ML20214E954
| ML20214E954 | |
| Person / Time | |
|---|---|
| Site: | Indian Point |
| Issue date: | 04/30/1987 |
| From: | Josiger W, Kelly L POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK |
| To: | NRC |
| References | |
| IP3-LMK-0129H, IP3-LMK-129H, IP3-WAJ-026Z, IP3-WAJ-26Z, NUDOCS 8705220339 | |
| Download: ML20214E954 (7) | |
Text
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-OPERATING: DATA l REPORT-__. y. '
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.Date
'05-01-87
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DocketiNo.:;50-286 6O.
,',a' Completed (By~.
L. Kelly 4..
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- Telephone 914-736-8340 -
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\\ < GOPERATING2 STATUS \\
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J1.CUnit(Name: nIndian-Point:No. 3 Nuclear Power Plant"
-Notes
'l2.Q R: porting Period:
April 1987 3..
Licensed Thermal' Power.(MWt):
~3025
,4;fNtmeplate;RatingL(Gross-MWe):
1013 5.-iD3 sign Electrical-Ratingl(Net MWe):
965 f6 M Mzximum Dependable Capacity'(Gross ~MWe): 965
- 7.'TMzximum Dependable Capacity.(Net
- MWe):
930-( 8'.s IIf Changes-Occ'urfitil Capacity Ratings (Items Number 3 ~through 7) Since Last Report.
'Give Reasons:
- 9.
Power Level to.Which Restricted, If Any (Net.MWe):'.930 Net MWe 10.d Reasons for Restrictions,,If Any: 1 33 Low Pressure Turbine was modified by replacing =
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-two rows of blades with baffle assemblies.
a This Month Yr. to Date Cumulative 4
hl'1[.rl Hours!InReporting' Period
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M12, : Number ~of1 Hours' React'or. Was ' Critical.
719#
2,879 93,504 633.42 2,616.52
-56,465.68 f13..."Reac' tor' Reserve. Shutdown Hours' 0
0
.0 14? Hours Generatiorf On-Line' 1
619.25-2,587.93 ~ 54,649.46
- 15. l Unit. Reserve-Shutdown Hours..
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M 16.;, Cross Thermal Energy Generated- (MWH) 1,809,631.89 7,638,285- -146,171,146-
-17MGross; Electrical'EnergyGenerated1(MWH) _
<564,450 2,423,390 45,728,005: >
r18;. Net Electrical. Generated (MWH)i 543,810
- 2,336,093-43,876,373 119.4 Unit' Service Factor'
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86.1
- 89.9 -
58.5-Y20.,UnitjAvailabilityFactor W.
86.1 89.9=
58.5:
'21~.f Unit 1CapacityiFactorl(Using MDC, Net)l 81.3-
-87.3 50.63*J
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22.;., Unit _ Capacity Factor (Using. DER Net):.
78.4 84.1-48.6-4 l23. -Unit Forced. Outage Rate'
&3.5 4.2 19.3-
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924.c Shutdowns Scheduled Over Next 6" Months (Type,Date,and DurationLofTEach):~* Weighted Average f Cycle '5/6 Refueling Outage (5/2/87/ thru 7/30/87)'
2b.UIf h$tsDownat_End'ofReportPeriod..EstimatedDateofStartup:
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in. I.
126;;; Units In' Test Status.(Prior to Commercial _ Operation):
Forecast Achieved.
INITIAL CRITICALITY' a,
INITIAL ELECTRICITY-COMMERCIAL OPERATION f.
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8705220339 870430
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' AVERAGE DAILY UNIT POWER LEVEL
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DOCKET.NO. :50-286-UNIT-IP,
DATE 01 COMPLETED BY
-L. Kelly
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TELEPHONE (914) 736-8340^
s MONTH
' April 1987 DAY
' AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVELE (MWe-Net)
..(MWe-Net) 1 0
17 224 2
'O 18 325' 3
0-19 867' 4
258 20 914 5
857 21 920-
-6 918' 22 918 7
920 23
- 918 8
919 24-919L 9
918 25 920
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10 917 26 916 11 914 27 915 12 913 28 916 13 914 29' 916-14.
912 30 916 15.
915 31 16-914 7
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INSTRUCTIONS:
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-in the reporting month. Compute to the nearest whole megawatt.
On this format, list the average daily unit power level in MWe-Net for each day.
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UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.
'50-286 UNIT NAME Indian Poi-t 3' 1
DATE- 05-01-87 REPORT MONTH APRIL 1987 TELEPHONE 914-736-R340 m
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wUI Licensee a
Ee Cause & Corrective e$
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Event O 45 E.'8 Action to j$
al jd Report i y0 j "'
Prevent Recurrence
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Date 03 870327 S
77.15 B
1 NA-CB PUMPXX B The unit was taken off the line in a controlled shutdown in order to replace No. 33 Reactor Coolant' Pump Sea]
l Package which had been exhibiting increases in. seal return flow.
i 04 870417 F
22.60 A
3 87-004-00 CJ-CKTBRK A A unit trip oc' curred when No. 32 Reactoi Coolant Pump lower oil reservior magnetrol grounded to its metal cover causing a drop'in voltage on instrument bus No. 33.
This resulted in an automatic reactor trip generated by a steam flow / feed flow mismatch coincident with low steam generator level. The oi]
level switch was repaired.
I 2
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F Forced Reason:
Method:
Exhibit F.- Instructions S: tekadulad A-Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance of Test 2-Manual Scram
. Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report-(LER) File (NUREG D-Regulatory Restriction 4-Other (Explain) 0161)
E-Operator Training & License Examination F-A4ministrative G-Operational Error (Explain) 5 N-Other (Explain)
Exhibit H - Same Source
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MONTHIX MAINTENANCE CATECORY I ' REPORT--~
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- "1987?'
.: Ap' hill
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1 MONTH.},J WR#
DATE EQUIPMENT MALFUNCTION-
-CORRECTIVE ACTION-7911 104/02/87f Primary Sampling System,.
LValve does'not stroke open
' Replaced valve' VCT Sample Isolation Valve 265'
' 10181
' 04/02/87 Containment (SuildingPurge
, Valve doec not operate
' Installed plug:.on exhaust Supply Solenoid Valve,.
-port.of'valveL S0V-1277-
' 10142-04/03/87-SteamGeneratorBlowdown,l
' Body t'o bonnet leak-
- RepairedIleaku 31 Steam Generator' Blowdown s
Isolation Valve, BD-1
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10020 04/10/87
- 33 Charging Pump
- 5 Cyclinder. packing leak'
- Repacked' pump-10123 04/13/87
- 31 Boric Acid-Transfer Pump Ruptured valve diaphram' Replaced compressor assembly.
4 Discharge Pressure Cauge-and diaphram Isolation Valve 10231 04/16/87
- 31 Boric icid Transfer; Pump. Valve leaks by; Replaced bonnet.
Discharge Pressure Gauge:
Isolation Valve 10228 04/22/87~
- 31 Boric Acid Transfer:
Pump seals damaged Replaced pump with spare
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.!NONTHLY-I'&LC CATEGORY I.'REPORTL
- -' Q' April W 1987?
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MONTH '
WRf DATE
- EQUIPMENT
- MALFUNCTION -
CORRECTIVE-ACTION'
- 6336, 04/01/87-
- 33 Reactor; Coolant Pump;
, Corroded RTD block:
'Repl' aced RTD and-rewired?
Seal' Inlet Temperature-,
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-1 Element,.TE-153-t,-.
6849-04/01/87' Reactor. Protection Relay.~-
Relay.does not energize.
JReplaced relay.with' spare.
. P-7-2 Train "A"J
'5652 04/01/87 "j
. #34 Reactor' Coolant' Pump Faulty RTD.
Replaced RTD i
. Seal Water Inlet Temperature;
' 0 7-'.
. Element, TE-152-
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6056 04/03/87
- 31 and #34 Reactor. Coolant!
- 31'and #34 RTD's wir'ed
. Repaired wiring.
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Pump Stator Temperature RTD incorrectly.
6846 04/21/87 Reactor Coolant Flow Current to' current (I/I).
Calibrated 2(I/I)
Indicator,'FI-435 isolation out'of calibration.
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6923 04/24/87
' Radiation ~ Monitoring System, ' Monitor: reads.high.
. Replaced and calibrated:
- 32 Main Steam'Line Monitor,
- detector R-62 c
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SUMMARY
.OF OPERATING EXPERIENCE-M
" APRIL 1987; W
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InhianPoint:Nnit #3 was synchronized to the bus for a. total ~of 619.25 hours2.893519e-4 days <br />0.00694 hours <br />4.133598e-5 weeks <br />9.5125e-6 months <br />,-
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producing ~a gros's generation of'564,450 MWe for this. reporting period.
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On March 27th-~at.1848 hours0.0214 days <br />0.513 hours <br />0.00306 weeks <br />7.03164e-4 months <br /> the unit.was taken off the'line-in. order:to repair 7 f.No.'33 Reactor Coolant Pump Se'l Package. In addition, No.;32 RCP Seal ~ Package a
(was replac'ed.a~sfa preventative maintenance effort.t Upon-completion of maintenance'and-testing of-the seal packages, the unit was returned to service--
on April 4th'at 0509 hours0.00589 days <br />0.141 hours <br />8.416005e-4 weeks <br />1.936745e-4 months <br />.-
'On' April 17th at 0555Ihours a unit trip. occurred when No. 32 Reactor Coolant Pump lower oil reservoir magnetrol grounded.to its metal. cover causing. circuit 119 on instrument Bus No. 33 to open.- A drop in voltage on'No.-33 instrument bus w.
occurred res~ulting in an'au'tomatic reactor trip generated by a' steam flow / feed
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flow mismatch. coincident with low steam generator. level. The' failed level-iswitch, which caused the voltage perturbation on -IB No. 33, 'was're' paired.' ;The
= unit was returned.to service on April. 18, 1987 at 0431 hours0.00499 days <br />0.12 hours <br />7.126323e-4 weeks <br />1.639955e-4 months <br /> and-continued-to-
' produce-electricity'for'the remainder of=the reporting period.,
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Inden Point 3 Nuclear Power Plant P.O. Box 215 Buchanan, NewWrk 10511 914 739.8200
- > NewYorkPbwer-tv Authority May 15, 1987 IP3-WAJ-026Z IP3-LMK-0129H Docket No.
50-286 License No. DPR-64 Director, Office of Inspection and Enforcement U.S.-Nuclear. Regulatory Commission Washington, D.C.
20555
Dear Sir:
Enclosed you will find the monthly operating report relating to Indian Point 3 Nuclear Power. Plant for the month of April, 1987.
Very truly yours, O
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'W am A J iger esident a ager Indian P i t 3 nuclear Power Plant sn:3:10 Enclosure cc:
U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.
20555 Dr. Thomas E. Murley, Regional Administrator Region-1 U.S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, Pennsylvania 19406 INPO Records Cettter Suite 1500 1100 Circle 75 Parkway Atlanta, Georgia 30339 f
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