance and Planning

22

-~

..... '

IP 37551:

IP 61726:

IP 62707:

IP 71707:

IP 71750:

IP 71714

INSPECTION PROCEDURES USED

Onsite Engineering

Surveillance Observations

Maintenance Observation

Plant Operations

Plant Support Activities

  • Cold Weather Preparations

ITEMS OPEN

50-255/98002-01

50-255/98002-02

VIO

NCV

Failure to ensure watertight door was properly secured

Required operator actions that were permitted by plant

design bases inadequately described in plant procedures

Containment radiation monitor system design deficiency

50-255/98002-03

NCV

50-255/98002-02

NCV

50-255/98002-03

NCV

ITEMS CLOSED

Required operator actions that were permitted by plant

design bases inadequately described in plant procedures

Containment radiation monitor system design deficiency

23

- .. _:.. .. i .. _

, *-***;.-;;

.;

JIS,

  • If

I

l

A LARA

AO

AP

ARP

BOP

CCP

ccw

CFR

CHR

CL

CRD

CROM

CRS

CRTL

CV

CWCL

080

DRP

ECCS

EOP

EP

HP

IP

LOCA

LPSI

MOV

NPAD

NRC

ONP

PCP

PCV

PMT

PPAC

QO

RO

SEO

SEP

SS

TM/LP

TMM

TSC

VHP

VIO

VOTES

LIST OF ACRONYMS USED

As Low As Reasonably Achievable

Axial Offset

Administrative Procedure

Annunciator Response Procedure

Balance of Plant

Configuration Control Project

Component Cooling Water

Code of Federal Regulations

Containment High Radiation

Check List

Control Rod Drive

Control Rod Drive Mechanism

Control Room Supervisor

Condition Review Team Leader

Control Valve

Cold Weather Check List

Design Basis Document

Division of Reactor Projects

Emergency Core Cooling Systems

Emergency Operating Procedure

Emergency Planning

High Pressure

Inspection Procedure

Loss of Coolant Accident

Low Pressure Safety Injection

Motor Operated Valve

Nuclear Performance Assessment Department

Nuclear Regulatory Commission

Off Normal Procedure

Primary Coolant Pump

Pressure Control Valve

Post Maintenance Test

Periodic and Predetermined Activity Control

Quarterly Operations (procedure) *

Reactor Operator

Site Emergency Director

Safety Evaluation Plant

Shift Supervisor

Thermal Margin/Low Pressure

Thermal Margin Monitor

Technical Support Center

--- --- Variable High Power

Violation

. Valve Operations and Testing Evaluation System

24