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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217L0421999-10-21021 October 1999 Forwards Insp Rept 50-382/99-20 on 990815-0925 & Notice of Violation.Two Severity Level IV Violations of NRC Requirements Identified & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20217N2111999-10-19019 October 1999 Forwards Insp Rept 50-382/99-14 on 990913-17 & 1004-08.No Violations Noted.Licensed Operator Requalification Program, Effective,Utilized Systems Approach to Training & Showed Continued Improvements Over Previous Insp Findings ML20217L0101999-10-18018 October 1999 Provides Update of Waterford 3 Effort for Review of Ufsar. Info Listed Includes Background Mgt Expectations,Review Status & Results,Clarifications Re Review & Conclusions ML20217L0141999-10-18018 October 1999 Submits Update to NRC Staff Re Circumstances & Plans for Submitting Certification Rept on Waterford 3 Plant Specific Simulator ML20217G7051999-10-14014 October 1999 Forwards Comments on Four of NRC RO Examination Questions for Exam Administered During Week of 991004 05000382/LER-1999-014, Forwards LER 99-014-00,providing Details of Reactor Shutdown Due to Loss of RCP Controlled bleed-off Flow.Attached Commitment Identification/Voluntary Enhancement Form Identifies All Commitments Contained in Submittal1999-10-12012 October 1999 Forwards LER 99-014-00,providing Details of Reactor Shutdown Due to Loss of RCP Controlled bleed-off Flow.Attached Commitment Identification/Voluntary Enhancement Form Identifies All Commitments Contained in Submittal ML20217D5151999-10-0707 October 1999 Forwards Application for Renewal of SRO License for C Fugate License SOP-43039-3,IAW 10CFR55.57.Without Encls ML20217C6251999-10-0505 October 1999 Informs That NRC Reviewed Util Ltr & Encl Exercise Scenario Package for Waterford 3 Emergency Plan Exercise Scheduled for 991013.Based on Review,Nrc Determined That Exercise Appropriate to Meet Objectives ML20212J6921999-09-29029 September 1999 Forwards Insp Rept 50-382/99-18 on 990830-0902.One Noncited Violation Identified Re Failure to Follow Procedural Instructions to Ensure That Members on Fire Brigade Shift Were Qualified ML20216G2441999-09-27027 September 1999 Forwards Insp Rept 50-382/99-19 on 990830-0903.No Violations Noted 05000382/LER-1999-013, Forwards LER 99-013-00,providing Details of Exceeding TS Limits for RCS Cooldown Rates.All Commitments Contained in Submittal Are Identified on Encl Commitment Identification/ Voluntary Enhancement Form1999-09-23023 September 1999 Forwards LER 99-013-00,providing Details of Exceeding TS Limits for RCS Cooldown Rates.All Commitments Contained in Submittal Are Identified on Encl Commitment Identification/ Voluntary Enhancement Form IR 05000382/19993011999-09-21021 September 1999 Informs That NRC License Exam Previously Associated with NRC Insp Rept 50-382/99-301 Will Be Incorporated Into NRC Insp Rept 50-382/99-14 ML20212D8761999-09-16016 September 1999 Informs That on 990818,NRC Staff Completed Midcycle PPR of Waterford 3.During Assessment Period,Number of Personnel Errors Occurred,Which Demonstrated Lack of Attention to Detail by Plant Personnel.Historical Listing of Issues,Encl ML20212C2471999-09-16016 September 1999 Forwards Five Final Applications for RO Licenses for G Esquival,Jm Hearn,Md Lawson,Re Simpson & PI Wood.Written Exam & Operating Test to Be Administered,Is Requested. Encls Withheld ML20212C2391999-09-16016 September 1999 Requests Cancellation of SRO Licenses for Bn Coble,License SOP-43835,due to Job Assignment Location & CA Rodgers, License SOP-43537-1,due to Resignation from Company, Effective 990901 ML20212C5881999-09-14014 September 1999 Forwards Insp Rept 50-382/99-15 on 990719-23 with Continuing in Ofc Insp Until 0819.No Violations Noted ML20211Q4421999-09-0909 September 1999 Forwards Insp Rept 50-382/99-07 on 990601-11.Three Violations Being Treated as Noncited Violations ML20211P4121999-09-0707 September 1999 Requests NRC Staff Review & Approval of Integrated Nuclear Security Plan (Insp) & Integrated Security Training & Qualification Plan (Ist&Q), for Use by All Entergy Operations,Inc.Encl Withheld,Per 10CFR2.790(d) ML20211M8391999-09-0303 September 1999 Forwards Revised Epips,Including Rev 25 to EP-001-020,rev 24 to EP-001-030,rev 25 to EP-001-040,rev 30 to EP-002-100,rev 22 to EP-001-010,rev 27 to EP-002-010,rev 26 to EP-002-102 & Rev 16 to EP-002-190.Listed Proprietary Revs to Epips,Encl ML20211L3681999-09-0202 September 1999 Forwards Five Preliminary Applications for Reactor Operator Licenses for Individuals Listed,Iaw 10CFR55.31.Encls Withheld ML20211K9741999-09-0101 September 1999 Forwards Insp Rept 50-382/99-16 on 990704-0814.Two Severity Level IV Violations Identified & Being Treated as Noncited Violations,Consistent with App C of Enforcement Policy 05000382/LER-1999-011, Forwards LER 99-011-00,providing Details of Reactor Shutdown Due to Loss of Controlled bleed-off Flow.All Commitments Contained in Submittal Identified on Attached Commitment Identification/Voluntary Enhancement Form1999-08-31031 August 1999 Forwards LER 99-011-00,providing Details of Reactor Shutdown Due to Loss of Controlled bleed-off Flow.All Commitments Contained in Submittal Identified on Attached Commitment Identification/Voluntary Enhancement Form ML20211M3641999-08-30030 August 1999 Forwards Written Examination,Operating Tests & Supporting Ref Matl Identified in Attachment 2 of ES-210,in Response to NRC .Encl Withheld ML20211G5751999-08-27027 August 1999 Forwards RAI Re IPEEE Submittal.Please Provide RAI within 60 Days of Receipt of Ltr,Per Util Response to GL 88-20,suppl 4 ML20211E3281999-08-26026 August 1999 Forwards fitness-for-duty Performance Data for Period of 990101-0630,IAW 10CFR26.71(d).Ltr Does Not Contain Commitments 05000382/LER-1999-009, Forwards LER 99-009-00 Re Discovery of Condition of Noncompliance with App R Involving Inadequate Separation of Essential Cables Routed in Fire Area RAB-30 in Rab. Compensatory Measures Were Established Immediately1999-08-26026 August 1999 Forwards LER 99-009-00 Re Discovery of Condition of Noncompliance with App R Involving Inadequate Separation of Essential Cables Routed in Fire Area RAB-30 in Rab. Compensatory Measures Were Established Immediately 05000382/LER-1999-010, Forwards LER 99-010-00,providing Details of Inadequate Pumping Capacity in Dry Cooling Tower Area.All Commitments Contained in Submittal Are Identified on Attached Commitment Identification Voluntary Enhancement Form1999-08-26026 August 1999 Forwards LER 99-010-00,providing Details of Inadequate Pumping Capacity in Dry Cooling Tower Area.All Commitments Contained in Submittal Are Identified on Attached Commitment Identification Voluntary Enhancement Form ML20211F5421999-08-24024 August 1999 Forwards Proposed marked-up TS Page Xviii, Index Administrative Controls, Correcting Page Number Re TS Change Request NPF-38-220.Editorial Changes for TS Change NPF-38-221 Discussed ML20211F3561999-08-24024 August 1999 Forwards CTS Pages & TS Proposed marked-up Pages for Insertion Into TS Change Request NPF-38-207 Re Efas, Originally Submitted on 980702.Original NSHC Determination Continues to Be Applicable ML20211F4611999-08-24024 August 1999 Informs That NRC Reviewed Ltr & Encl Objectives for Waterford 3 Emergency Plan Exercise Scheduled for 991013.Exercise Objectives Appropriate to Meet Emergency Plan Requirements ML20211G1731999-08-23023 August 1999 Informs That Info Submitted in ,B&W Rept 51-1234900-00,will Be Withheld from Public Disclosure,Per 10CFR2.790 ML20211C5101999-08-19019 August 1999 Forwards Certified Copies of Liability Insurance Policy Endorsements Issued in First Half of 1999 for Each Entergy Operations,Inc Nuclear Unit,Per 10CFR140.15 ML20210T9791999-08-18018 August 1999 Discusses Which Responded to Reconsideration of Violation Denial (EA 98-022) Enforcement Action Detailed in .Concludes That Violation Occurred as Stated ML20211A9501999-08-12012 August 1999 Discusses 990720-21 Workshop Conducted in Region IV Ofc,Re Exchange of Info in Area of Use of Risk Insights in Regulatory Activities.List of Attendees,Summary of Topic & Issues,Agenda & Copies of Handouts Encl ML20210S0561999-08-12012 August 1999 Submits Voluntary Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for NRC Fys 2000 & 2001 for Waterford 3 ML20210Q6161999-08-12012 August 1999 Forwards Corrected Copy of Monthly Operating Rept for July 1999 for Waterford 3.Original Rept,Submitted with ,Contained Typos ML20217F2661999-08-12012 August 1999 Forwards Copy of 1999 Waterford 3 Biennial Exercise Package to Be Performed Using Waterford 3 CR Simulator ML20210R9231999-08-11011 August 1999 Forwards Insp Rept 50-382/99-10 on 990719-23.Violations Noted.Nrc Has Determined That One Severity Level IV Violation of NRC Requirements Occurred ML20210L1461999-08-0303 August 1999 Informs That NRC Plans to Administer Gfes of Written Operator Licensing Exam on 991006.Requests Submittal of Ltr Identifying Individuals Taking Exam,Personnel Allowed Access to Exams & Mailing Address for Exams 05000382/LER-1999-008, Forwards LER 99-008-00,re Failure to Perform Testing of ESF Filtration Units Per TS Srs.Commitments Made by Util Also Encl1999-07-29029 July 1999 Forwards LER 99-008-00,re Failure to Perform Testing of ESF Filtration Units Per TS Srs.Commitments Made by Util Also Encl ML20210H4291999-07-29029 July 1999 Forwards Response to NRC Rai,Associated with TS Change Request NPF-38-208,proposing to Replace Ref to Supplement 1 with Ref to Supplement 2 of Calculative Methods for CE Small Break LOCA Evaluation Model, in ACs Section of TSs ML20210F9451999-07-27027 July 1999 Forwards Proprietary & non-proprietary Version of Rev 29 to EPIP EP-002-100, Technical Support Ctr Activation,Operation & Deactivation. Proprietary Info Withheld,Per 10CFR2.790 ML20210D3171999-07-23023 July 1999 Submits Proposal for Final Resolution of Reracking Spent Fuel Pool at Plant,Per License Amend 144,issued by NRC in .No New Commitments Are Contained in Ltr 05000382/LER-1999-007, Forwards LER 99-007-00,providing Details of Operation Outside Tornado Missile Protection Licensing Basis for turbine-driven Emergency Feedwater Pump Exhaust Stack & Steam Supply Piping.All Commitments Identified on Attached1999-07-23023 July 1999 Forwards LER 99-007-00,providing Details of Operation Outside Tornado Missile Protection Licensing Basis for turbine-driven Emergency Feedwater Pump Exhaust Stack & Steam Supply Piping.All Commitments Identified on Attached ML20210D8701999-07-23023 July 1999 Forwards Safety Evaluation Re First 10-yr Interval Inservice Insp Plan Requests for Relief ISI-018 Through ISI-020 for Entergy Operations,Inc,Unit 3 ML20210B1521999-07-15015 July 1999 Forwards Insp Rept 50-382/99-13 on 990523-0703.Three Violations Being Treated as Noncited Violations ML20209G9771999-07-13013 July 1999 Forwards Objectives & Guidelines for Waterford 3 Emergency Preparedness Exercise Scheduled for 991013.List of Objectives cross-referenced Where Applicable to Relevant Sections of NUREG-0654 IR 05000382/19990081999-07-12012 July 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-382/99-08 Issued on 990503 ML20209E5231999-07-0909 July 1999 Informs That as Result of NRC Review of Util Responses to GL-92-01,rev 1 & Suppl 1,staff Revised Info in Reactor Vessel Integrity Database & Releasing Database as Rvid Version 2.This Closes Staff Efforts Re TAC MA0583 ML20209D4051999-07-0707 July 1999 Forwards Revised TS Pages to Replace Attachment C,Entirely in Original TS Change Request NPF-38-207,per 990519 Discussion with C Patel of Nrc.Changes to Action 20 Delete Word Requirement & Revise Word Modes to Mode 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217L0101999-10-18018 October 1999 Provides Update of Waterford 3 Effort for Review of Ufsar. Info Listed Includes Background Mgt Expectations,Review Status & Results,Clarifications Re Review & Conclusions ML20217L0141999-10-18018 October 1999 Submits Update to NRC Staff Re Circumstances & Plans for Submitting Certification Rept on Waterford 3 Plant Specific Simulator ML20217G7051999-10-14014 October 1999 Forwards Comments on Four of NRC RO Examination Questions for Exam Administered During Week of 991004 05000382/LER-1999-014, Forwards LER 99-014-00,providing Details of Reactor Shutdown Due to Loss of RCP Controlled bleed-off Flow.Attached Commitment Identification/Voluntary Enhancement Form Identifies All Commitments Contained in Submittal1999-10-12012 October 1999 Forwards LER 99-014-00,providing Details of Reactor Shutdown Due to Loss of RCP Controlled bleed-off Flow.Attached Commitment Identification/Voluntary Enhancement Form Identifies All Commitments Contained in Submittal ML20217D5151999-10-0707 October 1999 Forwards Application for Renewal of SRO License for C Fugate License SOP-43039-3,IAW 10CFR55.57.Without Encls 05000382/LER-1999-013, Forwards LER 99-013-00,providing Details of Exceeding TS Limits for RCS Cooldown Rates.All Commitments Contained in Submittal Are Identified on Encl Commitment Identification/ Voluntary Enhancement Form1999-09-23023 September 1999 Forwards LER 99-013-00,providing Details of Exceeding TS Limits for RCS Cooldown Rates.All Commitments Contained in Submittal Are Identified on Encl Commitment Identification/ Voluntary Enhancement Form ML20212C2391999-09-16016 September 1999 Requests Cancellation of SRO Licenses for Bn Coble,License SOP-43835,due to Job Assignment Location & CA Rodgers, License SOP-43537-1,due to Resignation from Company, Effective 990901 ML20212C2471999-09-16016 September 1999 Forwards Five Final Applications for RO Licenses for G Esquival,Jm Hearn,Md Lawson,Re Simpson & PI Wood.Written Exam & Operating Test to Be Administered,Is Requested. Encls Withheld ML20211P4121999-09-0707 September 1999 Requests NRC Staff Review & Approval of Integrated Nuclear Security Plan (Insp) & Integrated Security Training & Qualification Plan (Ist&Q), for Use by All Entergy Operations,Inc.Encl Withheld,Per 10CFR2.790(d) ML20211M8391999-09-0303 September 1999 Forwards Revised Epips,Including Rev 25 to EP-001-020,rev 24 to EP-001-030,rev 25 to EP-001-040,rev 30 to EP-002-100,rev 22 to EP-001-010,rev 27 to EP-002-010,rev 26 to EP-002-102 & Rev 16 to EP-002-190.Listed Proprietary Revs to Epips,Encl ML20211L3681999-09-0202 September 1999 Forwards Five Preliminary Applications for Reactor Operator Licenses for Individuals Listed,Iaw 10CFR55.31.Encls Withheld 05000382/LER-1999-011, Forwards LER 99-011-00,providing Details of Reactor Shutdown Due to Loss of Controlled bleed-off Flow.All Commitments Contained in Submittal Identified on Attached Commitment Identification/Voluntary Enhancement Form1999-08-31031 August 1999 Forwards LER 99-011-00,providing Details of Reactor Shutdown Due to Loss of Controlled bleed-off Flow.All Commitments Contained in Submittal Identified on Attached Commitment Identification/Voluntary Enhancement Form ML20211M3641999-08-30030 August 1999 Forwards Written Examination,Operating Tests & Supporting Ref Matl Identified in Attachment 2 of ES-210,in Response to NRC .Encl Withheld ML20211E3281999-08-26026 August 1999 Forwards fitness-for-duty Performance Data for Period of 990101-0630,IAW 10CFR26.71(d).Ltr Does Not Contain Commitments 05000382/LER-1999-010, Forwards LER 99-010-00,providing Details of Inadequate Pumping Capacity in Dry Cooling Tower Area.All Commitments Contained in Submittal Are Identified on Attached Commitment Identification Voluntary Enhancement Form1999-08-26026 August 1999 Forwards LER 99-010-00,providing Details of Inadequate Pumping Capacity in Dry Cooling Tower Area.All Commitments Contained in Submittal Are Identified on Attached Commitment Identification Voluntary Enhancement Form 05000382/LER-1999-009, Forwards LER 99-009-00 Re Discovery of Condition of Noncompliance with App R Involving Inadequate Separation of Essential Cables Routed in Fire Area RAB-30 in Rab. Compensatory Measures Were Established Immediately1999-08-26026 August 1999 Forwards LER 99-009-00 Re Discovery of Condition of Noncompliance with App R Involving Inadequate Separation of Essential Cables Routed in Fire Area RAB-30 in Rab. Compensatory Measures Were Established Immediately ML20211F3561999-08-24024 August 1999 Forwards CTS Pages & TS Proposed marked-up Pages for Insertion Into TS Change Request NPF-38-207 Re Efas, Originally Submitted on 980702.Original NSHC Determination Continues to Be Applicable ML20211F5421999-08-24024 August 1999 Forwards Proposed marked-up TS Page Xviii, Index Administrative Controls, Correcting Page Number Re TS Change Request NPF-38-220.Editorial Changes for TS Change NPF-38-221 Discussed ML20211C5101999-08-19019 August 1999 Forwards Certified Copies of Liability Insurance Policy Endorsements Issued in First Half of 1999 for Each Entergy Operations,Inc Nuclear Unit,Per 10CFR140.15 ML20210Q6161999-08-12012 August 1999 Forwards Corrected Copy of Monthly Operating Rept for July 1999 for Waterford 3.Original Rept,Submitted with ,Contained Typos ML20210S0561999-08-12012 August 1999 Submits Voluntary Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for NRC Fys 2000 & 2001 for Waterford 3 ML20217F2661999-08-12012 August 1999 Forwards Copy of 1999 Waterford 3 Biennial Exercise Package to Be Performed Using Waterford 3 CR Simulator 05000382/LER-1999-008, Forwards LER 99-008-00,re Failure to Perform Testing of ESF Filtration Units Per TS Srs.Commitments Made by Util Also Encl1999-07-29029 July 1999 Forwards LER 99-008-00,re Failure to Perform Testing of ESF Filtration Units Per TS Srs.Commitments Made by Util Also Encl ML20210H4291999-07-29029 July 1999 Forwards Response to NRC Rai,Associated with TS Change Request NPF-38-208,proposing to Replace Ref to Supplement 1 with Ref to Supplement 2 of Calculative Methods for CE Small Break LOCA Evaluation Model, in ACs Section of TSs ML20210F9451999-07-27027 July 1999 Forwards Proprietary & non-proprietary Version of Rev 29 to EPIP EP-002-100, Technical Support Ctr Activation,Operation & Deactivation. Proprietary Info Withheld,Per 10CFR2.790 ML20210D3171999-07-23023 July 1999 Submits Proposal for Final Resolution of Reracking Spent Fuel Pool at Plant,Per License Amend 144,issued by NRC in .No New Commitments Are Contained in Ltr 05000382/LER-1999-007, Forwards LER 99-007-00,providing Details of Operation Outside Tornado Missile Protection Licensing Basis for turbine-driven Emergency Feedwater Pump Exhaust Stack & Steam Supply Piping.All Commitments Identified on Attached1999-07-23023 July 1999 Forwards LER 99-007-00,providing Details of Operation Outside Tornado Missile Protection Licensing Basis for turbine-driven Emergency Feedwater Pump Exhaust Stack & Steam Supply Piping.All Commitments Identified on Attached ML20209G9771999-07-13013 July 1999 Forwards Objectives & Guidelines for Waterford 3 Emergency Preparedness Exercise Scheduled for 991013.List of Objectives cross-referenced Where Applicable to Relevant Sections of NUREG-0654 ML20209D4051999-07-0707 July 1999 Forwards Revised TS Pages to Replace Attachment C,Entirely in Original TS Change Request NPF-38-207,per 990519 Discussion with C Patel of Nrc.Changes to Action 20 Delete Word Requirement & Revise Word Modes to Mode ML20209B6081999-06-30030 June 1999 Submits Response to NRC GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants. Disclosure Encl 05000382/LER-1999-005, Forwards LER 99-005-00,providing Details of Discovery of Untested Electrical Contacts in safety-related Logic Circuits1999-06-24024 June 1999 Forwards LER 99-005-00,providing Details of Discovery of Untested Electrical Contacts in safety-related Logic Circuits ML20196G5731999-06-24024 June 1999 Forwards Operator Licensing Exam Outlines Associated with Exam Scheduled for Wk of 991004.Exam Development Is Being Performed in Accordance with NUREG-1021,Rev 8 ML20212J4121999-06-23023 June 1999 Responds to NRC Re Reconsideration of EA 98-022. Details Provided on Actions Util Has Taken or Plans to Take to Address NRC Concerns with Ability to Demonstrate Adequate Flow Availability to Meet Design Requirements ML20196E9371999-06-22022 June 1999 Forwards Revs Made to EP Training Procedures.Procedures NTC-217 & NTC-217 Have Been Deleted.Procedure NTP-203 Was Revised to Combine Requirement Previously Included in Procedures NRC-216 & NTC-217 ML20196A1021999-06-17017 June 1999 Provides Supplemental Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, Per 990513 Request of NRC Project Manager ML20195F3671999-06-0909 June 1999 Forwards Rev 21,Change 0 to EP-001-010, Unusual Event. Rev Reviewed in Accordance with 10CFR50.54(q) Requirements & Determined Not to Decrease Effectiveness of Emergency Plan ML20195C7801999-06-0303 June 1999 Submits Response to Violations Noted in Insp Rept 50-382/99-08.Corrective Actions:All Licensee Access Authorization Personnel Were Retrained Prior to Completion of Insp ML20195C2951999-05-28028 May 1999 Forwards Annual Evaluation of Changes & Errors Identified in Abb CE ECCS Performance Evaluation Models Used for LOCA Analyses.Results of Annual Evaluation for CY98 Detailed in Attached Rept,Based Upon Suppl 10 to Abb CE Rept ML20195C0241999-05-28028 May 1999 Notifies NRC of Operator Medical Condition for Waterford 3 Opertaor Sp Wolfe,License SOP-43723.Attached NRC Form & Memo Contain Info Concerning Condition.Without Encls ML20196L3281999-05-24024 May 1999 Informs That Entergy Is Withdrawing TS Change Request NPF-38-205 Re TS 3.3.3.7.1, Chlorine Detection Sys & TS 3.3.3.7.3, Broad Range Gas Detection Submitted on 980629 ML20206S4691999-05-17017 May 1999 Requests Waiver of Exam for SRO Licenses for an Vest & Hj Lewis,Iaw 10CFR55.47.Both Individuals Have Held Licenses at Plant within Past Two Year Period,But Licenses Expired Upon Leaving Util Employment.Encl Withheld 05000382/LER-1999-004, Forwards LER 99-004-00 Re Discovery That Response Time Testing Had Not Been Performed for ESFAS Containment Cooling Function,As Required by TS SR 4.3.2.31999-05-14014 May 1999 Forwards LER 99-004-00 Re Discovery That Response Time Testing Had Not Been Performed for ESFAS Containment Cooling Function,As Required by TS SR 4.3.2.3 ML20206N1921999-05-10010 May 1999 Provides Revised Attachment 2 for Alternative Request IWE-02,originally Submitted 990429 Re Bolt Torque or Tension Testing of Class Mc pressure-retaining Bolting as Specified in Item 8.20 of Article IWE-2500,Table IWE-2500-1 ML20206J1471999-05-0606 May 1999 Requests That Implementation Date for TS Change Request NPF-38-211 Be within 90 Days of Approval to Allow for Installation of New Monitoring Sys for Broad Range Gas Detection Sys ML20206J1721999-05-0606 May 1999 Notifies That Proposed Schedule for Plant 1999 Annual Exercise Is Wk of 991013.Exercise Objective Meeting Scheduled for 990513 at St John Baptist Parish Emergency Operations Ctr ML20206G8021999-05-0404 May 1999 Provides Revised Response to NRC Re Violations Noted in Insp Rept 50-382/99-01.Licensee Denies Violation as Stated.Change Made Is Denoted by Rev Bar & Does Not Materially Impact Original Ltr ML20206E7811999-04-29029 April 1999 Proposes Alternatives to Requirements of ASME B&PV Code Section XI,1992 Edition,1992 Addenda,As Listed.Approval of Alternative Request on or Before 990915,requested ML20205T2531999-04-22022 April 1999 Forwards LER 99-S02-00,describing Occurrence of Contract Employee Inappropriately Being Granted Unescorted Access to Plant Protected Area ML20205R2611999-04-20020 April 1999 Forwards Rev 19 to Physical Security Plan,Submitted in Accordance with 10CFR50.54(p).Plan Rev Was Approved & Implemented on 990407.Rev Withheld,Per 10CFR73.21 ML20205Q3241999-04-16016 April 1999 Submits Addl Info Re TS Change Request NPF-38-215 for Administrative Controls TS Changes.Appropriate Pages from New Entergy Common QA Program Manual Provided as Attachment to Ltr 1999-09-07
[Table view] Category:UTILITY TO NRC
MONTHYEARW3P90-1505, Forwards Proposed Operator Licensing Exam Schedule & Proposed Requalification Exam Schedule,Per Generic Ltr 90-071990-09-17017 September 1990 Forwards Proposed Operator Licensing Exam Schedule & Proposed Requalification Exam Schedule,Per Generic Ltr 90-07 W3P90-1163, Forwards Relief Requests Associated w/10-yr Inservice Insp Program Per Section 50.55a(g)(6)(i) of 10CFR501990-09-0606 September 1990 Forwards Relief Requests Associated w/10-yr Inservice Insp Program Per Section 50.55a(g)(6)(i) of 10CFR50 W3P90-1191, Responds to Violations Noted in Insp Rept 50-382/90-15. Corrective Actions:Tech Spec Surveillance Procedure PE-005-004 Will Be Revised to Ensure That Normally Closed Valves Opened & Verified to Close for Toxic Gas Signal1990-08-31031 August 1990 Responds to Violations Noted in Insp Rept 50-382/90-15. Corrective Actions:Tech Spec Surveillance Procedure PE-005-004 Will Be Revised to Ensure That Normally Closed Valves Opened & Verified to Close for Toxic Gas Signal W3P90-1194, Submits Fitness for Duty Performance Data for 6-month Period from Jan-June 19901990-08-29029 August 1990 Submits Fitness for Duty Performance Data for 6-month Period from Jan-June 1990 W3P90-1184, Responds to Violations Noted in Insp Rept 50-382/90-14. Corrective Actions:Local Leak Rate Test Activities Shall Be Administratively Controlled to Require Use of Test Method Other than Pressure Decay1990-08-20020 August 1990 Responds to Violations Noted in Insp Rept 50-382/90-14. Corrective Actions:Local Leak Rate Test Activities Shall Be Administratively Controlled to Require Use of Test Method Other than Pressure Decay W3P90-1187, Forwards Booklet Entitled, Safety Info - Plans to Help You During Emergencies, Recently Distributed to General Public1990-08-17017 August 1990 Forwards Booklet Entitled, Safety Info - Plans to Help You During Emergencies, Recently Distributed to General Public W3P90-1189, Forwards Waterford 3 Steam Electric Station Emergency Preparedness Exercise for 901024. Annual Exercise Will Be Performed Using Control Room Simulator1990-08-17017 August 1990 Forwards Waterford 3 Steam Electric Station Emergency Preparedness Exercise for 901024. Annual Exercise Will Be Performed Using Control Room Simulator W3P90-1162, Forwards Rev 4 to 10-Yr Inservice Insp Program First Interval 1985-19951990-08-16016 August 1990 Forwards Rev 4 to 10-Yr Inservice Insp Program First Interval 1985-1995 W3P90-1174, Forwards Rev to Emergency Plan & QA Program,Consisting of Chart Indicating Changes to Util Organization1990-08-0707 August 1990 Forwards Rev to Emergency Plan & QA Program,Consisting of Chart Indicating Changes to Util Organization W3P90-1177, Forwards Revised Objectives for Emergency Preparedness Exercise Scheduled for 9010241990-08-0303 August 1990 Forwards Revised Objectives for Emergency Preparedness Exercise Scheduled for 901024 W3P90-1164, Forwards Waterford Steam Electric Station Unit 3 Basemat Monitoring Program Special Rept 3. Rept Documents Continued Integrity of Basemat as Verified by Program from Time of Inception of Monitoring in 1985 Through Mar 19901990-08-0303 August 1990 Forwards Waterford Steam Electric Station Unit 3 Basemat Monitoring Program Special Rept 3. Rept Documents Continued Integrity of Basemat as Verified by Program from Time of Inception of Monitoring in 1985 Through Mar 1990 W3P90-1167, Forwards Rev 12 to Emergency Plan Implementing Instruction EP-001-001, Recognition & Classification of Emergency Conditions, Reflecting Name Change of State Agency to Louisiana Radiation Protection Div1990-07-19019 July 1990 Forwards Rev 12 to Emergency Plan Implementing Instruction EP-001-001, Recognition & Classification of Emergency Conditions, Reflecting Name Change of State Agency to Louisiana Radiation Protection Div W3P90-1148, Responds to NRC 900503 Submittal Concerning Review of Util Rev 6,Change 1 to Inservice Testing Program for Pumps & Valves1990-07-17017 July 1990 Responds to NRC 900503 Submittal Concerning Review of Util Rev 6,Change 1 to Inservice Testing Program for Pumps & Valves W3P90-1143, Advises That 900404 Request for Addl Info Re Tech Spec Change Request NPF-38-103 Will Be Provided by 900803.Change Will Extend Test Frequency of Channel Functional Tests for ESF Actuation Sys & Reactor Protection Sys Instrumentation1990-07-0606 July 1990 Advises That 900404 Request for Addl Info Re Tech Spec Change Request NPF-38-103 Will Be Provided by 900803.Change Will Extend Test Frequency of Channel Functional Tests for ESF Actuation Sys & Reactor Protection Sys Instrumentation W3P90-1379, Provides Notification That Util Has Consolidated Operation of All Nuclear Facilities,Effective 9006061990-07-0202 July 1990 Provides Notification That Util Has Consolidated Operation of All Nuclear Facilities,Effective 900606 ML20044A5541990-06-26026 June 1990 Forwards Response to Generic Ltr 90-04 Requesting Info on Status of Licensee Implementation of Generic Safety Issues Resolved W/Imposition of Requirements or Corrective Actions ML20044A5551990-06-22022 June 1990 Describes Changes Required to Emergency Plan as Result of Transfer of Operations to Entergy Operations,Inc. Administrative Changes to Plan Necessary to Distinguish Support Functions to Be Retained by Louisiana Power & Light W3P90-1365, Provides Notification of Change in Operator Status Per 10CFR50.74 Due to Entergy Corp Consolidating Operation of All Nuclear Generating Facilities,Including Plant Under Util1990-06-19019 June 1990 Provides Notification of Change in Operator Status Per 10CFR50.74 Due to Entergy Corp Consolidating Operation of All Nuclear Generating Facilities,Including Plant Under Util ML20043G3431990-06-14014 June 1990 Requests That All NRC Correspondence Re Plant Be Addressed to RP Barkhurst at Address Indicated in 900523 Ltr ML20043F5121990-06-0808 June 1990 Forwards List of Directors & Officers of Entergy Operations, Inc.Operation of All Plants Transferred to Entergy on 900606 ML20043F2621990-06-0606 June 1990 Requests Withdrawal of 900504 Request to Extend Implementation Date of Amend 60 Re Transfer of Operations to Entergy,Inc.All Necessary Regulatory Approvals Obtained & License Conditions Implemented ML20043C1861990-05-29029 May 1990 Submits Response to 900426 Comments Re Investigation Case 4-88-020.Util Issued P.O. Rev Downgrading Order of Circuit Breakers & Eliminating Nuclear Requirements ML20043E5441990-05-24024 May 1990 Forwards Public Version of Change 1 to Rev 2 to EPIP EP-002-015, Emergency Responder Activation. Release Memo Encl ML20043B3501990-05-23023 May 1990 Forwards Response to Concerns Noted in Insp Rept 50-382/90-02.Response Withheld ML20043B3781990-05-23023 May 1990 Requests Change in NRC Correspondence Distribution List, Deleting Rt Lally & Adding DC Hintz,Gw Muench & RB Mcgehee. All Ref to Util Changed to Entergy Operations,Inc.Proposed NRC Correspondence Distribution List Encl W3P90-1314, Requests NRC Concurrence That Design/Controls/Testing to Minimize Potential for Common Header Blockage Acceptable Per 900510 Meeting.Tap Alternatives for Shutdown Cooling Level Indication Sys Discussed1990-05-21021 May 1990 Requests NRC Concurrence That Design/Controls/Testing to Minimize Potential for Common Header Blockage Acceptable Per 900510 Meeting.Tap Alternatives for Shutdown Cooling Level Indication Sys Discussed ML20043B3271990-05-21021 May 1990 Forwards Justification for Continued Operation Re Taped Splice for Use in Instrument Circuits,Per 900517 Request ML20042F5251990-05-0404 May 1990 Requests Extension of 90 Days to Implement Amend 60 to License NPF-38 in Order to Provide Securities & Exchange Commission Time to Review Transfer of Licensed Activities to Entergy Operations,Inc ML20042E5501990-04-17017 April 1990 Responds to Request for Addl Info Re Feedwater Isolation Valve Bases Change Request Dtd 891006 ML20012F4551990-04-10010 April 1990 Forwards Rev 10,Change 4 to Physical Security Plan.Encl Withheld ML20012F5491990-04-0606 April 1990 Advises That Util Installed Two Addl Benchmarks for Use as Part of Basemat Surveillance Program to Increase Efficiency of Survey Readings.New Benchmarks Will Be Shown on FSAR Figure 1.2.1 as Part of Next FSAR Rev ML20012F3181990-04-0606 April 1990 Forwards Util,New Orleans Public Svc,Inc & Entergy Corp 1989 Annual Repts ML20012E8971990-03-30030 March 1990 Submits Results of Evaluation of Util 900414 Response to Station Blackout Rule (10CFR50.63).Station Mod May Be Required to Change Starting Air Sys to Accomodate Compressed Bottled Air ML20012E2551990-03-27027 March 1990 Responds to Violation Noted in Insp Rept 50-382/90-01. Corrective Actions:Qa Review of Licensed Operator Medical Exam Records Conducted & Sys Implemented to Track Types & Due Dates of Medical Exams Required for Operators ML20012E0511990-03-27027 March 1990 Forwards Rev 10,Change 3 to Physical Security Plan.Rev Withheld ML20012D5461990-03-22022 March 1990 Forwards Documentation from Nuclear Mutual Ltd,Nelia & Nuclear Electric Insurance Ltd Certifying Present Onsite Property Damage Insurance ML20012D4911990-03-21021 March 1990 Responds to NRC 900208 Ltr Re Violations Noted in Investigation Rept 4-89-002.Corrective Action:Proper Sequence of Insp Hold Point Placed in Procedure Under Change Implemented on 880425 ML20012C0691990-03-14014 March 1990 Advises That Util Intends to Address Steam Generator Overfill Concerns (USI A-47) Utilizing Individual Plant Exam Process,Per Generic Ltr 89-14 ML20012C0421990-03-12012 March 1990 Forwards Questionnaire in Response to Generic Ltr 90-01, Request for Voluntary Participation in NRC Regulatory Impact Survey. Results Not Reflective of Particular Calendar Yr ML20012B6731990-03-0707 March 1990 Responds to NRC Bulletin 88-011,Action 1.a Re Insp of Surge Line to Determine Discernible Distress or Structural Damage & Advises That Neither Surge Line Nor Affiliated Hardware Suffered Any Discernible Distress or Structural Damage ML20006F5321990-02-22022 February 1990 Forwards Payment for Order Imposing Civil Monetary Penalty in Response to Enforcement Action EA-89-069 ML20011F1401990-02-21021 February 1990 Responds to Violations Noted in Insp Rept 50-382/89-41. Corrective Action:Review of Independent Verification Requirements Re Maint Activities Performed ML20006F1731990-02-19019 February 1990 Forwards Corrected Pages 9.2-21 & 9.2-22 of Rev 3 to FSAR, Per 891214 Ltr ML20006E5781990-02-13013 February 1990 Forwards Third Refueling Inservice Insp Summary Rept for Waterford Steam Electric Station Unit 3. ML20006D0571990-02-0202 February 1990 Responds to SALP Rept for Aug 1988 - Oct 1989.Contrary to Info Contained in SALP Rept,Civil Penalty Not Assessed by State of Nv for Radioactive Matl Transport Violations.Issue Resolved W/State of Nv W/O Issuance of Civil Penalty ML20006C1631990-01-30030 January 1990 Requests Extension of Commitment Dates in Response to Violations Noted in Insp Repts 50-382/89-17 & 50-382/89-22 to 900222 & 19,respectively.Violations Covered Use of Duplex Strainers & Missing Seismic Support for Cabinet ML20006C1581990-01-29029 January 1990 Forwards Response to Generic Ltr 89-13 Re safety-related Open Svc Water Sys.Instruments in Place on Component Cooling Water Sys/Auxiliary Component Cooling Water Sys HXs Which Connect to Plant Monitor Computer ML20006C1611990-01-29029 January 1990 Responds to NRC Bulletin 89-003 Re Potential Loss of Required Shutdown Margin During Refueling Operations. Instructions for Determining Acceptable Refueling Boron Concentration Provided in Procedure RF-005-001 ML20006B4121990-01-26026 January 1990 Informs That Photographic Surveys Discontinued,Per Basemat Monitoring Program.Monitoring Program Implementing Procedure Will Be Revised to Reflect Change ML20006A7091990-01-22022 January 1990 Forwards List of Individuals That No Longer Require Reactor Operator Licenses at Plant 1990-09-06
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- [ e yl LOUISIANA 17 BARONNE STREET + P. O. BOX 60340 NEW ORLEANS, LOUISlANA 70160 * (504) 595 3100 /
P O W E F1 & L I G H T p
$EE!EsYIU -
l November 13, 1986 W3P86i2800 A4105
.- QA Mr. Robert D. Martin Regional Administrator, Region IV hh U.S. Nuclear Regulatory Conimission v 611 Ryan Plaza Drive, Suite 1000 Ng 7 } %
Arlington, TX 76011 x
Subject:
Waterford 3 SES Docket No. 50-382 License No. NPF-38 NRC Inspection Reoort 86-16
Dear Mr. Martin:
Attac_hed is the Louisiana Power & Light Company (LP&L) response to Violation Nos. 8616-02, 8616-03 and 8616-05 which were cited in the subject NRC Inspection Report.
7 If you have any questions on the responses, please contact G.E. Wuller, Onsite Licensing, at (504) 464-3499.
Very truly yours, K.W. Cook Nuclear Support & Licensing Manager KWC:KLB:ssf cc: NRC, Director, Office of I&E G.W. Knighton, NRC-NRR J.H. Uilson, NRC-NRR NRC Resident Inspectors Office B.W. Churchill W.M. Stevensen 8612040068 861113 PDR G
ADOCK 05000382 ppg /- cy 0 t
/ )
h- "AN EQUAL OPPORTUNITY EMPLOYER"
ATTACHMENT to W3P86-2800 Sheet 1 off 8 LP&L RESPONSE TO VIOLATION NOS. 8616-02, 8616-03 and 8616-05 VIOLATION NO. 8616-02 Technical Specification (TS) 6.8.1.f. requires that written procedures covering the. implementation of the fire protection program be established and' implemented. fFP-1-017, Revision 2, " Transient Combustibles and Hazardous-Materials," is a procedure that implements a portion of the fire-protection program. Sections.6.1.18 and 6.3 of FP-1-017 require that combustible liquids shall be placed in. safety cans and stored in designated cabinets when not in use.
' Contrary to the above, on August 19, 1986, six safety cans, each partially full of combustible liquid, were found unattended in areas containing
- safety-related equipment.
.This is a Severity Level IV violation.
RESPONSE TO VIOLATION (1) ~ Reason for the Violation Appendix R to 10CFR50, Section K.1 and-2 mandates a licensee.to maintain in effect administrative controls to: (1) Govern the handling and limitation of the use of ordinary combustible materials, combustible and. flammable- gases and liquids.... and (2) Prohibit the
- storage of combustibles in safety-related areas or establish designated storage areas with appropriate fire protection..:Waterford 3 complies with this requirement by way of implementation of FP-1-017, Transient Combustibles and Hazardous Materials.- Specifically, section 6.3.2 states, " Approved safety cans (not exceeding 5 gallon capacity or 2 gallon capacity for Class I liquids) shall be used.for storing.
-transporting and dispensing quantities of flammable and combustible (to include lubricating oils) liquids in buildings"... Section 6.3.3
'goes on to say,."When not in use, safety cans containing flammable'and
- combustible liquids shall be stored in an approved flammable liquids storage cabinet"...
Due to a significant oil leak on the Main Steam Isolation Valves (MSIV) it became necessary to temporarily maintain a small quantity of Fyrquel lubricating oil adjacent to the MSIV skid. Fyrquel has a flashpoint of >>455'F and is therefore classified as a Class IIIB combustible liquid per NFPA-30, Flammable and combustible liquids code. The addition of this oil in the area constitutes a minor fire hazard at best. In fact, Roof Area E has an area of 3,216 fez , with an asgumption of 86 full 5 gallon 2
cans of lube oil yielding a total of 4.65E BTU or 1.44E BTU /FT this would produce a fire duration of less than 2 minutes for total consumption by fire. Therefore, the danger of safety-related equipment was negligible.
A
o . ;, ,
ATTACHMENT to W3P86-2800 Sheet 2 of 8
.(2) Corrective Action That Has Been Taken As a conservative means of corrective action an approved flammable liquids cabinet has been placed on the +46 RAB adjacent to the MSIV area so as'to allow for the long-term storage of oil in.the area-should expeditious oil addition become necessary. In the past the rate of consumption of the oil could more accurately be described as usage rather than storage.. In which case, a safety can would be the required method or container.
(3) Corrective Action That Will Be Taken No additional action is felt necessary in that the addition of the flammable liquids cabinet will serve as extra conservatism in providing verbatim compliance with the requirements of FP-1-017.
(4) Date When Full Compliance Will Be Achieved Waterford 3 is in full compliance at the present time.
5v
. .-r '
ATTACHMENT to W3P86-2800 g Sheet 3 of 8~
u,
- VIOLATION NO. 8616-03' .
10 CFR 73.55(b)(3)(1) requires, in part . written security procedures "which detail the duties of guards, watchmen, and other individuals responsible for security..."
TheWaterfordL3 physical. security-hlan'implementstherequirementsof10 CFR 73.55(b)(3)(1).
-PS-90-101, Revision 3 " Security Department Organization, Duties and
- Responsibilities," in part, implements the Waterford.3 physical security plan by detailing the duties and. responsibilities of security personnel including the secondary alare station console operation.(SASCO) and the
- security officer ~(S0). These duties and responsibilities include monitoring equipment on the SAS console in order to fully implement the site security program.
Contrary to the above, the duties and responsibilities specified in PS-90-101, Revision 3, were not properly implemented.in that, on August 29, 1986, the NRC inspector observed that the SAS console was not being properly monitored in that publications not related to the job are being read by.the SASCO in the SAS.
This is a Severity Level IV violation.
RESPONSE TO VIOLATION
-(1) : Reason for the Violation LP&LLacknowledges that on August 29, 1986, the Secondary Alarm Station
-(SAS)' Console Operator (CO) did have unauthorized reading material on-his post, the SAS.
The Waterford 3.SES Security Force utilized a Shift Supernumary to relieve security personnel for lunch and other breaks. The supernumary is normally dispatched through the SAS to job assignments.
On August 29, 1986 the supernumary was between job assignments and went to the SAS to await further instructions. Enroute to SAS, the supernumary stopped in the mens restroom. While in the restroom, the supernumary found the sports section of the daily newspaper. He picked up the newspaper and took it with him to the SAS.
Upon arrival (approximately 0953 hours0.011 days <br />0.265 hours <br />0.00158 weeks <br />3.626165e-4 months <br />) at the SAS the supernumary started reading the newspaper. He handed part of the newspaper to the SASCO.who also read the paper. The. resident _NRC inspector observed these actions and reported same to the Shift Supervisor. The Shift Supervisor relayed this information to the Security Shift Supervisor at approximately 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br />.
(2) Corrective Action That Has Been Taken Immediately upon notification Security supervisory personnel were
' dispatched to SAS to investigate the complaint. The supervisors
c" to W3P86-2800 Sheet 4 of 8 arrived-in.the SAS at 1004 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.82022e-4 months <br />. Upon arrival in the SAS, the supervisors confirmed the NRC complaint; both the-SASCO and the supernumary had part of the newspaper in their possession. Both-officers were relieved from duty and placed on suspension pending an investigation.
Disciplinary. action.was administered, as'follows:
SASCO: Two weeks suspension-without pay.
A 90 day reduction'in pay and-grade to that of a nuclear watchperson. (At the end of the 90 day probation period, the officer will be eligible to return to Security Officer status).
-SUPERNUMARY: One week suspension without pay.
A 90 day reduction in pay and grade to that of a nuclear watchperson. Reduction suspended, and officer placed on 90 day probation.
Waterford 3 SES has a written " Security Force Disciplinary Standard".
This standard prohibits having unauthorized reading material while on duty and was in place at the time of the occurrence. Both officers had signed statements that they had read and understood the policy.
However, we reissued this disciplinary standard to contract security personnel..
.(3) Corrective Action That Will Be Taken No futher action required.
(4).-Date When Full Compliance Will Be Achieved Action was taken immediately upon notification to Security supervisory personnel.
4 8
Il' f,g ,
? ATTACHMENT to W3P86-2800 Sheet 5' of 8 -
VIOLATION NO. 8616-05 l'0CFR50,.AppendiN B,' Criterion X required, in part, that, A program for
~
inspection of' activities affecting quality shall be established and executed.by;or for the organization performing the activity to verify conformance with the'_ documented instructions, procedures, and drawings for accomplishing the. activity..."
-Contrary to thefabove. the Louisiana Power and Light Company inspection program was not adequately executed to ensure proper installation of.
- certain. components as described below
1.: The front and rear anchor welds for the hydrogen recombiner. power supply panel B were not installed as required by the installation drawing.
- 2. .One of the anchor bolt nuts for the 120V nuclear instrumenta' tion static uninterruptible power supply 3MBS panel did not have the minimum. thread engagement required by installation specifications.
~This is a Severity Level IV violation.
RESPONSE'TO~ VIOLATION - PART I
. (1) -Reason for:the Violation Nonconformance Report W3-6744 was issued on 8/19/83 by the electrical subcontractor denoting that the equipment installation checklist for the Hydrogen Recombiner Panel was not completed, and the installation could-not be reverified due to inaccessibility to the interior of the
-panels.
The reasons for.the violations are: (1) the description of the noted
. ~ deficiency.(NCR-W3-6744) was not concise as to which particular installation. checklists were n'ot completed (2) the recommended disposition provided by the electrical contractor provided no proposed fix-to the problem so as to indicate what the deficiency was and (3) the. element of interface being significantly reduced as a result of the electrical contractor destaffing; were all contributing facters that caused the mismatch between problem description and recommended resolution, for the noted NCR.
To explain the aforementioned and how this could happ'en, the following information is provided. The noted NCR was submitted by the electrical contractor to the Architect-Engineer for logging and further processing as required by program. Per procedure, adequate supporting documentation was to accompany the NCR. Since no checklists were submitted with the NCR, it appears that the NCR was
-forwarded to the Electrical Engineering Department for review and evaluation of disposition (since it was written by the electrical-subcontractor). At'the time of the evaluation, it appears that the A-E Electrical engineer understood the lack of installation ,
verification to mean that the internals of the cabinet could not be i
. verified as completed rather that the physical mounting and attachment l l
l s :. 7 -
,14 ATTACHMENT:
to W3P86-2800
. Sheet 16 of 8
'oflthe' equipment to.its foundation as indicated by the checklists.
This could.be attributed to the fact that the incomplete checklists were not-provided as.NCR attachment'so as to specifically explain the.
, ' deficiency.
P
'The?A -E Electrical engineer-who evaluated the NCR provided.
. documentation attesting.to the fact that.the internals of the cabinet had been correctly-installed as the electrical acceptance tests were.
successful. The NCR was then closed by an A-E Quality Assurance-engineer based cn1 the. documentation provided by the. electrical engineer which. supported the acceptance of the cabinet internals, electrically.
(2) Corrective Action That Has Been Taken A. Temporary Alteration Request No.86-095 was issued on 9/4/86 to correct.the hardware deficiencies associated with the B Hydrogen Recombiner and work was completed on 9/5/86.
B. Station Modification Package (SMP) 1712 was initiated after it was determined that the seismic qualification of the Power Supply Panel B was deficient. This station modification was issued to revise.the' design-drawings to accurately reflect the as built configuration of the B panel. The update of the. drawings was complete on 10/13/86.
C. NCR-W3-6744 was annotated with SMP-1712 to-show reference to the
-document which actually~provided corrective action.-
D. Nonconformance reports which were generated during the-construction phase of the project were reviewed for technical adequacy.. The scope of this review included a sampling of NCR's
~
disportitioned and/or evaluated by the electrical engineer and those closed by the QA' Engineer who both had provided input to
.NCR-V3-6744. Also NCR's submitted by the electrical contractor which showed deficiencies as a result of-missing or incomplete documentation were reviewed. 'The intent of this documentation review was to verify that no other conditions similar to this violation exists as a result of misrepresented documentation.
~There were a total of thirteen (13) NCR's dispositioned or evaluated by the Electrical engineer that were reviewed to verify the disposition or evaluation adequately addressed the nonconforming condition. In all cases, the disposition or evaluation'did adequately address problem description.
There were a total' of twenty-six (26) NCR's closed by the QA engineer that were reviewed for adequate closure. The review determined that adequate justification for closure of-the NCR's did exist.
There were also twenty-six (26) NCR's that described incomplete or missing documentation by the electrical contractor that were reviewed. Many of these NCR's were the same ones closed by the
ATTACHMENT to W3P86-2800
. Sheet.7 of 8 QA engineer who closed NCR-W3-6744. It was noticed that these NCR's contained a more clear and concise definition of the problem and an amplified recommended disposition when compared.to the NCR.that documented the Hydrogen Recombiner deficiency. In all NCR's reviewed, it-was determined that the proposed resolution did match the deficiency and the corrective action taken was adequate.
(3) Corrective Action That Will Be Taken No further' action is deemed necessary.
(4) Date When Full Compliance Will Be Achieved A. SMP-1712 was complete on 10/13/86.
B. Physical work was complete on 9/5/86 via the Temporary Alteration Request No.86-095.
C. Review of,the NCR's was completed on 10/24/86.
D. NCR-W3-6744 was referenced with SMP-1712 notation on 10/31/86.
E r
-to W3P86-2800 Sheet 8 of 8 VIOLATION NO.' 8616-05 Continued I RESPONSE TO VIOLATION - PART II.
(1): Reason for the'ViolationD
' Based on available recosds, LP&L does not believe that the circumstances in this instance are sufficient cause for LP&L to be L. Teited as having violated.10CFR50 Appendix B, Criterion X.. Although two'of the' anchor bolt nuts on SU.3. panel _3MB-S were found upon recent-inspection to have less than full thread engagement, there is documented evidence that- a general QA inspection was performed on the -
subject anchor bolts following rework of the panel's installation via
~
CIWA-837910, in accordance:with the applicable inspection procedure
- (WQC-169) . - This inspection indicated that all bolts were-tightened at the time and that the work was acceptable. The inspection report no.
15-25-1 wording was of a general nature..and did not individually.
address verification of each specific criterion of the' applicable-construction procedure (CP-697). These criteria did require that a minimum of one thread of an anchor bolt must protrude through the nut, but did not require any torquing for ASTM A307 anchor bolts. The inspection report shows-no indication of not having met the minimum thread engagement' criterion.
-(2) Corrective Action That Has Been~Taken LP&L has performed calculations to reconfirm the seismic integrity of the as-found installation of.the pane 1~. These calculations were based on a thorough inspection of the panel mounting, including measurement of. thread engagements, bolt' angles, and nut-to-base plate contact surface areas. Results of these calculations show that the seismic qualification for this panel is still valid.
-(3)..-Corrective Action That Will Be Taken No further action is deemed'necessary.
(4)JDate When Full Compliance Will Be Achieved The calculations performed to reconfirm the installation was acceptable were completed on 9/10/86.
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