ML20141G044

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Insp Repts 50-327/97-04 & 50-328/97-04 on 970413-0524. Violations Noted.Major Areas Inspected:Operations Re Physics Testing,Maint,Engineering & Plant Support
ML20141G044
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 06/20/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20141G032 List:
References
50-327-97-04, 50-327-97-4, 50-328-97-04, 50-328-97-4, NUDOCS 9707030283
Download: ML20141G044 (21)


See also: IR 05000327/1997004

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U.S. NUCLEAR REGULATORY COMISSION

REGION II

Docket Nos:

50 327, 50 328

License Nos:

DPR 77, DPR 79

Report Nos:

50 327/97 04, 50-328/97-04

Licensee:

Tennessee Valley Authority (TVA)

Facility:

Sequoyah Nuclear Plant, Units 1 & 2

Location:

Sequoyah Access RotJ

Hamilton County, T.e 37379

Dates:

April 13 through May 24, 1997

Inspectors:

M. Shannon, Senior Resident Inspector

R. Starkey, Resident Inspector

D. Seymour, Resident Inspector

J. Blake, Senior Project Manager, RII, (Sections M1.2 and

M1.3)

Approved by:

M. Lesser, Chief, Projects Branch 6

Division of Reactor Projects

Enclosure 2

9707030283 970620

PDR

ADOCK 05000327

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EXECUTIVE SUMMARY

Sequoyah Nuclear Plant, Units 1 & 2

NRC Inspection Report 50 327/97 04, 50-328/97 04

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This integrated inspection included aspects of licensee operations,

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maintenance, engineering, plant support, and effectiveness of licensee

controls in identifying, resolving, and preventing problems. The report

covers a six-week period of resident inspection.

Operations

The conduct of operations during the inspection period was

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considered to be satisfactory.

However, weaknesses in plant

operation were identified during plant heatup and startup

evolutions (Section 01.1).

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A non cited violation was identified for failure to maintain the

reactor coolant system (RCS) tem3erature and pressere within the

procedural operating limits of t1e plant startup procedure

(Section 01.2).

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A violation was identified for failure to meet the surveillance

requirements of Technical Specification (TS) 4.10.3.2 and the

licensee's definition of " Start of Physics Testing" contained in

the Low Power Physics Testing procedure was considered to be

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inappropriate (Section 01.3).

A failure to follow procedures with multiple examples was

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identified related to exceeding the reactor fuel preconditioning

limitations.

Examples included failure to adequately control the

reactor power ramp rate to less than 3t; failure to properly log

plant status such as alarms, reactivity changes and surveillance

activities; and failure to properly notify the shift manager of

changes in plant status (Section 01.4).

The inspectors concluded that the licensee is meeting the intent

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of NUREG 0737 regarding shift turnover and relief procedures

(Section 01.5).

Steam generator level deviations on Unit 2 were continuing but had

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not caused significant operational difficulties.

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Maintenance

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The inspctors noted that work activities and the performance of

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surveillance activities were adequately performed with the

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exception of the steam dump valve maintenance (Section M1.1).

The licensee's pressure boundary and containment inservice

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inspection activities were well organized, implemented correctly,

and properly documented.

(Section M1.2).

ASME Section XI, repair and replacement activities, as

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demoristrated by the SG feedwater piping replacement, were well

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controlled and documented.

(Section M1.2).

The Design Change Notice for the feedwater pi aing replacement,

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completed in 1996, did not acknowledge that tie Code of Record for

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repair and replacement activities changed in December 1996.

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(Section M1.2).

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A weakness was identified in the area of the Unit 1 surveillance

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procedure for the leak testing of ASME Class 1 bolted connections,

in that the issued procedure was essentially the same as that used

for the last unit 2 outage, without considering lessons learned

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from implementation problems during that outage.

(Section M1.2).

The licensee's program for inspection of steam generators appears

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to be well managed and conducted in a conservative manner. The

analysis guidelines were found to be well written and easy to

interpret.

(Section M1.3).

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Mechanical maintenance did not verify that all work had been

completed prior to closing out the work packages on the Unit 1

steam dump valves. Procedure revisions to address the missed

steam dump bolt torquing requirements in 1996 on Unit 2. were not

sufficient to identify and correct all of the associated work

procedures, resulting in not torquing the bolts on Unit 1 (Section

M2.1).

Enaineerina

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The licensee was successful in implementing various modifications

to improve the operation of the Unit 1 steam dump system (Section

E2.1).

Plant Support

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An inspector follow up item was identified to review the

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licensee's completed corrective actions following an inadvertent

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spill of several thousand gallons of contaminated water

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(Section R1.1).

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Report Details

Summary of Plant Status

Unit 1 began the inspection period in Mode 6, Cycle 8 refueling activities.

Reactor startup and Mode 2 entry was made at 2:40 a.m., on May 11, 1997, and

Mode 1 entry was made at 6:32 a.m. on May 12, 1997. The unit operated at power

for the remainder of the inspection period.

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Unit 2 began the inspection period in power operation. The unit operated at

power for the duration of the inspection period.

Review of Updated Final Safety Analysis Report (UFSAR) Commitments

While performing inspections discussed in this report, the inspectors reviewed

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the applicable portions of the UFSAR that were related to the areas inspected.

The inspectors verified that the UFSAR wording was consistent with the

observed plant practices, procedures, and/or parameters.

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I. Doerations

01

Conduct of Operations

01.1 General Comments (71707)

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Using Inspection Procedure 71707, the inspectors conducted frequent

reviews of ongoing plant operations. The inspectors observed mid loop

oaerations, operation in Mode 4, entry into Mode 3. rod drop testing,

t1e reactor startup, portions of physics testing, and portions of the

power increase to 100%.

In general, the conduct of operations was

acceptable, however, weaknesses in plant operation were identified and

are detailed in following sections of the report.

During the Unit i reactor startup on May 11, 1997, the inspector noted

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that the designated Unit 2 senior reactor operator (SR0) was detailed to

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Unit 1 to assist in the unit startup. This condition left Unit 2.

without active SR0 oversight for over 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />. Although allowed by the

TSs, the inspector questioned the process of removing unit SR0 oversight

for non emergency plant evolutions / conditions. The inspector requested

the licensee to review their process / program for staffing during non-

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emergency plant evolutions / conditions.

01.2 Reactor Coolant System Heatuo To 330 340 F

a.

Insoection Scope (71707 and 40500)

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The inspector observed activities associated with plant heatup following

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the Unit 1 refueling outage. This included licensee preparations for

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entering Mode 3.

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b.

Observations and Findinas

On May 6, 1997, the inspector was observing routine control room

activities related to required surveillance testing prior to entering

Mode 3.

During the observations, the inspector noted that RCS

temperature was approaching 350 F and that exceeding 350 F would

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result in an unanticipated Mode change.

It was noted that the RCS

temperatures from the Integrated Computer System (ICS) were indicating

slightly higher than the control board indicators, and that the ICS

indicated that RCS temperature was above 349 *F.

The ICS temperature indications were discussed with the control room

operators. The control room operators stated that the control board

indicators were the official instruments and the ICS indications were

not used to determine Mode change. However, the inspector noted that

the ICS computer provided the only detailed history, down to tenths of

degrees, and was more accurate than the control board recorders,

therefore the ICS data should be evaluated / considered for use for

specific functions such as Mode changes.

During a subsequent review of the computer history of RCS temperature,

the inspector noted that RCS average temperatura had reached 349.95 F

during a transient while placing the steam dumps in service. The

inspector also noted that the operators had maintained RCS temperature

at about 345 F for several hours while awaitinc permission to enter

Mode 3.

A review of the oaerating procedure. 0 GO 1, Unit Startup From

Cold Shutdown To Hot Standay, noted that Section 5.6.22 required that

"If the unit is to be maintained at this plateau, THEN CONTROL RCS

temperature at 330 to 340 F and pressure between 330 and 350 psig."

Contrary to the arocedure requirement, the operators did not maintain

RCS temperature aetween 330 and 340

F, and as a result came very close

to an unanticipated Mode change.

In addition, the inspector noted that RCS pressure was approximately 372

psig, and a later review noted this was also above the procedural limits

in 0 G0 1.

However, prior to discussions with the licensee, the

inspector noted that the licensee's quality assurance (QA) operations

observer had noted the RCS pressure control deficiency and had initiated

PER No. SQ971353PER to document the failure to follow procedure. The QA

observer noted that RCS pressure had been increased to 500 psig,

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although the procedure in effect required RCS pressure be maintained

between 330 and 350 psig. The inspector verified that the plant was

maintained within the TS pressure and temperature requirements, even

though the procedural requirements were not met.

The inspector noted that the procedural limitations were administrative

in nature and that in this specific case did not compromise plaat

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safety.

In addition, the inspector noted that although the operators

approached Mode 3, the 350 F average RCS temperature Mode change

limitation was not exceeded.

In this case the operators failed to

follow the procedural limitations in plant startup procedure 0-G0-1,

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however, this event was considered to have low safety significance and

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the licensee subsequently implemented prompt corrective actions. These

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included refresher training on steam dumps, margin to operating limits,

improved guidance for mode changes and clearer o>erating parameter

guidance. This licensee corrected violation is

aeing treated as a non-

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cited violation (NCV), consistent with Section VII.B.1 of the NRC

enforcement Policy. (NCV 50-327/97 04-01).

c.

Conclusions

A non-cited violation was identified for failure to maintain the RCS

temperature and pressure within the procedural operating limits of the

plant startup procedure.

The licensee's OA organization identified that the operators failed to

maintain RCS pressure within the procedural operating limits of the

plant startup procedure. This is considered an example of positive QA

organization oversight.

01.3 Failure To Meet TS Recuirements For Physics Testina

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a.

Insoection Scope (71707)

The inspector observed activities associated with the entry into Mode 2,

the start of Physics Testing and the Unit I reactor startup following

refueling activities.

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b.

Observations and Findinas

The ins)ector observed the crew briefing for the Unit 1 Cycle 8 low

power p1ysics testing and observed the reactor startup. At 2:40 a.m.,

on May 5,1997, the operators began pulling control rods (Mode 2) and at

3:39 a.m., on May 5, 1997, the reactor was critical. The crew briefing

was detailed with appropriate cautions highlighted and the reactor

startup proceeded as expected with appropriate supervisory oversight.

During a subsequent review, the inspector noted a potential deficiency

with the interpretation of the " start of physics testing." TS

3/4.10.3.2 requires that the four power range nuclear instrument

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channels and the two intermediate range nuclear instruments shall be

subject to a channel functional test within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> prior to the start

of physics testing. The 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> surveillance was due to expire on

nuclear instrument NI 42 at 2:18 a.m.

This issue was discussed in the

control room between reactor engineering personnel and operation's

management.

Engineering noted that further surveillance testing would

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not be required if permission to start )hysics testing was granted by

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the shift manager. At 2:13 a.m., the slift manager authorized the plant

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startup, entry into Mode 2 and the start of physics testing. However,

due to feedwater pump and associated procedural problems, which hindered

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Mode 2 entry, reactor startup could not be initiated at this time.

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Subsequently the inspector performed a detailed review of TS 4.10.3.2

and the applicable operating procedures. The following was noted;

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0 RT NUC 000 003.0, Low Power Physics Testing, Section 6.1 6

requires the operator to record the time for Mode 2 entry and

initiation of )hysics testing and to INITIATE control bank

withdrawal. T1e time recorded in this block was 2:13 a.m.,

however, control bank withdrawal did not start until 2:40 a.m.

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The Unit Startup From Hot Standby To Critical

3rocedure. 0-G0 2,

Section 5.3 Note 1 "The unit enters Mode 2 w1en the contro'

banks are first withdrawn." Section 5.3 15.b. stated " START

WITHDRAWAL of control banks and DECLARE MODE 2.

Log in operators

journal." However, the operators logged Mode 2 entry at

2:13 a.m., and initial pulling of the control banks was not

initiated until 2:40 a.m.

In addition, the inspector noted that

actual Mode 2 entry is not made until core K effective is greater

than 0.99, which occurs during withdrawal of the control banks,

not when the first control banks are withdrawn.

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The Low Power Physics Testing procedure. 0 RT NUC 000 003.0,

Precautions and Limitations, Section 3.0 J defined "the start of

ohysics testina as the time that permission from the SR0 senior

reactor operator has been obtained to begin the first withdrawal

of control bank A.

This time would stop the clock on NIS channel

testing for startup." However, this definition was considered to

be inappropriate in that physics testing cannot be performed

unless the reactor is critical and it was also in conflict with

the procedural steps which require entry into Mode 2 and

withdrawal of control rods.

Prior to actual control bank withdrawal and Mode 2 entry at 2:40 a.m.,

the 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> surveillance requirements for power range nuclear instrument

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NI-42, expired at 2:18 a.m. and intermediate range nuclear instrument

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NI 36 expired at 2:32 a.m.

Plant startup and the actual start of

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physics testing commenced at 02:40 a.m.

Technical Specification

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4.10.3.2 requires each intermediate and power range instrument to be

subjected to a Channel Functional Test within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> of initiating

Physics Tests. The licensee's failure to meet the surveillance

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requirements of TS 4.10.3.2 is considered to be a violation (VIO 50-

327/97-04-02).

c.

Conclusions

The licensee's definition of " Start of Physics Testing" contained in the

Low Power Physics Testing procedure was considered to be inappropriate.

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A violation was identified for failure to meet the surveillance

requirements of TS 4.10.3.2

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01.4 Unit 1 Exceeds 3t Per Hour Ramo Rate Durina Fuel Preconditionina

a.

Insoection Scooe (71707)

The inspectors reviewed the circumstances during which Unit 1 increased

reactor power by approximately 6.4% during a time when power ramp rate

was limited to 3% for new fuel preconditioning.

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b.

Observations and Findinas

On May 15, 1997, with Unit 1 at 64% power, operators were performing

Surveillance Instruction (SI) 0 SI 0PS 068-137.0, Reactor Coolant System

Water Inventory, Revision 1, and were periodically withdrawing control

rods in order to maintain RCS average temperature (T avg) within one

degree of the initial starting temperature (563 F) as required by the

SI. During the performance of SI-137 T-avg varied from 2 F to 5 F

less than T-ref which was approximately 566

F.

Control rod Bank D was

withdrawn from 196 steps to 201 steps as operatort attempted to maintain

a stable RCS temperature for the leak rate calculation. During the data

gathering for SI-137.0, Delta I exceeded the target band upper limit of

+4.

When operators determined that they were unable to maintain a

stable RCS T avg temperature or to maintain Delta-I within the target

band, due to increasing xenon concentrations, they aborted the leak rate

procedure. Operators then began diluting the RCS in order to allow

repositioning the control rods to control Delta I.

According to

personnel statements and ICS data, six dilutions of 200 gallons each, a

total of 1218 gallons, were performed in approximately 32 minutes. As a

result of the dilutions, reactor power increased approximately 6.4% in a

52 minute period. Based on statements from operations personnel,

control rods were in " manual" during this dilution evolution.

Subsequently, the ins)ector reviewed the Unit 1 power history from the

ICS coaputer, using t1e power history from the nuclear instrumentation

channels.

In addition to the above power increase, the inspector noted

that during the power increase from 49% power to 65% power on May 15,

1997, that during t,pecific periods the power increase exceeded the 3%

per hour limitation specified in TI 40. The ICS computer history

indicated that from 10:03 a.m. to 11:03 a.m., on May 15, reactor power

was increased by an average of 3.551. The observed power increase did

not meet the procedural requirements for fuel conditioning specified in

TI-40.

Procedure 0-G0 5, Normal Power Operation, Revision 6 Section 5.1,

requires that ramp load rate increases shall be within the limits stated

in TI 40, Determination of Preconditioned Reactor Power, Revision 8.

TI-40 requires for the initial power increase following refueling, that

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the reactor power escalation rate should be limited to 3% power in an

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hour between 20% and 100% of full power. The TI further states that

small deviations are allowed from the 3% per hour ramp rate during power

increases, but the power increase must not exceed 3.5% in any one hour.

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Following discussions with the fuel vendors, the licensee concluded that

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no damage to the new fuel would be expected based on the actual power

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increases which had exceeded the 3% limitations for reactor power

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increase. The licensee's failure to follow the reactor fuel

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preconditioning power limitations / requirements specified in TI 40, is a

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failure to follow procedure and is considered to be a violation (VIO 50

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327/97 04 03).

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The inspectors became aware of the event while attending the operations

shift turnover on Monday morning, May 19, 1997. When the inspectors

reviewed the control room logs for information related to the evolution,

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only two entries could be found. At 8:09 p.m. on May 15, operators

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logged that SI 137.0 had been aborted because there had been an increase

in RCS temperature of greater than 1 degree from the initial conditions.

There were no subsequent entries regarding the six 200 gallon dilutions

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or that reactor power was increased by over 6%. The next logbook entry

was not until 1:00 p.m. on May 16, noted that during a review of ICS

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data, the licensee discovered the excessive power increase.

It was at

that time that operations initiated a PER and the fuel vendors were

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notified.

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The inspectors noted that operators had not logged various plant

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conditions or evolutions that would have assisted in reconstructing the

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time line for this event. The operators did not log the start of the

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RCS leak rate surveillance.

In addition, the operators did not log the

actuation of the AFD (delt6 flux) alarm conditions, the time the

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conditions cleared, or the total number of minutes in alarm, which is

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information used by reactor engineering. Also, operators did not log

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the six reactivity additions (200 gallon dilutions) in a 32 minute

period. The failure to make log book entries related to reactivity

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changes, the AFD alarm conditions, and the start of surveillance

activities, as required by SSP 12.1, Conduct of Operations. Section 3.8,

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Revision 17, is a failure to follow procedure and is considered to be a

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second example of VIO 50 327/97 04 03.

During review of the event, the licensee noted that the shift manager

(SM) had not been aware of the difficulties being experienced by the

Unit 1 operators. Statements indicated that the SM was not aware of the

AFD alarm conditions or that the operators had diluted the RCS with 1200

gallons of water.

Failure of the unit su>ervisor to coordinate with the

SM changing plant conditions as required )y SSP 12.1, Conduct of

0)erations, is a failure to follow procedure and is considered to be a

t11rd example of VIO 50-327/97 04 03.

c.

Conclusions

A violation was identified for the failure of operators to follow a

procedure which limited reactor power ramp rate to 3% per hour, for the

failure of operators to make log book entries regarding significant load

and reactivity changes, alarm conditions, and surveillance activities,

and for the failure to promptly notify the SM of reactivity changes to

the unit and plant alarm conditions.

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01.5 Review of Shift Turnover Checklist Commitment

a.

Insoection Scope (71707)

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In a letter to the NRC dated March 20, 1997 TVA notified the NRC of a

change in its commitments to satisfy NUREG 0737, Clarification of THI

Action Plan Requirements,Section I.C.2. Shift and Relief Turnover

Procedures. The inspectors reviewed the NRC's NUREG 0737 position

regarding shift turnover (as delineated in NUREG 0578, THI-2 Lessons

Learned Task Force Status Report and Short Term Recommendations, Section

2.2.1.c): the licensee's initial response to Section I.C.2 of NUREG-

0737: and the licensee's revised response to their shift turnover

commitment, in order to determine if the recent changes meet the intent

of NUREG 0737.

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b.

Observations and Findinos

The NRC position on Shift and Relief Turnover Procedures stated, in

part, that:

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A checklist shall be provided for oncoming and off going control

room operators and the oncoming shift supervisor to complete and

sign. The following items, as a minimum, shall be included in the

checklist:

a.

Assurance that critical plant parameters are within

allowable limits.

b.

Assurance of the availability and proper alignment of all

systems essential to the prevention and mitigation of

operational transients and accidents by a check of the

control console.

c.

Identification of systems and components that are in a

degraded mode of operation permitted by TS.

The initial position of TVA regarding shift turnover, committed to the

NRC in the early 1980's, was that a checklist or similar hard copy would

be completed by off going and oncoming shifts at each shift turnover.

The checklist would include critical plant parameters and allowable

limits, availability and proper alignments of safety systems, and a

listing of safety system components in a degraded mode along with length

of time in that mode. That checklist would be signed by the off going

Unit Operator and the oncoming Unit Supervisor and Unit Operator.

In May 1994, the licensee performed a safety assessment in support of

changes to various shift relief and turnover checklists.

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were revised in order to eliminate unnecessary data taking and several

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shift relief and turnover checklists were canceled.

In lieu of a

turnover checklist, 03erators were expected to perform a control board

walkdown, review " pin ( tags" which are placed on control board switches

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which were in an off-normal position, review the status board for off-

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normal equipment conditions, review work request stickers.and their

affect on plant ecuipment, and review the operator's logs. The safety

assessment concluced that the revised shift turnover procedures met the

intent of NUREG 0737. Item 2.2.1.c.

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It should be noted that in approximately 1995, the unit status boards

were eliminated and in 1996, work request stickers, with some

exceptions, were no longer attached to main control board instruments,

but were maintained in a separate " Control Room Deficiencies" binder in

the main control room.

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In its March 20, 1997, letter, TVA stated, "TVA has revised and

implemented the shift and relief turnover program and procedures. The

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current procedures arovide guidance to assure that the oncoming shift

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possesses adequate (nowledge of critical plant status information and

system availability. The current procedures require a shift turnover

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meeting and is conducted by the Shift Manager, SRO. The procedure

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indicated that the briefing should include a review of the plant status,

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problems with plant equipment, evolutions in process or planned for the

shift. Subjects pertinent to shift operations such as standing orders,

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procedures changes, etc. as deemed appropriate are discussed. A listing

of safety system components in a degraded mode along with the time of

entry, are included in the operator's log which are reviewed during

shift turnover. A periodic instruction is utilized following the

turnover process for designated Operations' shift positions."

SSP 12.1, Conduct of Operations, Revision 17, requires that a shift

turnover meeting be conducted by the Shift Manager (SM). The inspectors

routinely attend the shift turnover meeting and have made positive

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comments in recent inspection reports (IR 9611. IR 95 21, and IR 9518)

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concerning those meetings.

Prior to the turnover meeting, the oncoming

operators begin their turnover process in the control. room. This

turnover includes a board walkdown, a review of operator logs, and

discussions of plant status. The logs include information on degraded

equipment and any significant evolutions which have occurred on the

unit. The inspectors routinely review operator logs. The inspectors

have documented weaknesses or violations in operator log keeping in

seven inspection reports since'1995.

It appears that the TVA program is meeting the intent of the NRC

position on NUREG 0737 regarding shift and relief turnover procedures.

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Specifically, critical plant parameters are entered in the operator

computerized logs and are available for review by the oncoming

o>erators. Critical plant parameters are also readily available from

t1e control room ICS. As noted in the licensee's letter of March 20,

1997, a shift turnover meeting is conducted by the SM. That meeting

discusses current plant status, equipment problems, and evolutions

planned or in progress.

In addition to a control board walkdown

conducted jointly by the oncoming and off-goi'ig operators, the oncoming

operator at the controls (0ATC) and the control room operator (CRO) each

perform a Periodic Instruction (PI) which is a status check of vital

systems. All TS Limiting Condition for Operation (LC0) action

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statements which have been entered are listed on a computerized LC0

Tracking System and are reviewed by all oncoming operators.

Additionally, each oncoming operator reviews the control room log book.

Implementation of log keeping remains a 3roblem and when corrected, the

shift turnover process should be acceptaale.

c.

Conclusions

The inspectors concluded that the licensee's program meets the intent of

NUREG 0737 regarding shift turnover and relief procedures, however

improved implementation is necessary.

02

Operational Status of Facilities and Equipment

02.1 Steam Generator Level Deviations

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a.

Inspection Scoce (71707)

The inspectors reviewed the licensee's corrective actions related to

continued steam generator level deviations.

b.

Observations and Findinas

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IR 97 03 described a aroblem with Unit 2 steam generator level

deviations. This pro)lem first occurred in December 1996, and has

occurred numerous times on loops 1, 2 and 3 since December.

Programmed

steam generator level is 44%. The level deviations were typically 2 to

5% increases in level. There have been some instances were operators

took manual control of steam generator level to return it to program;

although, typically, steam generator level returned to the programmed

level after several minutes, without operators taking manual control.

The licensee has taken several actions to correct this problem. Some of

the licensee's actions included:

lubricating flow control valve stems,

recording and analyzing the signals from the level control system,

replacing relays in the controllers, and field tuning the flow

controllers. The licensee instituted a team to address the continuing

level control problems. The licensee is still investigating potential

causes for the level deviations.

c.

Conclusions

The inspectors concluded that the steam generator level deviations had

not caused significant operational difficulties, however, continued

licensee effort in resolving the level control problem is needed.

02.2 Outaae Related Operational Challences

a.

Inspection Scope (71707)

The inspectors reviewed the control room operational logs to determine

the type and frequency of equipment and system status related challenges

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imposed on the operators during the second half of the Unit 1 refueling

outage.

b.

Observations and Findinas

Interviews with the control room operators indicated a higher than

expected level of equipment problems were being observed during the

Unit 1 refueling outage. The inspector aerformed an integrated review

of the control room logs for the period 3etween April 12 and May 13 and

noted multiple potential problems with human performance, procedures,

equipment and plant status control. These problems appeared to have

posed daily challenges to the o)erators.

Further review is necessary to

determine the extent of the pro)lems and to review the licensee's

corrective actions. Therefore, further review of the refueling outage

related operational problems is being identified as an unresolved item

(URI 50 327/97-04 04).

II. Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a.

Insoection Scone (61726 & 62707)

The inspectors observed and/or reviewed all or portions of the following

work activities and/or surveillances:

e 1-S0-2/3-1

Condensate and Feedwater System

e 2 SI-0PS 082 007.B

Electrical Power System Diesel Generator 28 B

e 2-SI SXV-062 230.0

VCT Check Valve Test During Operation

e 2 SI-SXP 074-201.A

Residual Heat Removal Pump 2A A Performance Test

e 1 SI SXP 003 201.S

TDAFW Pump 1A-S Performance Test

e MI 10.54

Diesel Generator Battery Replacement and/or

Battery Bank Bus Rework (System 250)

e 0-PI-SXP 078 201.C

Spent Fuel Pit Cooling Pump C S Performance Test

e WO 97 007711

Diesel Generator 1A Voltage Regulator Repair-PMT

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e 0-SI-SXX 085-043.0

Rod Drop Time Measurements

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e 0-MI-MRR-003 461.0

TDAFW Pump Control Valve FCV-51 Repair

e S SI 0PS 003-118.0

AFW Pump and Valve Automatic Actuation

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e 1 SI 0PS 087 026.B

Loss of Offsite Power with SI-Diesel Generator

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1B B Containment Isolation ~ Test

b.

Observations and Findinas

'

The inspectors noted that the work activities and the performance of

surveillance activities were adequately performed with the exception of

the steam dump valve maintenance documented in Section M2.1.

M1.2 Inservice Insoection (ISI)

Unit 1

a.

Inspection Scope (IP 73753)

The inspector reviewed program plans, procedures, and documentation

related to the conduct of inservice inspection (ISI) Inspection during

the Spring 1997, Unit 1 Outage.

b.

Observations and Findinas

Pressure Boundary ISI

Sequoyah Unit 1 began commercial operation on July 1,1981, but because

of extended plant shutdowns, the first 10 year ISI inspection interval

was extended to December 15, 1995.

(Unit 2 which began commercial

operation on June 1,1982, was also deemed to have completed its first

10 year inspection interval on December 15, 1995.) The second ISI

inspection interval began on December 16, 1995, for both units, with a

common ASME Code of record: ASME Section XI, 1989 Edition, with no

addenda. The inspector partially reviewed Surveillance Instruction

0 SI DXI-000-114.2, "ASME SECTION XI ISI/NDE PROGRAM UNIT 1 and UNIT 2."

Revision 1, Effective Date March 20, 1997. As stated in the procedure,

'

Surseillance Instruction 0-SI DXI 000 114.2:

... implements the SON Unit 1 Technical Specification

"

(TS) Requirement 4.4.3.2.4 and partially satisfies the

requirements for both Unit 1 and Unit 2 TS

surveillance requirement 4.0.5: and fulfills the

requirements of Site Standard Practice, SSP-6.10,

'ASME SECTION XI ISI/NDE AND AUGMENTED NONDESTRUCTIVE

EXAMINATION PROGRAMS.'"

At the time of the inspection, the ISI examinations planned for this

outage had been essentially completed, thereforS the insaction focussed

on the ISI plan and the documentation of the results. T1e inspector

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reviewed documentation for visual, surface, and volumetric examinations

that were conducted during the Spring 1997 refueling outage. Records of

Ultrasonic Examinations (UT) reviewed in detail included the following:

ComDonent/ Weld

Examination

Comment

SIS 252 - Pipe to Elbow

0 .45 ,60

No Recordable Indications

6" dia. 3/4" wall, SS

UT

SIS-253

Elbow to Pipe

0 .45 .60

360 Indication in Pipe,

6" dia. 3/4" wall, SS

UT

outside area of interest. 45

Indication, not seen with 60

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geometric, possibly counterbore

RCS 040 - Elbow to Pipe

0 .45 ,60

No Recordable Indications

4" dia.1/2" wall, SS

UT

SIF-198 - Elbow to Boss

0 .45 ,60

Augmented IGSCC Exam

6" dia. 3/4" wall, SS

UT

No Recordable Indications

RCS 049

Pipe to Reducer

0 .45 .60

No Recordable Indications

6" dia.

67" wall, SS

UT

RCW-21

Nozzle to

0 .45 .60

63.74% Code Coverage, (Complex

Pressurizer Shell

UT

Calculation) No Indications

3.6" to 3.8" wall, CS

CVCS-148

Pipe to Elbow

0 .45 ,60

No Recordable Indications

4" dia.1/4" wall, SS

UT

SIS 237 - Elbow to Pipe

0 .45 .60

No Recordable Indications

6" dia. 3/4" wall, SS

UT

MSS 11 - Elbow to Pipe

0 .45 ,60

No Recordable Indications

32" dia.1.5" wall, CS

UT

CVCS 112

Pipe to Elbow

0 .45 ,60

2 Indications found with 45 ,

3" dia. 1/2" wall, SS

UT Plus

confirmed with 60 . Re-

additional

evaluation with 70 S, WSY 70 ,

angles

60 RL, 80 High Angle Creeping

Wave, and 0 L.

Determined to

be Geometric.

Containment ISI

Effective September 9,1996,10 CFR 50.55a, was amended to include the

requirements of ASME B&PV Code Section XI, Subsections IWE and IWL 1992

Edition, with 1992 Addenda.

Subsections IWE and IWL provide ISI

requirements for concrete containments, steel containments, and steel

liners for concrete containments. The amendment to the rule provided a

five year period, until September 9, 2001, before full implementation of

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Subsections IWE and IWL.

In correspondence with the industry,

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(November 6,1996, letter to Alex Marion, Nuclear Energy Institute from

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Gus Lainas, Office of Nuclear Reactor Regulation, concerning

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" Implementation of Containment Inspection Rule") NRC provided a Staff

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position that, in response to deficiencies noted prior to the full

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implementation IWE and IWL, re] air and replacement activities must be

conducted in accordance with tiose subsections.

,

The licensee has issued two temporary changes to Procedure No. N VT 1,

" VISUAL EXAMINATION PROCEDURE FOR ASME SECTION XI PRESERVICE AND

INSERVICE," Revision 25, dated December 3, 1996, to include the ASME

1

Code,1992 Addenda, visual _ ins)ection requirements for containments.

The changes were TC 97 03 whic1 included inspection requirements for

pressure retaining bolting materials and seals and gaskets, and TC 97 06

which provided inspection requirements for containment vessel surfaces.

The inspector conducted a walk through inspection of the Unit 1 up,)er

containment looking for indications of coating degradation, etc., which

should be indicative of potential inservice problems with the steel

containment. A part of the inspection was conducted on April 17, 1997,

using the remote video equipment used by health physics personnel for

surveillance of work activities in the upper containment. The rest of

d

the inspection was done using 7X binoculars during a containment entry

on April 18, 1997. The inspector noted that the majority of the u)per

containment walls and dome were only coated with what appeared to

3e

" carbo zinc" type of primer coating. There were a few areas of the wall

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that were coated with a light colored coating over the primer, these

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areas appeared to be in good shape with no evidence of peeling or

flaking.

Reoair and Reolacement

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At the time of the inspection, the licensee was replacing feedwater line

elbows on Steam Generators 3 and 4 due to thermal fatigue cracking in

the area of the weld connecting the elbow to the feedwater nozzle on the

SG.

The replacement elbow included a modification to include a thermal

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sleeve.

The inspector observed welding o)erations on the elbow to pipe weld on

the feedwater line for SG #3. T1e operations observed involved the

set up of the welding machine for the start of a weld aass and, the

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initiation and partial completion of the weld pass. T1e inspector

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reviewed the documentation package at the job site, and discussed

welding procedure requirements with the welding operators.

The inspector reviewed the documentation package for DCN No. M 11336 A

which was prepared to: " Remove existing steam generator feedwater nozzle

elbows and transition pieces and replace it with a new design with a

thermal liner for the purpose of mitigating cracking due to thermal

fatigue." For the most part, the documentation package for this DCN was

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very comprehensive.

One minor problem was noted on page 22 of 32 of Appendix G, " Safety

Assessment Checklist," Item 52, concerning ASME Section XI. The safety

assessment states that the Code of record for SG repair and replacement

at SON is ASME Section XI, 1980 Edition through Winter 1981 Addenda.

While this statement was true at the time that the safety assessment was

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completed in early 1995, as a part of the design of the modification, it

was no longer the case after December 15, 1996, when it was determined

that both Sequoyah units had completed the first 10-year ASME, ISI. As

of December 16, 1996, the Code of record for repair and replacement of

ASME Code related items at SQN became the 1989 Edition.

For the purpose

of this modification, this was a minor problem because the later edition

of the Section XI allowed the same design and fabrication rules to apply

that were permitted by the earlier edition of Section XI. The problem

was pointed out to the licensee as an example of something that

engineering support and design organizations should be made aware of

whenever a plant transitions from one ISI inspection interval to the

next, with a resulting change in Code of record.

Leak Testina of Bolted Connections

During review of ISI documents, the inspector inquired if ASME Code Case

N-533, " Alternative Requirements for VT 2 Visual Examination of Class 1

Insulated Pressure-Retaining Bolted Connections,Section XI,

Division 1," had been approved for use at Sequoyah by NRR. The

inspector also asked to review the procedure (s) for conducting the

Class 1 pressure tests.

The licensee provided the inspector with a copy of Surveillance

Instruction No.1 SI-SXI 068 201.0, " Leakage Test of the Reactor Coolant

Pressure Boundary," Revision 0, dated March 21, 1997: prepared for the

inspection of Unit 1 during the current refueling outcge. The licensee

also provided a copy of the documentation package for Surveillance 2 SI-

SXI 068-201.0, Revision 0, dated April 26, 1996, which had been used for

the pressure testing of Unit 2 during its last refueling.

During the review of the Unit 2 surveillance procedure documentation

package, in the section of the procedure devoted to the in:oection of

pressure retaining bolted connections, the inspector noted ' hat the

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procedure had been issued without a definitive list of i:elted

connections to be inspected.

Instead, the VT 2 examiner was provided

with a list of reference drawings and an inspection list of 25 blank

lines to be filled out as the inspection was completed. The

documentation package showed two obvious weaknesses with the Unit 2

procedure: 1) Twenty five lines were not enough, as there were numerous

entries written in the margin of the list; and 2) The use of a blank

list and a number of reference drawings did not provide an auditable

record to ensure that "all" of the pressure retaining bolted connections

had been examined. This latter point was shown by the fact that after

the Unit 2 surveillance was signed as complete, the licensee issued a

PER to inspect a number of bolted connections that had been missed.

The inspector also noted that the Unit 1 procedure was essentially a

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duplicate of the procedure issued for Unit 2.

In light of the fact that

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the review of the Unit 2 surveillance procedure had discovered two

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obvious problems during its initial implementation, the ir ,pector

informed the licensee that the failure to incorporate lessons learned in

the next iteration of a new procedure showed a lack of sensitivity to

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the problems and would be considered as a weakness in the area of

surveillance procedure development.

Licensee management agreed with the

inspector's assessment of the procedure, and Revision 1 of Procedure

1 SI SXI 068 201.0, was issued on April 18, 1997, containing a

definitive list of pressure retaining bolted connections, expected to be

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found within the Class 1 piping system boundary,

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c.

Conclusions

The licensee's pressure boundary and containment ISI activities were

well organized, implemented correctly, and properly documented.

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ASME Section XI, repair and replacement activities, as demonstrated by

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the SG feedwater piping replacement, were well controlled and

}

documented.

A weakness was identified in the area of the Unit 1 surveillance

procedure for the leak testing of ASME Class 1 bolted connections, in

that the issued procedure was essentially the same as that used for the

last Unit 2 outage, without considering lessons learned from

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implementation problems during that outage.

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M1.3 Steam Generator (SG) Inspection

Unit 3

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a.

Insoection Scope (IP 50002)

)

Through discussions with personnel and review of documentation, the

inspector reviewed the Eddy Current (ET) inspection of the Unit 1 SGs.

f

b.

Observations and Findinas

I

The Unit 1 SGs are Westinghouse Model 51 which contain low temperature,

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mill annealed, Inconel 600 tubing supported by carbon steel, drilled

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support plates, with WEXTEX tubesheet expansions.

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.

The inspector reviewed the Steam Generator Analysis Guideline for Eddy

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Current Data, Revision 1997.02 dated February 1997, along with

Evaluation Guideline Change Form #1, dated April 13, 1997. The

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inspector also conducted several discussions with inspection and

supervisory personnel to evaluate the ET activities and determine the

status of the SG inspections. The inspector also reviewed tabulated

results of the ET tests.

On April 17, 1997, the inspector participated in a conference call

between the licensee and NRC concerning the status of the ET testing.

During this call, the licensee presented a description of the ET testing

which had been accomplished; the preliminary results of the tests; and

the status of in situ pressure testing of SG tubes. Due to a

communications problem with transmitting the licensee's data tables to

the appropriate people in NRR, the conference call was continued on

April 18, 1997, after all parties were able to review the appropriate

data tables.

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The inspector also observed the in situ pressure testing of SG 4, tube

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R33C21, which was reported to have a 91% through wall, 4 inch long axial

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PWSCC indication at the first hot-leg support plate. The tube was

pressurized to 1600#, then 2800#, and finally 4750# with a two minute

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hold at each pressure level. There was no leakage from this tube during

the test.

c.

Conclusions

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The licensee's program for inspection of SGs appears to be well managed

and conducted in a conservative manner. The analysis guidelines were

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found to be well written and easy to interpret.

M2

Maintenance and Material Condition of Facilities and Equipment

4

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M2.1 Reoair of Unit 1 Steam Dumo Valves

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a.

Inspection Scooe (62707)

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On May 12, 1997, during a routine turbine building walk down, an NRC

resident inspector identified two Unit 1 steam dum) valves with loose

bolts on the valve operator. The licensee wrote PER No. SQ971375PER to

document this finding.

Subsequently, when the licensee closed the

!

valves to continue the plant heatup/startup, the valves indicated in the

mid position (both green and red lights lit).

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b.

Observations and Findinas

1

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Further review noted that the licensee had inspected /reiuebished all

twelve of the Unit 1 steam dump valves during the cycle 8 refueling

outage.

Mechanical maintenance had replaced the valve trim on some of

the valves during the outage and, following reassembly, instrument

maintenance was required to adjust the valve stroke and torque the

locking bolts.

Step 6.7 in 0 MI HVV 000 029.0, the mechanical

maintenance procedure dealing with the setting of the steam dump valve

stroke, was used for this work, however, this section had not been

completed. The licensee's investigation determined that the instrument

.

maintenance grou) used a different maintenance procedure to perform this

work, and that t1e specific instrument maintenance procedure did not

include the steps for torquing the locking bolts.

A similar problem occurred on Unit 2 following the Unit 2 cycle 7

refueling outage, when the locking bolt on a steam dump valve was found

broken.

During the Unit 2 cycle 7 outage, the licensee had not

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adequately set the stroke on all of the Unit 2 steam dump valves and the

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locking bolts had not been torqued.

Subsequently when steam dump valve

SD 107 was stroked the locking bolt was broken off. The valve was

.

isolated at that time and remains isolated until repairs can be made.

,

3

The licensee is investigating why the corrective actions for the first

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occurrence did not adequately correct all of the related maintenance

procedures.

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During the licensee's review of this deficiency, the licensee identified

that communications between the mechanical maintenance group and the

instrument group were poor, mechanical maintenance did not validate the

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work activities and supervisory oversight was weak. These findings were

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based on the fact that, although Section 6.7 of the mechanical

maintenance procedure was found to be blank, personnel did not verify

that all of the work had been completed by the instrument group prior to

closing out the work package.

The system is not safety-related and the problem is not considered to be

a regulatory concern, however this condition was considered to be

important because the failure of the locking bolts could result in a

loss of control of the steam dump valves and with the potential for the

valve to fail full open.

c.

Conclusions

Mechanical maintenance did not verify that all work had been completed

prior to closing out the work packages on the Unit 1 steam dump valves.

Procedure revisions to address the missed bolt torquing requirements in

1996 on Unit 2 were not sufficient to identify and correct all of the

associated work procedures, resulting in not torquing the bolts on

Unit 1.

M2.2 Failure of Voltaae Reculator on Emeraency Diesel Generator (EDG) 1A A

a.

Insoection Scope (62707)

The inspectors reviewed the sequence of events related to the repair of

the voltage regulator on EDG 1A A.

a.

Findii..s and Observations

On May 21, 1997, during performance of 1-SI 0PS 082 007.A. Electrical

Power System Diesel Generator 1A A, Revision 10, on EDG 1A A, operators

emergency stopped the EDG when generator voltage exceeded 9000 volts

(voltage should have been within the range of 6210 volts to 7590 volts).

The EDG was declared inoperable and the appropriate TS action statement

was entered. The licensee determined that no damage was done to the

generator and that the condition of high voltage existed for less than

five minutes.

Maintenance determined that a voltage regulator card had

failed. A replacement card was subsequently installed to replace the

one which had failed.

On May 23, 1997, the inspector observed the performance of a post

maintenance test (PMT) conducted under Work Order (W0) 97 007711. The

PMT tested the responsiveness of the repaired voltage regulator under

load and load reject conditions. The voltage regulator responded as

designed during the PMT, met the acceptance criteria of SI 0PS 082 007.A

and subsequently was declared operable.

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III. Enaineerina

E2

Engineering Support of Facilities and Equipment

E2.1 Unit 1 Steam Dumo System Modifications

a.

Inspection Scope (37551)

,

Due to previous problems with the operation of the steam dump systems on

both units, the inspectors observed the operation of the steam dump

system from the control room and locally during restart activities

following the Unit 1 refueling outage.

b.

Observations and Findinas

Following problems encountered with the Unit 2 steam dump system during

the October 11, 1996, plant shutdown, the licensee developed corrective

actions to address the various problems with the steam dump systems on

both units.

Inspection Report 50 327, 328/96 17 documented the proposed

corrective actions. During the Unit 1 refueling outage the licensee

implemented various system modifications to correct the problems with

the Unit 1 steam dump system.

During plant startup, the inspectors observed the o)eration of the steam

dump system.

Previously the steam dump system had seen observed with

mild water hammering due to water accumulation in the steam dump

discharge lines.

Modifications to the steam dump drain system appeared

to have successfully corrected this condition.

Although the recent modifications to the steam dump system appeared to

be effective. the inspectors noted a few operational / maintenance

problems regarding steam dump system operation during the startup. The

various problems encountered were as follows:

the steam dump system

master controller failed and had to be re) aired; the drain valve for

steam dump valve 50113 failed, causing t1e line to fill with water,

resulting in SD 113 being isolated during plant startup; and maintenance

did not torque the steam dump velve locking bolts (Section M2.1).

c.

Conclusions

The licensee was successful in implementing various modifications to

improve the operation of the Unit 1 steam dump system.

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)

IV. Plant Support

R

Status of RP&C Facilities and Equipment

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R1.1 Radioactive Water Soill

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a.

Inspection Scooe (71750)

The inspectors reviewed the licensee's actions in response to a large

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radioactive water spill on May 19, 1997.

b.

Observations and Findinas

I

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On May 19. 1997, a fire operations individual observed water flowing

down the stairwell on elevation 669 of the auxiliary building. The

licensee subsequently determined that the water came from a failed

conductivity probe on the inlet to the Modularized Fluidized Transfer

Demineralization System located in the 706 elevation in the railway bay.

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The licensee estimated that approximately 3000 gallons of radioactive

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water were spilled. Approximately 600 gallons of this water migrated to

the outside rad waste yard. Although the spill itself was contained in

the RCA (inside and outside in the rad waste yard), the licensee

measured contamination in the french drain system located underneath the

rad waste yard.

.

Contamination levels in the rad waste yard indicated up to 18,000

disintegrations per minute per 100 square centimeters. There were no

personnel contaminations as a result of the. spill or the clean up. The

licensee's immediate corrective actions included securing and posting

the areas, damming and cleaning up the affected areas, application of a

coating on the asphalt in the rad waste yard to prevent migration of the

i

contamination, and sampling the yard pond and storm drains.

Contamination was not detected in the yard pond or the storm drains.

The licensee also sampled the french drain system which runs underneath

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the rad waste yard and outside the RCA. Contamination was detected in

the french drain system at the boundary of the RCA.

The licensee started excavating the contaminated portions of the rad

waste yard and sections of the french drain system, including the gravel

underneath the french drain system, for removal and disposal of

contaminated material. TVA corporate hydrologists were involved in the

development of follow up actions.

c.

Conclusions

The inspectors concluded that the licensee's actions to contain and

,

mitigate the radioactive water spill were appropriate. An inspector

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follow up item (IFI) was identified for reviewing the licensee's

completed corrective actions for the spill (IFI 50 327, 328/97 04 05).

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V. Manaoement Meetinas

X1

Exit Meeting Summary

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The inspectors ) resented the inspection results to members of licensee

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management at tie conclusion of tne inspection on June 5,1997. The

licensee acknowledged the findings presented.

The inspectors asked tb 'icensee whether any materials would be

considered proprietary. No proprietary information was identified.

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

  • Adney, R., Site Vice President
  • Beasley, J., Acting Site Quality Manager

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Bryant. L., Outage Manager

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Driscoll

D., Training Manager

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  • Fecht, M. , Nuclear Assurance & Licensing Manager

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Fink,

F., Business and Work Performance Manager

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  • Flippo.

T., Site Support Manager

  • Herron, J.. P1 ant Manager

Kent, C., Radeon/ Chemistry Manager

  • Lagergren. B., Operations Manager

O' Brian, B., Maintenance Manager

Rausch, R. Maintenance and Modifications Manager

Reynolds,

J., Operations Superintendent

  • Rupert,

J., Engineering and Support Services Manager

  • Shell, R., Manager of Licensing and Industry Affairs
  • Smith,

J., Licensing Supervisor

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Summy, J., Assistant Plant Manager

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  • Valente,

J., Engineering & Materials Manager

  • Attended exit interview

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INSPECTION PROCEDURES USED

,

IP 37551: Onsite Engineering

IP 40500: Effectiveness of Licensee Controls In Identifying Resolving, &

Preventing Problems

IP 61726: Survaillance Observations

IP 62707: Maintenance Observations

)

IP 71707: Plant Operations

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IP 73753:

Inservice Inspection

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IP 50002: Steam Generators

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ITEMS OPENED. CLOSED. AND DISCUSSED

Opened

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T__ype Item Number

Status

Descriotion and Reference

NCV

50-327/97 04-01

Open/ Closed Failure to Maintain RCS Temper _ture

and Pressure Within the Limitations

of Plant Startup Procedure 0 G0 1

(Section 01.2).

VIO

50 327/97 04 02

Open

Failure to Meet the Surveillance

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Requirements of TS 4.10.3.2, For

Performing Functional Testing of the

Nuclear Instruments (Section 01.3).

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VIO

50 327/97 04-03

Open

Failure to Follow Procedure For

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Exceeding Fual Preconditioning

Limitations, Not Logging Changes In

Plant Conditions, and Not Informing

the Shift Manager of Changes In

Plant Conditions (Section 01.4).

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URI

50 327/97 04 04

Open

Further review of potential

regulatory issues noted in the

Unit 1 operational logs (Section

02.2).

IFI

50 327, 328/97 04 05

Open

Review licensee's corrective actions

following an inadvertent spill of

several thousand gallons of

contaminated water (Section R1.1).

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