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{{Adams | |||
| number = ML20209G062 | |||
| issue date = 04/08/1987 | |||
| title = Insp Repts 50-327/87-08 & 50-328/87-08 on 870206-0305. Violation Noted:Failure to Properly Frisk.Deviation Noted: FSAR Commitment to Perform Preventive Maint on Condensate Demineralizer Waste Evaporizer Equipment Not Met | |||
| author name = Branch M, Harmon P, Jenison K, Loveless D, Mccoy F, Poertner W | |||
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) | |||
| addressee name = | |||
| addressee affiliation = | |||
| docket = 05000327, 05000328 | |||
| license number = | |||
| contact person = | |||
| document report number = 50-327-87-08, 50-327-87-8, 50-328-87-08, 50-328-87-8, IEB-80-07, IEB-80-13, IEB-80-14, IEB-80-17, IEB-80-7, IEC-80-06, IEC-80-08, IEC-80-19, IEC-80-6, IEC-80-8, NUDOCS 8704300463 | |||
| package number = ML20209G008 | |||
| document type = INSPECTION REPORT, NRC-GENERATED, INSPECTION REPORT, UTILITY, TEXT-INSPECTION & AUDIT & I&E CIRCULARS | |||
| page count = 16 | |||
}} | |||
See also: [[see also::IR 05000327/1987008]] | |||
=Text= | |||
{{#Wiki_filter:i | |||
pa UNITED STATES | |||
/* rtk''o NUCLEAR REGULATORY COMMISSION | |||
[* '' , REolONli | |||
g ,j 101 MARIETTA STREET, N.W. | |||
*' * ATLANTA. GEORGI A 30323 | |||
\ * * | |||
/ | |||
Report Nos.: 50-327/87-08, 50-328/87-08 | |||
Licensee: Tennessee Valley Authority | |||
500A Chestnut Street | |||
Chattanooga, TN 37401 | |||
Docket Nos.: 50-327 and 50-328 License Nos.: DPR-77 and DPR-79 | |||
Facility Name: Sequoyah Units 1 and 2 | |||
Inspection Conducted: February 6 thru M h 5, 1987 | |||
Inspectors: [ 93 s - YD&te'/87 | |||
'K. M.~ 'Jeftf son, Senior Re Nt nfp~ector Signed | |||
W | |||
P. E.'Ha71nor3-Resident InspeGoF | |||
' | |||
~ | |||
_ | |||
- Y hl | |||
Vate/ Signed | |||
r 1x W | |||
Ifate Signed | |||
/ D. F. T.ovele% G5ioenT. Inspect y[' | |||
/ ( xW | |||
W. K. PoeMner, ResIcent Inspect | |||
~ | |||
A f bl | |||
Ddte 51gned | |||
Wm | |||
'M. W.' Ifranch,' Sequoyah | |||
M A | |||
Star Epc'rdinpr | |||
s%h | |||
' Rate Fig ed | |||
Approved by: - [ </h V~) | |||
F. R. McCby, Chief, Secdtn,A D3te/51gndd | |||
DivisioncfTVAProjects | |||
SUMMARY | |||
Scope: This routine, announced inspection involved inspection onsite by the | |||
Resident Inspectors in the areas of: operational safety verification | |||
(including operations performance, system lineups, radiation protection, ' | |||
safeguards and housekeeping inspections); maintenance observations; review of | |||
previous inspection findings; followup of events; review of licensee identified | |||
items; review of IE Information Notices; and review of inspector followup | |||
items. | |||
In addition this inspection included NRC activities associated with the startup | |||
of Unit 2, which were coordinated by the NRC Sequoyah restart coordinator. | |||
Some of these activities are described in paragraph 15 of this report. | |||
Results: One violation (VIO) and one deviation (DEV) were identified. | |||
VIO 327,328/87-08-03, failure to properly frisk, paragraph 5. | |||
0704300463 070494 | |||
PDR ADOCK 05000327 | |||
G pon | |||
. . | |||
2 | |||
DEV 327,328/87-08-01, deviation from FSAR commitment to perform | |||
presentive maintenance on condensate demineralizer waste evapo- | |||
rator (CDWE) equipment, paragraph 3. | |||
Three unresolved items (URIs) were identified: | |||
URI 327, 328/87-08-02, control room evacuation and plant | |||
shutdown, paragraph 14. | |||
URI 327, 328/87-08-04, inadequate diesel generator test, | |||
paragraph 8. | |||
URI 327, 328/87-08-05, cable tray jumpers, paragraph 8. | |||
. | |||
- - . . . _ _ _ _ _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _____ | |||
. . | |||
REPORT DETAILS | |||
, | |||
1. Licensee Employees Contacted | |||
H. L. Abercrombie, Site Director | |||
*L. M. Nobles, Acting Plant Manager | |||
B. S. Willis, Operations and Engineering Superintendent | |||
*B. M. Patterson, Maintenance Superintendent | |||
R. J. Prince, Radiological Control Superintendent | |||
M. R. Harding, Licensing Group Manager | |||
L. E. Martin Site Quality Manager | |||
D. W. Wilson, Project Engineer ( | |||
R. W. Olson, Modifications Branch Manager | |||
J. M. Anthony, Operations Group Supervisor | |||
R. V. Pierce, Mechanical Maintenance Supervisor | |||
M A. Scarzinski, Electrical Maintenance Supervisor | |||
*H. D. Elkins, Instrument Maintenance Group Manager | |||
J. T. Crittenden, Public Safety Service Chief | |||
*R. W. Fortenberry, Technical Support Supervisor | |||
*G. B. Kirk, Compliance Supervisor | |||
D. C. Craven, Quality Assurance Staff Supervisor | |||
*J. H. Sullivan, Plant Operations Review Staff | |||
*J. L. Hamilton, Quality Engineering Manager | |||
D. L. Cowart, Quality Engineering Supervisor | |||
*H. R. Rogers, Plant Operations Review Staff | |||
*R. H. Buchholz, Sequoyah Site Representative | |||
E. R. Ennis, Assistant to Plant Manager | |||
Other licensee employees contacted included technicians, operators, shift | |||
engineers, security force members, engineers and maintenance personnel. | |||
* Attended exit interview. | |||
2. Exit Interview | |||
The inspection scope and findings were summarized with the plant manager | |||
and members of his staff on March 6,1986. The violation and deviation | |||
described in this report's summary paragraph were discussed. The licensee | |||
acknowledged the inspection findings. The licensee did identify as | |||
proprietary one document reviewed by the inspectors during this inspec- | |||
tion. The document was a Westinghouse setpoint methodology paper and is | |||
addressed in paragraph 4 of this report. No proprietary documentation , | |||
provided by the IIcensee was retained by the inspector and no proprietary | |||
information appears in this report. During the reporting period, frequent | |||
discussions were held with the site director, plant manager and other | |||
managers concerning inspection findings. | |||
3. Licensee Action on Previous Inspection Findings (92702) | |||
(Closed) VIO 327, 328/86-42-06. This violation addressed the proper | |||
installation of heat trace on safety related portions of the chemical and | |||
' | |||
, | |||
i | |||
' | |||
_ . . , , , _ _ _ _ . . _ . - _ , - . , . . - - . . . , . . . - . . , - - , - , , _ . - - - - . - - , - - . - - | |||
. - -- _= - _ . _ .-~_- - _- - - - -- - | |||
. . | |||
! | |||
; volume control system (CVCS). The inspector reviewed the corrective | |||
i | |||
' | |||
actions initiated as a result of the licensee's response, dated | |||
October 24, 1986. The corrective actions appeared to be adequate. This | |||
issue is closed. | |||
. (0 pen) VIO 327, 328/86-28-01. This violation addressed the requirement to | |||
conduct a safety evaluation for system changes in the condensate deminera- | |||
; lizer waste evaporator system (CDWE). The inspector reviewed the correc- | |||
tive actions initiated as a result of the licensee's response, dated | |||
: July 15, 1986. This response stated that "the division of nuclear | |||
engineering (DNE) will prepare an evaluation which addresses the require- | |||
ments of Technical Specification (TS) 6.15, items d through g, by | |||
December 31, 1936." The document was forwarded to the Sequoyah site | |||
director, from DNE, on January 1,1987. The licensee stated in the | |||
i | |||
' | |||
July 15, 1986 response that the document would be approved by the Plant | |||
Operations Review Committee (PORC) within two weeks of the plant's | |||
j acceptance of the report. The evaluation was not PORC reviewed until | |||
; | |||
' | |||
January 23, 1987. It was subsequently approved February 6,1987. The | |||
inspector did review the engineering evaluation, and it appeared to meet | |||
the requirements of an unreviewed safety question determination (USQD) | |||
! | |||
review for normal plant conditions. The delay in processing the safety | |||
evaluation is a deviation from a commitment to the NRC. This issue will | |||
i | |||
be addressed in separate correspondence to the licensee. | |||
! | |||
(Closed) URI 327, 328/86-19-03. Section 11.2.4 of the Final Safety Evalua- | |||
. | |||
tion Report (FSAR) states that "All equipment installed to reduce | |||
! radioactive effluents to the minimum practicable level is maintained in | |||
i good operating order...In order to assure that these conditions are met, | |||
1 | |||
administrative controls are exercised on overall operation of the system; | |||
preventive maintenance is utilized to maintain equipment in peak | |||
condition; and experience available from similar plants is used in | |||
i planning for operation at Sequoyah nuclear plant." The inspector was not | |||
t | |||
able to identify any routine preventive maintenance performed on the CDWE | |||
, | |||
system and there is no objective evidence that industry experience is used | |||
; in planning for operation of the CDWE. The licensee is currently reviewing | |||
l changes to the FSAR and as of August 1986, has implemented a process to | |||
l establish preventive maintenance on required equipment. One of the | |||
: current FSAR changes proposed by the licensee is to eliminate the | |||
! requirement for preventive maintenance in this section of the FSAR. This | |||
j issue, which was previously addressed as URI 327, 328/86-19-03 is a | |||
: deviation from a commitment made in the FSAR, and will be identified as | |||
DEV 327, 328/87-08-01. | |||
l 4. Unresolved Items | |||
! | |||
Unresolved items are matters about which more information is required to | |||
I determine whether they are acceptable or may involve violations or | |||
; deviations. Three unresolved items were identified during this inspection, | |||
: and are identified in paragraphs 8 and 14. | |||
: | |||
(Closed) URI 327, 328/85-18-01, Operability of containment spray pump 1A. | |||
This item concerned the fact that the initial flow rates for containment | |||
! | |||
spray pump 1A were greater than 5500 gpm but dropped to 3500-4000 gpm in | |||
i | |||
i | |||
! | |||
. - . , - - . - _ - , , , . - - - _ . - . - . - . - _ _ , . _ , - , - - - , - , _ . - | |||
- - _ _ ____-__________ ._ _ __ _ _ _ _ _ _ _ _ _ ._______ _ _________ ________ _____________________-_ ___-_____ | |||
. . | |||
3 | |||
April 1981 and thereafter. The unresolved item concerned whether or not | |||
the pump was operable. The licensee's investigation revealed that the | |||
flow element (annubar) was bent. The licensee plans to replace the flow | |||
element prior to unit startup. This item is closed. | |||
4 (0 pen) URI 327, 328/87-02-03, Use of work request (WR) to perform | |||
modification by installing drip pans in control room ceiling. The | |||
inspector questioned the use of a WR to perform this work on the control | |||
building. The following items were reviewed with the licensee: | |||
a. The inspector discussed the effect of the installed drip pans on the | |||
operability of the ventilation system to which they were attached. | |||
The licensee had a PORC approved USQD to indicate that the drip pans | |||
would not affect the qualifications of the ventilation system. The | |||
overall weight of the gutters and pans was estimated to be around 85 | |||
pounds. This weight was distributed over a large area, | |||
b. The design was reviewed to determine the effect of the pans falling | |||
on safety related equipment located below them. The licensee stated | |||
that the false ceiling in the control room was a sturdy structure | |||
that could withstand the weight of the gutters falling. Considering | |||
' | |||
the weight distribution and the construction of the ceiling material | |||
the inspector considers this to be a plausible assumption. | |||
The licensee stated that the gutters were designed so that water | |||
would drain and not pool over the control panels. Therefore, the | |||
water leakage, should the pans fail, would only be that roof leakage | |||
; directly over the control panels. The only problem area determined | |||
at this time is the leakage directly over the CVCS panel. This panel | |||
" | |||
is required to assure that a boric acid flow path to the reactor is | |||
available per TS in this mode. | |||
During times of maximum leakage, the inspector estimated that | |||
approximately five gallons of water was collected in the entire | |||
system over a four day period. This indicates a leakage of less | |||
than one drop per minute. This should allow considerable time for | |||
operator action to catch the drips should the pans fail. In | |||
addition, the licensee stated that auxiliary unit operators (AU0s) | |||
could be dispatched to the 690 penetration room and to the boric acid | |||
pumps and a flow path to the reactor could be established in 3-5 | |||
minutes, | |||
c. Licensee procedures were reviewed to determine that appropriate | |||
actions were taken in installing the drip pans. The licensee | |||
installed the drip pans under WR 8214608 with an approved USQD from | |||
DNE. The approach and documentation used is consistent with the way | |||
the licensee would install temporary shielding or scaf folding as | |||
addressed in AI-33, Temporary Shielding of Radiation. | |||
d. The inspector expressed concern that permanent corrective action | |||
should be implemented in a timely manner. The licensee stated that | |||
the roofing material used on the control building roof requires that | |||
specific temperature and moisture parameters be met before the | |||
installation would be effective. Therefore, a warm Spring day during | |||
. . - _ _ _ - . __ _ _ _ | |||
- _ - - - _ - -__ - -. . _ - -. .. . | |||
. . | |||
4 | |||
a dry spell would be required. The licensee anticipated the roofing | |||
repair to be complete by the middle of April, | |||
e. The history of the control building roof leakage was reviewed to | |||
determine the appropriateness of the licensees action. Operations | |||
personnel discussed that initial leakage had been detected in the | |||
winter of 1985/86. This is consistent with the hypothesis that the | |||
roof damage was caused during the implementation of the " power block" | |||
security concept in the summer of 1985. Operations personnel stated | |||
that the leakage was never very bad and stopped in the early spring. | |||
In December 1986 the leakage started again and a WR was initiated to | |||
correct the problem. Following this maintenance, engineering per- | |||
sonnel discovered potential leakage paths. These were caulked until | |||
such time that permanent repairs could be made. The next rain no | |||
leakage was noted. The next storm was accompanied by very cold | |||
weather and resulted in a large amount of leakage. This indicated a | |||
temperature dependant crack. The drip pans were installed following | |||
this storm. | |||
The inspector does not consider this issue to be of safety-significance | |||
in this mode of operation but does consider the timeliness of actions to | |||
again be indicative of recognized problems in timely implementation of | |||
corrective actions. The licensee has stated that permanent control | |||
building roof repairs will be made prior to escalation into mode 4. | |||
This item will remain open pending satisfactory completien of roof | |||
repairs. | |||
(0 pen) URI 327, 328,/87-02-11, Reactor coolant system (RCS) spills from | |||
open steam generator (SG) manways. This item will remain open pending | |||
completion of licensee investigations. At the end of the present | |||
reporting period, two separate investigations by TVA were in progress; an | |||
investigationbytheplantoperationsreviewstaff(PORS),andtheNuclear | |||
Manager s Review Group (NMRG). The findings and conclusions of these | |||
independent investigations will be reviewed as part of the resolution | |||
process for this item. | |||
(0 pen) URI 327, 328/86-20-09, Containment penetration general design | |||
criteria. The inspector reviewed the following documents: | |||
" | |||
TVA letter Gridley/Youngblood L44 860530 807, dated May 30, 1986 - | |||
response to NRC's request for additional information made during a | |||
telephone conference call on May 15, 1986. | |||
* | |||
TVA letter Gridley/Youngblood S10 870129 800, dated January 29, | |||
1987 exemption from 10 CFR 50, Appendix A, general design criteria | |||
55 and 56 for RHR supply line from loop 1 and 2 hot legs and vacuum | |||
relief lines. | |||
" | |||
TVA lei.ter Gridley/Youngblood S10 870116 879, dated December 24, | |||
1986 - exemption from 10 CFR 50, Appendix A, general design criteria | |||
55 for reactor coolant pump seal injection lines. | |||
" | |||
NRC letter Olshinski/ White dated April 23, 1986 - forwarding inspec- | |||
tion report 327, 328/86-20. | |||
____ _ __. .__ _ ._ _ _ __. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ | |||
. . | |||
5 | |||
* | |||
TVA letter Gridley/Youngblood S10 861224 859, dated December 24, | |||
1986 - exemption from Appendix J leak testing for residual heat | |||
removal and upper head injection systems and pressure relief valves. | |||
* | |||
TVA letter Gridley/Youngblood L44 870102 804, dated January 2, 1987 - | |||
response to NRC questions concerning Sequoyah's containment isolation | |||
system design. | |||
* NRC minutes of August 13, 1986 meeting to discuss containment isola- | |||
tion. | |||
* | |||
! TVA minutes of August 13, 1986 meeting to discuss containment isola- | |||
tion. | |||
. | |||
J | |||
Based on the above stated review, it was determined that the commitments | |||
made by the licensee in TVA letter Gridley/Youngblood, dated January 2, | |||
1987 addressed the scope of URI 327, 328/86-20-09. Several of the | |||
commltments made by the licensee are long term in nature and do not | |||
represent issues that would prevent the startup of either unit. This | |||
unresolved item will remain open pending final resolution by NRR and TVA. | |||
, | |||
" | |||
' (Closed) URI 327, 328/86-19-03, FSAR commitment on the CDWE system. This | |||
unresolved item was discussed in paragraph 3 of this report and resulted | |||
in deviation 327,328/87-08-01. This item is closed. | |||
(Closed) URI 327, 328/86-19-04, Alert and evacuate personnel in the CDWE | |||
building. This unresolved item reviewed the regulrements to notify | |||
operators in the CDWE building of the need to evacuate and/or a condition | |||
of high airborne activity. There is one portable airborne monitor in the : | |||
CDWE building and it appeared to be operable. The licensee depends on ! | |||
administrative means, System Operating Instruction (501) - 77.183, to | |||
evacuate personnel from the CDWE building. This 501 requires the shift | |||
engineer to direct the CDWE operator when to evacuate. This process does | |||
not appear to be the most conservative policy. However, the inspector was ! | |||
; not able to identify any instances where oaerators needed to be removed | |||
j from the CDWE building and were not. The inspector was also not able to | |||
l identify any instances of excessive internal contamination of personnel. | |||
1 This item is closed. | |||
; | |||
(Closed) URI 327, 328/85-46-12, Adequacy of measuring and test equipment | |||
, used to adjust reactor protection system (RPS) setpoints. The inspector | |||
, reviewed the following documents both of which contained proprietarj | |||
' | |||
information: | |||
j NRCmemoThompson(NRR)/Gibson(RII)datedOctober1985 | |||
Westinghouse setpoint methodology for RPS dated September 1986 | |||
, | |||
; | |||
The adequacy of the measuring and test equipment used to calibrate and | |||
i adjust RPS setpoints was adequately addressed by the above two documents. | |||
Th s item is c'osed. | |||
. | |||
(0 pen) URI 327, 328/86-32-07, Testing of CREV Isolation in Chlorine Mode. | |||
This item is discussed in paragraph 7. , | |||
; | |||
- - _ _ - _ - _ _ - _ - - - - _ _ _ - _ - _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ - _ _ - - - - . _ - - - - - - | |||
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ | |||
. . | |||
6 | |||
5. Operational Safety Verification (71707) | |||
' | |||
l | |||
. | |||
a. Plant Tours | |||
The inspectors observed control room operations, reviewed applicable | |||
logs, conducted discussions with control room operators, observed | |||
i shif t turnovers, and confirmed operability of instrumentation. The | |||
inspectors verified the operability of selected emergency systems, | |||
and verified compliance with technical specification (TS) limiting | |||
I | |||
conditions for operation (LCO). The inspectors verified that main- | |||
tenance work orders had been submitted as required and that followup | |||
: activities and prioritization of work was accomplished by the | |||
, | |||
licensee. l | |||
Tours of the diesel generator, auxiliary, control, and turbine | |||
. | |||
buildings, and containment were conducted to observe plant equipment | |||
conditions, including potential fire hazards, fluid leaks, excessive | |||
: | |||
vibrations and plant housekeeping / cleanliness conditions. | |||
: The inspectors walked down accessible portions of the following | |||
i | |||
safety-related systems on Unit 1 and Unit 2 to verify operability and | |||
proper valve alignment: | |||
l Condensate Demineralizer Waste Evaporator Package | |||
Chemical Volume and Control System (Unit 2) | |||
l Component Cooling System (Unit 1) | |||
' | |||
No violations or deviations were identified. | |||
l | |||
i b. Safeguards Inspection | |||
l In the course of the monthly activities, the inspectors included a | |||
i review of the licensee's physical security program. The performance | |||
i of various shif ts of the security force was observed in the conduct | |||
' | |||
of daily activities including protected and vital area access | |||
i | |||
controls; searching of personnel and packages; escorting of visitors; | |||
, | |||
badge issuance and retrieval; patrols and compensatory posts. | |||
; In addition, the | |||
! protected and vitalinspectors observed | |||
areas' barrier protected | |||
integrity. Thearea lighting, | |||
inspectors ver i- | |||
i fled an interface between the security organization and operations or | |||
! | |||
maintenance. Spectfically, the resident inspectors: i | |||
l | |||
interviewed individuals with security concerns | |||
; inspected security during outages | |||
; reviewed a licensee security event report | |||
No violations or deviations were identified. I | |||
1 | |||
I i | |||
; i | |||
i | |||
i | |||
. . | |||
7 | |||
c. Radiation Protection | |||
The inspectors observed health physics (HP) practices and verified | |||
implementation of radiation protection control. On a regular basis, | |||
radiation work permits (RWPs) were reviewed and specific work activi- | |||
ties were monitored to ensure the activities were being conducted in | |||
accordance with applicable RWPs. Selected radiation protection | |||
instruments were verified operable and calibration frequencies were | |||
reviewed. | |||
During an auxiliary buildinc tour, the inspectors identified two | |||
craftsmen performing activit'es under work plan 12344 and RWP 252. | |||
The work being performed involved boring into cement with a large | |||
electrical drill . The workers did not have breathing protection and | |||
there was no air monitor near their activities. An HP supervisor was | |||
asked to evaluate these activities. This will be reviewed during | |||
the routine inspection program. | |||
During an auxiliary building tour the inspectors observed approx- | |||
imately six workers exit the radiologically controlled area (RCA) | |||
without properly frisking. tasks in the | |||
auxiliary building while wearing heavy work gloves.The workers were perf | |||
their gloves at the frisking station, frisked their hands and then | |||
replaced their gloves. The gloves were not frisked prior to leaving | |||
the area. TS 6.11 requires that procedures for personnel radiation | |||
protectian be prepared consistent with the requirements of 10 CFR 20 | |||
and shall be approved, maintained and adhered to for all operations | |||
involving personnel radiation exposure. Radiological Controls (RC) | |||
-1, Radiological Control Program, implements this requirement. RC-1 | |||
states that employees are responsible for properly monitoring them- | |||
selves prior to leaving RCAs. This is a violation 327,328/87-08-03. | |||
6. Engineered Safety features Walkdown (71710) | |||
The inspector verified operability of the residual heat removal system on | |||
Units 1 and 2 by completing a walkdown of the systems. | |||
No violations or deviations were identified. | |||
7. Monthly Surveillance Observations (61726) | |||
The inspectors observed / reviewed the below listed TS required surveillance | |||
testing and verified that testing was performed in accordance with | |||
adequate procedures; that test instrumentation was calibrated; that LCOs | |||
were met; that test results met acceptance criteria requirements and were | |||
reviewed by personnel other than the individual directing the test; that | |||
deficiencies were identified, as appropriate, and that any deficiencies | |||
identified during the testing were properly reviewed and resolved by | |||
. . | |||
8 | |||
management personnel; and that system restoration was adequate. For | |||
complete tests, the inspector verified that testing frequencies were met | |||
and tests were performed by qualified individuals. | |||
SI-304 Boric Acid Transfer Pump, with temporary change 87-141. | |||
The procedural change provides for pump data acquisition | |||
using special test instruinentation to comply with ASME | |||
section XI requirements for instrument accuracy. The local | |||
pump suction and discharge gages do not meet the accuracy | |||
and range standards of section XI. The change also pro- | |||
vided for a lineup deviation that changed the flow path | |||
from the boron injection tank (BIT), which is drained and | |||
not in service, to a recirculation path to and from the | |||
boric acid tank (BAT). The recirculation path provides | |||
back pressure conditions similar to the normal BAT to pump | |||
to BIT flow path conditions. The inspector will determine | |||
if the special test, when completed, meets the requirements | |||
of ASME section XI for system resistance. | |||
51-196 CalibrationofUpperHeadInjectionSystemInstrumentation. | |||
The licensee was using newly purchased test instrumentation | |||
to calibrate level switch LS-87-22, which isolates the | |||
upper head accumulator by closing valve 2-87-22. The new | |||
test equipment was | |||
Static 0-Ring (50R)type purchased | |||
switches.specifically to calibrate the | |||
SMI-0-43-1 Special Maintenance Instruction Chlorine Detector Func- | |||
tional Test. The inspector reviewed the following tests | |||
and documents in order to determine if the functional test | |||
of the chlorine detectors met the commitments made by the | |||
licensee in the Final Safety Analysis Report (FSAR). | |||
Work Recuest B227205 | |||
Standarc Practice (SQ) M - 2, Maintenance Management | |||
SQA-66,PlantHousekeeping | |||
51-240, Functional Test of Control Room Air Intake | |||
Chlorine Detection System | |||
As a result of the review it was determined that SMI-0-43-1 | |||
performed the functional test by placing sodium hyoochlo- | |||
rite near the detector. An activation time of approx- | |||
imatel | |||
tion. y 4 seconds | |||
The test didwas | |||
not achieved | |||
appear to by boththe | |||
satisfy trains of ventila- | |||
FSAR require- | |||
ment to test the ventilation intake to 'Le detector and | |||
therefore may not have satisfied the comm'tments as stated | |||
in the FSAR. This issue will be followed under URI 327, | |||
328/86-32-07 which will remain open. | |||
51-204.2 Functional Test of the Radiation Monitoring System. During | |||
a review of this surveillance it was determined that | |||
certain calculations were not independently verified. The | |||
. . | |||
9 | |||
licensee identified this issue two days before the | |||
inspector during a surveillance instruction review of | |||
SI-83.2. The licensee had implemented adequate corrective | |||
action through its surveillance instruction review program. | |||
This issue is considered to be a licensee identified item | |||
and will be considered as a component of the surveillance | |||
instruction program review. | |||
TS 5.5.1 Meteorological Tower. TS 5.5.1 states that, "The meteoro- | |||
logical tower shall be located as shown on Figure 5.1-1." | |||
The tower is not indicated in figure 5.1-1. This was | |||
brought to the attention of the 11censee. The licensee | |||
stated that this discrepancy had already been noted and was | |||
in the process of being corrected. A TS change request | |||
will be submitted by the licensee to the NRC prior to | |||
restart of unit 2 to correct this discrepancy. | |||
8. Monthly Maintenance Observations (62703) | |||
Station maintenance activities of safety-related systems and components | |||
were observed / reviewed to ascertain that they were conducted in accordance | |||
with approved procedures, regulatory guides, industry codes and standards, | |||
and in conformance with TS. | |||
The following items were considered during this review: LCOs were met | |||
while components or systems were removed from service; redundant | |||
components were operable approvals were obtained prior to initiating the | |||
work; activities were ac;complished using approved procedures and were | |||
inspected as applicable; procedures used were adequate to control the | |||
activity; troubleshooting activities were controlled and the repair record | |||
accurately reflected what actually took place; functional testing and/or | |||
calibrations were performed prior to returning components or systems to | |||
service; quality control records were maintained; activities were accom- | |||
plished by qualified personnel; parts and materials used were properly | |||
certified; radiological controls were implemented; QC hold points were | |||
established where required and were observed; fire prevention controls | |||
were implemented; outside contractor force activities were controlled in | |||
accordance with the approved quality assurance (QA) program; and house- | |||
keeping was actively pursued. | |||
The inspectors witnessed the disassembly of 2-FCV-3-103, the Unit 2 main | |||
feed control valve to steam generator 4. The valve was being disassembled | |||
to inspect its internals for indications of erosion-corrosion as part of | |||
the licensee's response to the feed line break at Surry, Maintenance | |||
personnel used maintenance instruction (MI)-11.12, Disassembly and Repair | |||
of Main Feedwater Regulating Valves 1,2-fCV-3-35,48,90, and 103. Minor | |||
indications were found at the valve internals and at the pipe elbow | |||
directly below the valve. Repairs will be effected to this elbow. The | |||
other three elbows will be inspected and repaired in a similar fashion. | |||
The inspectors witnessed performance of special maintenance instruction | |||
DPS0 SMI-1-DG, which verifies the functional operability of the emergency | |||
diesel generators (EDGs). Specifically, the inspector observed the | |||
. _ _ - . . . - - - . . . - . _ - - _~ .~ -- . .. | |||
. | |||
d | |||
. . | |||
10 | |||
i successful testing of the generator phase differential fault relay | |||
circuit. Af ter activating the fault relay, the technician is required to | |||
, attempt to start the EDG locally to ensure the relay locks out the start | |||
circuit. The procedure does not require a similar start attempt from the | |||
remote start panel (main control room). The inspector questioned whether | |||
a all circuits were adequately tested. This item will be followed as URI | |||
l 327, 328/87-08-04. | |||
1 | |||
Work plan 12365 was reviewed to evaluate whether field change request | |||
(FCR) 5142 was implemented in accordance with modifications and additions | |||
! instruction (M and AI) - 7. FCR 5142 addressed a cable tray jumper that | |||
. | |||
did not incorporate the use of a conduit. This will be followed as URI | |||
. 327, 328/87-08-05. | |||
! | |||
! | |||
The inspectors identified some portions of spent fuel pool piping that was | |||
; deformed. The apparent cause of the deformation was incorrectly applied | |||
! | |||
expansion tabs. The issue was discussed with the acting plant manager, who | |||
, | |||
in turn requested the Sequoyah project engineer to evaluate the issue. In | |||
j a memo Nobles / Wilson dated February 2, 1987, the licensee determined that | |||
i the deformation was the result of welding that was performed on these | |||
relatively thin walled pipes. The licensee further determined that there | |||
: | |||
were no safety considerations because the integrity of the pipe had not | |||
i been compromised. The inspector had no further questions. | |||
No violations or deviations were identified. | |||
) 9. Licensee Event Report (LER) Followup (92700) | |||
! The following LERs were reviewed and closed. The inspector verified that: | |||
reporting requirements had been met; causes had been identified; correc- | |||
; tive actions appeared appropriate; generic applicability had been | |||
: considered; the LER forms were complete; the licensee had reviewed the | |||
! event; no unreviewed safety questions were involved; and no violations of | |||
I regulations or TS conditions had been identified. | |||
; | |||
! LERs Unit 1 | |||
l 327/85-045 Diesel Generator Start. A review of this event determined that | |||
i this was an example of inadequate control of safety related maintenance | |||
, which resulted in damage to breaker connection pins. | |||
1 | |||
LERs Unit 2 | |||
i' 328/86-004 Incore Computer Program. The licensee's corrective actions to | |||
require independent verification for data used to determine incore flux | |||
mapping and other soft ware computer data entries appears to be adequate. | |||
I i | |||
! | |||
! | |||
: | |||
) | |||
4 | |||
_ _ _ _ . _ _ _ . _ _ _ _ _ ___._ _ _ _ _ _ _ _ . _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ . _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ __ _ _ _ | |||
. -_ -. .-. . | |||
. . | |||
11 | |||
10. Event Followup (93702, 62703) | |||
During the inspection period, the licensee made two separate immediate | |||
notification phone calls: | |||
On February 27, 1987, the licensee notified NRC through the emergency | |||
notification system (ENS) of an inadvertent emergency diesel genera- | |||
tor (EDG) start. The event was caused by personnel error involving | |||
i | |||
an instrument technician conducting a test of a breaker trip relay. | |||
The technician attached test leads to the wrong relay, and tripped | |||
the shutdown board instead of the intended ERCW pump feeder breaker. | |||
The EDGs started, load sheading on the affected bus occurred, and | |||
the EDG tied onto the deenergized bus. All blackout loads sequenced | |||
on correctly. After verifying off-site power availability, the | |||
operators reset the blackout relays, paralleled to off-site, and | |||
restored normal power to the bus. All ESF functions worked as | |||
required. This event will be further reviewed as part of the LER | |||
followup inspection program once the LER is issued. | |||
; On February 27, 1987, the licensee made a ENS notification of a late | |||
. report under the guidelines of 10CFR 50.72.b.2.iii. Continuing | |||
1 | |||
investigation of the RCS spill event of January 28, 1987, revealed | |||
that both trains of RHR had been out of service as a result of air | |||
binding of the RHR pumps. This condition was evidenced by pump | |||
' | |||
cavitation (pump amperage oscillation), flow variation, and miniflow | |||
recirc valve opening on the running pump. A conservative assumption | |||
is that both pumps were or would have become inoperable until proper | |||
RCS level was restored. | |||
a No deviations or violations were identified. | |||
11. IE Information Notices (92701) | |||
: The following IE Circulars (IECs) were reviewed and closed. The inspector | |||
verified that: corrective actions appeared appropriate; ceneric applica- | |||
; bility had been considered; the licensee had reviewed the event and that | |||
' | |||
appropriate plant personnel were knowledgeable; no unreviewed safety | |||
questions were involved; and that violations of regulations or TS condi- | |||
, | |||
. | |||
tions did not appear to occur. | |||
(Closed) IEC-80-06 Implant Therapy Sources. This IEC was transmit- | |||
i ted to medical licensees only and is not generic to | |||
Sequoyah. | |||
(Closed) IEC-80-08 BWR RPS Response Time. This IEC was written | |||
' | |||
discussing a difference between General Electric TS and the | |||
i design basis. This was not applicable to Sequoyah. | |||
(Closed) IEC-80-19 Noncompliance with License Requirements for | |||
Medical Licensees. This IEC was not applicable to | |||
Sequoyah. | |||
4 | |||
$ | |||
i | |||
,_.-e ._. . . _ . , _ . , _ _ _ _ _ _ _ . . _ . . . . . . _ , , , , . - , . . . _ . . - . . , _ , _ . . . _ _ _ _ , . - . _ _ . . , - _ , | |||
. . | |||
12 | |||
12. IE Bulletins (92703) | |||
IE Bulletins are documents issued by the NRC which require certain | |||
specific actions of the addressee. The ins'pector has reviewed the actions | |||
taken by the licensee as a response to the below listed IE Bulletins | |||
(IEBs). The inspector verified that: corrective actions appeared | |||
appropriate; generic applicability had been considered; the licensee had | |||
reviewed the event and that appropriate plant personnel were knowledge- | |||
able; no unreviewed safety questions were involved; and that violations of | |||
regulations or TS conditions did not appear to occur. | |||
(Closed) IEB-80-07 BWR Jet Pump ' Assembly Failure. This IEB was | |||
written to discuss problems with crack indications in Jet | |||
Pumps and is not applicable to Sequoyah. | |||
(Closed) IEB-80-13 Cracking in Core Spray Spargers. This IEB | |||
discussed problems generic to BWR equipment only. It is | |||
not applicable to Sequoyah. | |||
(Closed) IEB-80-14 Degradation of BWR Scram Discharge Volume | |||
Capacity. This form of scram system is used in BWR's only | |||
and is not applicable to Sequoyah. | |||
(Closed) IEB-80-17 Failure of Control Rods to Insert During a | |||
Scram at a BWR. This IEB discusses an event which occurred | |||
at Browns Ferry where the control rods failed to insert | |||
because of a hydraulic lock in the scram discharge volume. | |||
The rods at Sequoyah fall iato the core on a trip and do | |||
not require the functioning of a hydraulic system. This | |||
item is not applicable to Sequoyah. | |||
13. Inspector Followup Items | |||
Inspector followup items (IFIs) are matters of concern to the inspector | |||
which are documented and tracked in inspection reports to allow further | |||
review and evaluation by the inspector. The following IFIs have been | |||
reviewed and evaluated by the inspector. The inspector has either | |||
resolved the concern identified, determined that the licensee has | |||
performed adequately in the area, and/or determined that actions taken by | |||
the licensee have resolved the concern. | |||
l (Closed) IFI 327, 328/85-46-08, Temporary Alterations | |||
l | |||
l | |||
(Closed) IFI 327, 328/86-20-01, Temporary Alteration Program | |||
Improvements | |||
l The above two IFIs address the use and control of temporary alterations | |||
l on safety-related systems. The licensee committed to the Institute of | |||
Nuclear Power Operations (INP0) to clear all temporary alterations that | |||
l were in place on January 1,1984, before unit 1 startup following | |||
l cycle 4 completion. After the NRC identified the above IFIs the licensee | |||
did an engineering study on the then existing 64 safety related temporary | |||
alterations. The licensee determined that four outstanding temporary | |||
alterations required review and/or correction prior to the startup of | |||
l | |||
Unit 2. The licensee's corrective actions in this areas will be monitored | |||
! | |||
_ | |||
. . | |||
13 | |||
during the NRC maintenance team review of Nuclear Manager's Review Group | |||
(NMRG) item H-1 which was found to be open in inspection report 327, | |||
328/87-15. These followup items are administratively closed. | |||
(Closed) IFI 327, 328/86-15-02, Waste Evaporator Leak. | |||
The inspector reviewed the licensee's corrective actions to correct a | |||
defective seam in the CDWE building wall. Engineering change notices | |||
L6558 and L6417 were reviewed. The inspector had no further questions. | |||
This item is closed. | |||
14. Control Room Evacuation (71707) | |||
The inspector reviewed A0I-27, Control Room Inaccessibility. The pro- | |||
cedure describes the actions to be taken should the control room become | |||
uninhabitable. The procedure requires the dispatching of more personnel | |||
than are required as a minimum on-shift in TS 6.2.2.a. Appendix A of | |||
10 CFR 50 requires in GDC 19 that equipment at appropriate locations out- | |||
side the control room be provided with a design capability for prompt hot | |||
shutdown of the reactor, including necessary instrumentation and controls | |||
to maintain the unit in a safe condition during hot shutdown. This | |||
criteria is addressed in Regulatory Guide (RG) 1.68.2, Initial Startup | |||
Test Program to Demonstrate Remote Shutdown Capability for Water-Cooled | |||
Nuclear Power Plants. This RG states that startup testing should demon- | |||
strate that the number of personnel available to conduct the shutdown | |||
operation is sufficient to perform the many actions required by the | |||
procedure in a timely, coordinated manner. | |||
The documentation available on the startup test as described in item | |||
SU-1.2A of Table 14.1-3 in the FSAR will be reviewed. The following | |||
issues will be resolved: | |||
- | |||
Whether there is sufficient personnel and guidance to perform a safe | |||
and orderly shutdown from outside the control room with a minimum | |||
shift crew per the TS. | |||
- | |||
Whether procedures are adequate to address the limiting case of | |||
minimum shift manning. | |||
- | |||
Whether the initial startup test was performed utilizing the | |||
personnel indicated in the procedure or the TS minimum, and whether | |||
the procedure was adequate. | |||
This will be identified as URI 327,328/87-08-02. | |||
15. Startup Activities | |||
During this inspection period the inspector continued the review of | |||
Sequoyah readiness for restart. This review concentrated on evaluation of | |||
, . | |||
14 | |||
the numerous list of items that TVA considers non-restart for Sequoyah | |||
Unit 2. The lists being reviewed include the following: | |||
* | |||
Work requests | |||
Deficiency reports | |||
* | |||
* | |||
Problem identification reports | |||
Significant condition reports | |||
Condition adverse to quality reports | |||
Corrective action reports | |||
Employee concerns deficiency reports | |||
In addition to the above lists the inspector will review the " satellite" | |||
programs such as design baseline and employee concerns, to ensure imple- | |||
mentation of the restart criteria described in Standard Practice SQA-191, | |||
" Evaluation of Operational Readiness Prior to Plant Restart". | |||
16. TVA management changes: | |||
E. R. Ennis - appointed Assistant to the Plant Manager | |||
D. C. Craven - temporarily appointed to assist the surveillance instruc- | |||
tion review manager | |||
R. W. Fortenberry - temporarily appointed to assist the surveillance | |||
instruction review manager | |||
; | |||
. | |||
I | |||
}} |
Latest revision as of 12:10, 19 December 2021
ML20209G062 | |
Person / Time | |
---|---|
Site: | Sequoyah |
Issue date: | 04/08/1987 |
From: | Branch M, Harmon P, Jenison K, David Loveless, Mccoy F, Poertner W NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
To: | |
Shared Package | |
ML20209G008 | List: |
References | |
50-327-87-08, 50-327-87-8, 50-328-87-08, 50-328-87-8, IEB-80-07, IEB-80-13, IEB-80-14, IEB-80-17, IEB-80-7, IEC-80-06, IEC-80-08, IEC-80-19, IEC-80-6, IEC-80-8, NUDOCS 8704300463 | |
Download: ML20209G062 (16) | |
See also: IR 05000327/1987008
Text
i
pa UNITED STATES
/* rtko NUCLEAR REGULATORY COMMISSION
[* , REolONli
g ,j 101 MARIETTA STREET, N.W.
- ' * ATLANTA. GEORGI A 30323
\ * *
/
Report Nos.: 50-327/87-08, 50-328/87-08
Licensee: Tennessee Valley Authority
500A Chestnut Street
Chattanooga, TN 37401
Docket Nos.: 50-327 and 50-328 License Nos.: DPR-77 and DPR-79
Facility Name: Sequoyah Units 1 and 2
Inspection Conducted: February 6 thru M h 5, 1987
Inspectors: [ 93 s - YD&te'/87
'K. M.~ 'Jeftf son, Senior Re Nt nfp~ector Signed
W
P. E.'Ha71nor3-Resident InspeGoF
'
~
_
- Y hl
Vate/ Signed
r 1x W
Ifate Signed
/ D. F. T.ovele% G5ioenT. Inspect y['
/ ( xW
W. K. PoeMner, ResIcent Inspect
~
A f bl
Ddte 51gned
Wm
'M. W.' Ifranch,' Sequoyah
M A
Star Epc'rdinpr
s%h
' Rate Fig ed
Approved by: - [ </h V~)
F. R. McCby, Chief, Secdtn,A D3te/51gndd
DivisioncfTVAProjects
SUMMARY
Scope: This routine, announced inspection involved inspection onsite by the
Resident Inspectors in the areas of: operational safety verification
(including operations performance, system lineups, radiation protection, '
safeguards and housekeeping inspections); maintenance observations; review of
previous inspection findings; followup of events; review of licensee identified
items; review of IE Information Notices; and review of inspector followup
items.
In addition this inspection included NRC activities associated with the startup
of Unit 2, which were coordinated by the NRC Sequoyah restart coordinator.
Some of these activities are described in paragraph 15 of this report.
Results: One violation (VIO) and one deviation (DEV) were identified.
VIO 327,328/87-08-03, failure to properly frisk, paragraph 5.
0704300463 070494
PDR ADOCK 05000327
G pon
. .
2
DEV 327,328/87-08-01, deviation from FSAR commitment to perform
presentive maintenance on condensate demineralizer waste evapo-
rator (CDWE) equipment, paragraph 3.
Three unresolved items (URIs) were identified:
URI 327, 328/87-08-02, control room evacuation and plant
shutdown, paragraph 14.
URI 327, 328/87-08-04, inadequate diesel generator test,
paragraph 8.
URI 327, 328/87-08-05, cable tray jumpers, paragraph 8.
.
- - . . . _ _ _ _ _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _____
. .
REPORT DETAILS
,
1. Licensee Employees Contacted
H. L. Abercrombie, Site Director
- L. M. Nobles, Acting Plant Manager
B. S. Willis, Operations and Engineering Superintendent
- B. M. Patterson, Maintenance Superintendent
R. J. Prince, Radiological Control Superintendent
M. R. Harding, Licensing Group Manager
L. E. Martin Site Quality Manager
D. W. Wilson, Project Engineer (
R. W. Olson, Modifications Branch Manager
J. M. Anthony, Operations Group Supervisor
R. V. Pierce, Mechanical Maintenance Supervisor
M A. Scarzinski, Electrical Maintenance Supervisor
- H. D. Elkins, Instrument Maintenance Group Manager
J. T. Crittenden, Public Safety Service Chief
- R. W. Fortenberry, Technical Support Supervisor
- G. B. Kirk, Compliance Supervisor
D. C. Craven, Quality Assurance Staff Supervisor
- J. H. Sullivan, Plant Operations Review Staff
- J. L. Hamilton, Quality Engineering Manager
D. L. Cowart, Quality Engineering Supervisor
- H. R. Rogers, Plant Operations Review Staff
- R. H. Buchholz, Sequoyah Site Representative
E. R. Ennis, Assistant to Plant Manager
Other licensee employees contacted included technicians, operators, shift
engineers, security force members, engineers and maintenance personnel.
- Attended exit interview.
2. Exit Interview
The inspection scope and findings were summarized with the plant manager
and members of his staff on March 6,1986. The violation and deviation
described in this report's summary paragraph were discussed. The licensee
acknowledged the inspection findings. The licensee did identify as
proprietary one document reviewed by the inspectors during this inspec-
tion. The document was a Westinghouse setpoint methodology paper and is
addressed in paragraph 4 of this report. No proprietary documentation ,
provided by the IIcensee was retained by the inspector and no proprietary
information appears in this report. During the reporting period, frequent
discussions were held with the site director, plant manager and other
managers concerning inspection findings.
3. Licensee Action on Previous Inspection Findings (92702)
(Closed) VIO 327, 328/86-42-06. This violation addressed the proper
installation of heat trace on safety related portions of the chemical and
'
,
i
'
_ . . , , , _ _ _ _ . . _ . - _ , - . , . . - - . . . , . . . - . . , - - , - , , _ . - - - - . - - , - - . - -
. - -- _= - _ . _ .-~_- - _- - - - -- -
. .
!
- volume control system (CVCS). The inspector reviewed the corrective
i
'
actions initiated as a result of the licensee's response, dated
October 24, 1986. The corrective actions appeared to be adequate. This
issue is closed.
. (0 pen) VIO 327, 328/86-28-01. This violation addressed the requirement to
conduct a safety evaluation for system changes in the condensate deminera-
- lizer waste evaporator system (CDWE). The inspector reviewed the correc-
tive actions initiated as a result of the licensee's response, dated
- July 15, 1986. This response stated that "the division of nuclear
engineering (DNE) will prepare an evaluation which addresses the require-
ments of Technical Specification (TS) 6.15, items d through g, by
December 31, 1936." The document was forwarded to the Sequoyah site
director, from DNE, on January 1,1987. The licensee stated in the
i
'
July 15, 1986 response that the document would be approved by the Plant
Operations Review Committee (PORC) within two weeks of the plant's
j acceptance of the report. The evaluation was not PORC reviewed until
'
January 23, 1987. It was subsequently approved February 6,1987. The
inspector did review the engineering evaluation, and it appeared to meet
the requirements of an unreviewed safety question determination (USQD)
!
review for normal plant conditions. The delay in processing the safety
evaluation is a deviation from a commitment to the NRC. This issue will
i
be addressed in separate correspondence to the licensee.
!
(Closed) URI 327, 328/86-19-03. Section 11.2.4 of the Final Safety Evalua-
.
tion Report (FSAR) states that "All equipment installed to reduce
! radioactive effluents to the minimum practicable level is maintained in
i good operating order...In order to assure that these conditions are met,
1
administrative controls are exercised on overall operation of the system;
preventive maintenance is utilized to maintain equipment in peak
condition; and experience available from similar plants is used in
i planning for operation at Sequoyah nuclear plant." The inspector was not
t
able to identify any routine preventive maintenance performed on the CDWE
,
system and there is no objective evidence that industry experience is used
- in planning for operation of the CDWE. The licensee is currently reviewing
l changes to the FSAR and as of August 1986, has implemented a process to
l establish preventive maintenance on required equipment. One of the
- current FSAR changes proposed by the licensee is to eliminate the
! requirement for preventive maintenance in this section of the FSAR. This
j issue, which was previously addressed as URI 327, 328/86-19-03 is a
- deviation from a commitment made in the FSAR, and will be identified as
DEV 327, 328/87-08-01.
l 4. Unresolved Items
!
Unresolved items are matters about which more information is required to
I determine whether they are acceptable or may involve violations or
- deviations. Three unresolved items were identified during this inspection,
- and are identified in paragraphs 8 and 14.
(Closed) URI 327, 328/85-18-01, Operability of containment spray pump 1A.
This item concerned the fact that the initial flow rates for containment
!
spray pump 1A were greater than 5500 gpm but dropped to 3500-4000 gpm in
i
i
!
. - . , - - . - _ - , , , . - - - _ . - . - . - . - _ _ , . _ , - , - - - , - , _ . -
- - _ _ ____-__________ ._ _ __ _ _ _ _ _ _ _ _ _ ._______ _ _________ ________ _____________________-_ ___-_____
. .
3
April 1981 and thereafter. The unresolved item concerned whether or not
the pump was operable. The licensee's investigation revealed that the
flow element (annubar) was bent. The licensee plans to replace the flow
element prior to unit startup. This item is closed.
4 (0 pen) URI 327, 328/87-02-03, Use of work request (WR) to perform
modification by installing drip pans in control room ceiling. The
inspector questioned the use of a WR to perform this work on the control
building. The following items were reviewed with the licensee:
a. The inspector discussed the effect of the installed drip pans on the
operability of the ventilation system to which they were attached.
The licensee had a PORC approved USQD to indicate that the drip pans
would not affect the qualifications of the ventilation system. The
overall weight of the gutters and pans was estimated to be around 85
pounds. This weight was distributed over a large area,
b. The design was reviewed to determine the effect of the pans falling
on safety related equipment located below them. The licensee stated
that the false ceiling in the control room was a sturdy structure
that could withstand the weight of the gutters falling. Considering
'
the weight distribution and the construction of the ceiling material
the inspector considers this to be a plausible assumption.
The licensee stated that the gutters were designed so that water
would drain and not pool over the control panels. Therefore, the
water leakage, should the pans fail, would only be that roof leakage
- directly over the control panels. The only problem area determined
at this time is the leakage directly over the CVCS panel. This panel
"
is required to assure that a boric acid flow path to the reactor is
available per TS in this mode.
During times of maximum leakage, the inspector estimated that
approximately five gallons of water was collected in the entire
system over a four day period. This indicates a leakage of less
than one drop per minute. This should allow considerable time for
operator action to catch the drips should the pans fail. In
addition, the licensee stated that auxiliary unit operators (AU0s)
could be dispatched to the 690 penetration room and to the boric acid
pumps and a flow path to the reactor could be established in 3-5
minutes,
c. Licensee procedures were reviewed to determine that appropriate
actions were taken in installing the drip pans. The licensee
installed the drip pans under WR 8214608 with an approved USQD from
DNE. The approach and documentation used is consistent with the way
the licensee would install temporary shielding or scaf folding as
addressed in AI-33, Temporary Shielding of Radiation.
d. The inspector expressed concern that permanent corrective action
should be implemented in a timely manner. The licensee stated that
the roofing material used on the control building roof requires that
specific temperature and moisture parameters be met before the
installation would be effective. Therefore, a warm Spring day during
. . - _ _ _ - . __ _ _ _
- _ - - - _ - -__ - -. . _ - -. .. .
. .
4
a dry spell would be required. The licensee anticipated the roofing
repair to be complete by the middle of April,
e. The history of the control building roof leakage was reviewed to
determine the appropriateness of the licensees action. Operations
personnel discussed that initial leakage had been detected in the
winter of 1985/86. This is consistent with the hypothesis that the
roof damage was caused during the implementation of the " power block"
security concept in the summer of 1985. Operations personnel stated
that the leakage was never very bad and stopped in the early spring.
In December 1986 the leakage started again and a WR was initiated to
correct the problem. Following this maintenance, engineering per-
sonnel discovered potential leakage paths. These were caulked until
such time that permanent repairs could be made. The next rain no
leakage was noted. The next storm was accompanied by very cold
weather and resulted in a large amount of leakage. This indicated a
temperature dependant crack. The drip pans were installed following
this storm.
The inspector does not consider this issue to be of safety-significance
in this mode of operation but does consider the timeliness of actions to
again be indicative of recognized problems in timely implementation of
corrective actions. The licensee has stated that permanent control
building roof repairs will be made prior to escalation into mode 4.
This item will remain open pending satisfactory completien of roof
repairs.
(0 pen) URI 327, 328,/87-02-11, Reactor coolant system (RCS) spills from
open steam generator (SG) manways. This item will remain open pending
completion of licensee investigations. At the end of the present
reporting period, two separate investigations by TVA were in progress; an
investigationbytheplantoperationsreviewstaff(PORS),andtheNuclear
Manager s Review Group (NMRG). The findings and conclusions of these
independent investigations will be reviewed as part of the resolution
process for this item.
(0 pen) URI 327, 328/86-20-09, Containment penetration general design
criteria. The inspector reviewed the following documents:
"
TVA letter Gridley/Youngblood L44 860530 807, dated May 30, 1986 -
response to NRC's request for additional information made during a
telephone conference call on May 15, 1986.
TVA letter Gridley/Youngblood S10 870129 800, dated January 29,
1987 exemption from 10 CFR 50, Appendix A, general design criteria
55 and 56 for RHR supply line from loop 1 and 2 hot legs and vacuum
relief lines.
"
TVA lei.ter Gridley/Youngblood S10 870116 879, dated December 24,
1986 - exemption from 10 CFR 50, Appendix A, general design criteria
55 for reactor coolant pump seal injection lines.
"
NRC letter Olshinski/ White dated April 23, 1986 - forwarding inspec-
tion report 327, 328/86-20.
____ _ __. .__ _ ._ _ _ __. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
. .
5
TVA letter Gridley/Youngblood S10 861224 859, dated December 24,
1986 - exemption from Appendix J leak testing for residual heat
removal and upper head injection systems and pressure relief valves.
TVA letter Gridley/Youngblood L44 870102 804, dated January 2, 1987 -
response to NRC questions concerning Sequoyah's containment isolation
system design.
- NRC minutes of August 13, 1986 meeting to discuss containment isola-
tion.
! TVA minutes of August 13, 1986 meeting to discuss containment isola-
tion.
.
J
Based on the above stated review, it was determined that the commitments
made by the licensee in TVA letter Gridley/Youngblood, dated January 2,
1987 addressed the scope of URI 327, 328/86-20-09. Several of the
commltments made by the licensee are long term in nature and do not
represent issues that would prevent the startup of either unit. This
unresolved item will remain open pending final resolution by NRR and TVA.
,
"
' (Closed) URI 327, 328/86-19-03, FSAR commitment on the CDWE system. This
unresolved item was discussed in paragraph 3 of this report and resulted
in deviation 327,328/87-08-01. This item is closed.
(Closed) URI 327, 328/86-19-04, Alert and evacuate personnel in the CDWE
building. This unresolved item reviewed the regulrements to notify
operators in the CDWE building of the need to evacuate and/or a condition
of high airborne activity. There is one portable airborne monitor in the :
CDWE building and it appeared to be operable. The licensee depends on !
administrative means, System Operating Instruction (501) - 77.183, to
evacuate personnel from the CDWE building. This 501 requires the shift
engineer to direct the CDWE operator when to evacuate. This process does
not appear to be the most conservative policy. However, the inspector was !
- not able to identify any instances where oaerators needed to be removed
j from the CDWE building and were not. The inspector was also not able to
l identify any instances of excessive internal contamination of personnel.
1 This item is closed.
(Closed) URI 327, 328/85-46-12, Adequacy of measuring and test equipment
, used to adjust reactor protection system (RPS) setpoints. The inspector
, reviewed the following documents both of which contained proprietarj
'
information:
j NRCmemoThompson(NRR)/Gibson(RII)datedOctober1985
Westinghouse setpoint methodology for RPS dated September 1986
,
The adequacy of the measuring and test equipment used to calibrate and
i adjust RPS setpoints was adequately addressed by the above two documents.
Th s item is c'osed.
.
(0 pen) URI 327, 328/86-32-07, Testing of CREV Isolation in Chlorine Mode.
This item is discussed in paragraph 7. ,
- - _ _ - _ - _ _ - _ - - - - _ _ _ - _ - _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ - _ _ - - - - . _ - - - - - -
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
. .
6
5. Operational Safety Verification (71707)
'
l
.
a. Plant Tours
The inspectors observed control room operations, reviewed applicable
logs, conducted discussions with control room operators, observed
i shif t turnovers, and confirmed operability of instrumentation. The
inspectors verified the operability of selected emergency systems,
and verified compliance with technical specification (TS) limiting
I
conditions for operation (LCO). The inspectors verified that main-
tenance work orders had been submitted as required and that followup
- activities and prioritization of work was accomplished by the
,
licensee. l
Tours of the diesel generator, auxiliary, control, and turbine
.
buildings, and containment were conducted to observe plant equipment
conditions, including potential fire hazards, fluid leaks, excessive
vibrations and plant housekeeping / cleanliness conditions.
- The inspectors walked down accessible portions of the following
i
safety-related systems on Unit 1 and Unit 2 to verify operability and
proper valve alignment:
l Condensate Demineralizer Waste Evaporator Package
Chemical Volume and Control System (Unit 2)
l Component Cooling System (Unit 1)
'
No violations or deviations were identified.
l
i b. Safeguards Inspection
l In the course of the monthly activities, the inspectors included a
i review of the licensee's physical security program. The performance
i of various shif ts of the security force was observed in the conduct
'
of daily activities including protected and vital area access
i
controls; searching of personnel and packages; escorting of visitors;
,
badge issuance and retrieval; patrols and compensatory posts.
- In addition, the
! protected and vitalinspectors observed
areas' barrier protected
integrity. Thearea lighting,
inspectors ver i-
i fled an interface between the security organization and operations or
!
maintenance. Spectfically, the resident inspectors: i
l
interviewed individuals with security concerns
- inspected security during outages
- reviewed a licensee security event report
No violations or deviations were identified. I
1
I i
- i
i
i
. .
7
c. Radiation Protection
The inspectors observed health physics (HP) practices and verified
implementation of radiation protection control. On a regular basis,
radiation work permits (RWPs) were reviewed and specific work activi-
ties were monitored to ensure the activities were being conducted in
accordance with applicable RWPs. Selected radiation protection
instruments were verified operable and calibration frequencies were
reviewed.
During an auxiliary buildinc tour, the inspectors identified two
craftsmen performing activit'es under work plan 12344 and RWP 252.
The work being performed involved boring into cement with a large
electrical drill . The workers did not have breathing protection and
there was no air monitor near their activities. An HP supervisor was
asked to evaluate these activities. This will be reviewed during
the routine inspection program.
During an auxiliary building tour the inspectors observed approx-
imately six workers exit the radiologically controlled area (RCA)
without properly frisking. tasks in the
auxiliary building while wearing heavy work gloves.The workers were perf
their gloves at the frisking station, frisked their hands and then
replaced their gloves. The gloves were not frisked prior to leaving
the area. TS 6.11 requires that procedures for personnel radiation
protectian be prepared consistent with the requirements of 10 CFR 20
and shall be approved, maintained and adhered to for all operations
involving personnel radiation exposure. Radiological Controls (RC)
-1, Radiological Control Program, implements this requirement. RC-1
states that employees are responsible for properly monitoring them-
selves prior to leaving RCAs. This is a violation 327,328/87-08-03.
6. Engineered Safety features Walkdown (71710)
The inspector verified operability of the residual heat removal system on
Units 1 and 2 by completing a walkdown of the systems.
No violations or deviations were identified.
7. Monthly Surveillance Observations (61726)
The inspectors observed / reviewed the below listed TS required surveillance
testing and verified that testing was performed in accordance with
adequate procedures; that test instrumentation was calibrated; that LCOs
were met; that test results met acceptance criteria requirements and were
reviewed by personnel other than the individual directing the test; that
deficiencies were identified, as appropriate, and that any deficiencies
identified during the testing were properly reviewed and resolved by
. .
8
management personnel; and that system restoration was adequate. For
complete tests, the inspector verified that testing frequencies were met
and tests were performed by qualified individuals.
SI-304 Boric Acid Transfer Pump, with temporary change 87-141.
The procedural change provides for pump data acquisition
using special test instruinentation to comply with ASME
section XI requirements for instrument accuracy. The local
pump suction and discharge gages do not meet the accuracy
and range standards of section XI. The change also pro-
vided for a lineup deviation that changed the flow path
from the boron injection tank (BIT), which is drained and
not in service, to a recirculation path to and from the
boric acid tank (BAT). The recirculation path provides
back pressure conditions similar to the normal BAT to pump
to BIT flow path conditions. The inspector will determine
if the special test, when completed, meets the requirements
of ASME section XI for system resistance.51-196 CalibrationofUpperHeadInjectionSystemInstrumentation.
The licensee was using newly purchased test instrumentation
to calibrate level switch LS-87-22, which isolates the
upper head accumulator by closing valve 2-87-22. The new
test equipment was
Static 0-Ring (50R)type purchased
switches.specifically to calibrate the
SMI-0-43-1 Special Maintenance Instruction Chlorine Detector Func-
tional Test. The inspector reviewed the following tests
and documents in order to determine if the functional test
of the chlorine detectors met the commitments made by the
licensee in the Final Safety Analysis Report (FSAR).
Work Recuest B227205
Standarc Practice (SQ) M - 2, Maintenance Management
SQA-66,PlantHousekeeping
51-240, Functional Test of Control Room Air Intake
Chlorine Detection System
As a result of the review it was determined that SMI-0-43-1
performed the functional test by placing sodium hyoochlo-
rite near the detector. An activation time of approx-
imatel
tion. y 4 seconds
The test didwas
not achieved
appear to by boththe
satisfy trains of ventila-
FSAR require-
ment to test the ventilation intake to 'Le detector and
therefore may not have satisfied the comm'tments as stated
in the FSAR. This issue will be followed under URI 327,
328/86-32-07 which will remain open.51-204.2 Functional Test of the Radiation Monitoring System. During
a review of this surveillance it was determined that
certain calculations were not independently verified. The
. .
9
licensee identified this issue two days before the
inspector during a surveillance instruction review of
SI-83.2. The licensee had implemented adequate corrective
action through its surveillance instruction review program.
This issue is considered to be a licensee identified item
and will be considered as a component of the surveillance
instruction program review.
TS 5.5.1 Meteorological Tower. TS 5.5.1 states that, "The meteoro-
logical tower shall be located as shown on Figure 5.1-1."
The tower is not indicated in figure 5.1-1. This was
brought to the attention of the 11censee. The licensee
stated that this discrepancy had already been noted and was
in the process of being corrected. A TS change request
will be submitted by the licensee to the NRC prior to
restart of unit 2 to correct this discrepancy.
8. Monthly Maintenance Observations (62703)
Station maintenance activities of safety-related systems and components
were observed / reviewed to ascertain that they were conducted in accordance
with approved procedures, regulatory guides, industry codes and standards,
and in conformance with TS.
The following items were considered during this review: LCOs were met
while components or systems were removed from service; redundant
components were operable approvals were obtained prior to initiating the
work; activities were ac;complished using approved procedures and were
inspected as applicable; procedures used were adequate to control the
activity; troubleshooting activities were controlled and the repair record
accurately reflected what actually took place; functional testing and/or
calibrations were performed prior to returning components or systems to
service; quality control records were maintained; activities were accom-
plished by qualified personnel; parts and materials used were properly
certified; radiological controls were implemented; QC hold points were
established where required and were observed; fire prevention controls
were implemented; outside contractor force activities were controlled in
accordance with the approved quality assurance (QA) program; and house-
keeping was actively pursued.
The inspectors witnessed the disassembly of 2-FCV-3-103, the Unit 2 main
feed control valve to steam generator 4. The valve was being disassembled
to inspect its internals for indications of erosion-corrosion as part of
the licensee's response to the feed line break at Surry, Maintenance
personnel used maintenance instruction (MI)-11.12, Disassembly and Repair
of Main Feedwater Regulating Valves 1,2-fCV-3-35,48,90, and 103. Minor
indications were found at the valve internals and at the pipe elbow
directly below the valve. Repairs will be effected to this elbow. The
other three elbows will be inspected and repaired in a similar fashion.
The inspectors witnessed performance of special maintenance instruction
DPS0 SMI-1-DG, which verifies the functional operability of the emergency
diesel generators (EDGs). Specifically, the inspector observed the
. _ _ - . . . - - - . . . - . _ - - _~ .~ -- . ..
.
d
. .
10
i successful testing of the generator phase differential fault relay
circuit. Af ter activating the fault relay, the technician is required to
, attempt to start the EDG locally to ensure the relay locks out the start
circuit. The procedure does not require a similar start attempt from the
remote start panel (main control room). The inspector questioned whether
a all circuits were adequately tested. This item will be followed as URI
l 327, 328/87-08-04.
1
Work plan 12365 was reviewed to evaluate whether field change request
(FCR) 5142 was implemented in accordance with modifications and additions
! instruction (M and AI) - 7. FCR 5142 addressed a cable tray jumper that
.
did not incorporate the use of a conduit. This will be followed as URI
. 327, 328/87-08-05.
!
!
The inspectors identified some portions of spent fuel pool piping that was
- deformed. The apparent cause of the deformation was incorrectly applied
!
expansion tabs. The issue was discussed with the acting plant manager, who
,
in turn requested the Sequoyah project engineer to evaluate the issue. In
j a memo Nobles / Wilson dated February 2, 1987, the licensee determined that
i the deformation was the result of welding that was performed on these
relatively thin walled pipes. The licensee further determined that there
were no safety considerations because the integrity of the pipe had not
i been compromised. The inspector had no further questions.
No violations or deviations were identified.
) 9. Licensee Event Report (LER) Followup (92700)
! The following LERs were reviewed and closed. The inspector verified that:
reporting requirements had been met; causes had been identified; correc-
- tive actions appeared appropriate; generic applicability had been
- considered; the LER forms were complete; the licensee had reviewed the
! event; no unreviewed safety questions were involved; and no violations of
I regulations or TS conditions had been identified.
! LERs Unit 1
l 327/85-045 Diesel Generator Start. A review of this event determined that
i this was an example of inadequate control of safety related maintenance
, which resulted in damage to breaker connection pins.
1
LERs Unit 2
i' 328/86-004 Incore Computer Program. The licensee's corrective actions to
require independent verification for data used to determine incore flux
mapping and other soft ware computer data entries appears to be adequate.
I i
!
!
)
4
_ _ _ _ . _ _ _ . _ _ _ _ _ ___._ _ _ _ _ _ _ _ . _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ . _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ __ _ _ _
. -_ -. .-. .
. .
11
10. Event Followup (93702, 62703)
During the inspection period, the licensee made two separate immediate
notification phone calls:
On February 27, 1987, the licensee notified NRC through the emergency
notification system (ENS) of an inadvertent emergency diesel genera-
tor (EDG) start. The event was caused by personnel error involving
i
an instrument technician conducting a test of a breaker trip relay.
The technician attached test leads to the wrong relay, and tripped
the shutdown board instead of the intended ERCW pump feeder breaker.
The EDGs started, load sheading on the affected bus occurred, and
the EDG tied onto the deenergized bus. All blackout loads sequenced
on correctly. After verifying off-site power availability, the
operators reset the blackout relays, paralleled to off-site, and
restored normal power to the bus. All ESF functions worked as
required. This event will be further reviewed as part of the LER
followup inspection program once the LER is issued.
- On February 27, 1987, the licensee made a ENS notification of a late
. report under the guidelines of 10CFR 50.72.b.2.iii. Continuing
1
investigation of the RCS spill event of January 28, 1987, revealed
that both trains of RHR had been out of service as a result of air
binding of the RHR pumps. This condition was evidenced by pump
'
cavitation (pump amperage oscillation), flow variation, and miniflow
recirc valve opening on the running pump. A conservative assumption
is that both pumps were or would have become inoperable until proper
RCS level was restored.
a No deviations or violations were identified.
11. IE Information Notices (92701)
- The following IE Circulars (IECs) were reviewed and closed. The inspector
verified that: corrective actions appeared appropriate; ceneric applica-
- bility had been considered; the licensee had reviewed the event and that
'
appropriate plant personnel were knowledgeable; no unreviewed safety
questions were involved; and that violations of regulations or TS condi-
,
.
tions did not appear to occur.
(Closed) IEC-80-06 Implant Therapy Sources. This IEC was transmit-
i ted to medical licensees only and is not generic to
Sequoyah.
(Closed) IEC-80-08 BWR RPS Response Time. This IEC was written
'
discussing a difference between General Electric TS and the
i design basis. This was not applicable to Sequoyah.
(Closed) IEC-80-19 Noncompliance with License Requirements for
Medical Licensees. This IEC was not applicable to
Sequoyah.
4
$
i
,_.-e ._. . . _ . , _ . , _ _ _ _ _ _ _ . . _ . . . . . . _ , , , , . - , . . . _ . . - . . , _ , _ . . . _ _ _ _ , . - . _ _ . . , - _ ,
. .
12
12. IE Bulletins (92703)
IE Bulletins are documents issued by the NRC which require certain
specific actions of the addressee. The ins'pector has reviewed the actions
taken by the licensee as a response to the below listed IE Bulletins
(IEBs). The inspector verified that: corrective actions appeared
appropriate; generic applicability had been considered; the licensee had
reviewed the event and that appropriate plant personnel were knowledge-
able; no unreviewed safety questions were involved; and that violations of
regulations or TS conditions did not appear to occur.
(Closed) IEB-80-07 BWR Jet Pump ' Assembly Failure. This IEB was
written to discuss problems with crack indications in Jet
Pumps and is not applicable to Sequoyah.
(Closed) IEB-80-13 Cracking in Core Spray Spargers. This IEB
discussed problems generic to BWR equipment only. It is
not applicable to Sequoyah.
(Closed) IEB-80-14 Degradation of BWR Scram Discharge Volume
Capacity. This form of scram system is used in BWR's only
and is not applicable to Sequoyah.
(Closed) IEB-80-17 Failure of Control Rods to Insert During a
Scram at a BWR. This IEB discusses an event which occurred
at Browns Ferry where the control rods failed to insert
because of a hydraulic lock in the scram discharge volume.
The rods at Sequoyah fall iato the core on a trip and do
not require the functioning of a hydraulic system. This
item is not applicable to Sequoyah.
13. Inspector Followup Items
Inspector followup items (IFIs) are matters of concern to the inspector
which are documented and tracked in inspection reports to allow further
review and evaluation by the inspector. The following IFIs have been
reviewed and evaluated by the inspector. The inspector has either
resolved the concern identified, determined that the licensee has
performed adequately in the area, and/or determined that actions taken by
the licensee have resolved the concern.
l (Closed) IFI 327, 328/85-46-08, Temporary Alterations
l
l
(Closed) IFI 327, 328/86-20-01, Temporary Alteration Program
Improvements
l The above two IFIs address the use and control of temporary alterations
l on safety-related systems. The licensee committed to the Institute of
Nuclear Power Operations (INP0) to clear all temporary alterations that
l were in place on January 1,1984, before unit 1 startup following
l cycle 4 completion. After the NRC identified the above IFIs the licensee
did an engineering study on the then existing 64 safety related temporary
alterations. The licensee determined that four outstanding temporary
alterations required review and/or correction prior to the startup of
l
Unit 2. The licensee's corrective actions in this areas will be monitored
!
_
. .
13
during the NRC maintenance team review of Nuclear Manager's Review Group
(NMRG) item H-1 which was found to be open in inspection report 327,
328/87-15. These followup items are administratively closed.
(Closed) IFI 327, 328/86-15-02, Waste Evaporator Leak.
The inspector reviewed the licensee's corrective actions to correct a
defective seam in the CDWE building wall. Engineering change notices
L6558 and L6417 were reviewed. The inspector had no further questions.
This item is closed.
14. Control Room Evacuation (71707)
The inspector reviewed A0I-27, Control Room Inaccessibility. The pro-
cedure describes the actions to be taken should the control room become
uninhabitable. The procedure requires the dispatching of more personnel
than are required as a minimum on-shift in TS 6.2.2.a. Appendix A of
10 CFR 50 requires in GDC 19 that equipment at appropriate locations out-
side the control room be provided with a design capability for prompt hot
shutdown of the reactor, including necessary instrumentation and controls
to maintain the unit in a safe condition during hot shutdown. This
criteria is addressed in Regulatory Guide (RG) 1.68.2, Initial Startup
Test Program to Demonstrate Remote Shutdown Capability for Water-Cooled
Nuclear Power Plants. This RG states that startup testing should demon-
strate that the number of personnel available to conduct the shutdown
operation is sufficient to perform the many actions required by the
procedure in a timely, coordinated manner.
The documentation available on the startup test as described in item
SU-1.2A of Table 14.1-3 in the FSAR will be reviewed. The following
issues will be resolved:
-
Whether there is sufficient personnel and guidance to perform a safe
and orderly shutdown from outside the control room with a minimum
shift crew per the TS.
-
Whether procedures are adequate to address the limiting case of
minimum shift manning.
-
Whether the initial startup test was performed utilizing the
personnel indicated in the procedure or the TS minimum, and whether
the procedure was adequate.
This will be identified as URI 327,328/87-08-02.
15. Startup Activities
During this inspection period the inspector continued the review of
Sequoyah readiness for restart. This review concentrated on evaluation of
, .
14
the numerous list of items that TVA considers non-restart for Sequoyah
Unit 2. The lists being reviewed include the following:
Work requests
Deficiency reports
Problem identification reports
Significant condition reports
Condition adverse to quality reports
Corrective action reports
Employee concerns deficiency reports
In addition to the above lists the inspector will review the " satellite"
programs such as design baseline and employee concerns, to ensure imple-
mentation of the restart criteria described in Standard Practice SQA-191,
" Evaluation of Operational Readiness Prior to Plant Restart".
16. TVA management changes:
E. R. Ennis - appointed Assistant to the Plant Manager
D. C. Craven - temporarily appointed to assist the surveillance instruc-
tion review manager
R. W. Fortenberry - temporarily appointed to assist the surveillance
instruction review manager
.
I