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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217E9711999-10-13013 October 1999 Submits Notification of Major Changes to Trojan Liquid Radioactive Waste Treatment Sys,Iaw PGE-1201.Detailed Description of Change Provided ML20217C8171999-10-0606 October 1999 Forwards Notice of Receipt of Availability for Comment & Meeting to Discuss License Termination Plan,Per 990805 Application ML20216F7621999-09-23023 September 1999 Forwards Corrected Response to Request 2 Contained in NRC 990920 RAI Re Application of Pacificorp for Transfer of License NPF-1.Response 2 Should Have Stated That Na General Partnership Is Partnership Formed in Nv ML20216F2871999-09-20020 September 1999 Informs NRC of Developments That Have Occurred Since 990524 Application Was Filed Re Pacificorp Transfer of License of FOL NPF-1.NRC Is Urged to Act & Approve Transaction Expeditiously by 990930.Supporting Documentation Encl ML20211Q3281999-09-0909 September 1999 Forwards Insp Rept 50-344/99-06 on 990630-0701,21 & 0408-08. No Violations Noted.Insp Conducted to Review Decommissioning Activities Underway at Trojan Site & to Accompany Shipment of Reactor Vessel to Hanford,Washington for Burial ML20211J2101999-08-30030 August 1999 Forwards Request for Addl Info Re Application for Approval of Proposed Corporate Merger of Pacificorp & Scottishpower ML20211B6611999-08-16016 August 1999 Forwards fitness-for-duty Program Performance Data Rept for Period of 990101-0630,IAW 10CFR26.71(d) ML20211B4091999-08-16016 August 1999 Forwards Environ Assessment & Finding No Significant Impact to Application for an Exemption & License Amend Dated 980129.Proposed Exemption & License Amend Would Delete Security Plan Requirements of 10CFR50.54(p) & 10CFR73.55 ML20211A7131999-08-16016 August 1999 Forwards Environ Assessment & Finding of No Significant Impact to Application for Exemption & License Amend Dtd 980827.Proposed Exemption & License Amend Would Delete EP Requirements of 10CFR50.54(q),10CFR50.47(b) & 10CFR50,app E ML20210R7691999-08-11011 August 1999 Forwards Proposed Rev 23 to PGE-8010, Trojan Nuclear QAP, in Response to NRC 990708 RAI Re Relocation of TS ACs to Qap.Revised QAP Will Be Made Effective Concurrently with Implementation of License Change Application Lca 245 ML20210H5971999-07-27027 July 1999 Forwards Notice of Consideration of Approval of Application Re Merger & Opportunity for Hearing.Notice Being Forwarded to Ofc of Fr for Publication ML20216D6611999-07-23023 July 1999 Submits Summary of Proprietary Submittals for Transtor Part 71 & Part 72 & Trojan ISFSI Applications ML20210F8601999-07-22022 July 1999 Forwards Rev 1 to PGE-1076, Trojan Reactor Vessel Package Sar. Changes to Rept Contained in Rev 1 Received NRC Approval by Ltr ML20210A6401999-07-19019 July 1999 Corrects Ref in Item 4 of Which Constitutes Rev 2 of Authorization from Wf Kane, for Trojan Reactor Vessel Package as Approved Package for Shipment Under General License,Subj to Listed Conditions ML20210B4481999-07-12012 July 1999 Forwards Rept Describing Effects of Earthquake That Occurred on 990702 Near Satsop,Wa,Iaw Trojan Nuclear Plant Defueled Sar,Section 4.1.3.1 ML20209D6231999-07-0808 July 1999 Forwards RAI Re Licensee 980827 Request for Amend That Would Delete Number of License Conditions & TS Requirements That Would Be Implemented After All Sf Has Been Removed from 10CFR50 Licensed Area.Response Requested within 30 Days ML20209C6481999-07-0606 July 1999 Forwards Rev 8 to Defueled Sar,Including Changes Since Last Submittal.Attachment Includes Brief Description of Each Change Included in Rev ML20209B7821999-07-0101 July 1999 Responds to NRC 990609 RAI Re License Change Application 244 & Accompanying Request for Exemption.Detailed Info Supports Estimation of Remaining Radioactive Matl Previously Provided by Licensee ML20212J3281999-06-15015 June 1999 Forwards Amend 22 to PGE-1012, Trojan Nuclear Plant Fire Protection Plan, IAW 10CFR50.48(f).Amend Reflects Revs Made During Decommissioning Activities & Does Not Reduce Effectiveness of Fire Protection ML20195J0111999-06-0909 June 1999 Responds to Requesting License & Exemption Re Emergency Preparedness ML20207D3861999-06-0101 June 1999 Forwards Rev 1 to PGE-1077, Trojan Nuclear Plant Reactor Vessel & Internals Removal Project Transportation Safety Plan ML20196L1251999-05-24024 May 1999 Forwards Application for Amend to License NPF-1 for Indirect Transfer of License,To Extent That Such Approval Required Solely to Reflect Change in Upstream Economic Ownership of Pacificorp ML20207A2751999-05-14014 May 1999 Informs That NRC Office of Nuclear Reactor Regulation Reorganized Effective 990328.As Part of Reorganization, Division of Licensing Project Mgt Created.Organization Chart Encl ML20206N9411999-05-11011 May 1999 Forwards Revised Epips,Including Rev 7 to EPIP 3, Response Organization Checklists & Rev 9 to EPIP 5, Emergency Preparedness Test Propgram. Changes to EPIPs 3 & 5 Ref New Owners of on-site Railroad Line,Portland & Western Railroad ML20206J8681999-05-0707 May 1999 Forwards Insp Repts 50-344/99-05 & 72-0017/99-04 on 990419-22.No Violations Noted.Insp Observed Work Activities Associated with Lifting of Reactor Vessel in Preparation for Removal & Shipment to Hanford Reservation for Burial ML20206J7931999-05-0707 May 1999 Forwards Insp Repts 50-344/99-04 & 72-0017/99-02 on 990322- 25 & 29-0408.One Violations Identified & Being Treated as non-cited Violation,Consistent with App C of Enforcement Policy ML20206H4331999-05-0505 May 1999 Forwards Amend 201 to License NPF-1 & Se.Amend Revises PDTSs by Deleting ISFSI Area,Revises Subsection 4.1.1,replaces Figure 4.1-1 with New Figure 4.1-1 & Adds New Page to Figure 4.1-1 to Reflect Access Control (ISFSI) Area ML20206N1571999-05-0404 May 1999 Forwards Util Quarterly Decommissioning Status Rept for First Quarter of 1999,IAW State of or Energy Facility Siting Council Order Approving Trojan Decommissioning Plan, ML20206E1731999-04-29029 April 1999 Informs That NRC Staff Has Performed an Acceptance Review of Trojan Nuclear Plant License Termination Plan,Submitted by ,To Determine Whether LTP Provides Adequate Info to Allow Staff to Conduct Detailed Review ML20206E0211999-04-28028 April 1999 Forwards Copy of Environ Assessment & Finding of No Significant Impact Re 970212 Application for Amend.Proposed Amend Would Revise Trojan Permanently Defueled TS to Delete ISFSI Area ML20206C9591999-04-23023 April 1999 Forwards Amend 200 to License NPF-1 & Safety Evaluation. Amend Changes License NPF-1 by Revising License Condition 2.C.(10), Loading of Fuel Into Casks in Fuel Building ML20206C9221999-04-23023 April 1999 Forwards Amend 199 to License NPF-1 & Safety Evaluation. Amend Changes License NPF-1 by Adding New License Condition Entitled, Loading of Fuel Into Casks in Fuel Building ML20205S9761999-04-21021 April 1999 Forwards Trojan Nuclear Plant,Radiological Environ Monitoring Rept for CY98. Rept Submitted in Accordance with Trojan Permanently Defueled TS 5.8.1.2 & Sections IV.B.2, IV.B.3 & Iv.C of App I to Title 10CFR50 ML20205T5471999-04-20020 April 1999 Forwards Insp Repts 50-344/99-03 & 72-0017/99-03 on 990301-04,15-18 & 22-25.No Violations Noted ML20205N9061999-04-13013 April 1999 Forwards Insp Rept 50-344/99-02 on 990329-0401.No Violations Noted.Inspectors Examined Portions of Physical Security, Access Authorization & FFD Programs ML20205P7301999-04-0808 April 1999 Forwards PGE-1009-98, Operational Ecological Monitoring Program for TNP,Jan-Dec 1998, Including All Existing non-radiological Effluents ML20205B3661999-03-25025 March 1999 Transmits Completed Application for Renewal of NPDES Permit for Trojan Nuclear Plant,Iaw License NPF-1,App B,Epp,Section 3.2 ML20204G1781999-03-18018 March 1999 Forwards Rev 4 to PGE-1063, Suppl to Applicants Environ Rept - Post Operating License Stage ML20204B7551999-03-18018 March 1999 Forwards Updated TS 5.6 Re High Radiation Area,Per Telcons with Nrc.Justification for TS Was Provided Previously with Util Ltr Dtd 990317,but Has Been Updated & Is Included as Encl 2 ML20204C5151999-03-17017 March 1999 Forwards Licensee Comments on NRC Preliminary SER & License Re Trojan Isfsi.Encl Includes Justification for Inclusion in ISFSI TS of Alternative Method to 10CFR20.1601(c) for Controlling Access to High Radiation Areas ML20207J3721999-03-10010 March 1999 Forwards License Amend Application 247 Requesting Amend to License NPF-1 to Add License Condition Denoting NRC Approval of PGE-1078, Trojan Nuclear Plant License Termination Plan, Also Encl.With Certificate of Svc ML20207L0011999-03-0808 March 1999 Transmits Tnp co-owners Annual Rept of Status of Decommissioning Funding for Tnp.Rept Is Based on Most Recent Analysis of Tnp Decommissioning Estimate & Funding Plan,Per Rev 6 to Pge, Tnp Decommissioning Plan ML20207G9691999-03-0303 March 1999 Forwards Rev 6 to PGE-1061, Trojan Nuclear Plant Decommissioning Plan. Summary of Changes,Attached.Revised Portions Denoted by Side Bars ML20207D7751999-03-0202 March 1999 Forwards Amend 21 to PGE-1012, Trojan Nuclear Plant Fire Protection Plan, Per 10CFR50.48(f).Amend Reflects Revs Made During Decommissioning Activities ML20207B0441999-02-24024 February 1999 Forwards Endorsements 139 to Nelia Policy NF-0225 & 2 to Nelia Policy NW-0602 ML20207J0701999-02-11011 February 1999 Forwards Proposed Ts,Update to ISFSI SAR & Revised Calculation,Per Application for Trojan ISFSI License ML20202G4291999-02-0202 February 1999 Forwards Rev 0 to PGE-1076, Trojan Reactor Vessel Package Sar. Approval,With Certain Conditions,For one-time Shipment of Trojan Reactor Vessel Package Granted by Commission Via Ltr ML20202G0931999-01-26026 January 1999 Submits Following Info That Will Be Needed for NRC Staff to Complete Review & Issue Trojan ISFSI License,As Result of 990121 Meeting with NRC Following Insp & Observation of ISFSI Preoperational Testing During Wk of 990118 ML20202F2551999-01-25025 January 1999 Forwards Fitness for Duty Program Performance Data Rept for July-Dec 1998 ML20202C1621999-01-21021 January 1999 Forwards Insp Repts 50-344/98-04 & 72-0017/98-01 & NOV Re Inadequate Actions Taken by Radiation Protection Technician to Ensure That Radiological Conditions Safe Prior to Removing Warning Signs for Airborne Radioactivity Area 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217E9711999-10-13013 October 1999 Submits Notification of Major Changes to Trojan Liquid Radioactive Waste Treatment Sys,Iaw PGE-1201.Detailed Description of Change Provided ML20216F7621999-09-23023 September 1999 Forwards Corrected Response to Request 2 Contained in NRC 990920 RAI Re Application of Pacificorp for Transfer of License NPF-1.Response 2 Should Have Stated That Na General Partnership Is Partnership Formed in Nv ML20216F2871999-09-20020 September 1999 Informs NRC of Developments That Have Occurred Since 990524 Application Was Filed Re Pacificorp Transfer of License of FOL NPF-1.NRC Is Urged to Act & Approve Transaction Expeditiously by 990930.Supporting Documentation Encl ML20211B6611999-08-16016 August 1999 Forwards fitness-for-duty Program Performance Data Rept for Period of 990101-0630,IAW 10CFR26.71(d) ML20210R7691999-08-11011 August 1999 Forwards Proposed Rev 23 to PGE-8010, Trojan Nuclear QAP, in Response to NRC 990708 RAI Re Relocation of TS ACs to Qap.Revised QAP Will Be Made Effective Concurrently with Implementation of License Change Application Lca 245 ML20216D6611999-07-23023 July 1999 Submits Summary of Proprietary Submittals for Transtor Part 71 & Part 72 & Trojan ISFSI Applications ML20210F8601999-07-22022 July 1999 Forwards Rev 1 to PGE-1076, Trojan Reactor Vessel Package Sar. Changes to Rept Contained in Rev 1 Received NRC Approval by Ltr ML20210B4481999-07-12012 July 1999 Forwards Rept Describing Effects of Earthquake That Occurred on 990702 Near Satsop,Wa,Iaw Trojan Nuclear Plant Defueled Sar,Section 4.1.3.1 ML20209C6481999-07-0606 July 1999 Forwards Rev 8 to Defueled Sar,Including Changes Since Last Submittal.Attachment Includes Brief Description of Each Change Included in Rev ML20209B7821999-07-0101 July 1999 Responds to NRC 990609 RAI Re License Change Application 244 & Accompanying Request for Exemption.Detailed Info Supports Estimation of Remaining Radioactive Matl Previously Provided by Licensee ML20212J3281999-06-15015 June 1999 Forwards Amend 22 to PGE-1012, Trojan Nuclear Plant Fire Protection Plan, IAW 10CFR50.48(f).Amend Reflects Revs Made During Decommissioning Activities & Does Not Reduce Effectiveness of Fire Protection ML20207D3861999-06-0101 June 1999 Forwards Rev 1 to PGE-1077, Trojan Nuclear Plant Reactor Vessel & Internals Removal Project Transportation Safety Plan ML20196L1251999-05-24024 May 1999 Forwards Application for Amend to License NPF-1 for Indirect Transfer of License,To Extent That Such Approval Required Solely to Reflect Change in Upstream Economic Ownership of Pacificorp ML20206N9411999-05-11011 May 1999 Forwards Revised Epips,Including Rev 7 to EPIP 3, Response Organization Checklists & Rev 9 to EPIP 5, Emergency Preparedness Test Propgram. Changes to EPIPs 3 & 5 Ref New Owners of on-site Railroad Line,Portland & Western Railroad ML20205S9761999-04-21021 April 1999 Forwards Trojan Nuclear Plant,Radiological Environ Monitoring Rept for CY98. Rept Submitted in Accordance with Trojan Permanently Defueled TS 5.8.1.2 & Sections IV.B.2, IV.B.3 & Iv.C of App I to Title 10CFR50 ML20205P7301999-04-0808 April 1999 Forwards PGE-1009-98, Operational Ecological Monitoring Program for TNP,Jan-Dec 1998, Including All Existing non-radiological Effluents ML20205B3661999-03-25025 March 1999 Transmits Completed Application for Renewal of NPDES Permit for Trojan Nuclear Plant,Iaw License NPF-1,App B,Epp,Section 3.2 ML20204G1781999-03-18018 March 1999 Forwards Rev 4 to PGE-1063, Suppl to Applicants Environ Rept - Post Operating License Stage ML20204B7551999-03-18018 March 1999 Forwards Updated TS 5.6 Re High Radiation Area,Per Telcons with Nrc.Justification for TS Was Provided Previously with Util Ltr Dtd 990317,but Has Been Updated & Is Included as Encl 2 ML20204C5151999-03-17017 March 1999 Forwards Licensee Comments on NRC Preliminary SER & License Re Trojan Isfsi.Encl Includes Justification for Inclusion in ISFSI TS of Alternative Method to 10CFR20.1601(c) for Controlling Access to High Radiation Areas ML20207J3721999-03-10010 March 1999 Forwards License Amend Application 247 Requesting Amend to License NPF-1 to Add License Condition Denoting NRC Approval of PGE-1078, Trojan Nuclear Plant License Termination Plan, Also Encl.With Certificate of Svc ML20207L0011999-03-0808 March 1999 Transmits Tnp co-owners Annual Rept of Status of Decommissioning Funding for Tnp.Rept Is Based on Most Recent Analysis of Tnp Decommissioning Estimate & Funding Plan,Per Rev 6 to Pge, Tnp Decommissioning Plan ML20207G9691999-03-0303 March 1999 Forwards Rev 6 to PGE-1061, Trojan Nuclear Plant Decommissioning Plan. Summary of Changes,Attached.Revised Portions Denoted by Side Bars ML20207D7751999-03-0202 March 1999 Forwards Amend 21 to PGE-1012, Trojan Nuclear Plant Fire Protection Plan, Per 10CFR50.48(f).Amend Reflects Revs Made During Decommissioning Activities ML20207B0441999-02-24024 February 1999 Forwards Endorsements 139 to Nelia Policy NF-0225 & 2 to Nelia Policy NW-0602 ML20207J0701999-02-11011 February 1999 Forwards Proposed Ts,Update to ISFSI SAR & Revised Calculation,Per Application for Trojan ISFSI License ML20202G4291999-02-0202 February 1999 Forwards Rev 0 to PGE-1076, Trojan Reactor Vessel Package Sar. Approval,With Certain Conditions,For one-time Shipment of Trojan Reactor Vessel Package Granted by Commission Via Ltr ML20202G0931999-01-26026 January 1999 Submits Following Info That Will Be Needed for NRC Staff to Complete Review & Issue Trojan ISFSI License,As Result of 990121 Meeting with NRC Following Insp & Observation of ISFSI Preoperational Testing During Wk of 990118 ML20202F2551999-01-25025 January 1999 Forwards Fitness for Duty Program Performance Data Rept for July-Dec 1998 ML20199J1661999-01-14014 January 1999 Submits Summary of ISFSI Lid Welding Demonstration to Be Held 990118-25.Dates & Days Are Tentative & Can Be Adjusted as Necesssary or as Required ML20199J0801999-01-12012 January 1999 Forwards Schedule for Trojan Nuclear Plant ISFSI pre-op Test,Per Request ML20206Q0121999-01-0808 January 1999 Forwards Rev 1 to PGE-1073 Tnp ISFSI Security Plan,As Result of 981208 Telcon with Nrc.Encl Withheld,Per 10CFR73.21 ML20206P5991999-01-0404 January 1999 Requests That Svc List for Delivery of Documents from NRC Be Updated,Per 981230 Telcon.Substitute for Listings of HR Pate & J Westvold,Submitted ML20198T1651999-01-0404 January 1999 Forwards Rev 5 to PGE-1061, Trojan Nuclear Plant Decommissioning Plan. Table 2.2-5 Is Revised to Depict Major Components Removed from Plant During 1998.Revs Are Denoted by Side Bars ML20198E3981998-12-17017 December 1998 Forwards Updated ISFSI Emergency Plan,Per 981123 & Discussion in Meeting with NRC on 981119.Description of Changes Encl ML20196E2851998-11-25025 November 1998 Forwards Final Rept of Matl Properties of Neutron Shielding Matl to Be Used in Trojan ISFSI & Test Repts That Verified Matl Properties ML20196D9831998-11-24024 November 1998 Forwards Listed ISFSI Calculation Refs,Per 981110 Telcon ML20196B2321998-11-23023 November 1998 Informs That,Per Commitments Made in 981119 Meeting with Nrc,Rev to PGE-1075 Will Be Submitted No Later than 981218 ML20195J2321998-11-17017 November 1998 Forwards Rev 7 to Trojan Nuclear Plant Defueled Sar. Attachment to Ltr Includes Brief Description of Each Change Included in Rev ML20195E4811998-11-10010 November 1998 Forwards Rev 51 to Trojan Nuclear Plant Security Plan.Rev Withheld,Per 10CFR73.21 ML20155E0331998-10-27027 October 1998 Forwards Amend 7 to PGE-1052, Quality-Related List Classification for Tnp. Amend Removes Ref to Several Clean Up Sys,Deletes Exemptions Allowed by Reg Guide 1.143 & Deletes Figures No Longer Required to Support Discussion ML20154M4151998-10-14014 October 1998 Requests That Further Review of License Change Application LCA-238 Be Suspended as Result of Progress Made in Decommissioning,Installation of Natural Gas Pipe Line ML20154A4751998-09-28028 September 1998 Forwards Amend 20 to PGE-1012, Trojan Nuclear Plant Fire Protection Plan, Reflecting Revisions to Fire Protection Program Made During Decommissioning Activities ML20153D3021998-09-21021 September 1998 Forwards Rev 0 to PGE-1077, Tnp Reactor Vessel & Internals Removal Project Transportation Safety Plan, Per Request That Util Submit Description of Measures to Be Taken to Ensure Safe Transport of Tnp Rv & Internals Package ML20151X8571998-09-10010 September 1998 Provides Rev 2 to Poge, Trojan NPP Permanently Defueled TS Bases. Changes Identified in Revised Text by Side Bars ML20151X7171998-09-10010 September 1998 Forwards Rev 3 to PGE-1063, Trojan Nuclear Power Station, Suppl to Applicant Environ Rept. Section 4.5 Revised to Delete Ref to Selected Room Coolers ML20153B0001998-09-0909 September 1998 Forwards Figures & Tables Identifying Nodes Assigned for Trojan ISFSI Transfer Station Analysis,TI-056,Rev 1 ML20237E9421998-08-27027 August 1998 Requests Exemption of Emergency Plan Requirements of 10CFR50.54(q),10CFR50.47(b) & 10CFR50,App E Following Transfer of Spent Nuclear Fuel to ISFSI ML20151W5381998-08-25025 August 1998 Forwards Rev 22 to PGE-8010, Poge Nuclear QA Program for Trojan Nuclear Plant. Rev Reflects Administrative Changes That Continue to Meet Requirements of 10CFR50,App B ML20237E1811998-08-25025 August 1998 Forwards Description of Review Methodology & Summary of Results,Including List of Identified Variations from Guidance Contained in Std Review Plan,Per NUREG-1536 1999-09-23
[Table view] Category:UTILITY TO NRC
MONTHYEARML20059L6651990-09-21021 September 1990 Forwards Application for Amend to License NPF-1,consisting of License Change Application 203,Rev 1.Rev Reduces Scope of Previous Changes Re Tech Spec Table 3.6-1, Containment Isolation Valves ML20059J9691990-09-14014 September 1990 Forwards Estimates of Facility Operator Licensing, Requalification & Generic Fundamentals Exam Requirements for FY91-94,per Generic Ltr 90-07 ML20059J9841990-09-14014 September 1990 Responds to Re Violations Noted in Insp Rept 50-344/90-21.Corrective Action:Individual Employee Terminated on Day of Event ML20059J0321990-09-0707 September 1990 Requests That Six Listed Candidates Take PWR & Generic Fundamentals Exam to Be Administered on 901010 ML20059D8031990-08-31031 August 1990 Forwards Update on Actions for NRC Bulletin 88-008, Thermal Stresses in Piping Connected to Rcs ML20059D2401990-08-30030 August 1990 Extends Commitment Date from 900831 to 901031 to Amend FSAR Per Util 900404 Response to Notice of Violation ML20059D0831990-08-30030 August 1990 Revises Response to Violations Noted in Insp Rept 50-344/90-02.License Document Change Request Correcting FSAR Discrepancy Noted in App A,Violation C Re Request for Design Change Initiated & Will Be Incorporated Into Amend 14 ML20059C1741990-08-28028 August 1990 Forwards Rev 31 to Security Plan.Rev Withheld (Ref 10CFR73.21) ML20059D3201990-08-28028 August 1990 Responds to Deficiencies Identified by FEMA During 891115 Emergency Preparedness Exercise at Plant.Corrective Actions: Procedures Revised to Prioritize Roadblocks & Clearly Define Roadblocks for 5-mile & 10-mile Locations ML20059D5601990-08-28028 August 1990 Forwards Fitness for Duty Performance Rept for 900103-0630. Overall Positive Rate for All Testing Conducted at Plant from 900103-0630 Is 0.71% ML20058M7861990-08-0303 August 1990 Forwards Monthly Operating Rept for Jul 1990.W/o Encl ML20056A1551990-07-31031 July 1990 Forwards Updated Response to Address Maint/Surveillance Area of SALP for Period from Jan 1989 - Mar 1990.Overall Plant Performance During Period Acceptable & Found to Be Directed Toward Safe Operation ML20055J3421990-07-26026 July 1990 Forwards Decommissioning Financial Assurance Certification Rept for Plant,Per 10CFR50.75.Certifies That Finanical Assurance Utilizing Methodology as Listed Will Be Available to Decommission Plant ML20055G7131990-07-20020 July 1990 Comments on Operator Licensing Exams Administered on 900717 ML20055G7141990-07-19019 July 1990 Responds to NRC Bulletin 90-001, Loss of Fill-Oil in Transmitters Mfg by Rosemount. Plant Has Four Rosemount Model 1153DD6 Differential Pressure Transmitters Installed to Associated Logics for Safety Injection ML20055F8791990-07-16016 July 1990 Forwards 1989 Annual Repts for Portland General Corp,Eugene Water & Electric Board & Pacific Power & Light Co ML20055F6911990-07-13013 July 1990 Responds to Generic Ltr 90-04, Request for Info on Status of Implementation of Generic Safety Issues Resolved W/ Imposition of Requirements or Corrective Actions ML20055F8161990-07-13013 July 1990 Advises of New Addressee for Nrc/Util Correspondence ML20055F2441990-07-12012 July 1990 Forwards Response to SALP Evaluation for Jan 1989 - Mar 1990 Re Maint/Surveillance.Util Plans to Improve Performance in Areas of Operation Through Commitment of Support from Nuclear Div Mgt & Personal Involvement of Corporate Mgt ML20055F2961990-07-0606 July 1990 Forwards Addl Info Re ATWS Mitigating Sys Actuation Circuitry ML20055E3401990-07-0606 July 1990 Forwards Application for Renewal of Plant NPDES Permit ML20055E1751990-07-0606 July 1990 Provides Update to 891130 Response to Generic Ltr 88-14, Instrument Air Supply Sys Problems Affecting Safety-Related Equipment. Rev to Maint Procedure 12-4, Valve Air Actuators, to Include Maint Insp Completed in Apr 1990 ML20055E0241990-07-0606 July 1990 Responds to NRC Re Violations Noted in Insp Rept 50-344/90-11.Corrective Actions:Generic Issues That Contributed to Violation Will Be Discussed During Mgt Meetings & Quality Insp Supervisor Counseled ML20055E0281990-07-0606 July 1990 Informs That Actions Committed to in Util Re Replacement of Breaker During 1990 Refueling Outage & Provision of Rept Documenting Replacement of Breaker, Complete,Per NRC Bulletin 88-010 ML20058K4891990-06-30030 June 1990 Discusses Reduced Min Measured RCS Flow for Plant.Encl Figure 3.2-3 & Evaluation Support Operation W/No Tech Spec Setpoint Changes ML20055D0411990-06-29029 June 1990 Discusses Design Verification Program Re Main Steam Support Structure.Extension of Completion Date for Project Justified Since Documentation,Not Mod of Main Steam Support Structure Is Reason for Delay ML20055D0441990-06-29029 June 1990 Advises That Response to Generic Ltr 90-04 Re Status of Generic Safety Issues at Facility Delayed from 900629 to 900713 ML20055D7091990-06-26026 June 1990 Forwards Steam Generator Tube Plugging Rept,Per Inservice Insp ML20055C2691990-02-20020 February 1990 Responds to NRC Re Violations Noted in Insp Rept 50-344/89-30.Corrective Actions:Administrative Order 5-8 Temporary Mods to Be Evaluated for Need to Improve Control Over Temporary Mods Issued for Both Trains of Sys ML17311A1041989-10-30030 October 1989 Advises That Commitment Date for Performance of Surveillance Moved to 891130 to Allow for Incorporation in Biennial Audit Per Rev 1 to LER 89-08.NRC Resident Inspector Informed of Change on 891013 ML20248G7631989-10-0606 October 1989 Forwards Description of Alternate Compensatory Measures Implemented During Upgrade Activities.W/O Encl ML20248G3131989-10-0303 October 1989 Forwards Response to Generic Ltr 89-04, Guidance on Developing Acceptable Inservice Testing Programs. Revised Topical Rept PGE-1048 Will Be Submitted by 891117 ML20248E2391989-09-29029 September 1989 Forwards Summary of Action Plan to Resolve Fuel Bldg Overstress Conditions ML20248D3711989-09-29029 September 1989 Forwards Rept of Util Plan for Improving Performance of Nuclear Div Staff.New Mgt Described in Plan Will Serve as Catalyst for Decisive Performance Changes ML20248G9001989-09-29029 September 1989 Forwards Rev 1 to PGE-1049, Inservice Insp Program for Second 10-Yr Interval from 860520-960519 05000344/LER-1989-007, Informs That Rev 1 to LER 89-07 Will Be Submitted by 891013, Due to Forced Outage & Difficulties1989-09-28028 September 1989 Informs That Rev 1 to LER 89-07 Will Be Submitted by 891013, Due to Forced Outage & Difficulties ML20248G1071989-09-28028 September 1989 Advises That Util Will Submit Final Closeout of NRC Bulletin 88-004, Potential Safety-Related Pump Losss, by 900115 ML20248D6161989-09-28028 September 1989 Requests 14-day Extension Until 890928 to Respond to Violations Noted in Insp Rept 50-344/89-09.Individuals Involved in Providing Input to Response Currently Assigned to Solving Problems During Current Forced Outage ML20248D4211989-09-27027 September 1989 Suppls 881004 Response to NRC Bulletin 88-008, Thermal Stresses in Piping Connected to Rcs. NDE Confirmed That No Existing Flaws Exist in Critical Piping Locations Re Thermal Stratification ML20247G9011989-09-15015 September 1989 Responds to Generic Ltr 89-06 Re SPDS Requirements,Per NUREG-0737,Suppl 1 as Clarified by NUREG-1342.Concludes That Isolators Used Were Acceptable for Interfacing SPDS W/Safety Sys,Therefore Util Does Not Intend to Make Mods to SPDS 05000344/LER-1989-012, Advises That Rev 1 to LER 89-012 Will Be Submitted by 890920 Due to Extension of 1989 Refueling Outage & Plant Trip of 8908091989-09-0808 September 1989 Advises That Rev 1 to LER 89-012 Will Be Submitted by 890920 Due to Extension of 1989 Refueling Outage & Plant Trip of 890809 ML20247B9281989-09-0808 September 1989 Responds to NRC Re Violations Noted in Insp Rept 50-344/89-12 & Forwards Review of Closeout of First 10-yr Inservice Insp Interval.Concurs That Primary Reason for Individual Problems Was Lack of Insp Contractor Activities ML20247C2801989-09-0808 September 1989 Responds to NRC Re Violations Noted in Insp Rept 50-344/89-18.Corrective Action:Reevaluation of OAR 87-29, Involving Mods to Hydrogen Gas Supply Sys Implemented as Part of 1989 Refueling Outage ML20247E9371989-09-0707 September 1989 Discusses Nuclear Div Improvement Plan,Per Recent Event Re Containment Recirculation Sump.Util Corrective Actions, Including Organizational Changes,Encl.Plant Improvement Plan Will Be Submitted by 891001 ML20247A6171989-09-0505 September 1989 Informs That Intake Structure Mod Completed as Scheduled & Security Plan Rev Will Be Submitted by 891015 ML20246M5181989-08-31031 August 1989 Forwards Update on Action Plan Developed in Response to Generic Ltr 88-14, Instrument Air Supply Sys Problems Affecting Safety-Related Equipment ML20246M5651989-08-31031 August 1989 Discusses long-term Pipe Support Design Verification Program for Plant.Evaluation of Fuel Bldg Confirmed & Quantified Code Overstresses Existing Under Seismic & Tornado Loading Conditions.Details of Action Plan Will Be Sent by 890929 ML20246M5771989-08-31031 August 1989 Forwards Status of Progress in Achieving Improvement Goals Identified in 890515 SALP Response Re Safety Assessment/ Quality Verification.Addl Resources Applied to Qualify commercial-grade Suppliers ML20246J8641989-08-28028 August 1989 Responds to NRC Re Violations Noted in Insp Rept 50-344/89-02.Corrective Actions:Util Assembled Interdepartmental Task Force in Nov 1988 to Review Incidents & Determine Root Causes ML20246H5351989-08-25025 August 1989 Informs That Rev to Topical Rept PGE-1049, Trojan Nuclear Plant Inservice Insp Program for Second 10-Yr Interval Will Be Submitted for Approval by 890929 1990-09-07
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- mamma f M lhy r -E David W. Cockfield Vice President, Nuclear September 29, 1989 Trojan Nuclear Plant Docket 50-344 License NPF-1 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington DC 20555
Dear Sir:
Nuclear Division Improvement Plan Attached is a report of Portland General Electric (PCE) Company's plan for improving the performance of the Nuclear Division staff. PCE is committed to achieve success in Trojan Nuclear Plant performance. The attached plan describes those actions which have been taken and those to be taken to improve performance and to achieve excellence in the operation of Trojan. The new management team described in the plan will serva as the catalyst for decisive performance changes.
The plan is not meant to be a final document. As actions are taken, it is expected that adjustments or additions will need to be made.
Additionally, we will document in the plan the results of our actions and assess their success. In this regard, we will provide periodic updates of the plan to keep you informed of our progress. The first update will be provided by January 31, 1990. We expect, however, that before that time, you will see improved performance in your observation of our day-to-day activities.
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'I 8910040224 890929 PDR ADDCK 05000344 P PNU 121 S W Sa mon Street, PoTara Oregon 9720i
Pbetland Gener<d Bectric 00iiiptw ry 4
Document Control Desk september 29, 1989' Pete 2 .
I want' to assure you of. my comunitJhent to see that this plan succeeds and that the performance at Trojan wats my standards of excellence.
s sincerely.
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/N y Attachment c: Mr.' John B. Martin Regional Administrator, Region V
- U.S. Nuclear, Regulatory Commission Mr. David Stewart-Smith State of Oregon
-Department of Energy Mr.'R. C..Barr NRC Resident Inspector Trojan Nuclear Plant I<
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NUCLEAR DIVISION IMPROVEMENT PLAN SEPTEMBER 29, 1989
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NUCLEAR DIVISION' IMPROVEMENT: PLAN-J, CONTENTS e
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1$01- : INTRODUCTION .- . .. . .- .: .- . '.' . . . . ... . .
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< $ 11.21 . MANAGEMENT CHANGES .. . . . .. .:.. . . .... 1
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-: PGE's COMMITMENT TO EXCELLENCE-Y IN NUCLEAR OPERATIONS . . . : .. . . . . .J.'. . . 3 L ,
L2.0l ACTIONS'TO' IMPROVE PERFORMANCE .-. .' . ... . . .. '4 T2.1 : MANAGEMENT PERFORMANCE ...-. . . . .. . . . . . 4
'2.1.1: - Summary of Problem =. . . . . . ... . . . . ' . . . . . - 4 2.1.2- Discussion . ..m . . . .- . .- .:. . . . .. . . 4
'2.1.3 - Actions Taken/Pla9ned .-... . ... . . . . . . . . .
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2.1. 4 ~ - Overall Measure'of Effectiveness-
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( - 2.2 : ' ASSURANCE OF QUALITY . . . . . - . . . . .. . .. .- 8 c
' 2. 2.1. . Summary of Problem. . - . . . .. . . - - . ... . . . ' . .- 8 2.2.2 Discussion . . . .'.. . . . . ... . ... . . . . . . 8 2.2.3 . Action.Taken/flanned . . .- . ... . . . . . . .- . 8
!" 2. 2.4 ' . Overall Measure of Effectiveness . ... . . . . .- 9
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2.3.1J Other Actions Taken/ Planned.... . . . . . . . . . .
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- NUCI. EAR DIVISION IMPROVEMENT PIAN 1
1.0 Introduction 1.1 Purpong The purpose of the Nuclear Division Improvement Plan is to assess the performance problems at the Trojan Nuclear Plant in order to develop effective actions to improve performance. This plan contains three major parts : addressing concerns relating to management performance, assurance of quality. and other areas where it has been identified that improve-ments are required. The actions described herein complement actions which have already been taken toward achieving the desired level of performance.
The plan focuses on management effectiveness. The success or failure in achieving performance consistent with PGE's expectations is the responsi-bility of management. Safety and quality expectations will be met through an effectively managed organization. Due to the failure to demonstrate the ability to meet company expectations, leadership changes have been made in several areas. The complete impact of these changes has yet to be realized.
1.2 Manarement Changes One of the actions taken to improve management effectiveness was to replace several managers in the Trojan organization with key individuals selected both from within PGE as well as from other successful organizations. The specific changes are described below.
In November 1988, as a result of declining performance in Nuclear Security, the Manager, Nuclear Security, was replaced. Since that time,
-improved performance in this area has been observed. Some problems caused by previous management are still being uncovered but are effectively being corrected.
Due to a failure to see that management's expectations were being effectively implemented, the Plant General Manager was replaced in February 1989. The General Manager, Technical Functions was selected to fill the Plant General Manager position.
In concert with the move of the General Manager, Technical Functions to the-Plant General Manager position, the Manager, Nuclear Safety and Regulation was promoted to the position of General Manager, Technical Functions. The position of Manager, Nuclear Safety and Regulation, was filled from the outside by a manager with previous licensing experience l at two other utilities with operating nuclear power plants.
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- In April, 1989, a number of staffing changes were made in the Nuclear Quality Assurance' Department (NQAD) to deal with ongoing performance deficiencies. An individual with experience in licensing and compliance was appointed.to the position of Branch Manager, Quality Operations, and
,also acted as the NQAD manager. An experienced Trojan manager with a quality assurance' background was appointed to the position of Quality
- Support Services Branch Manager. In addition, an infusion of experienced
' technical' personnel was made to the NQAD staff through the addition of a
' Nuclear Engineer, a Mechanical Engineer, an Electrical Engineer, a Radiation Protection Engineer and an Instrumentation and Control (I&C) technician.
Two additional management changes in NQAD have been made to improve and strengthen the Quality Assurance program. First, the position of Manager Quality Assurance, has been upgraded to General Manager Quality Assurance, to put this position on equal level with the other senior !
managers.in the Nuclear Division. Second, a senior manager, with a l
proven track record in' nuclear quality assurance program development cnd management, was hired from the outside by PGE for the General Manager, Quality Assurance, position.
In the interest of enabling the Plant General Manager to focus his attention more on the day-to-day operations and maintenance of the plant, a new position, General Manager, Plant Support, was created to shift the responsibility for such areas as Planning and Scheduling, Material Control and Administrative Services from the Plant General Manager.
Training will also be shif ted to the General Manager, Plant Support, upon completion of a change to the Trojan Technical Specifications. The General Manager Plant Support position has been filled from the outside !
by a senior officer from the Navy Nuclear Power Program. l These management changes have resulted in improved performance of the affected organizations. The performance of the Plant Staff, however, was not significantly changed due to a strong resistance to change on the part of key managers within that organization. In retrospect, this resistance to change was tolerated too long, resulting in the problems evident during the Containment recirculation sump events. As a result of their performance, the Manager, Operations and Maintenance and the Branch Manager, Plant Systems Engineering were relieved of their duties. A supervising engineer from the Mechanical Engineering Branch of Nuclear Plant Engineering was selected to fill the Plant Systems Engineering i Branch Manager position. The position of Manager, Operations and Maintenance, is being split into two positions; Manager, Operations and Manager, Maintenance, to increase management oversight in these areas. ;
PGE is currently conducting a nationwide search to find the right candidates to fill these positions. A contract manager has been acquired to fill, temporarily, the Maintenance Manager's position.
In addition to these changes, the Maintenance Branch Manager will be relieved of his duties in order for him to participate in management improvement programs including gaining additional industry experience (potentially through a short-term assignment with the Institute of Nuclear Power Operations) followed by completion of his college degree i
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requirements.- Following this training, h'e will' be evaluated for assign- l ment to a management position in the Nuclear Division. The Manager of Technical. Services and the Branch Manager of Operations have been
- assigned 'to complete performance upgrade programs.
I PGE has also made changes in the executive-level management responsible l for the oversight of nuclear operations. The position of President, Generating Division and President, Energy Services Division have been -
. combined- and Ms. E. Kay Stepp has been named President. of PGE. Ms. Stepp
- has an excellent leadership background and an urvavering commitment to !
excellence. Ms. Stepp has been with PGE since 1978 and was previously )
- the' President _ of PGE's Energy Services Division. She has previously served as the Vice President of Marketing and Customer Relations, Vice President of Management Resources, and Vice President of Human Resources.
A Senior Vice President has been placed in charge of the Generating Division of PGE. Mr. Walter Higgins has been named to fill this position. Mr. Higgins has been with PGE since 1977 and'has been serving as the Vice President of Power Distribution since mid-1987. He has ;
previously ' served as the President of a PGE subsidiary, the General l Manager of Information Systems, the General Manager of Construction and l Maintenance, and the Manager of Engineering and Maintenance. Prior to )
joining PGE, Mr. HiF gins was employed by the Nuclear Regulatory Commission. !
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' 1.3 PGE's Commitment to Excellence in Nuclear Ooerations PGE has made major commitments in terms of operations and maintenance budgeting and personnel staffing to provide the resources necessary to
- achieve excellence in the company's nuclear operations. The operations and maintenance budget for the plant is adequate to achieve excellence in the operation of Trojan.
PGE has also built a new Training Building and installed a simulator at the plant site. These facilities became operational in 1989 and enable site specific training for Trojan employees. In 1989, PGE provided a new 3 office building at the plant site to enable relocation of the design ;
engineering, licensing and support groups to the site. In the short time l since this relocation occurred, the improved support and communications l has already become evident.
In his address to PGE managers regarding five-year goals and objectives, the Chairman and Chief Executive Officer of Portland General Corporation stressed his goal to achieve excellence in the area of nuclear opera- ]
tions. The Trojan Nuclear Plant is clearly PGE's greatest asset and the l need to make it a great success was clearly expressed to be of utmost importance. Having Trojan become a top performer is a specific goal in the corporate long-range plan.
These are but some of the examples of PGE's commitment to excellence in the operation of Trojan. The past performance at Trojan is not consis-tent with PGE's commitment to excellence. This plan is being generated to express PGE's commitment to correct these performance deficiencies.
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- y. 2.0 ACTIONS TO IMPROVE PERFORMANCE' 2.1 MANAGEMENT PERFORMANCE il
' 2.1.1 - S - ary of Problem Management ' performance has been inconsistent in the basic tasks of establishing and communicating expectations throughout the organization Land holding people accountable for'their actions.
Identified: problems with; procedure compliance' and recognition land resolu-tion of problems are symptomatic of management performance deficiencies and'the failure to implement accountability.-
2.1.'2 Discussion'-
For the past.two years,_ senior management in the Nuclear Division has espoused basic performance. standards and expectations'by which the Nuclear Division must operate.' These expectations iuclude:
.1. Demonstrating. personal accountability.
- 2. : Timely and thorough response to problems.
- 3. Procedure compliance.
4; Management must oversee daily activities.
- 5. Attentina to detail.
-6. Quality teamwork.
- 7. Establishment of an environment for success.
- 8. Always strive for higher standards of performance.
For the past two years these performance standards and expectations have not been fully realized. -There'are two basic reasons for this: (1) the expectations have not been effectively implemented throughout the organi-zation and, (2) the management chain has not consistently demonstrated accountability for meeting the performance standards and expectations.
In order to see improved performance, management must consistently enforce the performance standards and expectations. The change must begin with ownership by management of the performance standards and expectations ~, clear communication of the same to employees, and the resolve to hold people accountable for their actions.
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1211'.3 Actions Taken/ Planned-b .As discussed previously, several management changes have occurred. These changes were made.to improve Nuclear Division performance.. Open posi-tions have_been or will be filled with experienced managers who have a demonstrated ability to implement these ' standards and expectations.
- 1. For over two years, PGE has been.providing training for' managers and supervisors .to equip them to implement performance standards and L expectations. This. training has been referred to as the Trojan
? Excellence Program. This training has achieved success ~for those L~ ,
' managers who have implemented-the principles taught. A continued commitment to this training program will be made as the principles
, taught are. sound and will, if implemented', improve performance. The emphasis of-this commitment will be to have the remaining managers
" . implement these principles. The successes which have been achieved
[ will be utilized as examples in the training.
ACTION: Vice President DUE DATE: . Ongoing ,
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- 2. The Vice President and the Genera 1' Managers in the Nuclear Division have hosted communications breakfasts for managers and supervisors for the purpose of communicating performance standards and expecta-tionsuand allowing for an opportunity to provide feedback. These L
sessions have been beneficial to communication within the Nuclear Division and will be continued and expanded in the future.
ACTION:. Vice President DUE DATE: Ongoing i
- 3. The Vice President held.a series of meetings to communicate to all' employees what problems PGE is facing with regard to the operation
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of Trojan and'to' reinforce management expectations to correct performance deficiencies. These meetings will be followed by leadership meetings' involving the General Managers and the leadership of each department reporting to them to reinforce both the expectations and how each manager and supervisor will be held secountable for their actions. Managers and supervisors will then be required to conduct similar meetings with working' level e mployees. These latter meetings will be monitored by department managers or above to ensure the correct messages are communicated and to allow a forum for effective feedback. This action has already begun.
ACTION: Vice President, General Managers, Managers, Supervisors DUE DATE: October 31, 1989 l
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- 4. The information booklet entitled, " Guidelines for a Quality Working environment", was issued in 1987. This booklet contains sound principles for achieving success. This booklet will be expanded to provide.a clear statement of expectations and performance standards and will be reissued..
ACTION: General Manager, Plant Support DUE DATE: November 15, 1989
- 5. The existing Quality Line publication is being upgraded to include a discussion of the management principles and expectations. It will also' include a " lessons-learned" section to provide examples of how t
management expectations should be met. The " lessons-learned" articles will be prepared by Nuclear Division managers and distributed to employees.
ACTION: General Manager, Quality Assurance
.DUE DATE: Ongoing
- 6. One of-the identified weaknesses in management of the Nuclear Division.is a lack of adequate management / leadership training. Some managers and supervisors have been promoted from within to their current positions because they exhibited sound technical abilities.
More than good technical knowledge, however, is required to develop good managers. The Trojan Excellence Program was begun, in part, to respond to-this identified weakness. An additional management training program will be provided to selected managers and supervisors. This training will better equip these individuals for fulfilling their leadership role.
ACTION: Manager Training and General Managers DUE DATE: Ongoing; additional training to commence by December 15, 1989
- 7. Incorporate presentations by selected management personnel on Nuclear Division performance standards and expectations as a part of the General Employee Training and Retraining Programs.
ACTION: General Manager, Plant Support DUE DATE: December 31, 1989
- 8. A human resources assessment of key Nuclear Division managers /
supervisors will be performed using an outside consultant. The assessment will identify strengths and weaknesses of these managers and will recommend corrective measures where needed.
ACTION: Senior Vice President, Generating Division DUE DATE: December 31, 1989 ,
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, 9.-'In order for. management expectations to be met,= employees must see a F ' commitment to these. expectations. 1 As such, management needs to demonstrate its commitment by providing: positive examples of
-expected performance. One concrete area where this can be'accom-plished is by a' commitment to the. Plant material-condition.
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program?to reduce the backlog of_ Maintenance Requests (MRs) has been
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' implemented under the Maintenance Improvement. Plan. /This. program-is F being reviewed.to ensure proper goals'have been established and the
'irenources are being applied to achieve a. decisive reduction in the'-
..J f g backlog.: This backlog reduction is seen as a critical action to
^ = improve plant operation. and demonstrate a' visible commitment:to R..
4' ': higher ' standards. to plant ' personnel.
h, _ ACTION:1 Plant General' Manager (review goals and priorities)
DUE DATE: November 30, 1989 g , 211.4 Overail-Measurement of Effectiveness '
" This.section is-under development.
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2.2 -ASSURANCE OF OUALITY 2.2.1 Summary of Problem The Quality Assurance Program has not been an effective management tool.
2.2.2 Discussion Improvement in quality assurance has been a major emphasis in 1989.
Major actions have been completed including strengthening the Quality
-Assurance management and involving Quality Assurance in all aspects of plant operations. The continuation of the plan to improve PGE's assurance of quality at Trojan will be approached on two fronts. First, attitudes toward quality assurance will continue to be improved through a series of team building programs and by emphasis on quality by the management team. Second, while improvements in the attitudes toward quality assurance and teamwork will help improve quality at Trojan, this plan would be incomplete without delineating further improvements to the Quality Assurance Program. Quality Assuranc.e Program enhancements will seek to improve the technical capabilities of the NQAD organization.
Additionally, the Quality Assurance Program is being reevaluated to assure it provides a viable, critical self-assessment function for management. This change will require that performance-based techniques become a cornerstone of the program while continuing to pursue improvements in the ability to identify and effectively correct compliance issues.
2.2.3 Actions Taken/ Planned
- 1. Interdepartmental meetings have been taking place to enhance teamwork. These sessions included NQAD. PGE will further expand these team building sessions. These sessions will bring interdependent work groups together to clarify roles and identify and demonstrate support for common goals. These sessions will be aimed at increasing the understanding of different work group functions and reducing potential conflicts between these groups.
ACTION: General Managers and Department Managers DUE DATE: December 31, 1989
- 2. Future and current vacancies in technical disciplines within NQAD will be filled by degreed personnel whenever possible.
ACTION: General Manager, Quality Assurance DUE DATE: Ongoing b
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- 3. An aggressive training program is being developed to expand the technical skills necessary to implement performance-based QA techniques. This training curriculum will include mechanical and electrical maintenance, instrument and control, plant systems, operations, radiation protection, chemistry, and radiochemistry.
ACTION:- General Manager Quality Assurance DUE DATE: December 15, 1989 L 4. Specific measurable performance standards for NQAD personnel are I
being enhanced to improve communications of expectations and enhance accountability.
ACTION: General Manager, Quality Assurance DUE DATE: October 31, 1989
- 5. Trojan's corrective action systema are currently being reevaluated with the assistance of a consultant to identify enhancements, eliminate duplication, and improve effectiveness.
ACTION: General Manager, Quality Assurance DUE DATE: December 31,. 1989
- 6. Perfonnance-based QA techniques are being established and imple-mented in NQAD audits and surveillance.
ACTION: General Manager, Quality Assurance DUE DATE: Ongoing
- 7. NQAD audit, surveillance and trend reports are being reevaluated for their effectiveness. Nuclear Division management input will be sought to ensure that QA data is presented in a concise, effective and usable format for management.
ACTION: General Manager, Quality Assurance DUE DATE: November 15, 1989
- 8. An audit of NQAD has been requested by the General Manager Quality ;
Assurance and will be performed under the cognizance of the Trojan I Nuclear Operations Board to evaluate the action outlined above and determine if additional actions are necessary.
ACTION: Chairman, Trojan Nuclear Operations Board DUE DATE: December 31, 1989 2.2.4 Dverall Me.asure of Effectiveness This section is under development.
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2.3 OTHER IMPROVEMENT ACTIONS i
2.3.1 Other' Actions Taken/ Planned l
- 1. As a result of the most recent event involving the RHR system, it was identified that enhanced planning was needed to provide addi-tional assurance that maintenance will not be performed simultane-ously on two trains of the same equipment. The Plan of the Day (POD) has been established as the controlling mechanism for work,.
such that only items en the POD can be worked in a given day. The POD is reviewed and approved by.the Duty Plant General Manager.
ACTION: Plant General Manager DUE DATE: Complete
- 2. A qualified senior reactor operator or shift technical advisor will be involved in the maintenance and surveillance planning process to ensure the conditions required for the proposed activities are
- correctly determined. Emphasis will be placed on minimizing the number of times safety-related equipment is taken out of service and where prudent, maintenance will be deferred to modes where safety-related equipment is not required to be operable. Maintenance documentation relating to safety-related equipment will be boldly marked to indicate that safety-related equipment is involved.
ACTION: Plant General Manager DUE DATE: November 30, 1989
- 3. Lessons-learned training will be conducted covering recent events at Trojan. Managers from each work group will be involved in giving this training to their groups to ensure the unique concerns faced by their group in the day-to-day performance of work are fully under-stood and responded to. This training will be a continuing practice.
ACTION: General Manager, Plant Support DUE DATE: December 31, 1989 (initial sessions) 4 The corporation's commitment to nuclear safety will be further demonstrated by establishing a proactive ' Quality Team' to collect, investigate and resolve individual safety concerns. This team will monitor and respond to concerns including those on the current Quality Hotline system. Additionally, employees, including temporaries and contractors, leaving PGE will be interviewed by the team to determine if they have any safety concerns.
ACTION: General Manager, Technical Functions DUE DATE: January 31, 1990
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- 5. .The existing Design Basis Document (DBD) program is being upgraded.
All previously Essued DBDs will be reviewed and revised to provide additional design basis information. In addition, walkdowns of the systems will'be conducted by teams representing systems engineering, design engineering, and quality assurance.
ACTION: General Manager, Technical Functions DUE DATE: August 31, 1990.
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- 6. Significant improvements have been made in engineering in recent years. However, to ensure continued improvements in performance of design-related activities, an engineering Lnprovement program will be developed.
ACTION: Manager, Nuclear Plant Engineering DUE DATE: January 31, 1990 i
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