ML20004F289
| ML20004F289 | |
| Person / Time | |
|---|---|
| Site: | Indian Point |
| Issue date: | 06/01/1981 |
| From: | Connell C POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK |
| To: | |
| Shared Package | |
| ML20004F288 | List: |
| References | |
| NUDOCS 8106180105 | |
| Download: ML20004F289 (6) | |
Text
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OPERATING DATA REPORT v
DOCKET NO.
50-286 DATE June 1, 1981 COMPLETED BY C. Connell TELEPHONE (914) 739-8200 (ext: 242)
OPERATING STATUS Notes
- 1. Unit Name: InrM an Pnine Nn_1 vnn1,,, pnunr plane
"#Y 1901
- 2. Reporting Period:
- 3. Licensed Thermal Power (MWt):
1025
- 4. Nameplate Rating (Gross MWe):
1013
- 5. Design Electrical Rating (Net MWe):
965
- 6. Maximum Depenlable Capacity (Gross MWe):
926
- 7. Mairnum Deper.dable Capacity (Net MWe):
891
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
None
- 9. Power Level To Which Restricted,If Any (Net MWe):
gn7 wn m-n.,4 m pnwn. e nen.)
- 10. Reasons For Restrictions. lf Any: Unit Load is restricted to the canacity of one uain transformer.
This Month Yr. to.Date Cumulative
- 11. Hours in Reporting Period 744 3,623 41.664
- 12. Number Of Hours Reactor Was Critical 737.8 2,191.5 28,941.5 - 2
- 13. Reactor Reserve Shutdown Hours
- 14. Hours Generator On-Line 726.7 2,134.9 27,838
- 15. Unit Reserve Shutdown Hours !
- 16. Gross Thermal Energy Generated (MWH) 1.194.909 a.97.ogo 7,
3no_7,o
- 17. Gross Electrical Energy Generated (MWH) 392.980 1.283.970 22.975.471
- 18. Net Electric I Energy Generated (MWH) 370,071 1,215,573 21,929,733
- 19. Unit Service Factor 97.7 58.9 66.8' 97.7 58.9 66.8 l
- 20. Unit Availability Factor l
- 21. Unit Capaci y Factor (Using MDC Net) -
55.8 37.7 59.1-51.5 34.8 54.5
- 22. Unit Capacity Factor (Using DER Net)
- 23. Unit Forceo Outage Rate 2.3 41.1
'1 F. Y
- 24. Shutdowns Scheduled Over Next 6 Months (Type. Date,and Duration of Each):
e.s 2 week shutdown in July to connect new main transformer.
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
N/A
- 26. Units in Test Status IPrior to Commercial Operation):
Forecast Ac'hieve'd '
INITIA L CRITICALITY N/A N/A INITIA L ELECTRICITY N/A N/A COMM ERCIA L OPER ATION N/A N/A s
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t AVI.l(AGl. lialLY UNil l'OWI.it I.I. VEL DOCKET NO.
Sh25 Ino s an r.uint UNIT No 3 DATE June 1, 1981 COMPLETED BY - C. Connei1 TELEPllONE 914-739-8200 MONTII M3Y 1981 DAY AVERACE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe Net)
(MWe Net) 515 509 3
37 505 513 2
1S 3
'517 501 39 516 4
20 5
513 23 332 513 514 6_.
22 517 516 7
23 517 513 g
2-(
9 515 25 511 16 509 10 26 i
514 514 gg 7
i 517 516 t
12 2S 294 13 29 14 518 30 514 IS 518 33 515 16 518 INS 1 RUCTIONS On this format. list the aserage daily unit power leselin MWe. Net for each day in the repurong umnth. C 3:npute io the nearest whole megawatt.
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UNIT SilUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-286 UNIT NAME Indian Point #3-DATE Juna 1-19n1 COMPLETED BY C. Connell REPORT MONT1f May 1981 TELEPlf0NE 914-739-9200 Ext. 242
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..Ek Licensee
,E-r, c 1, Cause & Corrective No.
Date g
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jgy Esent F?
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Aoion to Report er LE 0
$U Prevent Recurrence'
$5 5
H 5 5 =@
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O 03 81 05 20 F
10.3 B
3 13/A EA Relay X Direct trip from Buchanan Substation D
caused by inadvertent relay operation while trouble shooting grounds.
04 81 05 29 F
7.0 B'
3 13/A EA Relay X Direct trip from Buchanan Substation caused by a transfer trip while per-forming relay checks.
I 2
3 4
F. Forced Reason:
Method:
Exhibit 7. Instructions S: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data R. Maintenance of Test 2-Manual Scram.
Entry Sheets for Licensee C-Refueling 3-Automatic Scram.
Event Report (1.ER) File (NUREG-D-Regulatory Restriction 4 Other (Explain) 0161)
E-Operator Training & License Examination F Administrative 5
G-Operational Error (Explain)
Exhibii II-Same Source 19/77)
Il-Oiher (Explain)
MO!mlLY MAINTENANCE REPORT May 1981 Month
) RTE W.R.
EQUIPMENT MALFUNCTION CORRECTIVE ACTION
,-11 I-1923 CCR A/C Refrig. Compressor Dirty Cooling & Sensing Lines Cleaned Condensers.
>-11 I-1931 CCR A/C Compressors Dirty Cooling & Sensing Lines.
Cleaned Condensers i-ll I-1698 CCR A/C Dirty Cooling & Sensing Lines.
Cleaned Condensers Valve Seat Damaged Replaced Valve i-15 I-1975 CVCS Valve C-lO2 2-20 1-1739 SOV 1429/1430 Erractic Operation Cleaned / Lubricated Valves
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Summary of Operating Experience May 1981 Indian Point Unit 3 was synchronized to the bus for a total of 726.7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />, producing a gross generation of 392,980 MWe for this reporting period.
The Unit experienced two trips during this reporting period.
The first trip, a direct trip from Buchanan substation, occurred on May 20 at 1909 hours0.0221 days <br />0.53 hours <br />0.00316 weeks <br />7.263745e-4 months <br />. The trip was caused by inadvertent reIty opera-tion while technicians were trouble shooting grounds in the associated relay wiring. The Unit was returned to service at 0527 hours0.0061 days <br />0.146 hours <br />8.713624e-4 weeks <br />2.005235e-4 months <br /> on May 21.
The second trip which was also a direct trip from Buchanan substation, occurred at 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> on May 29.
The trip was traced to misoperation while technicians were performing relay checks on 345 KV feeder Y88.
The unit was promptly returned to service at 0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br /> on the same day.
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