ML20247F346

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Special Team Insp Repts 50-327/89-05 & 50-328/89-05 on 890131-0209.Violations Noted.Major Areas Inspected:Radwaste, Radiological Controls,Corporate QA Audits & Site Chemistry
ML20247F346
Person / Time
Site: Sequoyah  
Issue date: 03/13/1989
From: Adamovitz S, Marston R, Potter J, Shortridge R, Testa E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20247F334 List:
References
50-327-89-05, 50-327-89-5, 50-328-89-05, 50-328-89-5, NUDOCS 8904030414
Download: ML20247F346 (23)


See also: IR 05000327/1989005

Text

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UNITED STATES .

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NUCLEAR REGULATORY COMMISSION .

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REGION 11

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101 MARIETTA ST., N.W.

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ATLANTA, GEORGIA 30323

MAR 161989

Report Nos.: 50-327/89-05 and 50-328/89-05

Licensee: Tennessee Valley Authority

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'6N38 A Lookout Place

1101 Market Street

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Chattanooga, TN 37402-2801

Docket Nos.: 50-327 and 50-328

License Nos.:

DPR-77 and DPR-79

Facility Name: Sequoyah 1 and 2

Inspection-Conducted: January 30-February 3, and February 8-9, 1989

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Inspectors: b 8,

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E. D. Testa

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RF B. Shortri ge

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Approved by:

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J.47. Pottar, Chief

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Facilities Radiation Protection Section

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Emergency Preparedness and Radiological

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Protection Branch

Division of Radiation Safety and Safeguards

SUMMARY

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Scope

This was a special, unannounced team assessment / inspection in the areas of

Corporate and Site nuclear chemistry, radioactive waste, radiological controls

and Corporate Quality Assurance (QA) audits.

Unit 1 was operating at

100 percent (%) and Unit 2 was approximately 16 days into a refueling outage.

Results

The licensee's radiological controls program appeared to be sound and

improving.

The use of remote handling tools for steam generator nozzle dam

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installation was a positive step in controlling worker dose as low as

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reasonably achievable (ALARA).

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ADOCK 05000327

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Corporate. QA audits in the areas inspected appeared detailed and complete.

Positive steps were being implemented to reduce the number of standing general

Radiation Work Permits (RWPs). The licensee corporate and site staffs appeared

knowledgeable and sensitive to established goals.

'Within the areas inspected, one violation was identified for failing to perform

an adequatt radiation survey necessary to evaluate the extent of radiation

hazards present prior to operator entry (Paragraph 11).

Six inspectnr followup items (IFIs) were identified:

Worker comfort problems associated with supplied breathing air

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(Paragraph 9).

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Evaluation of breathing zone air samples versus general air samples

for respirators (Paragraph 9).

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Expansion of the identification of specific categories of event root

causes tc provide better data for evaluations and analysis

(Paragraph 10).

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Unexpected high beta dose rate in the steam generators

(Paragraph 12).

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Unexpected high airborne iodine concentrations in the containment

(Paragraph 13).

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Labels for clean laundry containers to distinguish them from dirty

laundry shipments into and out of the same plant location

(Paragraph 14).

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REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • W. Aslinger, Assistar.t Site Representative for Employee Concerns
  • J. Barker, Manager, Rad Con

J. Bates Manager, Corporate Chemistry Support Group

  • H. Blair, QA Specialist NQA

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S. Bradley, Shift Supervisor Radiological Health

  • J. Bynum, Vice President Nuclear Power Production
  • R. Coleman, Radiological Assessor
    • M. Cooper, Compliance Licensing Supervisor
  • P. Crabtree, Shift Operations Supervisor

J. Dills, Quality Assurance Specialist - Corporate

  • A. Dyson, QA Evaluator /QSS
  • G. Fizer, Chemistry and Environmental Superintendent

R. Halton, Assistant Site Representative for Employee Cuncerns

  • R. Hays. Radwaste Processing Coordinator
  • J.

LaPoint, Site Director

  • M. McMilland, Maintenance / Rad Con Work Coordintor
  • J. Patrick, Operations Superintendent
  • T. Phifer, Plant Reporting Engineer

W. Raines, Chief, Environmental Radiological Monitoring and

Instrumentation Branch

  • H. Rogers, Plant Support Superintendent
  • V. Shankes, Program Manager Chemistry

B. Smith, Quality Assurance Auditor

  • J. Smith, Plant Reporting Supervisor
  • S. Smith, Plant Manager
    • S. Spencer, Licensing Engineer
  • M. Sullivan, Superintendent, Radiological Controir
  • K. Walker, Quality Evaluator
  • J. Watts, Quality Evaluator

Other licensee employees contacted during this inspection included

engineers, operators, mechanics, technicians, and administrative

personnel.

Nuclear Regulatory Commission

  1. J. Brady, Project Engineer, TVA Projects Division
  • P. Harmon, Senior Resident Inspector

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  1. L. Watson, Section Chief, TVA Projects Division
  • Attended exit ir.terview
  1. Participated in teleconference briefing on February 9, 1989

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2.

Licensee Action on Previous Enforcement Matters

.This subject was not addressed during this inspection.

3.

Radiation Protection, Plant Chemistry, Radwaste and Environmental:

Organization and Management Controls (83522)

a.

Water and Waste Processing Group

The inspector discussed the organization, responsibilities, and

operations of the Water and Waste Processing Group (WWPG) with

cognizant licensee representatives, reviewed pertinent documentation,

and examined the facilities and equipment used by the Group.

The inspector determined that WWPG Supervisory personnel met the

qualifications specified in their position descriptions.

The Manager, Water and Waste Processing, reported to the Plant

Operations Superintendent who, in turn, reported to the Plant

Manager. The WWPG was divided into five subgroups which:

Managed, directed, and supervised packaging, loading (radwaste

only), storage, and shipping of all radioactive materials and

radwaste.

Directed development and implementation of the decontamination

program.

Directed the ir.plementation of radwaste minimization programs

and radwaste segregation and storage, and prepared shipping

documents.

Provided technical support to other operations and engineering

staffs.

Managed the technical and water processing units of the WWPG.

Licensee representatives stated that the current approved level of

69 people in the Group was scheduled to be reduced to 59. A licensee

representative stated that the losses would be spread through the

Group so as to minimize the reduction-in-force impact.

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The inspector reviewed Standard Practice, SQA129, Site Goals and

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Objectives, Sequoyah Nuclear Plant, for Fiscal Year (FY) 1988, and

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reviewed the WWPG Performance Measure / Goal for FY 1989.

The Group

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goals appeared to implement the Plant goals.

Specific goals for WWPG

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(FY1989)were:

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Ship no more than 8,736 cubic feet (ft3) per unit of Dry Active

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Waste (DAW) during the fiscal year.

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Ship no more than 1,300 ft3 per unit of resins, sludges, and

evaporator bottoms during the fiscal year.

Release an average of less than 550,000 gallons per month of

Liquid Radioactive Effluents during the fiscal year.

Licensee representatives stated that the Group had identified its

most significant problems and had developed corrective actions to

solve them.

Projected personnel reductions and the current outage

made the completion schedule uncertain.

The inspector toured the accessible parts of the radwaste processing

and storage systems, and discussed systems' operation and training

with systems' operators and supervisors. The personnel appeared to be

knowledgeable on the systems and their operation.

The inspector reviewed audits, surveillance, and evaluations of the

radwaste program conducted within the past year.

The audit program

appeared to be thorough and in-depth.

Corrective actions, where

required, appeared to be appropriate and timely,

b.

Site Radiologic:1 Controls Group

The inspector discussed the organization, responsibil4 cies, and

operation of the Radiological Controls Group (Rad Con) with cognizant

licensee representatives, reviewed pertinent documentation, and

examined the facilities and equipment used by the Group.

The inspector determined that Rad Con Supervisory personnel met the

qualifications specified in their position descriptions. The Rad Con

Supervisor had been at the site in this position sin e June 1988. He

had worked in the corporate office and various nucir.ir power plants

prior to his current job assignment.

The Radiological Controls

Superintendent reported to the Plant Manager. The Rad Con group was

divided into four subgroups which were called and were responsible

for:

Radiological Protection - Technical Support including ALARA

Radiological Health - Balance of Plant

Field Operations - Shif t Coverage

Administration and Health Physics (HP)

Information

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Administration and Reports

Licensee representatives stated that they were operating at the

current approved manpower level of 91 people in group. The group had

identified its most significant problems and had developed aggressive

action plans to solve them.

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Site Chemistry Department

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The Chemistry Department was managed b.v a Chemistry and Environmental

Superintendent who reported directly to the Plant Manager.

The

department was divided into four sections which included

Environmental, Chemistry Control, Technical Support, and Process

Control. Staffing for the department totalled 48 personnel including

supervisors and staff.

Ten additional positions, which were to be

divided among the various sections, had been cancelled due to TVA's

reduction-in-forcc plans.

The inspector reviewed a series of position descriptions which

defined the minimum qualifications, responsibilities, and primary

functions of each position in the department. Minimum qualifications

for chemistry supervisory personnel generally required a bachelor's

degree in an associated engineering or scientific discipline and four

years related experience. A review of individual resumes showed that

the related work experience for the superintendent and the four

section supervisors totaled 83 years.

In general, the licensee appeared to have a dedicated, knowledgeable

staff concerning chemistry matters.

Additionally, the technical

support staff was available to assist in the resolution of special

problems and to evaluate data concerning plant parameters.

The

chemistry staff had been reduced by the reduction-in-force cuts;

however, current staffing was considered adequate to maintain the

regular program but not to accomplish planned long-term goals.

The

department had issued a " Chemistry Improvement Program," and the

assigned due dates were based upon the additional ten staff positions

which had been eliminated. The current level of staff was considered

insufficient to achieve the original due dates and, at the time of

this inspection, the licensee had not rescheduled the dates based on

the reduced staff.

The chemistry count room had seven analysts to

maintain 24-hour coverage and this resulted in the back shift being

manned by a single individual.

The count room had arranged for a

temporary assignment of two Watts Bar technicians to alleviate the

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aNitional work loads caused by outage sampling.

The count room

supervisor also explained that, if required, low level activity

samples could be sent to the Training Center for analysis should the

count room became too backlogged.

Chemistry management exhibited a positive attitude toward identifying

and correcting program weaknesses.

Chemistry program improvements

and goals for the FY 1989 had been documented in the plan " Chemistry

Goals and Performance Indicators for Fiscal Year 1989." This plan

covered management improvement, quality performance, program

improvements, and safe and efficient operation.

Management

improvements included additional training and timely performance

appraisals.

Quality performance goals involved conducting chemistry

operations in such a manner as to minimize the number of INP0

findings or NRC violations, to quickly address any problem areas,

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and to evaluate causes of recurring problems.

To assist in problem

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identification, the chemistry department had initiated a " Chemistry

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Group Observation Program."

These observations would serve as an

additional, informal audit program.

The department had also

established an observation schedule.

The schedule covered selected

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plant systems for sampling and analysis, instrument calibrations,

onsite chemical controls, and Post Accident Sampling System (PASS)

operation.

Other general program improvements detailed in the " Chemistry Goals

and Performance Indicators" included incorporating the use of the

Nuclear Data Microvax system for gamme spectroscopy, effluent

management, and chemistry database management; establishing a

chemistry control program to monitor and trend plant parameters;

providing technical expertise to eval" ate and implement chemical

treatments of various plant systems; ar.d improving control of the

facility's solid waste disposal.

The chemistry department had also identified a series of long-term

goals which were summarized in the "Sequoyah Chemistry Improvement

Program."

The Improvement Program identified eight areas which

included standards development, online instrumentation upgrade, QA/QC

program development,

procedures

upgrade,

Microvax

program

development, chemical traffic control program, training upgrade, and

equipment deficiency corrections.

Generally, the goals established

by this program were broader based than the specific improvements

identified in the " Chemistry Goals and Performance Indicators for

Fiscal Year 1989," and some due dates extended beyond the current

fiscal year.

Chemistry management indicated that the due dates for the Improvement

Program were based upon the additional ten positions which had

subsequently been eliminated.

Based upon the reduced staff,

reevaluation of the due dates would be necessary and some program

improvements would be necessarily postponed or eliminated. However,

the licensee management also indicated that the program in.provements

identified in the " Chemistry Goals and Performance Indicators" were

based upon the current staff level and that the goals were considered

attainable during the originally established time periods.

From the

broader based improvement plan, procedural upgrades had been

initiated for approximately 50 chemistry instructions or procedures.

No violations or deviations were identified.

4.

Post Accident Sampling System (84750)

The licensee's liquid Post Accident Sampling System (PASS) contained

inline monitors 1or chemistry parameters and utilized diluted or undiluted

grab samples for radioisotopic analysis.

Inline measurements for

chemistry parameters included dissolved oxygen, pH, conductivity,

hydrogen, and chloride concentrations.

Currently, due to the design of

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the PASS isolation valves, both units inust enter a Limiting Condition for

Operation (LCO) in order to use the system.

A design change request had

been initiated to modify the PASS so that the system could be operated

without entering an LCO.

Due dates for the design changes were April and

October 1990 for Units 1 and

2,

respectively.

Other scheduled

modifications for 1989 included replacing the PASS flow indicators and

modifying the PASS tubing to allow sampling of the reactor coolant off-gas

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for hydrogen.

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No violations or deviations were identified.

5.

Corporate Radiological Control (83522)

Corporate Radiological Control was composed of four departments.

The

departments

were

Environmental

Radiological

Monitorinq

and

Instrumentation, Radiological Heal th, Radiological Prote' lon, and

Radiological Waste. The organization was composed of a staf* mnager, two

site Radiological Assessors (Sequoyah and Browns Ferry), 42 me ers of the

Environmental Radiological Monitoring and Instrumentation Department, nine

members of the Radiological Health Department, nine members of the

Radiological Protection Department and 13 members of the Radwaste

Operation Department.

Corporate Radiological Control was established to

interact with the sites to develop standards, guidance and procedures.

The function of the Instrumentation Calibration, Repair and Control

Department was described by the licensee.

This department calibrated,

maintained, and provided inventory control for all portable radiation

survey instruments.

The purchase of new or replacement instruments and

the maintenance of a central instrument' inventory were provided by this

department.

The department also performed the environmental radiological

monituring program which included the design, review, and reporting of

sample data.

The function of the Radiological Health Department was described by the

licensee to cover three major areas.

They were external dosimetry,

internal dosimetry, and an integrated HP information system. The external

dosimetry program was National Voluntary Licensee Accreditation Program

(NVLAP) accredited.

The licensee described the functions of the Radiological Protection

department.

The principal missions of the department include:

planning

and developing radiation protection policy, providing technical support to

the site, and conducting a corporate assessment program to evaluate

program effectiveness and consistency.

The mission of the Radioactive Waste Department was described by the

licensee.

The department was tasked with the support of the sites in

processing, packaging, transportation, and disposal of solid radioactive

waste and processing, and packaging and decontamination of radioactive

waste materials.

Program assessment was a secondary mission.

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The inspector reviewed selected site support activities provided by the

corporate support group and found active, aggressive program interactions.

The inspector verified portable survey instrument calibration and

maintenance through discussion with licensee site personnel.

The

inspector also reviewed selected portions of the Radioactive Material

Shipment Manual.

This manual outlined responsibilities, packaging and

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shipping requirements, training, quality assurance and administration and

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state and disposal site requirements.

The licensee discussed the support

of Sequoyah restart stating that approximately 202 man-days of effort from

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the Radiological Protection Department were expended during 1988.

Personnel from the Radiological Protection Department were routinely

assigned to the site Radiological Control organization to provide support.

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Two personnel were assigned to the site during the current outage.

The inspector reviewed the FY 1989 Operating Plan and selectively

discussed the goals and status of Performance Measures (goals).

The

program appeared aggressive, forward looking, accountable and the

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personnel knowledgeable about current site refuelina activities.

No violations or deviations were identified.

6.

Corporate Chemistry (83522)

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The licensee discussed the corporate support for site chemistry.

Corporate support was derived from Nuclear Support Chemistry.

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organization was staffed by a Chemistry and Environmental Manager who was

supported by six Program Managers and six Project Managers.

Chemistry

Level 3 goals for FY 1989 had been established and the performance in

those areas was tracked.

Measurable objectives to assure accomplishment

of goals were in place.

The inspector reviewed the position descriptions

and responsibilities outlined for the Chemistry and Environmental

Protection Manager (PD NS-03-006).

The licensee discussed the Draft

Chemistry Assessment Program.

The program consisted of periodic

assessments of site chemistry and chemistry training programs and was

performed by the corporate office.

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The inspector selectively reviewed the resumes and work histories and

found a broad base of experience in major nuclear power plant chemistry

areas, including auditing, procedure development, program evaluation, and

program management.

Interviews and discussions with selected members of the staff indicated

involvement with the site chemistry program; however, at the time of the

inspection, the corporate organization was not fully aware of the

unexpected levels of beta activity found in the Unit 2 Steam Generators

opened during the current refueling outage.

Discussion with both site and

corporate personnel indicated that there was less than open and free

communication links established between the site chemistry and the

corporate chemistry support group. The need for better communications was

an area of concern in the February 17, 1988 Corporate Evaluation of the

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Site Chemistry Program. The communication concern involved both corporate

and site chemistry programs.

The inspector selectively reviewed the Corporate Sequoyah Chemistry Audit

and Assessments Results for 1988, and found them to be detailed, in-depth,

with identified weaknesses tracked.

The audits involved procedures,

organization, and communication.

No violations or deviations were identified.

7.

Corporate / Site Quality Assurance (83522)

The inspector reviewed the qualification and training of the Corporate QA

staff who performed quality assessment audits of Sequoyah Nuclear Plant in

the area of Radiological Protection.

Selective review of the resumes and

audit certification records indicated substantial technical experience in

the area of health physics, including practical job experience.

The inspector selectively reviewed and discussed the following audit

reports:

SS-A-88-805, dated March 1988, QA Program Radiological Control

SS-A-88-808, dated June 1988, Radwaste Shipping, Radwaste

Storage, Process Control Program and External Radiation Control

Program

SS-A-88-815, dated August 1988, ALARA Program, HP Training and

Staff Qualifications

SS-A-88-901, dated January 1989, Radiological Effluent and

Environmental Monitoring and Dose Assessment Activities

The inspector determined that the audits were detailed, in-depth, and

adequately tracked identified items.

The licensee's chemistry program wt, evaluated by a series of onsite and

corporate audits.

The inspector reviewed selected audits for calendar

year 1988 which included the following audit reports:

Sequoyah Inspection / Audit Summary for 1988

"

Corporate Assessment of Sequoyah Nuclear Plant Chemistry Program

conducted May 23, 1988 to June 10, 1988

Sequoyah Chemistry Data Management Assessment, and Corporate Monthly

Reports for the months of October, November, and December 1988

The audits appeared thorough and the auditors knowledgeable of the various

program areas.

Identified problems were tracked and corrective actions

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were documented and thorough.

Programmatic weaknesses were also

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identified and specific examples given. The Technical Support Section was

implementing a program to " observe" chemistry activities including

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sampling, analysis, system operation, instrument calibration, and

laboratory housekeeping.

These observations would provide an additional

internal assessment of the plant's chemistry program.

No violations or deviations were identified.

8.

Radiation Protection, Plant Chemistry, Radwaste, Transportation and

Environmental: Training and Qualifications (83523)

The inspector reviewed the training program established for the Radiation

Control, Chemistry, and Water and Waste Processing Groups.

The

requirements for the training program were specified in Administrative

Instruction Al-14, "Sequoyah Site Training Program," Revision 40,

October 24, 1988.

This document included training and retraining

requirements for Managers, Operators, Scientists, Engineers, and

Technicians in the specified Groups.

The training was broken down into

classroom and on-the-job training and required written and oral tests.

The training programs for all levels of the Radiation Control and the

Chemistry Groups were specified in detail.

The Radiochemical Laboratory

Analyst training was specified to be 14 weeks in the classroom and

90 weeks on-the-job-training.

The Rad Con Technician training was specified as:

Basic Phase - 16 weeks, consisting of 10 weeks of Core training and

six weeks of Specialized (Field Operations, Dosimetry, or

Instrumentation / Respiratory Protection)

In-Plant Phase - 24 months

The Technical Staff and Managers Training consisted of:

Orientation (four weeks)

Systems (two weeks)

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Advanced Phase (24 weeks)

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Segment I (17 weeks)

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Detailed Systems Study (eight weeks)

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Comprehensive Exams (one week)

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Simulator (six weeks)

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It was noted by the inspector that the training programs evaluated placed

emphasis on systems knowledge.

Several lesson plans used by the training staff in training Chemistry and

Rad Con personnel were reviewed and were determined to be adequate.

Administrative Instruction AI-14, Part II.E., specifies Unit Operator and

Assistant Unit Operator training and retraining requirements, and lesson

plans were reviewed for Decontamination Worker training.

Licensee

representatives stated that, when it was determined that training was

needed, such as packer / loader or shipping / handling, the Water and Waste

Processing Group would notify their corporate counterparts, who would

arrange for the training to be provided.

Licensee representatives

provided the inspector with a recently developed matrix showing training

requirements for Managers, Engineers, AU0s, A0s (Auxiliary Operators), and

00s.

They stated that this program for training and retraining would be

implemented in the future.

No violations or deviations were identified.

9.

Internal Exposure Control and Assessment (83525)

a.

Engineering Controls and Respiratory Protection

During the inspection, the inspection team observed licensee

personnel response to an apparent problem with the breathing air

system.

On Monday, January 30, 1989, personnel involved with the

installation of nozzle dams in steam generators #2 and #3 using

robotics, complained that air supplied to their bubble hoods was

inadequate.

An Instrumentation / Respiratory Protection technician

entered containment to verify that the air manifold pressure gauges

were set correctly.

The technician found no problems with the

pressure settings.

On Tuesday, January 31, 1989, the personnel

working the steam generator continued to complain about not enough

air to the bubble hood and also complained about being hot.

The

Superintendent

of

Radiological

Control

instructed

the

Instrumentation / Respiratory Protection (I/RP) group to increase air

hose lengths to 100 feet, in order to increase the pressure setting,

and possibly increase the air flow to the bubble hoods. This did not

resolve the problem.

The workers were still complaining about

insufficient air to the bubble hood and being hot on Wednesday.

The

I/RP group entered containment to verify that there was proper flow

of air at the end of the breathing air hose that attached to the

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bubble hood.

In addition, pressure settings and air flow were

checked on every breathing air manifold in containment.

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collected were within the ranges specified by the National Institute

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of Occupational Safety and Health (NIOSH), as required by 10 CFR,

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Part 20, Appendix A, Protection Factors for Respirators, footnote h.

At this point, the I/RP group came to the conclusion that the problem

was not insufficient air pressure to the bubble hoods and agreed to

do whatever possible to ir. crease worker comfort. On Thursday at the

7:30 a.m. outage status meeting, the plant manager stated that he was

not satisfied with the progress made in resolving the breathing air

problem and instructed the I/RP group to go out and " crank up" the

air pressure on the breathing air manifolds.

The Superintend e t of

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Radiological Controls, a member of the NRC Assessment Team, and two

members of the I/RP met with the plant manager in his office at 8:00

a.m. that morning.

The Superintendent of Radiological Protection

explained that, although the pressure gauges on the breathing air

manifolds have locked, anti-tampering devices, that someone had

previously turned a pressure regulator up to 75 psig, above the 45

psig NIOSH certification limit for a 100-foot hose, and for that

period of time the air pressure was at 75 psig, protection factors

were not taken. Also, that the pressure gauges on the manifolds were

at the limit for the NIOSH certification and to increase air pressure

beyond this limit would violate the NIOSH certification and result in

a violation of 10 CFR Part 20 NRC regulations.

The Plant Manager

stated that steam generator personnel were getting sick and were hot

and that worker comfort was his major concern.

The inspector

informed the Plant Manager that increasing the air manifold pressure

was a safety concern in that a bubble hood could be blown off a

person's head and result in possible personnel injury and that the

problem appeared to be one of heat stress.

As a result of the

potential of violating NRC requirements for breathing air, the senior

resident inspector (SRI), NRC Assessment Team Leader, and Assessment

Team Inspector attended a meeting with the Site Director and Plant

Manager.

During the meeting, the plant manager stated that he did

not intend to violate NRC regulations and apologized.

The NRC

Assessment Team Inspector ' evidenced a concern that this event may

have intimidated radiological control first line supervision.

The

NRC inspector discussed this issue with six first line supervisors.

The majority responded that the cressure to meet schedules did exist.

Later in the afternoon on Thursday, the decision was made to monitor

the breathing air manifolds and increase air pressure after bubble

hoods were donned.

This resulted in an increased flow rate of

approximately 20% while monitoring NIOSH flow rate and pressure

limits.

The inspection team informed the licensee that the

corrective actions taken would be reviewed during a subsequent

inspection and would be identified as IFI 50-327,328/89-05-01.

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b.

Air Sampling

10 CFR 20.103 establishes the limits for exposure of individuals to

concentrations of radioactive materials in air in restricted areas.

Section 20.103 also requires that suitable measurements of

concentrations of radioactive material be performed to detect and

evaluate the airborne radioactivity in restricted areas.

The inspector observed the preparation of a high integrity container

(HIC) for dewatering and the installation of dewatering equipment.

The operation was performed in the 706-feet elevation railroad bay in

accordance with RWP 89-0119 and procedure RHSI-6, Radwaste Handling

and Shipping Instructions.

Installation of the dewatering equipment,

on the HIC reading 50 rem per hour, was performed using good ALARA

and radiological work practices.

Prior to opening the HIC, a Rad Con

technician started a general area air sample that ran for the

duration of the 30-minute operation.

The air sample was located

approximately 25 feet from the work area.

Licensee representatives

stated that airborne radioactivity had not been encountered during

previous dewatering operations and that instructions in the pre-job

briefing specified a general area air sample instead of a breathing

zone (BZ) air sample.

The inspectors discussed the advantages of

evaluating BZ air samples taken for short durations during a job,

involving

highly

contaminated

components,

with

licensee

representatives.

The licensee agreed to evaluate air sampling

requirements in HPSIL-6, Airborne Radioactivity Surveys.

The

inspectors informed the licensee that-this would be reviewed during

subsequent inspections and would be tracked as IFI 50-327,

328/89-05-02.

No violations or deviations were identified.

10. Control of Radioactive Materials and Contamination, Surveys, and

Monitoring (83526)

An inspector discussed the method used to identify and correct adverse

trends for personnel contaminations with licensee representatives.

The

inspector reviewed the November 1988 monthly repcrt that trended a number

of indicators of plant performance. The inspector noted that the trend of

personnel contaminations did not reveal any adverse trends other than the

number of people contaminated.

Radiolo

Personnel Contamination Reports (PCRs)gical Control personnel stated that

were tracked and trended and a

trending analysis was performed.

When adverse trends were identified,

corrective actions were coordinated with the responsible people.

The

inspector reviewed a listino of personnel contaminations for one

department at the station that identified the root cause of the

contamination event and the type of event.

The trend report was sent to

the department with a request for their corrective actions to prevent

recurrence.

This initiative was recent and results from various station

departments could not yet be evaluated.

The inspector noted that while

the root cause of personnel contaminations were usually identified in the

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PCRs, categories for event causes had not been developed and that trends

to identify specific problem areas at the station could not be

established.

Licensee representatives stated that they would consider

expanding the identification of specific categories of event root causes

to provide better data for evaluation and analyses and trending.

The

inspector notified the licensee that this would be reviewed during

subsequent inspections and would be tracked as IFI 50-327, 328/89-05-03.

No violations or deviations were identified.

11.

External Occupational Exposure Centrol and Personal Dosimetry (83524)

10 CFR 20.201(b) requires each licensee to make or cause to be made such

surveys as (1) may be necessary for the licensee to comply with the

regulations and (2) are reasonable under the circumstances to evaluate the

extent of radiation hazards that may be present.

Technical Specification 6.12.1 requires that any individual or group of

individuals permitted to enter high radiation areas in which the intensity

of radiation is greater than 100 mrem / hour, but less than 1,000 mrem / hour

shall be provided with or accompanied by one or more of the following:

(a) a radiation monitoring device which continuously indicates the

radiation dose rate in the area, (b) a radiation monitoring device that

continuously integrates the radiation dose rate in the area and alarms

when a preset integrated dose is received, and (c) an individual qualified

in radiation protection procedures who is equipped with a radiation dose

rate monitoring device.

The licensee notified the NRC inspection team of an unplanned exposure

event at 4:00 p.m. on February 2, 1989.

Licensee representatives stated

that two AU0s were working in a high radiation area in Unit 1 auxiliary

building that was created by an inadvertent introduction of reactor

coolant or resin into the Chemical and Volume Control System (CVCS)

demineralized resin transfer piping.

The licensee representative stated

that the AU0s received doses of between 400 and 500 mrem and did not

exceed any administrative or NRC exposure limits. The inspectors learned

that the area was posted as a radiation area and that the workers did not

have an integrating dose rate monitoring device or an individual present

with a dose rate monitoring device to provide radiological protection job

coverage.

The event was in the preliminary stage of investigation and a

description of the event would be provided as soon as possible.

The

inspection team leader informed the licensee that this event would be

considered an unresolved iten.

The inspection team noted that licensee's

immediate corrective action was to post and lock the high radiation areas

in the Unit 1 and Unit 2, 690 elevation pipe chases.

Radiation surveys

revealed a contact reading on the piping for recirculating the refueling

storage tank water at 3,500 mrem / hour and 750 mrem / hour at 18 inches in

the Unit 1 pipe chase.

A survey of the Unit 2, 690 elevation pipe chase

revealed one hot spot on the piping of 2,500 mrem / hour and 500 mrem / hour

general area.

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The preliminary report of the event was received in Region 11 on

February 8, 1989. The .'eport stated that two AU0s entered the pipe chase,

that had been surveyed and posted as a radiation area on January 31, 1989,

at 11:25 a.m.

Two valves were opened for recirculation of the refueling

water storage tank to accommodate a chemistry sample.

At approximately

1:25 p.m., one of the AU0s in the 690 pipe chase read his self reading

pocket dosimeter (SRPD) (0-200 mrem) and noted it was offscale.

Both

AU0s' SRPDs read offscale.

Recirculation operations were secured one

minute later and the AU0s exited the area and notified HP.

One AU0's

thermoluminescent dosimeter (TLD) read 430 mrem and the other's (TLD)

479 mrem. These readings reflected doses for the quarter; however, it was

established that the majority of the AU0s' doses were received as a result

of this event.

Although the root cause of the unplanned high radiation

area created in the piping for both units and the apparent loss of the

cation demineralized bed has not Leen determined, the radiological aspects

of the event have been identified. On February 9, 1989, the NP,C notified

the licensee's regulatory compliance group by telephone that the

unresolved items would be changed and would be considered an apparent

violation (VIO) of 10 CFR 20.201(b) and Techanical Specification 6.12.1

for failure to adequately evaluate the radiation hazards present in the

690-foot elevation pipe chase in the Unit I auxiliary building

(VIO 50-327, 328/89-05-04).

The inspector observed the remote installation of nozzle dams in the

Unit 2 steam generator.

The radiation dose rate in the steam generator

were found to be as high as 150 Rad /hr beta and 10 R/hr gamma. The use of

robotics and careful control of worker position in relation to radiation

shield exhibited good ALARA work planning and prvctices. The licensee was

analyzing material deposits to determine the isotope (s) causing the

unusually high beta dose rate.

The inspector notified the licensee that

this would be reviewed during subsuquent inspections and would be tracked

as IFI 50-327, 328/89-05-05.

One violation was identified.

12. Radioactive Waste Systems; Water Chemistry; Confirmatory Measurements and

Radiological Environmental Monitoring (84750)

a.

Liquid and Gaseous Radwaste Systems

The inspector discussed liquid and gaseous radwaste systems with

cognizant licensee personnel.

Liquid effluent release points to the

environment included the Liquid Radwaste System, the Condensate

Demineralized System, the Turbine Building Sump, and the Units 1 and

l

2 Steam Generator Blowdown.

Inputs to the facility's liquid radwaste

system originated from the Reactor Building and the Auxiliary

Building Floor Drains. The liquid then flowed to the Tritiated Drain

Collector Tank (TDCT) and the Floor Drain Collector Tank (FDCT) which

were currently interconnected.

The original purposr; of the TDCT was

to reclaim reactor grade water by routing the water to the TDCT for

treatment by a filter-demineralized combination and then recycling,

t

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Nonreclaimable~ liquid whste would be collected in the FDCT for

further processing and' final discharge.

Future plans for the two

tenks included installing isolation valves in the TDCT so that. the

reusable water could be separated and the system's original intent

3

accomplished.

From the FDCT, the liquid waste was processed by

either the Condensate Demineralized Waste Evaporator (CDWE) or a

andor-supplied radwaste system.

Liquid flow was then routed to the

Waste Distillate Tanks (A or B) and subsequently to the Monitor Tank

or to the Cask Decontamination Collector Tank.

Final release was

accomp"ished via the Cooling Tower Blowdown line as a batch release.

At the time of this- inspection, the licensee was implementing a

program to evaluate a vendor demineralization system for.radwaste

irrowsing.

This system would be considered as a possible

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replacement for the CDWE.-

In order to maintain better control of plant water and waste. systems,

the licensee was working on a water management plan that was

scheduled for. implementation the end of calendar year 1989. The plan

included a contracted water balance study of major plant systems.

This water balance study would also identify liquid radwaste sources

and equipment leaks.

Radioactive waste streams-would be chemically

che.racterized in order to evaluate the most efficient processing and

disposal systems.

Suitable systems would be tested inplant and

possible alternatives to the present processing would be the final

step.

The licensee's gaseous effluent system utilized six monitored

effluent vents which were the Service Building Vent, Auxiliary

Building Vent, Shield Building Vents (Units 1 and 2), and the

Condenser Vacuum Exhausts (Units 1 and 2).

The Containment Vent

exhausted via the Auxiliary Building Vent, and the Shield Building

Vents exhausted gases from the waste gas header.

Inputs to the waste

gas header included nine Waste Gas Decay Tanks (WGDTs) and the

Auxiliary Building Gas Treatment System ( ABGTS).

The ABGTS and/or

the Emergency Gas Treatment System (EGTS) had to be operated in order

to discharge a WGDT.

The EGTS could be used under routine or

emergency conditions to draw vacuum in the annulus and exhaust to the

Shield Building.

Each WGDT had a design capacity of 600 ft3

l

The inspector discussed with the licensee the capacities of the

plant's radwaste systems to handle the additional effluents generated

by outage conditions.

The licensee indicated that the liquid and -

gaseous radwaste systems had been adequate to process outage

effluents.

No special equipment or additional storage had been

required.

Current levels in the various liquid process tanks were

less than 50 percent of the tanks' capacities.

The inspector reviewed selected procedures concerning radwaste system

operation, sampling and effluent analysis. The procedures SI-400.1,

!

" Liquid Waste Effluent Batch Release," Revision 18; SI-401, " Steam

i

Generator Blowdown Continuous Release," Revision 16; and 51-410.4,

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" Waste Gas Decay Tank Release," Revision 6, clearly defined the

division.of responsibilities between Chemistry and Operations. Upon

request by Operations, Chemistry would initiate a release data

package.

Effluent sampling and analysis were performed by Chemistry

personnel with Operations being responsible for actual valve line-up

and tank release.

The licensee also maintained a procedure, SI-544,

" Verification of Representative Sampling of Liquid and Gaseous

Effluents," Revision 6, to demonstrate compliance with representative

sampling techniques.

An appropriate recirculation time for liquid

tanks was determined to be the time required for recirculation of two

tank volumes or for the total gamma activity to reach a steady state.

For gaseous tanks, the total gamma activity of nuclides in the WGDTs

was compared to gaseous effluents. Analytical methods were discussed

in Technical' Instructions TI-11 and TI-12 for chemical and

radiological analysis, respectively.

The inspector determined that

the reviewed procedures and instructions adequately described the

licensee's program for radwaste die harges.

b.

Effluent Monitors

The inspector discussed process and effluent monitors maintenance and

calibration with Instrument Engineers.

Monitor calibrations were

performed by the Instrument Maintenance Section, and functional

checks were performed monthly.

Program modifications were being

considered to change the frequency of performance checks for

nontechnical specification monitors to quarterly.

The monitors

required by technical specifications would maintain monthly checks.

Licensee personnel indicated that recently there hadn't been

recurrent maintenance problems with the monitors.

In reviewing the

Semiannual Effluent Report for the first half of 1988, the inspector

noted that two monitors had been declared inoperable for periods

greater than 30 days.

The Turbine Building Station Sump Discharge

Monitor, 0-RM-90-212, required a design change in order for the

monitor to discharge directly to the Turbine Building Sump.

This

monitor was repaired and declared operable by March 2,1988.

Flow

indicators, FI-30-242, for Units 1 and 2 Shield Building Exhaust were

declared inoperable in October and November 1987, respectively. The

indicators could not measure exhaust flow rates of less than

8,000 fta per minute.

Thus the licensee was using design flow rates

of exhaust fans in operation to estimate exhaust rates.

The flow

indicators had not been repaired as of the issuance of the

January-June 1988 Effluent Report.

The inspector accompanied licensee representatives on several plant

tours during the week and examined several effluent monitors.

The

licensee had addressed the subject of unmonitored release pathways in

!

response to IE Bulletin 80-10

" Contamination of Nonradioactive

1

System and Resulting Potential for Unmonitored, Uncontrolled Release

I

of Radioactivity to Environment."

Seven plant systems were

identified as having the potential to become radioactive through

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interface with radioactive systems. These systems were monitored via

a sampling program.

c.

Main Condenser

The licensee had implemented an in-leakage reduction program for the

main condenser during 1988 and had successfully reduced the Unit 2

,

air in-leakage from 45 SCFM to an average of 5.1 SCFM for the fourth

quarter 1988.

The licensee was using the INP0 supplied values of

6.7 SCFM median and 4.0 SCFM best quartile as goals for maximum

in-leakage.

d.

Primary Water Storage Tank (PWST)

0xygen levels in the Unit 2 PWST were reported as being 2,000 to

3,000 ppb during 1988.

Plant specifications limit oxygen

concentration to 100 ppb for reactor coolant system make-up water.

The licensee indicated that the cause of the high levels of dissolved

oxygen were inoperable diaphrams and had initiated a design change

Demineralized Water Storage Tank (DWST) gen blanket.

request, DCR-2701, to install a nitro

Since the

supplied water to the PWST, a

design change request, DCR-2801, was also implemented for a nitrogen

blanket.

Current dissolved oxygen levels for the DWST were 200 to

300 ppb.

The licensee expected the changes to be completed during

1989, or the first part of 1990.

e.

Component Cooling System

The . Component Cooling System had reoccurring problems of excessive

system leakage and required frequent additions of highly concentrated

chemicals because of an ineffective chemical addition system.

Originally, chemicals had been added through the drain pump casing.

The licensee changed this method to add chemicals through the surge

tank.

Excessive system leakage had been minimizcd by a system

walkdown and tightening loose valves.

The licensee had not

.

experienced leaks in the heat exchangers since the latter part of

l

1987, and these were plugged at that time. Since the heat exchangers

were close to the plugging margin (10%) on the B and C loops, the

licensee chose to replace the exchangers.

The B heat exchanger for

the B loop was being replaced during the current outage.

The other

two exchangers were scheduled to be replaced during the next two

outages.

No violations or deviations were identified.

13. Outage Management Control

The inspection team observed a number of events where licensee personnel

failed to effectively communicate and/cr cooperate with approved outage

plans.

The following are examples of specific events identified by the

inspection team to plant management.

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. On. Monday, January 30, 1989, the outage planning work group

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identified the need to perform air samples at four-hour intervals in

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containment to locate the sources of airborne noble gas and iodine.

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Rad Con was not able to report on progress at the 7:30 a.m. planning

meeting on Tuesday and, was instructed to get with chemistry and

report back as to why this was not performed.

Investigation revealed

that . Rad Con and Chemistry were not in attendance -at the Monday

planning meeting and that no instructions had been placed.in the Rad

Con night order book to take the air samples.

On Tuesday, Rad Con

took 176 air samples to support routine outage operations and. to

locate the sources of .the elevated airborne- iodine activity.

On

Wednesday, Rad Con reported that the sources of airborne still~ had

not been located and were instructed by plant management to continue

'

air sampling but to map the location of air sat:ples.

On Thursday,

'

airborne concentrations of iodine were still above the 1 MPC limit

and .. personnel were still required to wear respirators into

containment.

The Plant Manager stated that 12 of the last 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

hed been lost due to high airborne in. containment and the inabil'ty

to open the equipment hatch to move needed material into and out of

-containment.

The inspector informed the licensee that the higher than anticipated

airborne radiciodine concentrations in the containment would be

tracked as IFI 50-327, 328/89-05-06.

On Thursday. Rad Con requested that 0perations ensure thet the

equipment hatch was closed to within four or five feet from the floor

prior to raising reactor vessel water from mid-loop. This was to be

a precaution to ensure that negative pressure was maintained in

containment and to minimize the possibility cf an uncontrolled

release of airborne radioactivity to the environment. The inspecticu

team learned on Friday that the reactor vessel water level was raised

from mid-loop in preparation for reactor head removal, but the

equipment hatch to Unit 1 was not partially closed.

No uncontrolled

release of airborne radioactivity to the environment had taken p'. ace,

however.

No violations or deviations were identified.

14. Plant Tour

The inspector, accompanied by the Superintendent, Radiological Controls,

during a tour of the facility, noted that dirty and clean laundry was

received and shipped from the railroad bay at the 706-foot elevation.

Licensee workers were observed obtaining bags of clean hoods from shipping

containers for clean laundry dress out inventory at the steam generator

dressout facility. Although magnetic signs that indicated " clean laundry"

l

were available, they had not yet been placed on the containers.

The

licensee agreed to review the receipt and identification of clean laundry

so that these containers are received and identified in a more timely

manner.

The inspector informed the licensee that this would be reviewed

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during subsequent inspections and would be tracked as IFI 50-327,

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328/89-05-07.

No violations or deviations were identified.

15. Radwaste Solidification Incident Followup (92701)

After the licensee started processing the laundry and hot shower drain

tank through the CDWE, it was discovered that the use of a laundry

detergent (Turco 4324 NP) left a residue in the evaporator bottoms which

caused an exothermic reaction when the vendor added stabilization,

solidification, and defoaming agents to the waste bottoms in the liners.

This reaction led to an expansion and overflow of the contents in the

liner. This occurred in May 1987. As an immediate corrective action, the

licensee issued a memorandum in July 1987 to suspend the use of the

cleaning agent "Turco."

During the inspection, the inspector, accompanied by a licensee

representative, inspected Warehouse 11.

The inspector discovered ten

5-gallon plastic containers marked "Turco."

The containers were very

dusty and some were tagged with tags which read, " Returned from

Harcsville," and dated either August 1987 or September 1987.

A licensee

representative later stated that the "Turco" had been sent to Hartsville,

and had apparently been returned. The licensee representative also stated

that since the "Turco" had never been reentered on the computer, it would

not have been issued for use.

No violations or deviations were identified.

16. Action on Previous Inspection findings (92701)

a.

(Closed) IFI 50-327/88-31-01:

Followup on the inclusion of the

topics, hot particles, and hot particle control into general employee

training (GET) and continuing training.

The inspector reviewed the GET lesson plan GET 002.1-5, Controlled

Areas and HP Retraining, '2.5 Level I retraining and determined that

the subject of het particles had been included in instructions to

workers. This item is considered closed.

b.

(Closed)IFI 50-327/88-04-03: Followup on development of a procedure

to monitor for iodine during emergency conditions.

The inspector reviewed Radiological Control

Instruction 20,

Radiciodine Monitoring During Accident Conditions.

The instruction

provided the operational requirements necessary for the protection of

employees from airborne radiciodine during accident conditions. This

item is considered closed.

c.

(Closed) IFI 50-327, 328/88-38-04: Evaluation of the Nonradiological

Confirmatory Measurements results.

Nonradiological samples had been

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left with the plant che.nistry group with instructions for each sample

to be analyzed in triplicate by three different analysts (where

possible).

The analyses were completed by August 5,1988, and the

results sent to the NRC on August 11, 1980.

The NRC evaluated the

results and sent them to the licensee in the Nonradiological

Confirmatory Measurement Results Supplement to Inspection Report

Nos. 50-327/88-38 and 50-328/88-38. This item is considered closed.

17.

Followup on Employee Concerns Program

The inspector followed up on an Employee Concern in the area of radwaste

shipment.

The concern dealt with the possible shipment of unsolidified

resin bottoms to the licensed burial site.

The time table of events of

this concern were as follows:

December 9. 1908, concern received in Employee Concern Program

December 9,1988, at approximately 12:20 p.m. management briefed on

concern

December 9, 1988, File ECP-88-SQ-Q45 opened

January 5,

1989, Results of internal investigation received in

Employee Concern

January 5, 1989, upgraded to Concern ECP-89-SQ-020-01

January 26, 1989, Management Brief to Site Director

Plant deportability investigations underway

January 39, 1989, Senior level management briefing

February

1, 1989, Conclusions and recommendation preparations

Employee Concern was still in the process of completing the final report

al.d awaiting management action.

No final determination could be made by

the inspector until the licensee completed the final report and

appropriate management action had beer. taken.

18.

Exit Interview

The inspection scope and findings were summarized on February 3,1989,

with those persons indicated in Paragraph 1.

The inspector described the

areas inspected and discussed in detail the inspection results listed

below.

Although proprietary material was reviewed during the inspection,

proprietary information is not contained in this report.

During a

teleconference between NRC and licensee representatives on February 9,

1989, the licensee report on the AU0's entrance into the high radiation

areas was discussed.

Dissenting comments were not received from the

licensee.

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Item Number

Description and Reference

50-327, 328/89-05-01

IFI - Determine the cause of

wearer comfort probit's during the

use of hoods and supplied

breathing air (Paragraph 9.a).

50-327, 328/89-05-02

IFI - Evaluate breathing air

sample versus general air sample

requirements in Procudure HPSIL-6,

Airborne Radioactivity Surveys

(Paragraph 9.b).

50-327, 328/39-05-03

IFI - Expand the identification of

specific categories of events root

causes to provide better data for

evaluation

and

analysis

(Paragraph 10).

50-327, 328/89-05-04

VIO - Failure to perform radiation

surveys necessary to evaluate the

extent of radiation hazards

present prior to entrance of two

AU0's into a high radiation area

(Paragraph 11).

50-327, 328/89-05-05

IFI - Determine the cause of the

higher than anticipated beta dose

rates in the steam generators at

shutdown (Paragraph 11).

50-327, 328/89-05-06

IFI - Determine the cause of

higher that expected airborne

radiciodine concentrations in the

containment (Paragraph 13).

50-327, 328/89-05-07

IFI - Provide positive control of

shipment and receipt of laundry

(Paragraph 14).

Licensee management was informed that IFIs discussed in Paragraph 16 were

considered closed.

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