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MONTHYEARML20238D0221987-12-22022 December 1987 Forwards List of Deficiencies in Util 871109 Application for Amend to License NPF-1,changing Tech Spec Section 3.9.9 Re Containment Ventilation Isolation Sys.Application Should Be Revised & Resubmitted Project stage: Other ML20147B5401988-02-25025 February 1988 Forwards Response to NRC 871222 Request for Addl Info Re Util License Change Application 159 Concerning Proposed Changes to Tech Spec 3.9.9, Containment Ventilation Isolation Sys Project stage: Request 1987-12-22
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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217E9711999-10-13013 October 1999 Submits Notification of Major Changes to Trojan Liquid Radioactive Waste Treatment Sys,Iaw PGE-1201.Detailed Description of Change Provided ML20217C8171999-10-0606 October 1999 Forwards Notice of Receipt of Availability for Comment & Meeting to Discuss License Termination Plan,Per 990805 Application ML20216F7621999-09-23023 September 1999 Forwards Corrected Response to Request 2 Contained in NRC 990920 RAI Re Application of Pacificorp for Transfer of License NPF-1.Response 2 Should Have Stated That Na General Partnership Is Partnership Formed in Nv ML20216F2871999-09-20020 September 1999 Informs NRC of Developments That Have Occurred Since 990524 Application Was Filed Re Pacificorp Transfer of License of FOL NPF-1.NRC Is Urged to Act & Approve Transaction Expeditiously by 990930.Supporting Documentation Encl ML20211Q3281999-09-0909 September 1999 Forwards Insp Rept 50-344/99-06 on 990630-0701,21 & 0408-08. No Violations Noted.Insp Conducted to Review Decommissioning Activities Underway at Trojan Site & to Accompany Shipment of Reactor Vessel to Hanford,Washington for Burial ML20211J2101999-08-30030 August 1999 Forwards Request for Addl Info Re Application for Approval of Proposed Corporate Merger of Pacificorp & Scottishpower ML20211B6611999-08-16016 August 1999 Forwards fitness-for-duty Program Performance Data Rept for Period of 990101-0630,IAW 10CFR26.71(d) ML20211B4091999-08-16016 August 1999 Forwards Environ Assessment & Finding No Significant Impact to Application for an Exemption & License Amend Dated 980129.Proposed Exemption & License Amend Would Delete Security Plan Requirements of 10CFR50.54(p) & 10CFR73.55 ML20211A7131999-08-16016 August 1999 Forwards Environ Assessment & Finding of No Significant Impact to Application for Exemption & License Amend Dtd 980827.Proposed Exemption & License Amend Would Delete EP Requirements of 10CFR50.54(q),10CFR50.47(b) & 10CFR50,app E ML20210R7691999-08-11011 August 1999 Forwards Proposed Rev 23 to PGE-8010, Trojan Nuclear QAP, in Response to NRC 990708 RAI Re Relocation of TS ACs to Qap.Revised QAP Will Be Made Effective Concurrently with Implementation of License Change Application Lca 245 ML20210H5971999-07-27027 July 1999 Forwards Notice of Consideration of Approval of Application Re Merger & Opportunity for Hearing.Notice Being Forwarded to Ofc of Fr for Publication ML20216D6611999-07-23023 July 1999 Submits Summary of Proprietary Submittals for Transtor Part 71 & Part 72 & Trojan ISFSI Applications ML20210F8601999-07-22022 July 1999 Forwards Rev 1 to PGE-1076, Trojan Reactor Vessel Package Sar. Changes to Rept Contained in Rev 1 Received NRC Approval by Ltr ML20210A6401999-07-19019 July 1999 Corrects Ref in Item 4 of Which Constitutes Rev 2 of Authorization from Wf Kane, for Trojan Reactor Vessel Package as Approved Package for Shipment Under General License,Subj to Listed Conditions ML20210B4481999-07-12012 July 1999 Forwards Rept Describing Effects of Earthquake That Occurred on 990702 Near Satsop,Wa,Iaw Trojan Nuclear Plant Defueled Sar,Section 4.1.3.1 ML20209D6231999-07-0808 July 1999 Forwards RAI Re Licensee 980827 Request for Amend That Would Delete Number of License Conditions & TS Requirements That Would Be Implemented After All Sf Has Been Removed from 10CFR50 Licensed Area.Response Requested within 30 Days ML20209C6481999-07-0606 July 1999 Forwards Rev 8 to Defueled Sar,Including Changes Since Last Submittal.Attachment Includes Brief Description of Each Change Included in Rev ML20209B7821999-07-0101 July 1999 Responds to NRC 990609 RAI Re License Change Application 244 & Accompanying Request for Exemption.Detailed Info Supports Estimation of Remaining Radioactive Matl Previously Provided by Licensee ML20212J3281999-06-15015 June 1999 Forwards Amend 22 to PGE-1012, Trojan Nuclear Plant Fire Protection Plan, IAW 10CFR50.48(f).Amend Reflects Revs Made During Decommissioning Activities & Does Not Reduce Effectiveness of Fire Protection ML20195J0111999-06-0909 June 1999 Responds to Requesting License & Exemption Re Emergency Preparedness ML20207D3861999-06-0101 June 1999 Forwards Rev 1 to PGE-1077, Trojan Nuclear Plant Reactor Vessel & Internals Removal Project Transportation Safety Plan ML20196L1251999-05-24024 May 1999 Forwards Application for Amend to License NPF-1 for Indirect Transfer of License,To Extent That Such Approval Required Solely to Reflect Change in Upstream Economic Ownership of Pacificorp ML20207A2751999-05-14014 May 1999 Informs That NRC Office of Nuclear Reactor Regulation Reorganized Effective 990328.As Part of Reorganization, Division of Licensing Project Mgt Created.Organization Chart Encl ML20206N9411999-05-11011 May 1999 Forwards Revised Epips,Including Rev 7 to EPIP 3, Response Organization Checklists & Rev 9 to EPIP 5, Emergency Preparedness Test Propgram. Changes to EPIPs 3 & 5 Ref New Owners of on-site Railroad Line,Portland & Western Railroad ML20206J8681999-05-0707 May 1999 Forwards Insp Repts 50-344/99-05 & 72-0017/99-04 on 990419-22.No Violations Noted.Insp Observed Work Activities Associated with Lifting of Reactor Vessel in Preparation for Removal & Shipment to Hanford Reservation for Burial ML20206J7931999-05-0707 May 1999 Forwards Insp Repts 50-344/99-04 & 72-0017/99-02 on 990322- 25 & 29-0408.One Violations Identified & Being Treated as non-cited Violation,Consistent with App C of Enforcement Policy ML20206H4331999-05-0505 May 1999 Forwards Amend 201 to License NPF-1 & Se.Amend Revises PDTSs by Deleting ISFSI Area,Revises Subsection 4.1.1,replaces Figure 4.1-1 with New Figure 4.1-1 & Adds New Page to Figure 4.1-1 to Reflect Access Control (ISFSI) Area ML20206N1571999-05-0404 May 1999 Forwards Util Quarterly Decommissioning Status Rept for First Quarter of 1999,IAW State of or Energy Facility Siting Council Order Approving Trojan Decommissioning Plan, ML20206E1731999-04-29029 April 1999 Informs That NRC Staff Has Performed an Acceptance Review of Trojan Nuclear Plant License Termination Plan,Submitted by ,To Determine Whether LTP Provides Adequate Info to Allow Staff to Conduct Detailed Review ML20206E0211999-04-28028 April 1999 Forwards Copy of Environ Assessment & Finding of No Significant Impact Re 970212 Application for Amend.Proposed Amend Would Revise Trojan Permanently Defueled TS to Delete ISFSI Area ML20206C9591999-04-23023 April 1999 Forwards Amend 200 to License NPF-1 & Safety Evaluation. Amend Changes License NPF-1 by Revising License Condition 2.C.(10), Loading of Fuel Into Casks in Fuel Building ML20206C9221999-04-23023 April 1999 Forwards Amend 199 to License NPF-1 & Safety Evaluation. Amend Changes License NPF-1 by Adding New License Condition Entitled, Loading of Fuel Into Casks in Fuel Building ML20205S9761999-04-21021 April 1999 Forwards Trojan Nuclear Plant,Radiological Environ Monitoring Rept for CY98. Rept Submitted in Accordance with Trojan Permanently Defueled TS 5.8.1.2 & Sections IV.B.2, IV.B.3 & Iv.C of App I to Title 10CFR50 ML20205T5471999-04-20020 April 1999 Forwards Insp Repts 50-344/99-03 & 72-0017/99-03 on 990301-04,15-18 & 22-25.No Violations Noted ML20205N9061999-04-13013 April 1999 Forwards Insp Rept 50-344/99-02 on 990329-0401.No Violations Noted.Inspectors Examined Portions of Physical Security, Access Authorization & FFD Programs ML20205P7301999-04-0808 April 1999 Forwards PGE-1009-98, Operational Ecological Monitoring Program for TNP,Jan-Dec 1998, Including All Existing non-radiological Effluents ML20205B3661999-03-25025 March 1999 Transmits Completed Application for Renewal of NPDES Permit for Trojan Nuclear Plant,Iaw License NPF-1,App B,Epp,Section 3.2 ML20204G1781999-03-18018 March 1999 Forwards Rev 4 to PGE-1063, Suppl to Applicants Environ Rept - Post Operating License Stage ML20204B7551999-03-18018 March 1999 Forwards Updated TS 5.6 Re High Radiation Area,Per Telcons with Nrc.Justification for TS Was Provided Previously with Util Ltr Dtd 990317,but Has Been Updated & Is Included as Encl 2 ML20204C5151999-03-17017 March 1999 Forwards Licensee Comments on NRC Preliminary SER & License Re Trojan Isfsi.Encl Includes Justification for Inclusion in ISFSI TS of Alternative Method to 10CFR20.1601(c) for Controlling Access to High Radiation Areas ML20207J3721999-03-10010 March 1999 Forwards License Amend Application 247 Requesting Amend to License NPF-1 to Add License Condition Denoting NRC Approval of PGE-1078, Trojan Nuclear Plant License Termination Plan, Also Encl.With Certificate of Svc ML20207L0011999-03-0808 March 1999 Transmits Tnp co-owners Annual Rept of Status of Decommissioning Funding for Tnp.Rept Is Based on Most Recent Analysis of Tnp Decommissioning Estimate & Funding Plan,Per Rev 6 to Pge, Tnp Decommissioning Plan ML20207G9691999-03-0303 March 1999 Forwards Rev 6 to PGE-1061, Trojan Nuclear Plant Decommissioning Plan. Summary of Changes,Attached.Revised Portions Denoted by Side Bars ML20207D7751999-03-0202 March 1999 Forwards Amend 21 to PGE-1012, Trojan Nuclear Plant Fire Protection Plan, Per 10CFR50.48(f).Amend Reflects Revs Made During Decommissioning Activities ML20207B0441999-02-24024 February 1999 Forwards Endorsements 139 to Nelia Policy NF-0225 & 2 to Nelia Policy NW-0602 ML20207J0701999-02-11011 February 1999 Forwards Proposed Ts,Update to ISFSI SAR & Revised Calculation,Per Application for Trojan ISFSI License ML20202G4291999-02-0202 February 1999 Forwards Rev 0 to PGE-1076, Trojan Reactor Vessel Package Sar. Approval,With Certain Conditions,For one-time Shipment of Trojan Reactor Vessel Package Granted by Commission Via Ltr ML20202G0931999-01-26026 January 1999 Submits Following Info That Will Be Needed for NRC Staff to Complete Review & Issue Trojan ISFSI License,As Result of 990121 Meeting with NRC Following Insp & Observation of ISFSI Preoperational Testing During Wk of 990118 ML20202F2551999-01-25025 January 1999 Forwards Fitness for Duty Program Performance Data Rept for July-Dec 1998 ML20202C1621999-01-21021 January 1999 Forwards Insp Repts 50-344/98-04 & 72-0017/98-01 & NOV Re Inadequate Actions Taken by Radiation Protection Technician to Ensure That Radiological Conditions Safe Prior to Removing Warning Signs for Airborne Radioactivity Area 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217E9711999-10-13013 October 1999 Submits Notification of Major Changes to Trojan Liquid Radioactive Waste Treatment Sys,Iaw PGE-1201.Detailed Description of Change Provided ML20216F7621999-09-23023 September 1999 Forwards Corrected Response to Request 2 Contained in NRC 990920 RAI Re Application of Pacificorp for Transfer of License NPF-1.Response 2 Should Have Stated That Na General Partnership Is Partnership Formed in Nv ML20216F2871999-09-20020 September 1999 Informs NRC of Developments That Have Occurred Since 990524 Application Was Filed Re Pacificorp Transfer of License of FOL NPF-1.NRC Is Urged to Act & Approve Transaction Expeditiously by 990930.Supporting Documentation Encl ML20211B6611999-08-16016 August 1999 Forwards fitness-for-duty Program Performance Data Rept for Period of 990101-0630,IAW 10CFR26.71(d) ML20210R7691999-08-11011 August 1999 Forwards Proposed Rev 23 to PGE-8010, Trojan Nuclear QAP, in Response to NRC 990708 RAI Re Relocation of TS ACs to Qap.Revised QAP Will Be Made Effective Concurrently with Implementation of License Change Application Lca 245 ML20216D6611999-07-23023 July 1999 Submits Summary of Proprietary Submittals for Transtor Part 71 & Part 72 & Trojan ISFSI Applications ML20210F8601999-07-22022 July 1999 Forwards Rev 1 to PGE-1076, Trojan Reactor Vessel Package Sar. Changes to Rept Contained in Rev 1 Received NRC Approval by Ltr ML20210B4481999-07-12012 July 1999 Forwards Rept Describing Effects of Earthquake That Occurred on 990702 Near Satsop,Wa,Iaw Trojan Nuclear Plant Defueled Sar,Section 4.1.3.1 ML20209C6481999-07-0606 July 1999 Forwards Rev 8 to Defueled Sar,Including Changes Since Last Submittal.Attachment Includes Brief Description of Each Change Included in Rev ML20209B7821999-07-0101 July 1999 Responds to NRC 990609 RAI Re License Change Application 244 & Accompanying Request for Exemption.Detailed Info Supports Estimation of Remaining Radioactive Matl Previously Provided by Licensee ML20212J3281999-06-15015 June 1999 Forwards Amend 22 to PGE-1012, Trojan Nuclear Plant Fire Protection Plan, IAW 10CFR50.48(f).Amend Reflects Revs Made During Decommissioning Activities & Does Not Reduce Effectiveness of Fire Protection ML20207D3861999-06-0101 June 1999 Forwards Rev 1 to PGE-1077, Trojan Nuclear Plant Reactor Vessel & Internals Removal Project Transportation Safety Plan ML20196L1251999-05-24024 May 1999 Forwards Application for Amend to License NPF-1 for Indirect Transfer of License,To Extent That Such Approval Required Solely to Reflect Change in Upstream Economic Ownership of Pacificorp ML20206N9411999-05-11011 May 1999 Forwards Revised Epips,Including Rev 7 to EPIP 3, Response Organization Checklists & Rev 9 to EPIP 5, Emergency Preparedness Test Propgram. Changes to EPIPs 3 & 5 Ref New Owners of on-site Railroad Line,Portland & Western Railroad ML20205S9761999-04-21021 April 1999 Forwards Trojan Nuclear Plant,Radiological Environ Monitoring Rept for CY98. Rept Submitted in Accordance with Trojan Permanently Defueled TS 5.8.1.2 & Sections IV.B.2, IV.B.3 & Iv.C of App I to Title 10CFR50 ML20205P7301999-04-0808 April 1999 Forwards PGE-1009-98, Operational Ecological Monitoring Program for TNP,Jan-Dec 1998, Including All Existing non-radiological Effluents ML20205B3661999-03-25025 March 1999 Transmits Completed Application for Renewal of NPDES Permit for Trojan Nuclear Plant,Iaw License NPF-1,App B,Epp,Section 3.2 ML20204G1781999-03-18018 March 1999 Forwards Rev 4 to PGE-1063, Suppl to Applicants Environ Rept - Post Operating License Stage ML20204B7551999-03-18018 March 1999 Forwards Updated TS 5.6 Re High Radiation Area,Per Telcons with Nrc.Justification for TS Was Provided Previously with Util Ltr Dtd 990317,but Has Been Updated & Is Included as Encl 2 ML20204C5151999-03-17017 March 1999 Forwards Licensee Comments on NRC Preliminary SER & License Re Trojan Isfsi.Encl Includes Justification for Inclusion in ISFSI TS of Alternative Method to 10CFR20.1601(c) for Controlling Access to High Radiation Areas ML20207J3721999-03-10010 March 1999 Forwards License Amend Application 247 Requesting Amend to License NPF-1 to Add License Condition Denoting NRC Approval of PGE-1078, Trojan Nuclear Plant License Termination Plan, Also Encl.With Certificate of Svc ML20207L0011999-03-0808 March 1999 Transmits Tnp co-owners Annual Rept of Status of Decommissioning Funding for Tnp.Rept Is Based on Most Recent Analysis of Tnp Decommissioning Estimate & Funding Plan,Per Rev 6 to Pge, Tnp Decommissioning Plan ML20207G9691999-03-0303 March 1999 Forwards Rev 6 to PGE-1061, Trojan Nuclear Plant Decommissioning Plan. Summary of Changes,Attached.Revised Portions Denoted by Side Bars ML20207D7751999-03-0202 March 1999 Forwards Amend 21 to PGE-1012, Trojan Nuclear Plant Fire Protection Plan, Per 10CFR50.48(f).Amend Reflects Revs Made During Decommissioning Activities ML20207B0441999-02-24024 February 1999 Forwards Endorsements 139 to Nelia Policy NF-0225 & 2 to Nelia Policy NW-0602 ML20207J0701999-02-11011 February 1999 Forwards Proposed Ts,Update to ISFSI SAR & Revised Calculation,Per Application for Trojan ISFSI License ML20202G4291999-02-0202 February 1999 Forwards Rev 0 to PGE-1076, Trojan Reactor Vessel Package Sar. Approval,With Certain Conditions,For one-time Shipment of Trojan Reactor Vessel Package Granted by Commission Via Ltr ML20202G0931999-01-26026 January 1999 Submits Following Info That Will Be Needed for NRC Staff to Complete Review & Issue Trojan ISFSI License,As Result of 990121 Meeting with NRC Following Insp & Observation of ISFSI Preoperational Testing During Wk of 990118 ML20202F2551999-01-25025 January 1999 Forwards Fitness for Duty Program Performance Data Rept for July-Dec 1998 ML20199J1661999-01-14014 January 1999 Submits Summary of ISFSI Lid Welding Demonstration to Be Held 990118-25.Dates & Days Are Tentative & Can Be Adjusted as Necesssary or as Required ML20199J0801999-01-12012 January 1999 Forwards Schedule for Trojan Nuclear Plant ISFSI pre-op Test,Per Request ML20206Q0121999-01-0808 January 1999 Forwards Rev 1 to PGE-1073 Tnp ISFSI Security Plan,As Result of 981208 Telcon with Nrc.Encl Withheld,Per 10CFR73.21 ML20206P5991999-01-0404 January 1999 Requests That Svc List for Delivery of Documents from NRC Be Updated,Per 981230 Telcon.Substitute for Listings of HR Pate & J Westvold,Submitted ML20198T1651999-01-0404 January 1999 Forwards Rev 5 to PGE-1061, Trojan Nuclear Plant Decommissioning Plan. Table 2.2-5 Is Revised to Depict Major Components Removed from Plant During 1998.Revs Are Denoted by Side Bars ML20198E3981998-12-17017 December 1998 Forwards Updated ISFSI Emergency Plan,Per 981123 & Discussion in Meeting with NRC on 981119.Description of Changes Encl ML20196E2851998-11-25025 November 1998 Forwards Final Rept of Matl Properties of Neutron Shielding Matl to Be Used in Trojan ISFSI & Test Repts That Verified Matl Properties ML20196D9831998-11-24024 November 1998 Forwards Listed ISFSI Calculation Refs,Per 981110 Telcon ML20196B2321998-11-23023 November 1998 Informs That,Per Commitments Made in 981119 Meeting with Nrc,Rev to PGE-1075 Will Be Submitted No Later than 981218 ML20195J2321998-11-17017 November 1998 Forwards Rev 7 to Trojan Nuclear Plant Defueled Sar. Attachment to Ltr Includes Brief Description of Each Change Included in Rev ML20195E4811998-11-10010 November 1998 Forwards Rev 51 to Trojan Nuclear Plant Security Plan.Rev Withheld,Per 10CFR73.21 ML20155E0331998-10-27027 October 1998 Forwards Amend 7 to PGE-1052, Quality-Related List Classification for Tnp. Amend Removes Ref to Several Clean Up Sys,Deletes Exemptions Allowed by Reg Guide 1.143 & Deletes Figures No Longer Required to Support Discussion ML20154M4151998-10-14014 October 1998 Requests That Further Review of License Change Application LCA-238 Be Suspended as Result of Progress Made in Decommissioning,Installation of Natural Gas Pipe Line ML20154A4751998-09-28028 September 1998 Forwards Amend 20 to PGE-1012, Trojan Nuclear Plant Fire Protection Plan, Reflecting Revisions to Fire Protection Program Made During Decommissioning Activities ML20153D3021998-09-21021 September 1998 Forwards Rev 0 to PGE-1077, Tnp Reactor Vessel & Internals Removal Project Transportation Safety Plan, Per Request That Util Submit Description of Measures to Be Taken to Ensure Safe Transport of Tnp Rv & Internals Package ML20151X8571998-09-10010 September 1998 Provides Rev 2 to Poge, Trojan NPP Permanently Defueled TS Bases. Changes Identified in Revised Text by Side Bars ML20151X7171998-09-10010 September 1998 Forwards Rev 3 to PGE-1063, Trojan Nuclear Power Station, Suppl to Applicant Environ Rept. Section 4.5 Revised to Delete Ref to Selected Room Coolers ML20153B0001998-09-0909 September 1998 Forwards Figures & Tables Identifying Nodes Assigned for Trojan ISFSI Transfer Station Analysis,TI-056,Rev 1 ML20237E9421998-08-27027 August 1998 Requests Exemption of Emergency Plan Requirements of 10CFR50.54(q),10CFR50.47(b) & 10CFR50,App E Following Transfer of Spent Nuclear Fuel to ISFSI ML20151W5381998-08-25025 August 1998 Forwards Rev 22 to PGE-8010, Poge Nuclear QA Program for Trojan Nuclear Plant. Rev Reflects Administrative Changes That Continue to Meet Requirements of 10CFR50,App B ML20237E1811998-08-25025 August 1998 Forwards Description of Review Methodology & Summary of Results,Including List of Identified Variations from Guidance Contained in Std Review Plan,Per NUREG-1536 1999-09-23
[Table view] Category:UTILITY TO NRC
MONTHYEARML20059L6651990-09-21021 September 1990 Forwards Application for Amend to License NPF-1,consisting of License Change Application 203,Rev 1.Rev Reduces Scope of Previous Changes Re Tech Spec Table 3.6-1, Containment Isolation Valves ML20059J9691990-09-14014 September 1990 Forwards Estimates of Facility Operator Licensing, Requalification & Generic Fundamentals Exam Requirements for FY91-94,per Generic Ltr 90-07 ML20059J9841990-09-14014 September 1990 Responds to Re Violations Noted in Insp Rept 50-344/90-21.Corrective Action:Individual Employee Terminated on Day of Event ML20059J0321990-09-0707 September 1990 Requests That Six Listed Candidates Take PWR & Generic Fundamentals Exam to Be Administered on 901010 ML20059D8031990-08-31031 August 1990 Forwards Update on Actions for NRC Bulletin 88-008, Thermal Stresses in Piping Connected to Rcs ML20059D2401990-08-30030 August 1990 Extends Commitment Date from 900831 to 901031 to Amend FSAR Per Util 900404 Response to Notice of Violation ML20059D0831990-08-30030 August 1990 Revises Response to Violations Noted in Insp Rept 50-344/90-02.License Document Change Request Correcting FSAR Discrepancy Noted in App A,Violation C Re Request for Design Change Initiated & Will Be Incorporated Into Amend 14 ML20059C1741990-08-28028 August 1990 Forwards Rev 31 to Security Plan.Rev Withheld (Ref 10CFR73.21) ML20059D3201990-08-28028 August 1990 Responds to Deficiencies Identified by FEMA During 891115 Emergency Preparedness Exercise at Plant.Corrective Actions: Procedures Revised to Prioritize Roadblocks & Clearly Define Roadblocks for 5-mile & 10-mile Locations ML20059D5601990-08-28028 August 1990 Forwards Fitness for Duty Performance Rept for 900103-0630. Overall Positive Rate for All Testing Conducted at Plant from 900103-0630 Is 0.71% ML20058M7861990-08-0303 August 1990 Forwards Monthly Operating Rept for Jul 1990.W/o Encl ML20056A1551990-07-31031 July 1990 Forwards Updated Response to Address Maint/Surveillance Area of SALP for Period from Jan 1989 - Mar 1990.Overall Plant Performance During Period Acceptable & Found to Be Directed Toward Safe Operation ML20055J3421990-07-26026 July 1990 Forwards Decommissioning Financial Assurance Certification Rept for Plant,Per 10CFR50.75.Certifies That Finanical Assurance Utilizing Methodology as Listed Will Be Available to Decommission Plant ML20055G7131990-07-20020 July 1990 Comments on Operator Licensing Exams Administered on 900717 ML20055G7141990-07-19019 July 1990 Responds to NRC Bulletin 90-001, Loss of Fill-Oil in Transmitters Mfg by Rosemount. Plant Has Four Rosemount Model 1153DD6 Differential Pressure Transmitters Installed to Associated Logics for Safety Injection ML20055F8791990-07-16016 July 1990 Forwards 1989 Annual Repts for Portland General Corp,Eugene Water & Electric Board & Pacific Power & Light Co ML20055F6911990-07-13013 July 1990 Responds to Generic Ltr 90-04, Request for Info on Status of Implementation of Generic Safety Issues Resolved W/ Imposition of Requirements or Corrective Actions ML20055F8161990-07-13013 July 1990 Advises of New Addressee for Nrc/Util Correspondence ML20055F2441990-07-12012 July 1990 Forwards Response to SALP Evaluation for Jan 1989 - Mar 1990 Re Maint/Surveillance.Util Plans to Improve Performance in Areas of Operation Through Commitment of Support from Nuclear Div Mgt & Personal Involvement of Corporate Mgt ML20055F2961990-07-0606 July 1990 Forwards Addl Info Re ATWS Mitigating Sys Actuation Circuitry ML20055E3401990-07-0606 July 1990 Forwards Application for Renewal of Plant NPDES Permit ML20055E1751990-07-0606 July 1990 Provides Update to 891130 Response to Generic Ltr 88-14, Instrument Air Supply Sys Problems Affecting Safety-Related Equipment. Rev to Maint Procedure 12-4, Valve Air Actuators, to Include Maint Insp Completed in Apr 1990 ML20055E0241990-07-0606 July 1990 Responds to NRC Re Violations Noted in Insp Rept 50-344/90-11.Corrective Actions:Generic Issues That Contributed to Violation Will Be Discussed During Mgt Meetings & Quality Insp Supervisor Counseled ML20055E0281990-07-0606 July 1990 Informs That Actions Committed to in Util Re Replacement of Breaker During 1990 Refueling Outage & Provision of Rept Documenting Replacement of Breaker, Complete,Per NRC Bulletin 88-010 ML20058K4891990-06-30030 June 1990 Discusses Reduced Min Measured RCS Flow for Plant.Encl Figure 3.2-3 & Evaluation Support Operation W/No Tech Spec Setpoint Changes ML20055D0411990-06-29029 June 1990 Discusses Design Verification Program Re Main Steam Support Structure.Extension of Completion Date for Project Justified Since Documentation,Not Mod of Main Steam Support Structure Is Reason for Delay ML20055D0441990-06-29029 June 1990 Advises That Response to Generic Ltr 90-04 Re Status of Generic Safety Issues at Facility Delayed from 900629 to 900713 ML20055D7091990-06-26026 June 1990 Forwards Steam Generator Tube Plugging Rept,Per Inservice Insp ML20055C2691990-02-20020 February 1990 Responds to NRC Re Violations Noted in Insp Rept 50-344/89-30.Corrective Actions:Administrative Order 5-8 Temporary Mods to Be Evaluated for Need to Improve Control Over Temporary Mods Issued for Both Trains of Sys ML17311A1041989-10-30030 October 1989 Advises That Commitment Date for Performance of Surveillance Moved to 891130 to Allow for Incorporation in Biennial Audit Per Rev 1 to LER 89-08.NRC Resident Inspector Informed of Change on 891013 ML20248G7631989-10-0606 October 1989 Forwards Description of Alternate Compensatory Measures Implemented During Upgrade Activities.W/O Encl ML20248G3131989-10-0303 October 1989 Forwards Response to Generic Ltr 89-04, Guidance on Developing Acceptable Inservice Testing Programs. Revised Topical Rept PGE-1048 Will Be Submitted by 891117 ML20248E2391989-09-29029 September 1989 Forwards Summary of Action Plan to Resolve Fuel Bldg Overstress Conditions ML20248D3711989-09-29029 September 1989 Forwards Rept of Util Plan for Improving Performance of Nuclear Div Staff.New Mgt Described in Plan Will Serve as Catalyst for Decisive Performance Changes ML20248G9001989-09-29029 September 1989 Forwards Rev 1 to PGE-1049, Inservice Insp Program for Second 10-Yr Interval from 860520-960519 05000344/LER-1989-007, Informs That Rev 1 to LER 89-07 Will Be Submitted by 891013, Due to Forced Outage & Difficulties1989-09-28028 September 1989 Informs That Rev 1 to LER 89-07 Will Be Submitted by 891013, Due to Forced Outage & Difficulties ML20248G1071989-09-28028 September 1989 Advises That Util Will Submit Final Closeout of NRC Bulletin 88-004, Potential Safety-Related Pump Losss, by 900115 ML20248D6161989-09-28028 September 1989 Requests 14-day Extension Until 890928 to Respond to Violations Noted in Insp Rept 50-344/89-09.Individuals Involved in Providing Input to Response Currently Assigned to Solving Problems During Current Forced Outage ML20248D4211989-09-27027 September 1989 Suppls 881004 Response to NRC Bulletin 88-008, Thermal Stresses in Piping Connected to Rcs. NDE Confirmed That No Existing Flaws Exist in Critical Piping Locations Re Thermal Stratification ML20247G9011989-09-15015 September 1989 Responds to Generic Ltr 89-06 Re SPDS Requirements,Per NUREG-0737,Suppl 1 as Clarified by NUREG-1342.Concludes That Isolators Used Were Acceptable for Interfacing SPDS W/Safety Sys,Therefore Util Does Not Intend to Make Mods to SPDS 05000344/LER-1989-012, Advises That Rev 1 to LER 89-012 Will Be Submitted by 890920 Due to Extension of 1989 Refueling Outage & Plant Trip of 8908091989-09-0808 September 1989 Advises That Rev 1 to LER 89-012 Will Be Submitted by 890920 Due to Extension of 1989 Refueling Outage & Plant Trip of 890809 ML20247B9281989-09-0808 September 1989 Responds to NRC Re Violations Noted in Insp Rept 50-344/89-12 & Forwards Review of Closeout of First 10-yr Inservice Insp Interval.Concurs That Primary Reason for Individual Problems Was Lack of Insp Contractor Activities ML20247C2801989-09-0808 September 1989 Responds to NRC Re Violations Noted in Insp Rept 50-344/89-18.Corrective Action:Reevaluation of OAR 87-29, Involving Mods to Hydrogen Gas Supply Sys Implemented as Part of 1989 Refueling Outage ML20247E9371989-09-0707 September 1989 Discusses Nuclear Div Improvement Plan,Per Recent Event Re Containment Recirculation Sump.Util Corrective Actions, Including Organizational Changes,Encl.Plant Improvement Plan Will Be Submitted by 891001 ML20247A6171989-09-0505 September 1989 Informs That Intake Structure Mod Completed as Scheduled & Security Plan Rev Will Be Submitted by 891015 ML20246M5181989-08-31031 August 1989 Forwards Update on Action Plan Developed in Response to Generic Ltr 88-14, Instrument Air Supply Sys Problems Affecting Safety-Related Equipment ML20246M5651989-08-31031 August 1989 Discusses long-term Pipe Support Design Verification Program for Plant.Evaluation of Fuel Bldg Confirmed & Quantified Code Overstresses Existing Under Seismic & Tornado Loading Conditions.Details of Action Plan Will Be Sent by 890929 ML20246M5771989-08-31031 August 1989 Forwards Status of Progress in Achieving Improvement Goals Identified in 890515 SALP Response Re Safety Assessment/ Quality Verification.Addl Resources Applied to Qualify commercial-grade Suppliers ML20246J8641989-08-28028 August 1989 Responds to NRC Re Violations Noted in Insp Rept 50-344/89-02.Corrective Actions:Util Assembled Interdepartmental Task Force in Nov 1988 to Review Incidents & Determine Root Causes ML20246H5351989-08-25025 August 1989 Informs That Rev to Topical Rept PGE-1049, Trojan Nuclear Plant Inservice Insp Program for Second 10-Yr Interval Will Be Submitted for Approval by 890929 1990-09-07
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M s Pbrtland General ElectricCoirpiny David W. Cockfield Vice President, Nuclear February 25, 1988 Trojan Nuclear Plant Docket 50-344 License NPF-1 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington DC 20555
Dear Sir:
License Change Application 159
Reference:
NRC to PGE Letter License Change Application 159 (TAC 66638),
December 22, 1987 Pursuant to the above reference, responses to questions on License Change Application (LCA) 159 are provided in Attachment 1. This LCA proposed changes to Trojan Technical Specification 3.9.9 (Containment Ventilation Isolation System) to resolve inconsistencies within the Technical Specifi-cations. The responses to the questions have been incorporated into the significant hazards consideration determination for the LCA as appropriate in Attachment 2.
Sincerely, r
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Attachments c: Mr. John B. Martin Mr. William Dixon Regional Administrator, Region V State of Oregon U.S. Nuclear Regulatory Commission Department of Energy Mr. Michael J. Sykes Mr. R. C. Earr NRC Resident Inspector Chairman of County Commissioners Trojan Nuclear Plant s
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-LCA 159 Attachment-1 1Page 1 of 3 NRC Ouestions Although the proposed change is categorized as an "Administrative'" change, -
the application fails to consider:
- 1. . the appropriateness of Technical Specification =(TS)'3.9.4 and proposed TS-3.9.9 during those Mode 6 periods when core alterations or movement of irradiated fuel within the. containment is not in progress,'yet heavy load (eg, reactor vessel head, overhead loads) activities may be in progress over the refueling cavity; ,
2.- the absence of a TS under such conditions, which would petuit such operations to be conducted without requiring containment isolation capability;
- 3. the appropriateness of TS 3.9.4 and proposed.TS 3.9.9 during Mode 6 3'
operations (not core alterations),'in light of Trojan's loose fuel particle / contamination experience, and the need for containment isolation capability; and
- 4. the inconsistency of TS 3.9.4 with respect to TS 3.9.9 vice the reverse. ,
PGs Response
- 1. An analysis of the consequences of heavy load drops in the vicinity of the reactor vessel was provided in PGE to NRC letter, "Control of Heavy Loads, NUREG-0612", January 22, 1982. The heavy loads of concern were the reactor vessel head, the core upper internals, and the missile shields.
While removing the reactor vessel head, the potential exists to drop the head back onto the vessel. This drop could occur through air or a combination of air and water and could occur from various heights.
To evaluate the separate cases, an analysis was performed using con-ventional energy balance methods similar to those described in Westinghouse Topical Report WCAP-9198 "Reactor Vessel Head Drop Analyses". These Plant-specific analyses determined the consequences to the reactor vessel and its sv.pports, and verified the conclusions
- reached in the Westinghouse report that "there will be no consequen-tial damage to the structural integrity of the vessel nozzles and core-coolir.g capability, and the integrity of the fuel cladding will be maintained".
A drop of the missile shields from their maximum lift height was analyzed to determine the effects on the reactor vessel and head.
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LCA 159 Attachrent 1 Page 2 of 3
-Assuming a worst-case orientation of a missile shield on impact with the head, the analysis showed that penetration of the pressure boundary would not occur. The consequences to the reactor vessel and its supports would be~1ess severe then discussed in the head drop analysis above, since the impact energies of the missile shields dropped from their maximum height are less than the energy of the worst-case ' reactor vessel head drop.
Analysis of a potential drop of the reactor vessel core upper internals into the reactor vessel was performed to determine if unacceptable damage would occur to fuel in the core or to the reactor vessel. The anL2ysis demonstrated that fuel would not be impacted and the reactor vessel would not be unacceptably damaged.
A summary'of the above' analysis is provided in Final Safety Analysis Report (FSAR) Section 9.1.5.
? Administrative Order (AO) 3-20. "Control of Heavy. Loads and Special Lif ting Devices", is the Trojan procedure used to control the lif ting of heavy loads inside Containment. The procedure precludes the lifting of heavy loads over the reactor vessel for which specific analyses were not perforzad by designating safe' load paths.
The NRC Safety Evaluation Report (SER) of July 18, 1983 on Trojan's review of heavy loads concluded that ". . . PGE has stated and defined safe load paths based on appropriate consideration for minimizing the exposure of spent fuel. . . The definition and implementation of safe load paths at the Trojan Plant provide a degree of protection from the consequences of a load drop equivalent to that contained in NUREG-0612."
The ausluation of heavy loads was performed independent of the availability of design featursa such as Containment ventilation isolation. Therefore, changes proposed to Trojan Technical Specifi-cation 3.9.9 do not alter the review, and acceptance by the NRC, of the Trojan heavy loads analysis.
- 2. Generic Letter 85-11. "Completion of Phase II of ' Control of Heavy Loads at Nuclear Power Plants', NUREG-0612", concluded that imple-mentation of controls and analyses for heavy loads provides sufficient protection such that risk from heavy lo&d drops is acceptably small and no further generic action is required. Based on this, and the NRC issuance of the aforementioned SER on heavy loads, the need for a Technical Specification on heavy loads is not evident.
- 3. The contamination that occurred at Trojan in April 1987 due to dis-crete radioactive particles was not significant enough to initiate a Containment ventilation isolation signal. Therefore, the operability
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LCA 159 Attachment 1 Page 3 of 3 of the Containment ventilation isolation system was irrelevant to this perticular event. Since that event,' extensive changes have been implemented to enhance the capability to detect and control discrete radioactive particles, which should reduce the likelihood and magni-tude of contamination from discrete radioactive particles in the future.
- 4. In Revisions 0 and 1 of the Westinghouse Standard Technical Specifica-tions (M-STS), NUREG-0452 Technical Specification 3.9.9 was noted as applicable in Mode 6. Trojan Technical Specifications were modelled after these versions of the M-STS. In Revision 2 of the M-STS (July
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1979), Technical Specification 3.9.9 was revised to only be applicable during core alterations or movement of irradiated fuel within he Containment. The current version of the M-STS (Revision 4) is the same as Revision 2, insofar as applicability of the Technical Specifi-cation is concerned. In addition, a review of the Technical Specifi-cations for other plants (Diablo Canyon, Wolf Creek, and Vogtle) indicates that this Technical Specification is only applicable during core alterations or movement of irradiated fuel within the Contain-ment. Therefore, it is evident that changing the applicability of Trojan Technical Specification 3.9.9 from "Mode 6" to "during core alterations or movement of irradiated fuel within the Containment",
would not only be consistent with the M-STS as issued by the NRC, but also would be consistent with the Technical Specifications issued by the NRC for other similar nuclear plants.
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LCA 159
. Att01hment 2 page 1 of 4 DgSCRIPTION OF CHANGs Trojan Technical Specification (TTS) 3.9.9 - Containment Ventilation Isolation System
- Applicability is changed from "N0DE 6" to "During CORE ALTERATIONS or movement of irradiated fuel within the Containment".
- The Action statement is changed to specify closing Containment Ventilation penetrations providing direct access from the Contain-ment atmosphere to the outside atmosphere if the Containment Ven-tilation Isolation System (CVIS) is inoperable.
REASON FOR CHANGE ,
The reasons for the change to the Applicability are to resolve an in-consistency between TTS 3.9.9 (CVIS) and TTS 3.9.4 (Containment Building penetrations) Limiting Conditions For Operation, and to resolve an incon-sistency between TTS 3.9.9 Applicability and Surveillance Requirements.
TTS 3.9.4 establishes closure requirements for Containment Building penetrations during Refueling Operations when CORE ALTERATIONS or fuel movement is in progress inside the Containment. At other times in Mode 6, the Containment Building may be opened up, with the airlocks, equipment hatch and other penetrations open.
l TTS 3.9.9 requires that each penetration providing direct access from the Containment atmosphere to the outside stmosphere be closed while in Mode 6 if the CVIS is inoperable. Since the Containment is normally open in Mode 6 as permitted by TTS 3.9.4, it is inconsistent to single out containment Ventilation dampers for closure if CVIS operability is not maintained. In addition, the Surveillance Requirements of TTS 3.9.9 are required to be perforsed only before starting and while conducting CORE ALTERATIONS. No Surveillance Requirements for Mode 6 are specified if fuel movement or CORE ALTERATIONS are not in progress. The change, thus, removes this inconsistency between TTS 3.9.9 Applicability and Surveil-lance Requirements.
j The reason for the change to the TTS 3.9.9 Action statement is to make it clear that only Containment Ventilation penetrations must be closed as a result of CVIS inoperability.
SICMIFICANT HAZARDS CONSIDERATION DETERMINATION This proposed change will revise the Applicability statement for the CVIS Refueling Operations Technical Specification. The CVIS is presently required to be operable at all times in Mode 6. This change will revise the CVIS Refueling Operations Technical Specification such that it is applicable during CORE ALTERATIONS or movement of irradiated fuel within
LCA 159
. Attcchment 2 Page 2 of 4 the Containment. Additionally, the Action statement is revised to specify closing Containment Ventilation penetrations if CVIS is inoperable.
This change does not involve a significant increase in the probability or consequences of an accident. Status of the CVIS does not affect accident probability, because this system functions to isolate Containment Venti-lation penetrations after an accident has occurred. Operability of the CVIS enables automatic isolation of the Containment Ventilation penetra-tions. Containment Building penetration closure, while in Mode.6, is relied upon only while CORE ALTERATIONS or movement of irradiated fuel !
within the Containment is in progress per TTS 3.9.4. This Technical Specification requires the containment equipment door be closed, one door in each air lock be closed, and each penetration from Containment atmos-phere to outside atmosphere be either closed or capable of being closed by a Containment Ventilation isolation valve. These operating and clo-sure restrictions on Containment Building penetrations are sufficient to restrict radioactive material release from a fuel element rupture while in the Refueling mode. As a result of this change, the same Applica- ,
bility requirements will apply to CVIS as apply to Containment Building penetrations. The CVIS will be required to be operable to support Con-tainment Building penetration closure requirements. The change to the Action statement is an administrative change to provide clarification that only valves which rely on CVIS for automatic closure are required to be closed should CVIS become inoperable. The consequences of an accident are, thus, not increased, since this change does not involve a substan-tive change to the condition of the Containment Building in Mode 6.
This change does not create the possibility of a new or different kind of accident from any previously evaluated. The operability of CVIS is not relevant to accident creation, since CVIS functions to mitigate the con-sequences of an accident after it has occurred.
This change does not involve a significant reduction in a margin of safety. The requirements for CVIS operability will match those for Con-tainment Building penetration closure during Refueling Operations, and affected Containment Ventilation valves will be closed should CVIS become inoperable. Penetration closure and CVIS operability will be required during CORE ALTERATIONS and fuel movement in Containment. Relaxation of CVIS operability requirements will be permitted only when these evolu-tions are not in progress. The required status of the Containment Build-ing will not be materially affected during Mode 6.
An analysis of the consequences of heavy load drops in the vicinity of the reactor vessel was provided in PGE to NRC letter, "Control of Heavy Loads, NUREG-0612", January 22, 1982. The heavy loads of concern were the reactor vessel head, the core upper internals, and the missile shields. The analysis demonstrated that a drop of these loads would not result in unacceptable fuel damage. A summary of this analysis is
O LCA 159
- Attcchment 2 Page 3 of 4 provided in Final Safety Analysis Report (FSAR) Section 9.1.5.
Administrative Order (AO) 3-20, "Control of Heavy Loads and Special Lifting Devices", is the Trojan procedure used to control the lifting of heavy loads inside Containment. The procedure precludes the lif ting of heavy loads over the reactor vessel for which specific analyses were not performed by designating safe load paths. The NRC Safety Evaluation Report (SER) of July 18, 1983 on Trojan's review of heavy loads concluded that ". . . PGE has stated and defined safe load paths based on appropri-ato consideration for minimizing the exposure of spent fuel. . . The definition and implementation of safe load paths at the Trojan Plant provide a degree of protection from the consequences of a load drop equivalent to that contained in NUREG-0612."
In addition, this change will not result in a significant reduction in a margin of safety in regard to recent operating experience associated with discrete radioactive particles. The contamination that occurred at Trojan in April 1987 due to discrete radioactive particles was not sig-nificant enough to initiate a Containment ventilation isolation signal.
Therefore, the operability of the Containment ventilation isolation sys-tem was irrelevant to this particular event. Since that event, extensive changes have been implemented to enhance the capability to detect and control discrete radioactive particles, which should reduce the likeli-hood and magnitude of contamination from discrete radioactive particles in the future.
In the March 6, 1986 Federal Remister, the NRC published a list of examples of amendments that are not likely to involve significant hazards concerns. The following example from that list applies to this proposed change, demonstrating why this amendment is not considered likely to involve a significant hazards consideration:
"A purely administrative change to Technical Specifi-cations, eg, a change to achieve consistency through-out the Technical Specifications, correction of an error, or a change in nomenclature."
This change is administrative in nature to achieve consistency throughout the Technical Specifications. Additionally, the change is consistent with the regulatory guidance of NUREC-0452, Revision 4. Standard Techni-cal Specifications for Westinghouse Pressurized Water Reactors (W-STS).
TTS 3.9.4 and 3.9.9 presently have different Applicability and Action statements for very similar and interrelated Limiting Conditions For Operation (LCO). This change will make these two specifications consis-tent with each other. Additionally, the Surveillance Requirements for LCO 3.9.9 are keyed to the commencement of CORE ALTFRATIONS. Therefore, this change would make Technical Specification 3.9.9 Applicability and Action consistent with its Surveillance Requirements.
LCA 159
. Attcchment 2
.Page 4 of 4 W-STS 3.9.9 for Containment purge and exhaust isolation system (equiva-lent to TTS 3.9.9) is applicable during CORE ALTERATIONS or movement of '
irradiated fuel within the Containment. Its Action statement requires purge and exhaust penetrations providing direct access from the Contain-ment atmosphere to outside atmosphere be clossd when the isolation system is inoperable. The requirements of this proposed license change are thus equivalent to that of regulatory guidance per M-STS.
Based on the above evaluation, this change does not pose a significant hazard.
SAFETY / ENVIRONMENTAL EVALUATION Safety and environmental evaluations were performed as required by Title 10 Code of Federal Regulations, part 50 and the TTS. This review determined that the proposed change does not create an unreviewed safety question since it is administrative in nature to achieve consistency throughout the TTS.
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