ML20134A726

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Forwards Insp Repts 50-317/85-16 & 50-318/85-14 & Mgt Meeting Repts 50-317/85-72 & 50-318/85-72 on 850624-28 & 0711,respectively.Deficiencies Noted.Enforcement Conference Scheduled for 850814
ML20134A726
Person / Time
Site: Calvert Cliffs  Constellation icon.png
Issue date: 08/08/1985
From: Martin T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Lundvall A
BALTIMORE GAS & ELECTRIC CO.
Shared Package
ML20134A727 List:
References
RTR-NUREG-0737, RTR-NUREG-737 NUDOCS 8508150400
Download: ML20134A726 (2)


See also: IR 05000317/1985016

Text

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AUG 0 81985

Docket Nos. 50-317

50-318

Baltimore Gas and Electric Company

ATTN: Mr. A. E. Lundvall, Jr.

[

Vice President, Supply

P. O. Box 1475

. Baltimore, Maryland 21203

Gentlemen:

Subject: Combined Inspection Report Nos. 50-317/85-16 and 50-318/85-14

On June 24-28, 1985, an announced inspection was conducted by a team led

by Mr. John R. White of our office at the Calvert Cliffs Nuclear Power

Plant, Units 1 and 2, for the purpose of reviewing the licensee's

implementation of certain specifications of NUREG 0737, Clarification of

TMI Action Plan Requirements, relative to post-accident sampling and

monitoring. Enclosure 1 provides the results of that inspection, which

were discussed with Mr. J. A. Tiernan and others of your staff at the

conclusion of the inspection.

Our review of this area indicates that your efforts to implement these

specifications, particularly with regard to post accident sampling were

less than adequate. Significant technical deficiencies were identified

in each area inspected, and several apparent violations with regulatory

requirements were noted. As a result, a management meeting with

representatives of your staff was held on July 11, 1985, at the NRC

' Region I office. Enclosure 2 is a report of that meeting.

Of particular concern is that you appear to have failed to implement and

maintain a post-accident sampling capability in terms of either, (1) the

in-line analytical system that was described in submittals to the

Commission, and confirmed in the NRC " Order Confirming Licensee

Commitments on Post-TMI Related Issues," dated March 14,1983; or (2)

the preplanned alternate sampling method that is required by Technical

Specification 3/4.7.13, " Post Accident Sampling", when the in-line

analytical system is inoperative.

As a result of these findings an Enforcement Conference will be held

with your staff on August 14, 1985, at the NRC Region I Office to

discuss the implications of these findings, the status of corrective

measures completed or planned since this inspection, and determine what

enforcement action is warranted in this matter.

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flotwithstanding the results of that meeting you are requested to respond

in writing relative to the technical deficiencies identified in this

report within 30 days of the date of this letter. Your response should

identify actions taken or planned to resolve the deficiencies noted.

Thank you for your cooperation.

Sincerely, original signed By;

&dQ 00

Thomas T'. Martin, Director

Division of Radiation Safety

and Safeguards

1

Enclosures:

1. Combined NRC Region I Inspection Report Numbers

50-317/85-16 and 50-318/85-14

2. Management Meeting Report Number 85-72

cc w/encls:

R. M. Douglass, Manager, Quality Assurance

L. B. Russell, Plant Superintendent

.

Thomas Magette, Administrator, Nuclear Evaluations

R. C. L. Olson, Principal Engineer

J. A. Tiernan, Manager, Nuclear Power

R. E. Denton, General Supervisor, Training and Technical Services

PublicDocumentRoom(PDR)

Local Public Document. Room (LPDR)

Nuclear Safety Information Center (NSIC)

NRC Resident Inspector

State of Maryland (2)

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bec w/encls:

Region I Docket Room (with concurrences)

Senior Operations Officer (w/o encl)

DRP Section Chief

Jane Axelrad, D/ES

D. Holody, RI

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