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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20248B2371998-03-31031 March 1998 Revised Monthly Operating Rept for March 1998 for Indian Point Station Unit 2 ML20029C7801994-03-31031 March 1994 Monthly Operating Rept for Mar 1994 for Indian Point Unit 1. W/940415 Ltr ML20247G5171989-04-30030 April 1989 Monthly Maint Category I Rept Pages from Monthly Operating Rept for Apr 1989 for Indian Point ML20154M5661988-08-31031 August 1988 Monthly Operating Rept for Aug 1988 for Indian Point Station Unit 2 ML20154M5691988-07-31031 July 1988 Revised Page to Monthly Operating Rept for Jul 1988 for Indian Point Station Unit 2 ML20236P9861987-10-31031 October 1987 Monthly Operating Rept for Oct 1987 ML20235Y9681987-09-30030 September 1987 Monthly Operating Rept for Sept 1987 ML20236A5811987-09-30030 September 1987 Monthly Operating Rept for Sept 1987 ML20234D7771987-08-31031 August 1987 Monthly Operating Rept for Aug 1987 ML20237J6511987-07-31031 July 1987 Monthly Operating Rept for Jul 1987 ML20235U7571987-06-30030 June 1987 Monthly Operating Rept for June 1987 ML20215F3711987-05-31031 May 1987 Monthly Operating Rept for May 1987 ML20214H5111987-04-30030 April 1987 Monthly Operating Rept for Apr 1987 ML20214E9541987-04-30030 April 1987 Monthly Operating Rept for Apr 1987 ML20206Q6951987-03-31031 March 1987 Monthly Operating Rept for Mar 1987 ML20206R6201987-03-31031 March 1987 Monthly Operating Rept for Mar 1987 ML20207T1321987-02-28028 February 1987 Monthly Operating Rept for Feb 1987 ML20207R6861987-02-28028 February 1987 Monthly Operating Rept for Feb 1987 ML20206R6451987-02-28028 February 1987 Revised Monthly Operating Rept for Feb 1987 ML20211E1381987-01-31031 January 1987 Monthly Operating Rept for Jan 1987 ML20211J1481987-01-31031 January 1987 Monthly Operating Rept for Jan 1987 ML20212P8891986-12-31031 December 1986 Monthly Operating Rept for Dec 1986 ML20207P9801986-12-31031 December 1986 Monthly Operating Rept for Dec 1986 ML20215E8501986-11-30030 November 1986 Monthly Operating Rept for Nov 1986 ML20211Q0501986-11-30030 November 1986 Monthly Operating Rept for Nov 1986 ML20212L9131986-10-31031 October 1986 Monthly Operating Rept for Oct 1986 ML20214D0211986-10-31031 October 1986 Monthly Operating Rept for Oct 1986 ML20203P1081986-09-30030 September 1986 Monthly Operating Rept for Sept 1986 ML20209J0801986-08-31031 August 1986 Monthly Operating Rept for Aug 1986 ML20214K4281986-07-31031 July 1986 Monthly Operating Rept for Jul 1986 ML20207C3021986-06-30030 June 1986 Monthly Operating Rept for June 1986 ML20207C3171986-06-30030 June 1986 Monthly Operating Rept for June 1986 ML20211F7351986-05-31031 May 1986 Monthly Operating Rept for May 1986 ML20198A2731986-04-30030 April 1986 Monthly Operating Rept for Apr 1986 ML20205P6911986-04-30030 April 1986 Monthly Operating Rept for Apr 1986 ML20141E6071986-03-31031 March 1986 Monthly Operating Rept for Mar 1986 ML20141E6121986-03-31031 March 1986 Monthly Operating Rept for Mar 1986 ML20140B8481986-02-28028 February 1986 Monthly Operating Rept for Feb 1986 ML20154P0171986-02-28028 February 1986 Monthly Operating Rept for Feb 1986 ML20141D2331986-01-31031 January 1986 Monthly Operating Rept for Jan 1986 ML20153E3491986-01-31031 January 1986 Monthly Operating Rept for Jan 1986 ML20140B8541986-01-31031 January 1986 Rev I to Monthly Operating Rept for Jan 1986 ML20140A8211985-12-31031 December 1985 Monthly Operating Rept for Dec 1985 ML20141J1861985-12-31031 December 1985 Monthly Operating Rept for Dec 1985 ML20138P4981985-11-30030 November 1985 Monthly Operating Rept for Nov 1985 ML20138M5941985-11-30030 November 1985 Monthly Operating Rept for Nov 1985 ML20136E8811985-10-31031 October 1985 Monthly Operating Rept for Oct 1985 ML20138J7921985-09-30030 September 1985 Monthly Operating Rept for Sept 1985 ML20205C7241985-08-31031 August 1985 Monthly Operating Rept for Aug 1985 ML20134F6881985-07-31031 July 1985 Monthly Operating Rept for Jul 1985 1998-03-31
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H8501999-10-14014 October 1999 Safety Evaluation Supporting Amend 197 to License DPR-64 ML20206U2551999-02-0909 February 1999 Safety Evaluation Supporting Amend 187 to License DPR-64 ML20236Y1571998-08-0303 August 1998 Part 21 Rept Re ASTM A351,GR. CF8 Matl at Indian Point Being Out of Specifications in Molybdenum & Chromium.Cause & Corrective Actions Are Not Stated ML20236V4281998-07-13013 July 1998 Safety Evaluation of TRs WCAP-14333P & WCAP-14334NP, PRA of RPS & ESFAS Test Times & Completion Times. Repts Acceptable ML20236T5511998-06-24024 June 1998 Consolidated Edison Co of Ny,Indian Point Unit 2,Drill Scenario Number 1998C ML20248B2371998-03-31031 March 1998 Revised Monthly Operating Rept for March 1998 for Indian Point Station Unit 2 ML17264A9381997-07-10010 July 1997 Deficiency Rept Re Potential Safety Hazard Associated w/FM-Alco 251 Engin,High Pressure Fuel tube-catalog: 4401031-2 in Which Dual Failure Mode Exists.Caused by Incorrect Forming Process ML18153A1431997-06-10010 June 1997 Part 21 Rept Re Possible Machining Defect in Certain Stainless Steel Swagelok Tube Fitting Bodies.Facilities Have Been Notified About Possible Problem ML20210E3591997-03-27027 March 1997 Part 21 Rept Re Sorrento Electronics Inc Has Determined Operation & Maint Manual May Not Adequately Define Requirements for Performing Periodic Surveillance of SR Applications.Caused by Hardware Failures.Revised RM-23A ML1005008001997-02-28028 February 1997 Conditional Extension of Rod Misalignment TS for Indian Point 3. ML20115J3981996-07-22022 July 1996 Interim Part 21 Rept Re 3/4 Schedule 80 Pipe Furnished to Consolidated Power Supply.Investigation Revealed Only One Nuclear Customer Involved in Sale of Matl ML20096E5101995-12-31031 December 1995 Resubmitted Rev 13 to QA Program ML17059A3611994-07-0606 July 1994 Emergency Action Level Verification & Validation Rept. ML17311A0181994-05-13013 May 1994 New York State EAL Upgrade Project Verification & Validation Rept. ML20029C7801994-03-31031 March 1994 Monthly Operating Rept for Mar 1994 for Indian Point Unit 1. W/940415 Ltr ML20056E5171993-08-31031 August 1993 Technical Review Rept, Tardy Licensee Actions ML20062J2281993-07-23023 July 1993 Consolidated Edison Co of Ny Indian Point Unit 2,Drill Scenario 1993 ML20118A2681992-12-31031 December 1992 Consolidated Edison Co of Ny Indian Point,Unit 2 Exercise Scenario,1992 ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20096H2301992-05-21021 May 1992 Special Rept:On 920504,south Side Lower Electrical Tunnel Detection Sys 8 Taken Out of Svc for Mod to Reposition Detection Sys Run of Conduit.Detection Sys Declared Operable on 920520 After Mod Completed & Sys Retested ML20079F9181991-05-31031 May 1991 Structural Evaluation of Indian Point,Units 2 & 3 Pressurizer Surge Lines,Considering Effects of Thermal Stratification ML20059E9461990-08-31031 August 1990 Nonproprietary Rev 2 to Indian Point 2 Tube Fatigue Reevaluation ML20059G2011990-07-31031 July 1990 Final Rept on Steam Generator Insp, Repair & Restoration Efforts During 1990 Midcycle Insp ML20058K4151990-06-30030 June 1990 Steam Generator Insp,Repair & Restoration Program Presentation to Nrc ML20058K4121990-06-30030 June 1990 Status Rept,Indian Point Unit 2 Mid-Cycle Steam Generator Insp Presentation to Nrc ML20043A4891990-05-30030 May 1990 Nonproprietary Indian Point Unit 2 Steam Generator Insp, Repair & Restoration Program. ML20042F1441989-12-31031 December 1989 New York Power Authority Annual Rept for 1989. W/900430 Ltr ML19332B9371989-11-30030 November 1989 Nonproprietary Info Presented to NRC Re Indian Point Unit 2 Steam Generator Secondary Side Loose Objects. ML19332D6661989-10-31031 October 1989 Nonproprietary Rev 2 to Indian Point Unit 2 Steam Generator Girth Weld/Feedwater Nozzles Rept Spring,1989 Outage. ML20247J8161989-07-31031 July 1989 Safety Evaluation for UHS Temp Increase to 95 F at Indian Point Unit 3 ML20248B3171989-06-30030 June 1989 Rev 1 to Nonproprietary WCAP-12294, Indian Point Unit 2 Steam Generator Girth Weld/Feedwater Nozzles Rept,Spring 1989 Outage ML20248D3631989-06-30030 June 1989 Rev 1,to Indian Point Unit 3 Reactor Vessel Fluence & Ref Temp PTS Evaluations ML20247N5331989-05-31031 May 1989 Nonproprietary Indian Point Unit 2 Steam Generator Girth Weld/Feedwater Nozzles Rept Spring,1989 Outage ML20247J8071989-05-31031 May 1989 Containment Margin Improvement Analysis for Indian Point Unit 3 ML20247G5171989-04-30030 April 1989 Monthly Maint Category I Rept Pages from Monthly Operating Rept for Apr 1989 for Indian Point ML20244C3311989-04-10010 April 1989 Safety Evaluation Supporting Amend 137 to License DPR-26 ML20248F4211989-03-31031 March 1989 NSSS Stretch Rating-3,083.4 Mwt Licensing Rept ML20235V5931989-03-0202 March 1989 Special Rept:During Cycle 6/7 Refueling Outage Scheduled from Feb-May 1989,openings Will Be Made in Plant Penetration Fire Barriers in Order to Install Various Mods. Fire Watches Posted & Fire Detection Tests Completed ML20248F3001988-12-31031 December 1988 10CFR50.59(b) Rept of Changes,Tests & Experiments Completed in 1988 ML20246E2711988-12-31031 December 1988 Con Edison 1988 Annual Rept ML20196D3011988-10-31031 October 1988 Reactor Vessel Matl Surveillance Program for Indian Point Unit 2 Analysis of Capsule V ML20155H2541988-09-30030 September 1988 Rev 2 to Indian Point Unit 2 (NRC Bulletin 88-008 Thermal Stresses in Piping Connected to RCS) Indentification of Unisolable Piping & Determination of Insp Locations ML20154M5661988-08-31031 August 1988 Monthly Operating Rept for Aug 1988 for Indian Point Station Unit 2 ML20154M5691988-07-31031 July 1988 Revised Page to Monthly Operating Rept for Jul 1988 for Indian Point Station Unit 2 ML20151N7881988-07-31031 July 1988 Rev 1 to Charpy Toughness & Brittle Transition Temp Characterization of HAZ High Hardness Zone of Indian Point Unit 2 Steam Generator Girth Weld by Gleeble Weld Thermal Cycle Simulation ML20006B4741988-05-31031 May 1988 Nonproprietary Indian Point Unit 2 Evaluation for Tube Vibration Induced Fatigue. ML20151N7821988-05-31031 May 1988 Fracture Sensitivity Study of Girth Weld 6 Repaired Configuration,Indian Point Unit 2 ML20153F9161988-04-28028 April 1988 Changes,Tests & Experiments - 1986 ML20151T4681988-01-31031 January 1988 Experimental & Finite Element Evaluation of Spent Fuel Rack Damping & Stiffness 1999-02-09
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OPERATING DATA REPORT 4
Docket No. 50-286 Date 12-01-86
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_ Completed By . L. Kelly Telephone 914-739-8200
' OPERATING STATUS-
- 1. Unit Name: Indian Point No. 3 Nuclear Power Plant Notes
-2. Reporting Period: November 1986 3.. Licensed Thermal Power (MWt):
3025
- 14. -Nameplate Rating (Gross MWe): 1013 J5. Design Electrical Rating (Net MWe): 965
.6 . Maximum Dependable Capacity (Gross MWe): 965
- 7. . Maximum Dependable Capacity (Net MWe): 930
- 8. If Changes Occur in Capacity Ratings (Items Number 3 through 7) Since Last Report.
.Give Reasons:
'9. Power Level to Which Restricted, If Any (Net MWe): 930 Net MWe 10 Reasons for Restrictions, If Any: # 33 Low pressure turbine was modified by replacing two rows of blades with baffle assemblies.
This Month Yr. to Date Cumulative
- 11. Hours In Reporting Period 720 8,016 89,881
- 12. Number of Hours Reactor Was Critical 703.80 5,837.78 53,105.16
- 13. Reactor Reserve Shutdown Hours 0 0 0
- 14. Hours Generator On-Line 698.98 5,688.62 51,321.59
- 15. Unit Reserve Shutdown Hours 0 0 0
- 16. Gross Thermal Energy Generated (MWH) 2,010,045.46 15,507,304 136,285,079
- 17. Gross Electrical Energy Generated OKWH) 640,420 5,020,410 42,584,945
- 18. Net Electrical Generated (MWH) 617,228 4,831,006 40,845,645
- 19. Unit-Service Factor 97.1 71.0 56.9
.20. Unit Availability Factor 97.1 71.0 56.9 21.'-Unit Capacity Factor (Using MDC Net) 92.2 63.3* 49.03*
- 22. Unit Capacity Factor (Using DER Net) ___88.8 62.5 47.1
- 23. Unit Forced Outage Rate ,,,,J.9 23.5 20.1
- 24. Shutdowns Scheduled Over Next 6 Months (Tysd.l te , al Duration of Each):
- Weighted Average Cycle 5/6 Refueling Outage Est. May, 198", , ,
- 25. -If Shut Down at End of Report Period. Estimated Date of Startup:
- 26. Units In Test Statt 1 (Prior to Commercial Operation): Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION ,
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, 8612230144 861130 q PDR ADOCK 05000288 R PDR p.q I
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- g; AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-286 UNIT IP-3 DATE 12-1-86
. COMPLETED BY L. Kelly TELEPHONE (914) 739-8200 MONTH November 1986 1
DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL
- (MWe-Net) (MWe-Net) 1 828 17 934 2 931 18 935 3 932 19 934 4 932 20 931 5 930 21 931 6 931 22- 930 7 932 23 932 8 933 24 932 9 933 25 933 10 933 26 932 11 932 27 424 12 932 28 779 13 932 29 933 14 367 30 934 15 177 31 ---
16 773 INSTRUCTIONS:
On this format, list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.
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UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-286' UNIT NAME Indi n Pri t 3~ '
DATE - 1 >_o1_sc REPORT MONTH November 1986 TELEPHONE 914-739-8200 l
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u o i a F" h o Oe E oUE Licensee a Eo Cause & Corrective 4
$ %$ $ .0 $ " Event 0$ E.3 ' Action to No. Date j:E $ ji Report-# x0 .!" Prevent Recurrence i
14 861114 F 21.02 G 3 86-012-00 EC CKTBRK A While performing wiring verification as part of an~ ongoing drawing update program in No. 31'DC Power Panel, Breaker 16 was inadvertently opened i causing.a unit trip.
- 15 861127 S 0 H 4 N/A CA VALVEX G Load reduction to facilitate repair ori
- charging valve 204-A.
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i 1 2 3 4 F: Forced Reason: Method: . Exhibit F - Instructions.
S: Scheduled A- Equipment Failure (Explain) 1- Manual for Preparation of Data
- B- Maintenance of Test 2- Manual Scram Entry Sheets for Licensee i
C- Refueling
! D- Regulatory Restriction 4- Other (Explain) 0161)
E- Operator Training & License Examination F- Administrative i G- Operational Error (Explain) 5 H- Other (Explain) Exhibit H - Same Source
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.U MONTHLY'I &'C CATEGORY I REPORT ' H November 1986-MONTH WR# DATE EQUIPMENT MALFUNCTION CORRECTIVE ACTION 6269 11/18/86 Reactor Coolant System, Bistable and Resistance' Recalibrated R/E.
Pressurizer Spray Line to Voltage (R/E) board out of Low Temperature Alarm specification.
6220 11/19/86 Gaseous Waste Disposal Transmitter out of calibration. Calibrated indicator.-
System, Vent Header Pressure Transmitter PT-1025 6231 11/19/86 Nuclear Instrument System Chart recorder motor broken. Replaced motor.
.N-41 Power Range Current Recorder 6303 11/20/86 Safety Injection System ' Electrical box filled with Dried and sealed electrical Containment Sump water. box.
Isolation Valve, MOV-885A 6246 11/24/86 Containment Pressure Current to voltage (I/E) Replaced and calibrated Transmitter PT-1422 board not working properly I/E board. Recalibrated and recorder out of calibration. recorder.
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MONTHLY I'& C' CATEGORY I REPORT !
November- 1986~
MONTH WR# DATE EQUIPMENT MALFUNCTION CORRECTIVE ACTION 6160 10/22/86 Radiation Monitoring System, Filter paper advance drive: ' Replaced motor.
Plant Vent Particulate motor not turning properly.
Monitor R-13 6191 11/01/86 Service Water System, Fan Positioner out of calibration. Recalibrated. positioner.
Cooler Unit Temperature control Valve TCV-1103.
6113 11/06/86 Steam Generator Level Indicator reads low. Calibra'ted level' monitor Indicator LI-437C LM-437C.
6120 11/07/86 #35 Service Water Zurn Differential alarm inoperable. Replaced microswitch.
Strainer 6219 11/07/86 Reactor Coolant System, Indication light socket broken.. Replaced light socket.
Pressurizer High Level Bistable 6198 11/12/86 Reactor Coolant System, Indicator out of calibration. Calibrated indicator.
Flow Indicator FI-424 6199 11/12/86 Reactor Coolant System, Indicator out of calibration. Calibrated indicator.
Flow Indicator FI-446 6255 11/12/86 Nuclear Instrument System, Rate circuit and associated Replaced and calibrated N-41 Power Range bistables not working properly, rate circuit and
.bistables.
5097 11/17/86 Component Cooling Water, Indicator inoperative. Replaced flow indicator.
Spent Fuel Pit Cooling Flow Indicator FI-603 6193 11/17/86 Reactor Coolant System, Meter out of calibration. Recalibrated PM-474A.
Channel IV Pressurizer Pressure Meter'PM-474A 5911 11/18/86 Radiation Monitoring System, Noisy indfr'. tor. Replaced indicator.
Containment High. Range R-26 Remote Indicator
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' MONTHLY MAINTENANCE CATEGORY I REPORT. ' :C
=No'vember 1986 MONTH i .
, WRf DATE EQUIPMENT MALFUNCTION CORRECTIVE ACTION- '
Insta'lled new packing.
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9279 11/10/86 No. 32 Service Water Pump Packing leak.
No. 31 Spent Fuel. Pit Pump No pump flow.
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8463 11/14/86 Overhauled' rotating-assembly.
9338 11/14/86
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No. 31 Auxiliary Boiler Overheated bearing. Replaced thrust bearing.
Feed Pump 9311 11/17/86 No. 32 Primary Auxiliary Overheated bearing. Replaced bearing.
Building / Vapor Containment Exhaust Fan d
9363 11/19/86 Boron Injection Heat. Trace Not heating. Replaced section of heat Circuit No. 63 trace.
3 8988 11/21/86 No. 32 Instrument Air Refrigerant charge' low. Recharged' dryer.
3 Refrigerant Dryer J
9412 11/28/86 No. 32 Charging Pump Packing leak. Repacke'd pump.
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SUMMARY
[0F' OPERATING EXPERIENCE NOVEMBER'1986 xIndianPoint. Unit #31wassynchronizedtofthe-busforlatotal'of.698;98 hours0.00113 days <br />0.0272 hours <br />1.62037e-4 weeks <br />3.7289e-5 months <br />, f producing a gross generation of 640,420 MWe for this reporting period.
-On November 14' 1986 at 0923 hours0.0107 days <br />0.256 hours <br />0.00153 weeks <br />3.512015e-4 months <br />'while_ performing a drawing update program-wiring yerification, two operations personnel, under the supervision of a Senior Reactor Operator, were replacing tha twenty-one square . foot metal- cover of. #31
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'DC power panel. ,This metal cover slipped and breaker 16'in #31.DC Power. Panel ,
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was inadvertantly opened causing a:losslof power to No. 311DC Distribution Panel' resulting in a unit. trip. ;No damage to plant equipment occurred during this
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Levent. The unit was returned to service on November 15, at 0624 hours0.00722 days <br />0.173 hours <br />0.00103 weeks <br />2.37432e-4 months <br />.:
On November'27, 1986 at 0030 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> a scheduled load reduction'to approximately 34%. power wasicommenced to: facilitate repair to charging valve 204-A. At.
approximately 1630 hours0.0189 days <br />0.453 hours <br />0.0027 weeks <br />6.20215e-4 months <br /> after the leaking valve was repaired the unit commenced
_ . load escalations to return to 100% power.-
- Indian ^ Point #3 continued to run at 100% power for the remainder of'the
-reporting period. e s
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i-Indian Point 3 Nucteer Power Plant P.O. Box 215 Buchanan, NewWrk 10511 914 739.8200
- > NewWrkPbwer 4# Authority December 3, 1986 IP3-WAJ-059Z IP3-LMK-278H Docket No. 50-286 License No. DPR-64 Director, Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Washington, D.C. 20555 Attention: Document Control Desk
Dear Sir:
Enclosed you will find twelve copies of the monthly operating report relating to Indian Point 3 Nuclear Power Plant for the month of November, 1986.
Very truly yours,
~
JYd2 - M /
liam A. osiger '
Residen anager a:3:05 Enclosures (12 copies) cc: Dr. Thomas E. Murley, Regional Administrator Region 1 U.S. Nuclear Regulatory Co*amission' 631 Park Avenue King of Prussia, Pennsylvania 19406 ,
IP3 Resident Inspectors' Office George Wilverding (SRC), WPO J.C. Brons, WPO S.V. Fuller, NYO W.R. Yario, NYO INPO Records Center Suite 1500 1100 circle 75 Parkway gI Atlanta, Georgia 30339 /
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