ML19242D115: Difference between revisions
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: 3. Licensed 1 hennal Power (MWt): _ 3025 | : 3. Licensed 1 hennal Power (MWt): _ 3025 | ||
: 4. Nameplate Itatin;;(Gross MWe): _ 1013 | : 4. Nameplate Itatin;;(Gross MWe): _ 1013 | ||
: 5. Design ElectricalItatin;; tNet MWel: | : 5. Design ElectricalItatin;; tNet MWel: | ||
: 6. Maximum Dependable Capaci.y (Gross MWe): - ICOO | : 6. Maximum Dependable Capaci.y (Gross MWe): - ICOO | ||
Line 33: | Line 32: | ||
: 10. I!casons for !!estrictions. If Any: N/A | : 10. I!casons for !!estrictions. If Any: N/A | ||
'lhis Month Yr..t o.Da t e Cumulatise 744 5087 25,584 | 'lhis Month Yr..t o.Da t e Cumulatise 744 5087 25,584 | ||
: 11. !!ours In Rcrortm3 Period 4907.1 20,568 744 | : 11. !!ours In Rcrortm3 Period 4907.1 20,568 744 | ||
: 12. Number Of Hours Reactor Was Critical . | : 12. Number Of Hours Reactor Was Critical . | ||
Line 50: | Line 48: | ||
: 24. Shutdowns S-hednicd Oscr Nest 6 Monti:s (Type. Date.and Duration of f.ich t: | : 24. Shutdowns S-hednicd Oscr Nest 6 Monti:s (Type. Date.and Duration of f.ich t: | ||
Refuelinu Outage Sep teric 1979 2.>. If Shul Dow n At Fud Of !!cport Period !Niiinatcil Date of Startup: | Refuelinu Outage Sep teric 1979 2.>. If Shul Dow n At Fud Of !!cport Period !Niiinatcil Date of Startup: | ||
: 26. Umts In l est St.itus (l'aior to Cunnnercr il Operationi: 1:urceast Achicscil | : 26. Umts In l est St.itus (l'aior to Cunnnercr il Operationi: 1:urceast Achicscil INill Al. Cilll! cal tl Y % __ | ||
INill Al. Cilll! cal tl Y % __ | |||
INill \l. I'I.I'Clllit t rY , | INill \l. I'I.I'Clllit t rY , | ||
COMMI !!CI A l. Ol'1 !! A 1 ION , | COMMI !!CI A l. Ol'1 !! A 1 ION , | ||
3 I ,' | 3 I ,' | ||
79081405m 63 eml | 79081405m 63 eml | ||
AVI.IC AGE I) AILY UNil POWI 1( !.l VLL DOCKET NO. Ch2"6 liio i an Po i n t. | AVI.IC AGE I) AILY UNil POWI 1( !.l VLL DOCKET NO. Ch2"6 liio i an Po i n t. | ||
UNIT No 3 DATE | UNIT No 3 DATE COMPLETED g;y C . Connell TELEPIl0NE 914-739-3200 MONT!! July 1979 DAY AVERAGE D A!LY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL (MWe NetJ (MWe Net) y 618 37 610 615 614 2 18 . | ||
COMPLETED g;y C . Connell TELEPIl0NE 914-739-3200 MONT!! July 1979 DAY AVERAGE D A!LY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL (MWe NetJ (MWe Net) y 618 37 610 615 614 2 18 . | |||
3 617 39 612 615 20 603 4 | 3 617 39 612 615 20 603 4 | ||
5 615 21 6"4 616 593 615 589 7 3 g 614 2.g 594 613 586 9 25 612 26 597 10 | 5 615 21 6"4 616 593 615 589 7 3 g 614 2.g 594 613 586 9 25 612 26 597 10 | ||
Line 69: | Line 61: | ||
27 All 610 636 g | 27 All 610 636 g | ||
33 608 29 635 g 593 638 30 15 604 31 631 16 - | 33 608 29 635 g 593 638 30 15 604 31 631 16 - | ||
Fo' | Fo' INS 1 RUCTIONS On this fornut. hst the nerage daily unit power levelin MWe. Net for each day in the repostnig anonth.Coinpute to the riestest w hole niegawatt. - | ||
INS 1 RUCTIONS On this fornut. hst the nerage daily unit power levelin MWe. Net for each day in the repostnig anonth.Coinpute to the riestest w hole niegawatt. | |||
(9/77) | (9/77) | ||
,. n j n\ OL | ,. n j n\ OL t .i | ||
t .i | |||
)\ | )\ | ||
50-286 UNITS!!UTDOWNS AND POWER REDUCTIONS DOC}:ET NO. . | 50-286 UNITS!!UTDOWNS AND POWER REDUCTIONS DOC}:ET NO. . | ||
UNil N etE Indian Point ,,o . 3 | UNil N etE Indian Point ,,o . 3 DATE 9 'l COMPLETED DY o - r-nM1 REPORT MONTl! July 1979 TELEril0NE 914 73o a2''O | ||
- E E No. Date g | |||
DATE 9 'l COMPLETED DY o - r-nM1 REPORT MONTl! July 1979 TELEril0NE 914 73o a2''O | |||
- E E No. Date | |||
g | |||
.5 ? 3 4 Yl Licensee ,Eg, {% Cause & Corrective 3g g ,g g 5 Esent gg o-3 Action to | .5 ? 3 4 Yl Licensee ,Eg, {% Cause & Corrective 3g g ,g g 5 Esent gg o-3 Action to | ||
$E cf Igg | $E cf Igg | ||
< g Report # to O [U O | < g Report # to O [U O | ||
Line 98: | Line 75: | ||
29 790729 P .7 A 1 N/A IIII VALVEX F Load reduction caused by decreasing condenser vacuum due to low level in boiler feed pump seal collecting tack. | 29 790729 P .7 A 1 N/A IIII VALVEX F Load reduction caused by decreasing condenser vacuum due to low level in boiler feed pump seal collecting tack. | ||
Corrective Action: | Corrective Action: | ||
Serviced level control valve | Serviced level control valve T'* g | ||
T'* g | |||
% l | % l | ||
-eg i | -eg i | ||
Line 108: | Line 83: | ||
(9/77) Il 04her (Explain) Exhibi.B Same Sourec | (9/77) Il 04her (Explain) Exhibi.B Same Sourec | ||
'MO!;THLY MAINTE!!A!!CE REPCRT | 'MO!;THLY MAINTE!!A!!CE REPCRT July 1979 Month DATE W.R. 4 EQUIPME!;T MALFUNCTION CORRECTIVE ACTIO!J 7-5-79 I-569-1B Charging Pump Press. Gauge Weld leak Removed pipe to tubing adapter, stop Valve #229 welded in new one. | ||
July 1979 Month DATE W.R. 4 EQUIPME!;T MALFUNCTION CORRECTIVE ACTIO!J 7-5-79 I-569-1B Charging Pump Press. Gauge Weld leak Removed pipe to tubing adapter, stop Valve #229 welded in new one. | |||
7-13-79 I-576-2 #31 Charging Pump Seals leak Replaced seals in all 5 cylinders 7-15-79 I-578-1A #32 Boric Acid Transfer Mechanical seal leaks Replaced nochanical seal | 7-13-79 I-576-2 #31 Charging Pump Seals leak Replaced seals in all 5 cylinders 7-15-79 I-578-1A #32 Boric Acid Transfer Mechanical seal leaks Replaced nochanical seal | ||
'N | 'N | ||
, 2 "W. | , 2 "W. | ||
MO:THLY I & C CATEGORY I REPORT | MO:THLY I & C CATEGORY I REPORT July 1979 Month Date I W.R. # Equ ipr.c nt | ||
July 1979 Month Date I W.R. # Equ ipr.c nt | |||
* Malfunction Corrective Action 7/23/79 IC-1-432-2 R-ll Containment APD Filter paper does not advanca Corrected misalignment between gear housing and paper drive motor. | * Malfunction Corrective Action 7/23/79 IC-1-432-2 R-ll Containment APD Filter paper does not advanca Corrected misalignment between gear housing and paper drive motor. | ||
T =g Qjd | |||
T =g | |||
Qjd | |||
.a a | .a a | ||
SU.UARY OF CP3RATII;G EXPERIEt;CE July, 1979 Indian Point Unit 3 vas synchronized to the bus for a total of 744 hours, producing a gross gencration of 477,46] mwh for this re-porting period. | SU.UARY OF CP3RATII;G EXPERIEt;CE July, 1979 Indian Point Unit 3 vas synchronized to the bus for a total of 744 hours, producing a gross gencration of 477,46] mwh for this re-porting period. | ||
The unit operated at 70% power for the major part of the month and experienced one scheduled power ascension and one load reduction. | The unit operated at 70% power for the major part of the month and experienced one scheduled power ascension and one load reduction. | ||
Line 138: | Line 99: | ||
At that time, the unit experienced a condenser vacuum transient due tc a failure in level control of Boiler Fced Pump seal collecting tank. Gen-erator output was reduced to 460 mw for approximately one hour. | At that time, the unit experienced a condenser vacuum transient due tc a failure in level control of Boiler Fced Pump seal collecting tank. Gen-erator output was reduced to 460 mw for approximately one hour. | ||
- ,- , j / | - ,- , j / | ||
t j i 0 | t j i 0 | ||
..}} | ..}} |
Latest revision as of 02:32, 2 February 2020
ML19242D115 | |
Person / Time | |
---|---|
Site: | Indian Point |
Issue date: | 08/03/1979 |
From: | Connell C POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK |
To: | |
Shared Package | |
ML19242D109 | List: |
References | |
NUDOCS 7908140516 | |
Download: ML19242D115 (6) | |
Text
to Ol'EltAlING DATA Ill.PoltT DOCKl.T NO. 5 0 h 6 DAll 8/3/79 COM11Eil D !!y C, conne11 TELLPilONE (914 ) 7i"-0200 OPI:lt ATING STAT US Notes
- 1. Unit Name: 3" H m Po i n+-
Mo. 3 Mucim Power Plant
- 2. !!cporting I'eriod: Julv 1979
- 3. Licensed 1 hennal Power (MWt): _ 3025
- 4. Nameplate Itatin;;(Gross MWe): _ 1013
- 5. Design ElectricalItatin;; tNet MWel:
- 6. Maximum Dependable Capaci.y (Gross MWe): - ICOO
"< 5
- 7. blasimum Dependable Capacity (Net MWeJ:
- 8. If Changs Occur in Capacity Ratin;;s (Items Number 3 Throu;;h 7) Since Last Iteport. Gise Reasons:
None
- 9. Power Lese! To Which Restricted. lf Any (Net MWel:
- 10. I!casons for !!estrictions. If Any: N/A
'lhis Month Yr..t o.Da t e Cumulatise 744 5087 25,584
- 11. !!ours In Rcrortm3 Period 4907.1 20,568 744
- 12. Number Of Hours Reactor Was Critical .
0 0 0
- 13. Itcactor Pesene Shutdown llours 4878.5 20,086.2 744
- 14. I!aurs Generatcr On-Line 0 0 0
- 15. Unit !!cscne Shutdown flours 53,921,647 1,601,186 13,520,678
- 16. Grow The mal l nergy Gen; : d (MWil) 17,736,181 477,460 4,353,410
- 17. Gross Electric.il Energy Generaicd (MWill 454,669 4,196,640 17,045,450
- 18. Net Electrical Energy Generated (MWil) lon 95.9 78.5
- 19. Unit Senice I actor 78.5 100 95.9
- 20. Unit As.n!.ibility F.ictor 63.T 85.5 69.0
- 21. Unit Cap.icity Factor (Using MDC Net) 61.3 85.5 69.0
- 22. Unit Capiuty Factor (Using DER Net) 3.9 0 .6
- 23. Unit I orecil Outage R.cre
- 24. Shutdowns S-hednicd Oscr Nest 6 Monti:s (Type. Date.and Duration of f.ich t:
Refuelinu Outage Sep teric 1979 2.>. If Shul Dow n At Fud Of !!cport Period !Niiinatcil Date of Startup:
- 26. Umts In l est St.itus (l'aior to Cunnnercr il Operationi: 1:urceast Achicscil INill Al. Cilll! cal tl Y % __
INill \l. I'I.I'Clllit t rY ,
COMMI !!CI A l. Ol'1 !! A 1 ION ,
3 I ,'
79081405m 63 eml
AVI.IC AGE I) AILY UNil POWI 1( !.l VLL DOCKET NO. Ch2"6 liio i an Po i n t.
UNIT No 3 DATE COMPLETED g;y C . Connell TELEPIl0NE 914-739-3200 MONT!! July 1979 DAY AVERAGE D A!LY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL (MWe NetJ (MWe Net) y 618 37 610 615 614 2 18 .
3 617 39 612 615 20 603 4
5 615 21 6"4 616 593 615 589 7 3 g 614 2.g 594 613 586 9 25 612 26 597 10
!! C '
27 All 610 636 g
33 608 29 635 g 593 638 30 15 604 31 631 16 -
Fo' INS 1 RUCTIONS On this fornut. hst the nerage daily unit power levelin MWe. Net for each day in the repostnig anonth.Coinpute to the riestest w hole niegawatt. -
(9/77)
,. n j n\ OL t .i
)\
50-286 UNITS!!UTDOWNS AND POWER REDUCTIONS DOC}:ET NO. .
UNil N etE Indian Point ,,o . 3 DATE 9 'l COMPLETED DY o - r-nM1 REPORT MONTl! July 1979 TELEril0NE 914 73o a2O
- E E No. Date g
.5 ? 3 4 Yl Licensee ,Eg, {% Cause & Corrective 3g g ,g g 5 Esent gg o-3 Action to
$E cf Igg
< g Report # to O [U O
Present Recurrentt C
29 790729 P .7 A 1 N/A IIII VALVEX F Load reduction caused by decreasing condenser vacuum due to low level in boiler feed pump seal collecting tack.
Corrective Action:
Serviced level control valve T'* g
% l
-eg i
s1 1 2 3
- F: Forced 4 Ressen: Method:
ya S: Schedu!ed A Equ:pment Faiture(Explain) Exhibit F Instructions 1 Manual for Preparation of Data B-Maintenance ci Test 2 Manual Scram. Entry Sheets for Licensee C Refueling 3 Automatic Scram D-Regulatory Restriction Esent Report ILER) File (NUREG-4-Ot her (E xplain ) 0161) 1 -Operator Training 1 License Examination F AJnanistr:tbe 5 G-Operational Error (Explain)
(9/77) Il 04her (Explain) Exhibi.B Same Sourec
'MO!;THLY MAINTE!!A!!CE REPCRT July 1979 Month DATE W.R. 4 EQUIPME!;T MALFUNCTION CORRECTIVE ACTIO!J 7-5-79 I-569-1B Charging Pump Press. Gauge Weld leak Removed pipe to tubing adapter, stop Valve #229 welded in new one.
7-13-79 I-576-2 #31 Charging Pump Seals leak Replaced seals in all 5 cylinders 7-15-79 I-578-1A #32 Boric Acid Transfer Mechanical seal leaks Replaced nochanical seal
'N
, 2 "W.
MO:THLY I & C CATEGORY I REPORT July 1979 Month Date I W.R. # Equ ipr.c nt
- Malfunction Corrective Action 7/23/79 IC-1-432-2 R-ll Containment APD Filter paper does not advanca Corrected misalignment between gear housing and paper drive motor.
T =g Qjd
.a a
SU.UARY OF CP3RATII;G EXPERIEt;CE July, 1979 Indian Point Unit 3 vas synchronized to the bus for a total of 744 hours0.00861 days <br />0.207 hours <br />0.00123 weeks <br />2.83092e-4 months <br />, producing a gross gencration of 477,46] mwh for this re-porting period.
The unit operated at 70% power for the major part of the month and experienced one scheduled power ascension and one load reduction.
Until July 27, 1979, the urit was operating at 70% power in order to extend the operating cycle. At 14:32 that date, the unit load was increased to 75% power in order to meet with sche duling for a September 15, 1979 Refueling Outage start date. The unit rema; ed at 75% power for the rest of the month.
The load reduction occurred on July 29, 1979 at approximately 19:30.
At that time, the unit experienced a condenser vacuum transient due tc a failure in level control of Boiler Fced Pump seal collecting tank. Gen-erator output was reduced to 460 mw for approximately one hour.
- ,- , j /
t j i 0
..