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t AVI.l(AGl. lialLY UNil l'OWI.it I.I. VEL DOCKET NO. Sh25 Ino s an r.uint UNIT No 3 DATE June 1, 1981 | t AVI.l(AGl. lialLY UNil l'OWI.it I.I. VEL DOCKET NO. Sh25 Ino s an r.uint UNIT No 3 DATE June 1, 1981 | ||
, COMPLETED BY - C. Connei1 TELEPllONE 914-739-8200 MONTII M3Y 1981 DAY AVERACE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe Net) (MWe Net) 3 515 37 509 505 513 2 1S 3 '517 39 501 516 4 20 5 513 23 332 | , COMPLETED BY - C. Connei1 TELEPllONE 914-739-8200 MONTII M3Y 1981 DAY AVERACE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe Net) (MWe Net) 3 515 37 509 505 513 2 1S 3 '517 39 501 516 4 20 5 513 23 332 | ||
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<- v i 03 81 05 20 F 10.3 B 3 13/A EA Relay X Direct trip from Buchanan Substation D caused by inadvertent relay operation while trouble shooting grounds. | <- v i 03 81 05 20 F 10.3 B 3 13/A EA Relay X Direct trip from Buchanan Substation D caused by inadvertent relay operation while trouble shooting grounds. | ||
04 81 05 29 F 7.0 B' 3 13/A EA Relay X Direct trip from Buchanan Substation caused by a transfer trip while per-forming relay checks. | 04 81 05 29 F 7.0 B' 3 13/A EA Relay X Direct trip from Buchanan Substation caused by a transfer trip while per-forming relay checks. | ||
; I 2 3 4 | ; I 2 3 4 F. Forced Reason: Method: Exhibit 7. Instructions S: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data R. Maintenance of Test 2-Manual Scram. Entry Sheets for Licensee C-Refueling 3-Automatic Scram. Event Report (1.ER) File (NUREG-D-Regulatory Restriction 4 Other (Explain) 0161) | ||
F. Forced Reason: Method: Exhibit 7. Instructions S: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data R. Maintenance of Test 2-Manual Scram. Entry Sheets for Licensee C-Refueling 3-Automatic Scram. Event Report (1.ER) File (NUREG-D-Regulatory Restriction 4 Other (Explain) 0161) | |||
E-Operator Training & License Examination F Administrative 5 G-Operational Error (Explain) Exhibii II- Same Source 19/77) Il-Oiher (Explain) - ' | E-Operator Training & License Examination F Administrative 5 G-Operational Error (Explain) Exhibii II- Same Source 19/77) Il-Oiher (Explain) - ' | ||
Latest revision as of 18:40, 17 February 2020
ML20004F289 | |
Person / Time | |
---|---|
Site: | Indian Point |
Issue date: | 06/01/1981 |
From: | Connell C POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK |
To: | |
Shared Package | |
ML20004F288 | List: |
References | |
NUDOCS 8106180105 | |
Download: ML20004F289 (6) | |
Text
[
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L-I '
l ; OPERATING DATA REPORT v
DOCKET NO. 50-286 DATE June 1, 1981 COMPLETED BY C. Connell
. TELEPHONE (914) 739-8200 (ext: 242)
OPERATING STATUS
- 1. Unit Name: InrM an Pnine Nn_1 vnn1 ,,, pnunr plane Notes .
- 2. Reporting Period: "#Y 1901 *
- 3. Licensed Thermal Power (MWt): 1025
- 4. Nameplate Rating (Gross MWe): 1013 ,
- 5. Design Electrical Rating (Net MWe): 965
- 6. Maximum Depenlable Capacity (Gross MWe): 926
- 7. Mairnum Deper.dable Capacity (Net MWe): 891
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
None
- 9. Power Level To Which Restricted,If Any (Net MWe): gn7 wn m- n.,4 m pnwn. e nen.)
- 10. Reasons For Restrictions. lf Any: Unit Load is restricted to the canacity of one uain
- transformer.
This Month Yr. to.Date Cumulative
- 11. Hours in Reporting Period 744 3,623 41.664 737.8
- 12. Number Of Hours Reactor Was Critical 2,191.5 28,941.5 2
- 13. Reactor Reserve Shutdown Hours
- 14. Hours Generator On-Line 726.7 2,134.9 27,838
- 15. Unit Reserve Shutdown Hours 16. Gross Thermal Energy Generated (MWH) 1.194.909 a.97.ogo 7, 3no_7,o
- 17. Gross Electrical Energy Generated (MWH) 392.980 _ 1.283.970 22.975.471
- 18. Net Electric I Energy Generated (MWH) 370,071 1,215,573 21,929,733
- 19. Unit Service Factor 97.7 58.9 66.8'
- 20. Unit Availability Factor 97.7 58.9 66.8 l
l 21. Unit Capaci y Factor (Using MDC Net) - 55.8 37.7 59.1-
- 22. Unit Capacity Factor (Using DER Net) 51.5 34.8 54.5
- 23. Unit Forceo Outage Rate 2.3 41.1 '1 F. Y
- 24. Shutdowns Scheduled Over Next 6 Months (Type. Date,and Duration of Each): e.s 2 week shutdown in July to connect new main transformer. -
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup: N/A
- 26. Units in Test Status IPrior to Commercial Operation): Forecast Ac'hieve'd '
INITIA L CRITICALITY N/A N/A INITIA L ELECTRICITY N/A N/A COMM ERCIA L OPER ATION N/A N/A s
8106180 k @ gf773
- ~
t AVI.l(AGl. lialLY UNil l'OWI.it I.I. VEL DOCKET NO. Sh25 Ino s an r.uint UNIT No 3 DATE June 1, 1981
, COMPLETED BY - C. Connei1 TELEPllONE 914-739-8200 MONTII M3Y 1981 DAY AVERACE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe Net) (MWe Net) 3 515 37 509 505 513 2 1S 3 '517 39 501 516 4 20 5 513 23 332
, 513 6_ .
514 22 517 516 7 23 g 517 513 2-(
9 515 511 25 16 509
< 10 26 i
gg 514 514 7
i 517 516 t 12 2S _
13 294 29 14 518 514 30 IS 518 33 515 ___
16 518 INS 1 RUCTIONS On this format. list the aserage daily unit power leselin MWe. Net for each day in the repurong umnth. C 3:npute io
, the nearest whole megawatt.
L (9/77)
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UNIT SilUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-286 '.
UNIT NAME Indian Point #3-DATE Juna 1- 19n1 REPORT MONT1f May 1981 COMPLETED BY C. Connell TELEPlf0NE 914-739-9200 ,
Ext. 242 2 ~
- , 3? 3(; . .Ek Licensee ,E-r, c 1, Cause & Corrective No. Date g gg jgy Esent F? o? Aoion to H
$5 5 Report er LE 0 $U Prevent Recurrence' 5 5 O=@
<- v i 03 81 05 20 F 10.3 B 3 13/A EA Relay X Direct trip from Buchanan Substation D caused by inadvertent relay operation while trouble shooting grounds.
04 81 05 29 F 7.0 B' 3 13/A EA Relay X Direct trip from Buchanan Substation caused by a transfer trip while per-forming relay checks.
- I 2 3 4 F. Forced Reason
- Method: Exhibit 7. Instructions S: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data R. Maintenance of Test 2-Manual Scram. Entry Sheets for Licensee C-Refueling 3-Automatic Scram. Event Report (1.ER) File (NUREG-D-Regulatory Restriction 4 Other (Explain) 0161)
E-Operator Training & License Examination F Administrative 5 G-Operational Error (Explain) Exhibii II- Same Source 19/77) Il-Oiher (Explain) - '
MO!mlLY MAINTENANCE REPORT May 1981 ,
Month W.R. EQUIPMENT MALFUNCTION CORRECTIVE ACTION
) RTE #
,-11 I-1923 CCR A/C Refrig. Compressor Dirty Cooling & Sensing Lines Cleaned Condensers.
CCR A/C Compressors Dirty Cooling & Sensing Lines. Cleaned Condensers
>-11 I-1931 Dirty Cooling & Sensing Lines. Cleaned Condensers i-ll I-1698 CCR A/C
- Valve Seat Damaged Replaced Valve i-15 I-1975 CVCS Valve C-lO2 2-20 1-1739 SOV 1429/1430 Erractic Operation Cleaned / Lubricated Valves
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Summary of Operating Experience May 1981 Indian Point Unit 3 was synchronized to the bus for a total of 726.7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />, producing a gross generation of 392,980 MWe for this reporting period.
The Unit experienced two trips during this reporting period.
The first trip, a direct trip from Buchanan substation, occurred on May 20 at 1909 hours0.0221 days <br />0.53 hours <br />0.00316 weeks <br />7.263745e-4 months <br />. The trip was caused by inadvertent reIty opera-tion while technicians were trouble shooting grounds in the associated relay wiring. The Unit was returned to service at 0527 hours0.0061 days <br />0.146 hours <br />8.713624e-4 weeks <br />2.005235e-4 months <br /> on May 21.
The second trip which was also a direct trip from Buchanan substation, occurred at 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> on May 29. The trip was traced to misoperation while technicians were performing relay checks on 345 KV feeder Y88.
The unit was promptly returned to service at 0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br /> on the same day.
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