ML17352A531

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Monthly Operating Repts for Mar 1994 for Turkey Point Units 3 & 4.W/940413 Ltr
ML17352A531
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 03/31/1994
From: MOWREY C L, PLUNKETT T F
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-94-086, L-94-86, NUDOCS 9404180387
Download: ML17352A531 (14)


Text

ACCELERATED DISTMBUTION DEMONSTRATION SYSTEM t t~REGULATORY INFORMATION DISTRXBUTION SYSTEM (RIDS)ACCESSXON NBR:9404180387 DOC.DATE: 94/03/31 NOTARXZED:

NO FACIL:50-250 Turkey Point Plant,, Unit 3, Florida Power and Light C 50-251 Turkey Point Plant, Unit 4, Florida Power and Light C AUTH.NAME AUTHOR AFFILIATXON MOWREY,C.L.

Florida Power&Light Co.PLUNKETT,T.F.

Florida Power&Light.Co.RECIP.NAME RECIPIENT AFFILXATION DOCKET g 05000250 05000251 gR I

SUBJECT:

Monthly operating repts for Mar 1994 for Turkey Point Units 3&4.W/940413 ltr.DISTRIBUTION CODE: IE24D COPIES RECEIVED:LTR ENCL SIZE: TITLE: Monthly Operating Report (per Tech Specs)NOTES: D A RECIPIENT ID CODE/NAME PD2-2 PD INTERNAL: AEOD/DOA N~RJJ30 S OEAB E~IM 01 EXTERNAL: EG&G BRYCE,J.H NSIC COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME CROTEAU,R AEOD/DS P/TPAB NRR/DRIL/RPEB RGN2 NRC PDR COPXES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 D D D NOTE TO ALL"RIDS" RECIPIENTS'LEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT.20079)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LINIS FOR DOCUMENTS YOU DON'T NEED!TOTAL NUMBER OF COPIES REQUIRED: LTTR 11 ENCL 11 D D

FPL',pp i 8"i934 L-94-086 10 CFR 50.36 U.S.Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.20555 Gentlemen:

Re: Turkey Point Units 3 and 4 Docket Nos.50-250 and 50-251 Monthl 0 eratin Re ort In accordance with the requirements of Turkey Point Units 3 and 4 Technical Specification 6.9.1.5, and the guidance of NUREG-0020, attached are the March 1994 Operating Status and Summary of Operating Experience Reports for Turkey Point Units 3 and 4.Very truly yours, T.F.Plunkett Vice President Turkey Point Plant TFP/CLM/cm Attachments cc: S.D..Ebneter, Regional Administrator, Region II, USNRC T~P.Johnson, Senior Resident Inspector, USNRC, Turkey Point Plant g~OQ QQ5 9404180387 940331 I.I PDR ADOCK 05000250 R , PDR an Fpt Group company I(

1 AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.UNIT DATE COMPLETED BY TELEPHONE 50-250 Turke Point 3 A ril 11 1994 C.L.Mowre 305-246-6204 MONTH MARCH 1994 AVERAGE DAILY POWER LEVEL (MWe-Net)3/01/94 3/02/94 3/03/94 3/04/94 3/05/94 3/06/94 3/07/94 3/08/94 3/09/94 3/10/94 3/11/94 3/12/94 3/13/94 3/14/94 3/15/94 3/16/94 3/17/94 3/18/94 3/19/94 3/20/94 3/21/94 3/22/94 3/23/94 3/24/94 3/25/94 3/26/94 3/27/94 3/28/94 3/29/94 3/30/94 3/31/94 691 692 695 700 698 693 687 682 680 677 681 690 691 687 687 687 684 684 682 677 663 663 660 665 667 666 665 667 668 673 677 UNIT SHUTDOWNS:

AND POWER REDUCTIONS DOCKET NO.UNIT NAME: DATE: COMPLETED BY: TELEPHONE:

50-250 Turke Point$3 A ril 11 1994 C.L.Mowre 305 246-6204 REPORT MONTH MARCH 1994 No.N/A Date N/A Type'/A Duration (Hours)N/A Reason2 N/A Method of Shutting Down Reactor N/A Licensee Event Reports N/A System Code N/A Component code N/A N/A Cause S Corrective Action to Prevent Recurrence F-Forced S-Scheduled Reason A-Equipment Failure B-Maintenance or Test C-Refueling D-Regulatory restriction E-Operator Training S License Examination F-Administrative G-Operational Error (Explain)H-Other (Explain)Method 1-Manual 2-Manual Scram 3-Automatic Scram 4-Continued 5-Load Reduction 9-Other (Explain)Exhibit G-instructions for Preparation of Data Entry Sheets Licensee Event Report (LER)File (NUREG-0161)

Exhibit 1-Same Source

OPERATING STATUS OPERATING DATA REPORT DOCKET NO 50-250 DATE 4/1 1/94 COMPLETED BY C.L.MOWREY TELEPHONE 305/246/6204 1.UNIT NAME: TURKEY POINT UNIT 3 2.REPORTING PERIOD: MARCH 1994 3.LICENSED THERMAL POWER (MWT): 2200 4.NAMEPLATE RATING (GROSS MWE): 760 5.DESIGN ELECTRICAL RATING (NET MWE): 693 6.MAXIMUM DEPEMDAELE CAPACITY (DRESS M~WE 699 7.MAXIMUM DEPENDABLE CAPACITY (NET MWE): 666 8.IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7)SINCE LAST REPORT, GIVE REASONS: 9.POWER LEVEL TO WHICH RESTRICTED, IF ANY (NET MWE)10.REASONS FOR RESTRICTIONS, IF ANY: MONTHLY-YTD-CUMULATIVE 11.HOURS IN REPORT PERIOD: 12.NUMBER OF HOURS REACTOR WAS CRITICAL 13.REACTOR RESERVE SHUTDOWN HOURS 14.HOURS GENERATOR ON-LINE 15.UNIT RESERVE SHUTDOWN HOURS 16.GROSS THERMAL ENERGY GENERATED (MWH)17.GROSS ELECTRICAL ENERGY GENERATED (MWH)18.NET ELECTRICAL ENERGY GENERATED (MWH)19.UNIT SERVICE FACTOR 20.UNIT AVAILABILITY FACTOR 21.CAPACITY FACTOR (USING MDC NET)22.CAPACITY FACTOR (USING DER NET)23.UNIT FORCED OUTAGE RATE 24.SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS CYCLE 014 REFUELING OUTAGE, APRII 744 744.0 0.0 744.0 1637553 529680 505949 100.0 100.0 102.1 98.1 0.0 1994 2160 2160.0 0.0 2112.2 4612879 1507515 1437959 97.8 97.8 100.0 96.1 2.2 186897.6 123420.2 844.4 121645.5 121.8 252752717 81089331 76707464 65.1 65.2 62.6 59.2 11.7 25.IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:

SUMMARY

OF OPERATING EXPERIENCE DOCKET NO.UNIT DATE: COMPLETED BY TELEPHONE:

50-250 Turke Point 3 A ril 11 1994 C.L.Mowre 305 246-6204 REPORT MONTH MARCH 1994 Unit 3 began the month at essentially 100%and maintained that level throughout the month.

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.UNIT DATE COMPLETED BY TELEPHONE 50-251 Turke Point 4 A ril 11 1994 C.L.Mowre 305-246-6204 MONTH MARCH 1994 AVERAGE DAILY POWER LEVEL (MWe-Net)3/01/94 3/02/94 3/03/94 3/04/94 3/05/94 3/06/94 3/07/94 3/08/94 3/09/94 3/10/94 3/11/94 3/12/94 3/13/94 3/14/94 3/15/94 3/16/94 3/17/94 3/18/94 3/19/94 3/20/94 3/21/94 3/22/94 3/23/94 3/24/94 3/25/94 3/26/94 3/27/94 3/28/94 3/29/94 3/30/94 3/31/94 696 696 698 703 701 698 692 688 686 257 0 0 0 0 0 0 0 351 619 676 672 671 671 670 672 673 673 674 675 682 685

~~UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.UNIT NAME: DATE COMPLETED BY: TELEPHONE 50-251 A ril 11 1994 C.L.Mowre 305 246-6204 REPORT MONTH MARCH 1994 No.02 03 Date 031094 031894 Type Duration (Hours)184.77 0.0 Reason Yethod of Shutting Down Reactor Licensee Event Reportf 251-94-002 N/A System Code CC Component Code PIPEXX PIPEXX Cause 4 Corrective Action to Prevent Recurrence Shutdown to repair Yovable Incore Detector Flux Yapper Guide Tube Steam Generator Chemistry Hold-point at 30%F-Forced S-Scheduled Reason A-Equipment Failure B-Haintenance or Test C-Refueling D-Regulatory restriction E-Operator Training 4 License Examination F-Administrative G-Operational Error (Explain)H-Other (Explain)Yethod 1-Yanual 2-Yanual Scram 3-Automatic Scram 4-Continued 5-Load Reduction 9-Other (Explain)Exhibit 0-Instructions for Preparation of Data Entry Sheets Licensee Event Report (LER)File (NUREG-0161)

Exhibit 1-Same Source OPERATING STATUS OPERATING DATA REPORT DOCKET NO 50-251 DATE 4/11/94 COMPLETED BY C.L.MOWREY TELEPHONE 305/246/6204

~~1.UNIT NAME: TURKEY POINT UNIT 4 2.REPORTING PERIOD: MARCH 1994 3.LICENSED THERMAL POWER (MWT): 2200 4.NAMEPLATE RATING (GROSS MWE): 760 5.DESIGN ELECTRICAL RATING (NET MWE): 693 6.MAXIMUM DEPENDASLE CAPACITY (GRDSE M~WE: 699 7.MAXIMUM DEPENDABLE CAPACITY (NET MWE): 666 8.IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7)SINCE LAST REPORT, GIVE REASONS: 9.POWER LEVEL TO WHICH RESTRICTED, IF ANY (NET MWE)10.REASONS FOR RESTRICTIONS>

IF ANY: MONTHLY-YTD-CUMULATIVE 11.HOURS IN REPORT PERIOD: 12.NUMBER OF HOURS REACTOR WAS CRITICAL 13.REACTOR RESERVE SHUTDOWN HOURS 14.HOURS GFNERATOR ON-LINE 15.UNIT RESERVE SHUTDOWN HOURS 16.GROSS THERMAL ENERGY GENERATED (MWH)17.GROSS ELECTRICAL ENERGY GENERATED (MWH)18.NET ELECTRICAL ENERGY GENERATED (MWH)19.UNIT SERVICE FACTOR 20.UNIT AVAILABILITY FACTOR 21.CAPACITY FACTOR (USING MOC NET)22.CAPACITY FACTOR M(USING DER NET)23.UNIT FORCED OUTAGE RATE 24.SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS NONE 744 568.9 0.0 559.2 1210387 392485 372330 75.2=75.2 75.1 72.2 24.8 2160 1984.9 0.0 1975.2 4279371 1396955 1330585 91.4 91.4 92.5 88.9 8.5 180629.0 119265.2 166.6 115300.2 577.3 243339326 77750925 73565817 63.8 64.2 62.1 58.8 12.7 25.IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:

~~~'UMMARY OF OPERATING EXPERIENCE DOCKET NO.UNIT: DATE COMPLETE BY: TELEPHONE:

50-251 Turke Point 4 A ril 11 1994 C.L.Mowre 305 246-6204 REPORT MONTH MARCH 1994 Unit 4 began the month of March at essentially 100%power.On March 10, 1994, the unit was shut down to repair a leak on a guide tube for the Movable Incore Detector flux mapping system.Following completion of the repair, the unit had a hold-point at 30%for steam generator chemistry.

The unit was returned to essentially 100%power on March 19, and remained at that level through the end of the month.