ML20216H784

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Insp Repts 50-327/98-03 & 50-328/98-03 on 980201-0314. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML20216H784
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 04/10/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20216H631 List:
References
50-327-98-03, 50-327-98-3, 50-328-98-03, 50-328-98-3, NUDOCS 9804210224
Download: ML20216H784 (30)


See also: IR 05000327/1998003

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U.S. NUCLEAR REGULATORY COMMISSION

REGION II

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Docket Nos:

50-327. 50-328

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License Nos:

DPR-77. DPR-79

Report No: 50-327/98-03. 50-328/98-03

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Licensee:

Tennessee Valley Authority (TVA)

Facility:

Sequoyah Nuclear Plant. Units 1 & 2

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Location:

Sequoyah Access Road

Hamilton County. TN 37379

Dates:

February 1 through March 14. 1998

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Inspectors:

M. Shannon. Senior Resident Inspector

R. Starkey Resident Inspector

R. Telson Resident Inspector

C. Smith. Reactor Inspector (Section E2.1)

E. Testa. Reactor Inspector (Sections R1, R2. R7. R8)

Approved by:

H. Christensen. Chief

Reactor Projects Branch 6

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Division of Reactor Projects

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Enclosure 2

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9804210224 980410

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ADOCK 05000327

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EXECUTIVE SUMMARY

Sequoyah Nuclear Plant. Units 1 & 2

NRC Inspection Report 50-327/98-03, 50-328/98-03

This integrated inspection included aspects of licensee operations,

maintenance, engineering, plant support. and effectiveness of licensee

controls in identifying. resolving, and preventing problems; in addition, it

includes the results of a radiological control inspection and an engineering

inspection.

Ooerations

A negative finding was identified due to a lack of instructions in

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surveillance procedure 0-SI-SXV-063-266.0 for establishing the necessary

plant conditions prior to valve stroke testing (Section 01.2).

A negative finding was identified for operations management not ensuring

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that operators periodically review the printout from the

annunciator / alarm printer (Section 01.3).

The inspectors noted a potential problem requiring further review for a

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potential failure to enter the action statement of Technical Specification (TS) 3.11.2.5 when chemistry grab samples indicated a high

oxygen concentration in Unit 1 pressurizer relief tank (PRT) (Section

01.4).

The inspectors noted several potential problems during the review of the

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high oxygen concentration in Unit 1 PRT.

Further review will be

necessary for the following items: potential failure to meet the Updated

Final Safety Analysis Report (UFSAR) requirements for having an

automatic gas analyzer. not adequately revising the UFSAR to describe

actual plant configuration for the gas analyzer, inappropriately closing

the design change package and not establishing a periodic

oxygen / hydrogen sampling program for the various waste gas collection

tanks (Section 01.4).

Mair,tenance

In general, the conduct of maintenance and surveillance activities was

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good (Section M1.1).

Enaineerina

The inspectors noted that the licensee's American Society of Mechanical

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Engineers (ASME)Section XI valve testing program may not include all

necessary/ required valve testing and further review will be necessary to

resolve this issue (Section E1.1).

The Corrective Action Program was generally implemented in accordance

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with the requirements of procedure SSP-3.4. Corrective Action. Revision

23. The program follows the guidance of Generic Letter 91-18. Revision

1. for disposition of degraded and non-conforming conditions and fully

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satisfies- the' requirements of 10 CFR 50 Appendix B.' Criterion XVI.

(Section E2.1).

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Plant Sucoort

A violation was identified for' failure to initiate a problem evaluation

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report (PER) afterLchemistry analysis of Unit 1 PRT sample -indicated a

high oxygen concentration. A second example of this' violation was

identified for_ the failure to initiate a work request when chemistry

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personnel could not obtain a PRT sample due;to apparent blockage of the

sample line (Section 01.4).

Radiological facility conditions and housekeeping in radioactive waste

storage areas. health abysics facilities, auxiliary building and

refueling floor were 03 served to be good, material was labeled

appropriately. and areas were properly posted (Section R1.1).

Radiation work activities were planned.. radiation worker doses were

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being maintained well;below regulatory limits and the licensee was

continuing to maintain exposures as low as reasonably achievable

(Section.R1.1).

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' Contamination control was effective (Section R1.1).

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The licensee had effectively implemented a program for shipping and

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receiving radioactive materials as required by NRC and Department of

Transportation (DOT) regulations (Section R1.2).

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The water chemistry control program.for monitoring primary and secondary

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water quality had been implemented._for_those parameters reviewed. in

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accordance with the TS requirements (Section R1.3).

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The meteorological. instrumentation had been adequately maintained and

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the meteorological monitoring program had been effectively implemented

_ Section R2).

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The inspectors' determined the licensee was effectively conducting formal

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radiation protection (RP) audits as required by TS and conducting self-

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assessments. The licensee was effectively developing corrective action

plans and completing corrective actions in a timely. manner (Section R7).

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Report Details

Summary of Plant Status

Unit 1 operated at full power for the entire inspection period.

Unit 2 operated at full power for the entire inspection period.

Review of Updated Final Safety Analysis Reoort (UFSAR) Commitments

While performing inspections discussed in this report, the inspectors reviewed

the applicable portions of the UFSAR that were related to the areas inspected.

The inspectors verified that the UFSAR wording was generally consistent with

the observed plant practices, procedures, and/or parameters.

However, during

the review of the UFSAR for the operation of the waste gas analyzer, the

inspectors noted that the recently installed waste gas analyzer could not

function as stated in the UFSAR.

This issue is discussed in Section 01.4 of

this report.

I. Operations

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Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent

reviews of ongoing plant operations.

In general, the conduct of

operations was considered to be good.

01.2 Unit 2 Inadvertent Boration Event

a.

Insoection Scooe (71707)

The inspectors reviewed the circumstances surrounding a Unit 2

inadvertent boration event as a result of an American Society of

Mechanical Engineers (ASME) Code Section XI valve stroke test. The

inspectors reviewed the Problem Evaluation Report (PER) No. SO980188PER:

the Unit 2 control room log: Procedure 0-SI-SXV-063-266.0. "ASME Section

XI Valve Testing." Rev. 3. Data Sheet No. FCV-63-7: the ASME Section XI

Code: Volume Control Tank (VCT) level and pressure trends: charging

system drawings: and engineering calculations.

The inspectors also

interviewed the system engineer, engineering department supervision, and

operations personnel as to their review and investigation into the

event.

b.

Observations and Findinas

On February 25. 1998 at approximately 2:15 a.m.. the licensee was

performing ASME Code Section XI stroke testing of valve 2-FCV-63-7.

" Safety Injection System (SIS) Pump Suction from Residual Heat Removal

(RHR) Pump Discharge." The control room operators noted a power level

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decrease of approximately 34 Mwt.

Subsequently, the operators

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determined the )ower decrease to be from an inadvertent boron addition.

Actions were tacen to enter Abnormal Operating Procedure (AOP) C.02.

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" Dilution and Rod Movements to Maintain Reactor Power." Reactor power

was stabilized and normal operations resumed without further incident.

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The AOP was exited at 5:35 a.m.

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The performance of surveillance )rocedure 0-SI-SXV-063-266.0 stroked 2-

FCV-63-7 established a flowpath Jetween the Refueling Water Storage Tank-

'(RWST) and the charging pump suction.

Normal charging operation

provides suction from the VCT. However, during performance of this test

VCT level was approximately 24% with pressure approximately 20 asig.

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Operating at those conditions established an equivalent static lead

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pressure in both the VCT and RWST.

Therefore due to the flowpath

already established for stroke testing of 2-FCV-63-7 borated water from

the RWST was directly supplied to the charging pump suction.

As a result of this event, the licensee revised the surveillance

procedure to include steps to establish a minimum VCT level and pressure-

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prior to performance of the subject valve stroke testing. The licensee

is also conducting a review of other valve stroke procedures to

determine if'other flowpaths could be established that may cause an

inadvertent dilution or boration event.

c.

Conclusions

A negative. finding was identified due to a lack of instructions in

surveillance procedure 0-SI-SXV-063-266.0 for establishing the necessary

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plant conditions prior to valve stroke testing.

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01.3 Ooerators 00 Not Periodically Review Annunciator-Printer

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a.

.Insoection Scooe (71707)

The inspectors reviewed the circumstances which led to the

identification by the licensee that the main control room annunciator

printer printout was not routinely reviewed by control room operators.

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b.

Observations and Findinas

-On February 24, 1998, the licensee initiated PER No. SO980185PER which

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documented an intermittent (occasionally flickering) " protection set .I

trouble" status light on Unit 2.

The intermittent status light wa's of

such a short duration (approximately one-tenth of a second) that

.o>erators seldom observed the-flickering light. Upon further' review.

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t1e licensee discovered that during the month of February that the

channel I protection set alarm had been recorded on the annunciator

printer approximately four times and that the channel IV protection set

trouble alarm had been recorded approximately 20 times. The licensee

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subsequently. installed monitoring equipment on the protection set

channels in order to identify the source of the alarms.

On March 17.

1998. the licensee identified and replaced a faulty card in an

instrument rack which a) pears to have corrected the problem with the

intermittent status lig1ts.

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When the licensee identified that the intermittent status lights had

been recording on the alarm printer. they discovered that there was no

procedural requirement or expectation that operators periodically review

the annunciator 3rinter.

The inspectors reviewed SSP-12.1. Conduct of

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Operations and t7e operators' turnover procedures and confirmed that

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neither addressed a requirement for operators to review the annunciator

printer printout.

As an interim corrective action. the licensee initiated Standing Order

98-014. dated March 16, 1998. which stated that operators shall verify

at the beginning and end of their shift that the alarm printout does not

contain any entries indicating an unknown problem, document the review

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in the unit log. and inform the unit supervisor and shift manager of any

abnormal annunciator entries. The long term corrective action will be

to revise the operators' turnover procedures (1-PI-0PS-000--21.1 and 2-

PI-0PS-000.023.1) to include a review of the annunciator printer at the

beginning and end of each shift.

c.

Conclusions

A negative finding was identified for operations management not ensuring

that operators periodically review the printout from the

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annunciator / alarm printer.

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01.4 Potentially Hiah Concentrations of Oxvaen and Hydroaen In the

Pressurizer Relief Tank (PRT)

a.

Insoection Scoce (71707 and 84750)

The inspectors reviewed the licensee's followup and corrective actions

after grab samples indicated high concentrations of oxygen and hydrogen

-were present in the PRT.

b.

Observations and Findinas

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On February 6. 1998. the licensee sampled the Unit 1 PRT. Analysis of

the sample. indicated that the hydrogen concentration was 22.8% and the

oxygen concentration was 12.1%.

This sample indicated that a flammable

or explosive mixture of hydrogen and oxygen was present in the PRT. On

February 7. the licensee resampled the Unit 1 PRT. Analysis of the

sample indicated that the hydrogen concentration was 22.8% and the

oxygen concentration was 12%.

Later on February 7. the issue was

discussed between the shift manager, shift technical advisor. Unit 1

senior reactor operator and plant licensing.

Licensing concluded that

the PRT was not part of the Waste Gas Holdup System as defined in TS , 3.11.2.5 and thus was not a regulatory concern that would ) lace the

plant in a LCO condition.

The shift manager concurred wit 1 this

interpretation. The Unit'l control room logs noted that a caution order

would be placed on the PRT vent isolation valve to the waste gas header

and that chemistry department personnel would investigate and resolve

concerns with the suspect sampling technique / problem.

On February 8.

1998, the licensee obtained another sample of the Unit 1 PRT and the

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analysis again indicated high concentrations of hydrogen at 35% and

oxygen at 9%.

During the last week of February, the inspectors conducted an integrated

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review of the control. room logs and noted the February 7 and February 8

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entries concerning the high concentrations of oxygen and hydrogen in the

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PRT.

The licensee was requested to discuss the issue on March 2 with

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the inspectors.

The licensee stated that the high concentration of

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. Oxygen indicated in the PRT was due to a sampling problem and that the

PRT did not contain a high oxygen concentration.

The licensee also

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indicated that a PER would be initiated to track resolution of this

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issue. The inspectors requested to be informed prior to the next PRT

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vent or sample evolution so that the evolution could be observed.

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On March 12. 1998, further discussions were conducted with operations

and chemistry departments. Based on these discussions, the inspectors

noted that plant startup activities following the last refueling outage

could have introduced oxygen into the PRT: the licensee did not

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continuously monitor or periodically sample the PRT: the licensee could

not sample the PRT without drawing a vacuum on the PRT sample line; a

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work request to troubleshoot the problem with drawing a PRT sample had

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not been written: a PER had not been initiated to address the

potentially high concentrations of hydrogen and oxygen from the February

6. 7 and 8 sample results: and the licensee had not confirmed by sample

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analysis that the PRT did not have a high concentration of oxygen.

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On March 17. 1998, the licensee initiated a procedure revision to'the

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System Operating Instruction 1 S0-68-5. Pressurizer Relief Tank, to

' provide procedural instructions for venting the PRT while in Modes 1. 2.

3 and 4.

On March 18, 1998, the. Unit 2 PRT was sampled, pressurized

with nitrogen and sampled, and vented to the waste gas vent header and

sampled.

Analysis of the sam)les indicated that the oxygen

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concentration in the PRT was Jelow the revised procedure limit of 2%

limit.

On March 19. 1998, the Unit 1 PRT was sampled, pressurized with

nitrogen and sampled, and vented to the waste gas vent header and

sampled.

Analysis of the samples indicated oxygen concentrations of

ap)roximately 5% with hydrogen concentrations of about 25%.

During

su) sequent venting of the PRT to the waste gas vent header, the waste

gas analyzer indicated that the waste gases being processed from the PRT

contained less than a 1% concentration of oxygen. A manual grab sample

-of the waste gas decay tank also indicated that waste gases being

-processed from the PRT contained less than 1% oxygen. The online

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monitor and the additional manual grab sample of the PRT supported the

licensee's conclusion that the previous PRT sampling process had been

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providing erroneous.results.

The inspectors noted various problems during the ongoing reviews and

discussions of the PRT and sample monitor issues.

The following

paragraphs document the inspectors findings.

TS 3.11.2.5. Explosive Gas Mixture, requires that the concentration of

oxygen in the waste gas holdup system shall be limited to less than or

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equal to 2% by volume whenever the hydrogen concentration exceeds 4% by

volume. The surveillance recuirement SR 4.11.2.5 requires that the

concentration of hydrogen anc oxygen in the waste gas holdup system

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shall be determined to be within the above limits by monitoring the

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waste gas additions to the waste gas holdu) system with the hydrogen and

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oxygen monitors. Amendment 12 of the UFSA1. Section 11.3.2. states that

"The automatic gas analyzer determines the quantity of oxygen and

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hydrogen in the volume control tank, pressurizer relief tank, holdup

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tanks, evaporators, gas decay tanks, and spent resin storage tank and

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provides an alarm on high oxygen and hydrogen concentration." Amendment

13 to the UFSAR removed the ~ Automatic" requirement for the gas analyzer

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and stated. "The online gas analyzer determines the quantity of oxygen

and hydrogen in the volume control tank, pressurizer relief tank, holdup

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tanks, gas decay tanks, and spent resin storage tank by monitoring the

waste gas header, or by selecting the individual sample Joint. The

waste gas analyzer provides an alarm on high oxygen and lydrogen

concentration." . Based on the UFSAR statements, it ap) eared that the

" waste gas holdup system" documented in TS 3.11.2.5 s1ould include the

tanks where waste gases were collected (holdup tanks. PRT. etc.).

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associated piping and compressors, and the waste gas decay tanks and

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that TS 3.11.2.5 would be applicable to the entire waste gas collection,

processing and storage system.

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On February 6 and 7, 1998, the licensee sampled the PRT and noted high

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concentrations of hydrogen (23%) and oxygen (12%). however: the

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. licensee may have-inappropriately concluded that the PRT was not a part

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of the waste gas holdup system and therefore did not enter the action

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= statement,for TS 3.11.2.5.

TS 3.11.2.5 b states that "with the

concentration of oxygen in a waste gas holduo tank greater than 4% by

volume and the hydrogen concentration greates than 2% by volume, without

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delay suspend all additions of waste gases to the affected waste gas

holdup tank and reduce the concentration of oxygen to less than or equal

to 2% by volume without delay." Not entering the TS 3.11.2.5 LCO action

statement is being identified as an unresolved item pending 'further

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review.-(URI 50-327/98-03-01).

On February 6 and 7. 1998, when the initial PRT sampling )roblems were

noted, the licensee failed to initiate a PER to resolve t1e issue.

During discussions with the NRC on March 2. 1998, the licensee stated

that a PER would be initiated to address the issue; however on March

12. the ins)ectors noted that a PER still had not been initiated.

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March 13. PER No. SO980240PER was initiated to document the ongoing

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investigation into the PRT sampling and analysis difficulties. The

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licensee's Site Standard Practice procedure SSP-3.4. Corrective Action.

Section 3.0.A. requires personnel to promptly report adverse conditions

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on a work request / work order and/or a PER.

The failure of site

personnel to initiate a PER after the analysis of the PRT sample

indicated a high oxygen concentration is considered to be a failure to

follow the Corrective' Action procedure and is identified as a violation

(VIO 50-327/98-03-02).

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On February 6.1998 the licensee was unable to obtain a sample from the

pressurized (3-6 psig) PRT without using a vacuum ) ump. This adverse

condition was not addressed by initiation of a worc request until after

the March 12 discussion with the NRC. The failure to initiate a work

request is considered to be another example of a failure to follow the

Corrective Action procedure and is identified as a second example of

violation (VIO 50-327/98-03-02).

Amendment 12 of the UFSAR noted that "The automatic gas analyzer

determines the quantity of oxygen and hydrogen in the volume control

tank, pressurizer relief tank holdup tanks evaporators gas decay

tanks, and spent resin storage tank and 3rovides an alarm on high oxygen

and hydrogen concentration." However, t1e licensee stated during

discussions with the inspectors that the system had not been capable of

performing the automatic sampling as specified in the UFSAR. Amendment

13 of the UFSAR noted that. "The online gas analyzer determines the

quantity of oxygen and hydrogen in the volume control tank, pressurizer

relief tank, holdup tanks, gas decay tanks, and spent resin storage tank

by monitoring the waste gas header, or by selecting the individual

sample point." However, the inspectors noted that the system was not

capable of sampling the various tanks by " selecting individual sample

points." Following the installation of a new waste gas analyzer in

October 1997 the waste gas analyzer could no longer be aligned to

sample individual tanks.

The only way to sample the collection tanks

would be to perform a manual grab sample.

In addition, discussions with

the licensee indicated that a program to periodically sample the tanks

following the plant modification to the gas analyzer had not been

established.

During the review, the licensee noted that the October 1997 design

change of the gas analyzer had not been implemented correctly in that

the necessary changes to the UFSAR had not been processed although the

modification package was signed off as complete and was in " closed"

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status. The potential failure to meet the UFSAR requirements for having

a gas analyzer that could sample the individual tanks not adequately

revising the UFSAR to describe actual plant configuration for the gas

analyzer, inappropriately closing the modification package and not

establishing a periodic sampling program for the various waste gas

collection tanks is considered to be an unresolved item pending further

review (URI 50-327, 328/98-03-03).

Further discussions indicated that the licensee's original intent for

sampling the " individual sample points." referenced in the UFSAR.

amendment 13, was to aerform periodic manual grab samples that would

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then be analyzed in t1e chemistry lab.

The licensee indicated that all

necessary changes to the description for the waste gas analyzer would be

incorporated into Amendment 14 of the UFSAR.

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The inspectors reviewed the System Operating Instruction 1-S0-68-5 for

the Pressurizer Relief Tank and noted that the Precauticos and

Limitations section of the procedure provided limits for oxygen and

hydrogen concentrations in~the PRT.

Section 3.0.C stated "The PRT

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oxygen concentration limit is less than 5% by volume and the PRT

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hydrogen concentration limit is less than 4% by volume." Discussions

indicated that the licensee had not evaluated the PRT procedural limits

following the February 6 and 7 sample results because they considered

the sample results to be erroneous.

Based on the way the procedure

limits were written. the February 6, 7 and 8 samples indicated that.both

the hydrogen and oxygen concentrations exceeded the procedural

limitations. This procedural issue was considered to be a part of the

previous violation for failure to initiate a PER, as discussed in

Section 01.4 of this report.

c.

Conclusions

An unresolved item was identified for not entering the action statement

of TS'3.11.2.5 when chemistry grab samples indicated a high oxygen

concentration in the Unit 1 PRT.

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A violation was identified for the failure of site personnel to initiate

a PER after the' chemistry analysis of the Unit l'PRT sample indicated a

high oxygen concentration. A second example of this violation was

identified for the licensee's failure to initiate a work request when

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chemistry personnel could not obtain a PRT sample due to apparent

blockage of the sample line.

An unresolved item was identified for the potential failure to meet the

UFSAR requirements for having an automatic gas analyzer, not adequately

revising the UFSAR to describe actual plant configuration for the gas

analyzer inappropriately closing the design change. package and not

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establishing a periodic sampling program for the various waste gas

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collection tanks.

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Operational Status of Facilities and Equipment

02.1 Loss of Emeraency Sirens

a. .Insoection Scope (71707)

The inspectors reviewed the February 4,1998.10 CFR 50.72 notification

due to a partial loss of emergency siren capability caused by inclement

weather.

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b.

Observations and Findinas

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On February-4,1998, at approximately 10:12 a.m., inclement weather in

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'the area caused a loss of-power to areas around the plant.

This caused

- a loss of approximately 29 out of 107 emergency sirens. The state of

. Tennessee and the NRC were promptly notified of the condition.

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majority of the sirens were restored by 12:00 p.m.

on February 5. and

all of the sirens were functioning as required by 8:00 a.m. on February-

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Licensee actions appeared to be appropriate during the inclement

weather conditions.

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Miscellaneous Operations Issues (92901)

08.1

(Closed) EA 97-232 (01013). Failure to Identify and Take Corrective

Actions for Loss of RCS Inventory Control While Drainino Pressurizer

(Closed) EA 97-232 (01023). Failure to Properly Loa a Unit 1 RCS Drain

Down Evolution

The inspectors verified the corrective actions for the above two

violations described in the licensee's response letter. dated August 11.

1997, to be comprehensive and reasonable.

The inspectors verified that

all corrective action items have been completed with the exception of

replacing the pressurizer upper-tap angle root valves.

The licensee's

response letter committed to replacing the pressurizer upper-tap angle

root valves during the Unit 1 Cycle 9 refueling outage (fall 1998) and

the Unit 2 Cycle 9 refueling outage (spring 1999).

08.2 (Closed) EA 97-409 (01013). Failure to Maintain Ooerable DC Vital

Battery Channels

(Closed) EA 97-409 (01023). Failure to Follow Procedures While Alianina

a Soare Vital Battery

(Closed) EA 97-409 (01033). Failure to Include Indeoendent Verification

Per Procedure While Alianina Vital Batteries

The inspectors verified the corrective actions for the above three

violations described in the licensee's response letter dated. January 7.

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1998, to be reasonable and complete with the following exception.

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A)plicable plant procedures in the Operations. Maintenance and

C1emistry areas have been reviewed to ensure that verification

requirements are correct and standardized: however, the procedure

revisions are pending.

The licensee committed in their response letter

to revise the applicable procedures by March 27, 1998.

08.3 (Closed) LER 50-327. 328/97011. Revision 0. Ooeration of Vital Battery

Board #4 Without a Battery Source

(Closed) LER 50-327. 328/97011. Revision 1. Doeration of Vital Battery

Board #4 Without a Battery Source

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The events described in these LERs were addressed in the closure of

violations, related to the same event. in Section 08.2 of this report.

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No new issues were revealed by the LERs.

II. Maintenance

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Conduct of Maintenance

M1.1 General Comments

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Insoection Scooe (61726 & 62707)

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Using inspection procedures 61726 and 62707, the inspectors conducted

frequent reviews of ongoing maintenance and surveillance activities.

The inspectors observed and/or reviewed all or portions of the following

work activities and/or surveillances:

0-SI-SXP-067-201.P

Essential Raw Cooling Water Pump L-B

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Performance Test. Rev. 0

0-SI-SXV-063-266.0

ASME Section XI Valve Testing: FCV-63-7

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Rev. 3

0-SI-SXV-070-201.0

CCS Pump C-S Discharge Check Valve (0-70-

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504) Quarterly Closing Test. Rev.1

0-50-70-1

Component Cooling Water System ~B" Train.

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Rev. 11

2-SI-SXP-070-201.B

Component Cooling Pump 2B-B Performance

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Test. Rev. 0

WO 97-943700-002

Implement DCN T-12958-A: Replace Existing

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Thermocouples with New System Design on

1B-B EDG

WO 98-305500-000

EDG 1B-B Electrical Outage: Generator

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Windings Repair

WO 98-002996-000

Auxiliary Charging Pump 2B Rebuild due to

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Low Output Flow: SON-2-PMP-084-0021

WO 98-344081-021

Calibrate Fuel Oil System Instrument PI-

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140 EDG 18-B

0-SI-0PS-083-151.B

Six Month Test Requirement on Electric

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Hydrogen Recombiner System Train B

WO 98-002297

Replace SCR on Hydrogen Recombiner B Phase

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b.

Observations and Findinas

In general the conduct of maintenance and surveillance activities

observed were good.

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During performance of surveillance procedures 0-SI-SXV-070-201.0 and 2-

SI-SXP-070-201.B the inspectors questioned the test methodology by which

the licensee tests the discharge check valves to satisfy ASME Section XI

code requirements for testing of check valves.

Specifically. the

licensee's procedure has the operating pump shut down after another pump

has been started.

The differential pressure developed between the

operating Jump and the pump just shutdown allows the discharge check

valve of tlat pump to be slammed shut.

This action could cause

potential damage to the valves over an extended period of time.

In

(

L

-

.

l

10

!

discussions with operations personnel the licensee indicated that these

L

valves had been replaced previously. As a result, the inspectors

!

requested the licensee to review the procedure and determine if a better

i

testing method is possible to mitigate potential damage to the valves.

L

Until that review is completed this item is identified as Inspection

Followup Item (IFI 60-327/98-03-04). Valve Testing Methodology Review.

-The inspectors observed portions of the planned maintenance outage on

the 1B-B EDG.

During performance of WO 98-305500 the licensee

identified that small sections of the diesel generator winding

insulation had become degraded.-

Specifically, in two sections of.the

windings the insulation was burnt. -With further examination, through

use of a thermography camera, the licensee identified several other.

areas with higher than normal temperatures in the windings. These areas

were suspect to similar insulation damage, although not visually

apparent. However. the licensee repaired the identified areas and

completed the maintenance activity without further delay.

Pending

further review and determination of the root cause for the degraded

winding insulation condition and examination of the other EDGs. this

issue is identified as an Inspection Followup Item (IFI 50-327/98-03-

05). EDG Degraded Generator Winding Insulation.

c; Conclusions

In general the conduct of maintenance and surveillance activities

observed were good.

M8

Miscellaneous Maintenance Issues (92902)

M8.1

(Closed) IFI 50-327. 328/96-04-13. Weak Freeze Protection Proaram The

freeze protection program was most recently discussed in Inspection

Report 50-327. 328/97-14. dated December 8.-1997.

Since that

inspection. the inspectors have continued to monitor the implementation

of the freeze protection program during the winter of 1997/1998.

No

significant equipment deficiencies have been noted during that period.

The inspectors concluded that the licensee has made significant

improvements to the material . condition of the various heat trace systems

and to the implementation of the freeze protection program.

III. Enaineerina

.El

Conduct of Engineering.(37551)

E1;1.Section XI Testina of Comoonent Coolina System (CCS) Valves

i

a.

Insoection Scooe (61726)

The inspectors reviewed the licensee's program for testing the operation

and reliability of remotely operated valves in the component cooling

,

system.

l

--_-__

.

.

,

11

b.

Observations and Findinas

The inspectors observed preparations for testing of CCS pump discharge

valves and discussions during the pre-evolution briefing.

Operators

noted that the system crosstie valves had not operated properly in the

past and that the assistant unit operator (AUO) may have to manually

,"

.open the valve off its closed seat and then operate the valve using the

motor operator. When the operators operated CCS crosstie valve 1-FCV-

70-26, the valve would not o)en and required manual operator action.

The licensee initiated a worc request to address the failure.

Further review indicated that this valve. in addition to several others,

were listed in various emergency abnormal procedures and that it would

be necessary to operate these valves in order to mitigate certain plant

conditions or as part of the plant recovery actions.

However, the

inspectors determined that none of the valves were in the licensee's

ASME Section XI testing program.

Further licensee review was being

conducted to determine if the valves were in any other periodic testing

program.

The inspectors ex)anded the review to other CCS system valves and

determined that t1e CCS ~B" train system was designed with both unit 1

and unit 2 "B" train ECCS headers connected in parallel.

The

operational design for the system is such that during an accident the

accident unit would be aligned to the ~B" train supply header and flow

would be increased in the unit's "B" train RHR heat exchanger to greater

than 5000 gpm. The non-accident unit flow would be throttled down to

prevent exceeding the Jump design flow of 7000 gpm.

Opening and closing

of 1-FCV-70-153 and 2

CV-70-153 would be used to meet the design flow

for the accident unit.

However these valves were not in the licensee's

Section XI program for stroking in the " Closed" direction.

CCS containment isolation valves supplying the RCPs lube oil and motor

coolers and containment isolation valves supplying the RCP thermal

barriers automatically close on a containment isolation signal.

In

addition, in many of the emergency procedure recovery actions, the

l

isolation valves are reopened in order to sup)1y cooling to the RCP

j

seals and/or to restart the RCPs.

However, t1ese valves were not in the

'

licensee'sSection XI program for stroking in the "Open" direction.

The inspectors expanded the review and determined that many remotely

operated valves controlled from the safe shutdown panel were not

included in the licensee'sSection XI valve testing program.

Of 63

j

valves reviewed, only 31 were included in the Section XI program and

many of those were stroke time tested in only one direction. Tne

initial review indicated that testing of some of the valves would be

required to meet the Section XI valve testing program.

i

The licensee'sSection XI valve testing program as required by Oma-1988

Part 10 provides the basis for testing of remotely operated valves.

Section 1.1 states that. "The active or passive valves covered are those

.

which are required to perform a specific function in shutting down a

-

_-

_

a

.

12

reactor to cold shutdown condition, in maintaining the cold shutdown

condition, of in mitigating the consequences of an accident."

In

addition.-Section 1.2 provides exclusions to the code such as "(1)

valves used.only for operating convenience such as vent, drain,

instrument, and test valves: valves used only for system control, such

as pressure regulating valves: valves used only for system or component

maintenance."

In addition.10 CFR 50. Appendix B Criterion XI. Test Control, requires

that "a test program shall be established to assure that all testing

required to demonstrate that structures, systems, and components will

perform satisfactorily. in service is identified and performed in

accordance with written test procedures." The inspectors noted that

valves manipulated for contingency actions as directed by the various

levels of emergency procedures and valves manipulated during shutdown of

the plant would be recuired to be tested in accordance with written test

procedures as requirec by 10 CFR 50. Appendix B Criterion XI.

It

appeared to the inspectors that some

tested;however,furtherreviewwill.Qlveswerenotbeingadequately-

,

'

be necessary to resolve this issue.

The potentially inadequate valve testing is being identified as an

unresolved item pending further review. (URI 50-327. 328/98-03-06).

c.

Conclusions

1

The-licensee's valve testing p/ required valve testing.

rogram scope appeared to be too narrow and

may not include all necessary

This issue is

identified as an unresolved item.

E2

Engineertug Support of Facilities and Equipment

E2.1 Corrective Action Procram (405001

a.

Insoection Scooe

The inspectors reviewed corrective actions developed and implemented for

a random sample of Level A and B problem evaluation reports (PERs) for

which Site Engineering had responsibility. These PERs were written for

)lant deficiencies identified from September 1.1996, through

,

l-

r bruary 23, 1998. A total of 9 level A and 154 level B PERs were

e

identified as having been written during this time interval.

Thirteen

'

PERs were selected from this population and the following attributes of

the Corrective Action Program were evaluated:

Determination of licensee's root cause of equipment failure or

problem.

Determination of licensee's extent of condition review performed

for the deficiency.

Timeliness of engineering controls in identifying. rrclving and

implementing corrective actions for the deficiency.

i

. _ _ _ _ _ _ _ _ _ _ _ _ _ _

_ _ _ _ _ _ _ _ _ _ _ _ _ - _ .

-

.

13

Technical adequacy of any plant modifications or temporary

.

alterations developed for resolution of the deficiency.

Technical adequacy of any Justification for continued Operation

.

(JCO).

The above attributes were evaluated for com)liance with the guidance of

Generic Letter (GL) 91-18. Revision 1 and t1e licensee's procedure SSP-

3.4. Corrective Action, Revision 23.

b.

Observations and Findinas

The following PERs were reviewed in order to verify compliance with the

requirements of the Corrective Action Program delineated in procedure

SSP-3.4. Corrective Action. Revision 23:

SO962632PER. Level B. Use of work Orders for implementing

.

temporary alterations.

SO971519PER. Level B. 2-FCV-62-69 failed close resulting in loss

.

of normal letdown.

SO970170PER. Level B. Foxboro 62H controller output inappropriate

.

for given input.

S0970009. Level B. Decrease in reactor thermal power durir

aric

.

acid pump high discharge operation.

SO971204. Level B. Failure of pressurizer safety valves to meet

.

Technical Specification requirements.

SO97]928PER. Level B. Operations procedures do not fully reflect

.

the requirements / restrictions of 0122618.

j

S0970846PER. Level A. Control air containment isolation valve 1-

.

VLV-32-297 third failure of LLRT.

SO972471PER. Level B. Duct work access door for inspection of

.

Damper 2-DMP-313-1784 not sealed.

SO970378PER. Level B. Environmental qualification of flow switches

.

did not consider internal heat rise,

l

SO970423PER. Level B. Diesel engine IA-1 cylinder 8 piston-to-head

.

clearance fou.d outside acceptance criteria.

SO971778PER. Level B. Environmental Qualification Binder

.

Assessment. NA-50-97-36. identified numerous errors with binders.

SO972492PER. Level B. ASME Class Il and III relief valves failed

.

to meet test acceptance criteria.

-

.

14

S0971463. Level B. Recurring and apparently repetitive fan and fan

.

bearing failure / vibration problems.

Procedure SSP-3.4 established requirements for resolving degraded or

non-conforming conditions affecting safety or quality related equipment.

Specific hardware deficiencies have been identified which require the

initiation of a PER.

Root cause analyses are performed for all level

"A" PERs.

Additionally, responsibility has been assigned to the

Management Review Committee (MRC) to identify the need for root cause

analyses for all level "B" PERs, when necessary. Alternatively, an

apparent cause is documented for level B. C and D PERs where sufficient

cause determination information is collected to enable performance

monitoring and trend analysis.

The inspectors performed independent

reviews of the above PERs and verified that root cause analyses were

performed for deficiencies involving equipment degradation documented on

level B PERs.

The extent of condition reviews documented for the listed

deficiencies were sufficiently broad to reasonably identify the primary

root cause along with the contributing root causes.

The developed

corrective action plans were also determined to be adequate to ersure

recurrence control for the listed plant deficiencies.

Operability and

reportability reviews performed for the PERs were acceptable.

PERs for which a) parent causes had been prepared were reviewed in order

to verify that t1e degraded or non-conforming conditions associated with

the equipment had been adecuately resolved.

PERs No. S0970423PER and

SO972492PER documented harcware deficiencies which were resolved using

the assistance of the original ecuipment manufacturer (DEM).

A total of

. six PERs were dispositioned basec on apparent cause analyses.

The

extent of conditions reviews Jerformed for these PERs were determined to

be adequate. Additionally, tie apparent cause analysis and corrective

actions implemented were acceptable with the exception of PER No.

50971928PER.

PER No. SO971928PER was writtein to document a condition in which

operations procedures did not reflect precautions and limitations

specified in design change notice DCN No. 012261B for transferring loads

between 6.9 KV Common Boards A and B.

The precaution specified in the

DCN included load shedding of 2 reactor coolant pumps fed from 6.9 KV

Unit Board 2A and 2C prior to transferring the Common Board loads.

This

precaution was intended to maintain the common station service

transformer (CSST) windings within their respective capacity and

capability ratings and would have precluded the board transfer during

operational modes 1 through 3.

Based on review of past performances of

procedure PM029420000 the licensee determined that common board load

,

transfers had occurred in September of 1996 without complying with the

!

restrictions in the DCN.

l

The licensee performed operability and reportability evaluations for

this event and concluded that the event w6s not re)ortable because CSST

A was fully opera'cle at the time the Common Board 3 loads were

transferred.

The licensee concluded that no loss of functional

,

capability or component degradation resulted from this event and no

-

_

e

15

compensatory actions or alternate functional capabilities were required.

Additionally, immediate corrective actions taken for resolution of this

problem included revising procedure 0-S0-202-2, 6900 Volts Common

Boards.

The licensee also performed an extent of condition review and

identified the electrical equipment within the scope of DCN No. 0122618.

The following electrical equipment was listed:

6.9 KV Shutdown Boards

.

480 Volts Shutdown Boards

e

480 Volts ERCW MCCs

e

480 Volts RMOV. C&A Vent. Reactor Vent and Diesel Aux. Boards

.

480 Volts AC Transfer Switches

.

480 Volts Preferred Transfer Switches

e

6.9 K. Common Boards

e

480 Volts Boards fed from the Common Boards and the Fire

.

Protection Distribution Panel

The apparent cause documented for this problem was inappropriate use of

a ODCN plant modification which did not raauire impact reviews for

ensuring that plant procedures would have e n revised to incorporate

the precautions and limitations delineated in.che design output

documents. The use of ~0DCNs" to transmit design information was no

longer permitted and procedure SSP-9.3 established requirements for

impact reviews of all design changes to preclude occurrence of this

condition. Additional corrective actions documented in the PER included

the operations staff performing reviews of procedures and caution orders

(COs) to ensure that requirements / restrictions specified in DCN No.

012261B have been adecuately addressed and the procedures and C0s have

been revised as needec. The c apletion date shown for this corrective

I

action was November 14. 1997

Based on review of the PER the inspectors determined that the PER had

been rejected by site OA because of administrative problems identified

with the closure package.

The inspectors discussed this rejection with

,

!

site OA personnel and concurred with their observations that the closure

l

package lacked objective evidence which was required to support closure.

'

t'

Procedure SPP-9.4. 10 CFR 50.59 Evaluations of Changes. Tests and

Experiments, requires that procedures and revision to procedures shall

be evaluated in accordance with screening criteria to determine if a

safety evaluation is required.

If the conclusion of this process

indicates that a safety evaluation is required the safety evaluation

shall be prepared in accordance with the requirements of this procedure.

The inspectors requested TVA management to present objective evidence

which demonstrated that the plant procedures for the electrical

i

-

.

16

equipment listed above had been revised in accordance with procedure

SPP-9.4.

Upon receipi, of this request TVA management stated that this information

was not readily available.

They further stated that this information

would be included in the res)onse to site OA for resolution of the

rejection of the closure paccage.

The inspectors were informed that

j

this response would be available on March 27. 1998.

Based on a lack of

'

objective evidence within the PER which provides reasonable assurance

that: 1) an adequate extent of condition review had been aertormed to

identify plant 3rocedures that required revision and 2) tlat the

procedures had Jeen revised in accordance with the requirements of SPP-

9.4 this item is identified as URI 50-327.328/98-03-10 Revise plant

3rocedures to include precautions and load limitation requirements of

JCN No. 0122618.

1

c.

Conclusions

j

The inspectors concluded that equipment operability problems involving

degradations and non-conformances were being evaluated in accordance

with the guidance of Generic Letter 91-18. Revision 1.

Also,

implementation of the Corrective Action Program was generally in

j

accordance with the requirements of procedure SSP-3.4, Revision 23. and

j

met the regulatory requirements of 10 CFR 50 Appendix B. Criterion XVI.

'

IV. Plant Suonort

R1

Radiological Protection and Chemistry (RP&C) Controls

R1.1 Review of Radiation Protection Procram

a.

Insoection Scone (83750. 84750)

The inspectors reviewed implementation of . selected elements of the

licensee's radiation protection program.

The review included

'

observation of radiological protection activities including personnel

monitoring, radiological postings high radiation area controls, and

l

verification of posted radiation dose rates. contamination controls

within the radiologically controlled area (RCA). and container labeling.

In addition ALARA work planning, pre-job worker briefings. and job

execution observations were performed. The inspectors also reviewed

licensee records of personnel radiation exposure and discussed ALARA

program details, implementation and goals.

Requirements for these areas

were specified in 10 CFR 20 and Technical Specifications.

>

b.

Observations and Findinos

The inspectors toured the health physics facilities, truck ba.)

including the refueling floor, turbine building outside radica I M

material storage areas, and radwaste prc essing area. At the t m of

the inspection housekeeping was observed to be good.

Records reviewed

determined the licensee was tracking and trending personnel

.

o

17

contamination events (PCEs). The licensee had tracked approximately 48

personnel contamination reports (PCRs) for the 1998 fiscal year to date

which included skin and clothing contaminations.

Radiologically

controlled areas including radioactive material storage areas (RMSAs).

High Rad Areas. and Locked High Rad Areas were appro)riately posted and

radioactive material was appropriately stored and la)eled.

The inspectors reviewed operational and administrative controls for

entering the RCA and performing work. These controls included the use

of radiation work permits (RWP3) to be reviewed and understood by

workers prior to entering the RCA. The inspectors reviewed selected

RWPs for adequer

of the radiation protection requirements based on work

scope? locatica and conditions.

For the RWPs reviewed, the inspectors

noted that appropriate protective clothing. and dosimetry were required.

During tours of the plant, the inspectors observed the adherence of

plant workers to the RWP requirements. The inspectors observed personal

dosimetry was being worn in the appropriate location.

The inspectors discussed ALARA goals and annual exposures with licensee

management and determined the organizational structure and

responsibilities for the ALARA staff were clearly defined in

organizational charts.

The inspectors took independent smears to verify contamination control

in the Auxiliary Building Turbine Building, Radwaste processing area,

refueling floor roof, storage areas. and on the refueling floor. Al!

j

smears were counted and determined to be " acceptable." The inspectors

also independently walked posted control boundaries with a survey meter

on the refueling floor, storage areas, and tank storage areas and

determined that the radiation levels were all as stated on the most

recent survey.

The inspectors observed workers properly using friskers at the exit

locations from controlled areas. The inspectors observed workers

properly exiting the protected area through of the exit portal monitors.

l

l

The inspectors reviewed the active " Hot Spot" log as of February 5, 1998

and, at the time of the inspection, there were 49 labeled active hot

'

spots being tracked. The inspectors reviewed the " Hot Spot" removal

efforts -1997.

There were 8 successful campaigns and 2 unsuccessful

campaigns.

The most successful dose reduction was from 460 mrem / hour

contact before to 36 mrem / hour contact after removal efforts.

Two " Hot

Spots" located in the RHR/CS Hx rooms were reduced.during U1 and U2

outages; however, the dose rates returned essentially to pre-outage

levels upon start-up.

The inspectors reviewed the use of contamination containment devices, by

a records (log) review and selectively observed the devices at their

locations during tours of the plant.

At the time of the inspection

there were 62 contamination c u.h &ntainments. The inspectors found

that the earliest catch containment as put in 31 ace in 1995. The

licensee identified the reducti e nf these catc1 containments in

-

.

18

December 1997 as a Manager..1t. Focus area.

However the inspectors were

unable to review an action plan to track or reduce this work list.

The

licensee was informed that this focus area would be tracked as an

Inspector Follow up Item (IFI 50-327. 328/98-03-07). Review an action

plan to track and reduce the number of contaminated catch basins.

The Fiscal Year 1998 site exposure goal was set at 399 person-rem. At

the time of the inspection. the site person-rem was about 148.343

3erson-rem (not TLD corrected).

The inspectors uetermined that there

lad been no positive whole body counts during the U2C8 outage that

required additional assessments.

The U2C8 outage dose was 140 person-

rem which was the lowest dose for a Sequoyah refueling. The dose was 70

person-re"i lower than the previous best outage dose of 212 person-rem.

Individual radiation worker internal and external doses were being

maintained well below regulatory limits and the licensee was continuing

to maintain exposures ALARA.

The calendar year collective dose per unit

has trended downward from a high of about 850 person-rem in 1990 to

about 175 person-rem per unit in 1997.

The inspectors reviewed the Contaminated Square Footage Data and

observed that the licensee has reduced the area from a high in July 1990

of 14% to the present 0.75% on January 28. 1998. The licensee considers

326.522 square feet as the largest possible contaminated area

(denominator).

The 0.75% represents about 2449 square feet.

The inspectors reviewed the fiscal year generation of radwaste for the

period 1991 to 1/24/98. The total generated is shown by the following

table:

Fiscal iear

Cubic Feet Generated

j

1991

55545

1992

58865

1993

27560

'

1994

21586

!

1995

17989

i

1996

17466

1

l

1997

  • 8139

l

1998

  • 5050 (as of 1/24/98)

Note: * This does not include the excavated contaminated soil and

asphalt generated by the spills of May 19. 1997 (SO971429PER) 5500 cubic

i

feet and January 10,1998 (S0980021PER) 2007 cubic feet.

This reduction of the generation of radwaste demonstrates aggressive

management.

The inspectors reviewed Unit 2 Additional Equipment Building Sump Spill

on January 10. 1998. PER No.50980021PER and the actions taken by the

licensee in response to the identified problen.' The inspect. ors reviewed

the reportability requirements in the Offsite Dose Calculation Manual

(ODCM) Section 1.2.2.1 and Emergency Preparedness Implementing Procedure

_

.

19

Emeroency Plan Classification Matrix (EPIP-1) Section 7.2 Liquid

Effluents and concurred that the spill was not reportable.

The inspectors reviewed PER No. S0980110PER and the actions taken by the

licensee in response to the identified problem.

Late in the inspection

period, the licensee discovered that the computer based survey map

generation system had lost some required data.

One map survey 020598-6

lost both postings and smear survey results.

The inspectors discussed

his concern about the data loss and informed the licenseo that this

problem resolution would be tracked as an Inspection Fellowup Item (IFI

50-327, 328/98-03-08). Review the resolution of the survey mag

generation data loss.

c.

Conclusions

Radiological facility conditions and housekeeping in radioactive waste

storage areas, health 3hysics facilities, auxiliary building and

refueling floor were o] served to be good. Material was labeled

appropriately, and areas were pro

devices were appropriately worn. perly posted.Personnel dosimetry

Radiation work activities were

approariately planned.

Radiation worker doses were being maintained

well 3elow regulatory limits and the licensee was maintaining exposures

ALARA,

Contamination control was effective. Two Inspection Followup

Iteres were identified.

R1.2 Transoortation of Radioactive Materials

a.

Insoection Scooe (86750)

The inspectors evaluated the licensee's transportation of radioactive

. materials program for implementing the revised Department of

Transportation (DOT) and NRC trans)ortation regulations for shipment of

radioactive materials as required )y 10 CFR 71.5 and 49 CFR Parts 100

through 177.

b.

Observations and Findinas

The inspectors reviewed selected precedures and determined that they

adequately addressed the following:

1) assuring that the receiver has a

license to receive the material being shipped: 2) assianing the form.

quantity type, and proper shipping name of the material to oe shipped:

3) classifying waste destined for burial: 4) selecting the type of

package required: 5) assuring that the radiation and contamination

limits were met; and 6) preparing shipping papers.

The inspectors reviewed a sample of shipping papers and receipt surveys.

The inspectors determined that the shipping papers were complete and the

shipping as well as the receipt surveys were complete and met the

requirements.

h

.

20

c.

Conclusions

Based on the above reviews, the inspectors determined that the licensee

had effectively implemented a program for shi) ping and receiving

radioactive materials as required by NRC and X)T regulations.

R1.3 Water Chemistry Controls

a.

Insoection Scooe (84750)

The inspectors reviewed implementation of selected elements of the

licensee's water chemistry control program for monitoring primary and

secondary water quality. The review included examination of program

guidance and implementing procedures and analytical results for selected

chemistry parameters. Annual training for Post Accident Sampling was

observed.

b.

Observations and Findinas

The inspectors reviewed technical soecifications (TSs), which described

,

the operational and surveillance requirements for reactor coolant

activity and chemistry, and Final Safety Analysis Report (FSAR). Section

10.3.5, Water Chemistry. The section indicated that guidelines for

maintaining reactor coolant and feedwater quality were derived from

vendor recommendations and the current revisions of the Electric Power

Research Institute (EPRI) Pressurized Water Reactor (PWR) Primary and

Secondary Water Chemistry Guidelines.

The FSAR also indicated that

detailed operating specifications for the chemistry of those systems

were addressed in the Station Chemistry Section.

L

The inspectors reviewed selected analytical results recorded for Unit 1

I

'

and Unit 2 reactor coolant and secondary samples taken during the

inspection period. The selected parameters reviewed for primary

,

l

chemistry included dissolved oxygen, chloride, fluoride, and sulfate

levels.

The selected parameters reviewed for f.econdary chemistry

included hydrazine, iron, and cop)er levels. Those primary parameters

reviewed were maintained well witlin the relevant TS limits and within

the EPRI guidelines for power operations.

The inspectors reviewed procedure Post-Acci_ dent Samolina and Analysis

(1-TI-CEM-043-066.1 Rev.8) and attended the Radiochemical Laboratory

Analysis Continuing Training Annual Pass Training.

The inspectors

observed the training walk through demonstration of the procedure.

During the performance of the procedural steps the inspectors observed a

work request on the gas chromatograph. The work request (WR C008715)

i

had a 1993 date.

The inspectors inquired as to how the hydrogen

analysis would be performed with the on-line gas chromatograph out-of-

'

service. The licensee responded that a grab sample would be drawn and

i

transported to the chemistry lab for analysis.

The current final Safety

Analysis Report Section 9.5.10.2.2 (Rev. 12) Chemical Analysis System

i

states "The sample taken from the liquid sampling panel (LSP) is routed

j

to the on-line chemical analysis where the following analyses are

<

.

21

>

performed.

1.

Hydrogen concentration using gas chromatography".

No

reference was made to the use of an alternate analysis method. The

licensee provided additional data to support their belief that the

alternate method was acceptable.

These documents include the following:

Technical Specification (TS) Change 94-15. "Postaccident Sampling

.

(PAS) dated April 6.1995

"Living" UFSAR targeted for submittal to the NRC in early March

1998

The inspectors informed the licensee that the acceptability of using the

alternate method of analyzing a post accident hydrogen sample would be

tracked as an Unresolved Item (URI 50-327. 328/98-03-09). Determine the

acceptability of using an alternate method of analyzing post accident

hydrogen samples.

c.

Conclusions

Based on the above reviews it was concluded that the licensee's water

chemistry control program for monitoring primary and secondary water

quality had been implemented, for those parameters rcviewed. in

accordance with the TSs requirements. An Unresolved Item was

identified.

R2

Status of RP&C Facilities and Equipment

R2.1 Meteorolooical Monitorina Eauioment

a.

Insoection Scooe (84750)

Final Safety Analysis Report (FSAR) Rev. 12 Section 2.3.3.2 titled

On-Site Meteoroloaical Measurement Proaram described the operational

and surveillance requirements for the meteorological monitoring

instrumentation,

b.

Observations and Findinos

The inspectors toured the Nuclear Environmental Data Station with

cognizant licensee personnel to determine if the meteorological

instrumentation was operable and that data for wind speed. wind

direction, air temperature, and precipitation were being collected as

described in the FSAR.

The inspectors reviewed records and determined

the licensee had maintained a high level of operability for meteorology

equipment during 1997.

Wind speed and wind direction instruments at

thirty three, one hundred fifty and three hundred feet were operable

approximately 94% for 1997.

For the period 1993-1997 the equipment

availability was approximately 96%. The licensee's operability goal was

90%.

-

.

22

c.

Conclusions

Based on the above reviews and observations, it was concluded that the

meteorological instrumentation had been adequately maintained and that

the meteorological monitoring program had been effectively implemented.

R7

Quality Assurance in Radiation Protection and Chemistry

.

R7.1 Quality Assurance and Self Assessment

a.

Insoection Scoce (83750. 84750. 86750)

Licensee quality assurance activities and self-assessment programs were

reviewed to determine the adequacy of identification and corrective

action programs for deficiencies in the area of Chemistry and Health

Physics.

,

b.

Observations and Findinas

Reviews by the inspectors determined that quality assurance audits and

self-assessment efforts in the areas of chemistry and RP were

accomplished by reviewing chemistry and RP procedures, observing work,

reviewing industry documentation, and performing plant walkdowns to

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indude surveillance of work areas by supervisors and technicians during

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normal work coverage.

Documeritation of problems by licensee

representatives were included in Quality Assurance Audits and self-

assessment Reports.

Corrective actions were included in the licensee's

Problem Investigative Process.

Closecuts of identified items were

completed in a timely manner.

The inspectors found the nuclear assurance reports insightful, and

detailed.

Identified items were trended and tracked for closecut. A

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selected sample of closeout actions were determined to be timely.

c.

Conclusions

The inspectors determined the licensee was conducting formal RP and

Chemistry audits as required by Technical Specifications and conducting

self-assessments.

The licensee was developing corrective action plans.

trending, and completing corrective actions in a timely manner.

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R8

Miscellaneous RP&C Issues (92904)

R8.1

(Closed) VIO 50-327.50-328/97-06-11: Failure to identify and promptly

correct an adverse condition resulting in the Auxiliary Building

Railroad Bay not being at a slight negative pressure and railroad track

seals not being installed.

The inspectors reviewed the Reply To Notice of Violation closure package

dated August 27. 1997 and independently verified the installation of

door seals.

PER No. SO971642PER closecut actions including the work

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order 97-008520-000 to grout the door openings and the results of 0-TI-

SXX-000-016.0 were reviewed and found acceptable. This item is closed.

V. Manaoement Meetinas.

XI.

Exit Meeting Summary

The inspectors ) resented the inspection results to members of licensee

management at tie conclusion of the inspection on March 27, 1998. The

radiological control inspection exit was conducted on February 6,1998

and the engineering corrective action review inspection exit was

conducted on March 13, 1998. The licensee acknowledged the findings

presented.

During the inspection period, the inspectors asked the licensee whether

any materials would be considered proprietary.

No proprietary

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information was identified.

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

  • Bajestani. M., Site Vice-President
  • Burton, .C. . Engineering and Support Systems Manager
  • Butterworth. H., Operations Manager

Gates

J., Site Support Manager

  • Freeman

E. Maintenance and Modifications Manager

Herron, J. . Plant Manager

  • Kent, C., Radcon/ Chemistry Manager
  • Koehl'. D. Assistant Plant Manager

O'Brien. B. , Maintenance Manager

.

  • Salas. P.

Manager of Licensing and Industry Affairs

  • Valente J. . Engineering-& Materials Manager
  • Attended exit interview

INSPECTION PROCEDURES USED

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IP 37551: Onsite Engineering

E

IP 61726:

Surveillance Observations

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IP 62707: ' Maintenance Observations

IP 71707: Plant Operations-

IP 83750: Occupational Radiation Exposure

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IP 84750:

Radioactive Waste Treatment and Effluent and Environmental

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Monitoring-

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IP 86750:

Solid Radioactive Waste Management and Transportation Of

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Radioactive Materials

IP 92901: . Followup.- Operations

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-IP 92902: Followup - Maintenance

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-IP 92903: Followup - Engineering

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'IP 92904: Followup - Plant Support

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ITEMS OPENED AND CLOSED

Ooened

Ty.p.e item Number

-Status

Descriotion and Reference

_

URI

50-327/98-03-01

Open

Potential Failure to Enter TS 3.11.2.5 LCO

Action Statement When Samples Indicated

High Concentrations of Oxygen in the PRT

(Section 01.4).

.

VIO

50-327/98-03-02

Open-

Failure of Site Personnel to Initiate a

PER After Analysis of the PRT Sample

)

Indicated a High Oxygen Concentration

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(Section 01.4).

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URI 50-327, 328/98-03-03

Open

Potential Failure to Meet UFSAR

{

Requirements. Failure to Revise the

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UFSAR. Inappropriately Closing a

Modification Package, and not

Establishing a Periodic Sampling

Program for the Waste Gas Collection

)

System (Section 01.4).

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IFI 50-327/98-03-04

Open

Follow Licensee's Review of the

Section XI Valve Testing Procedure

to Determine if a Better Method

would be Available to Test the CCS

Pump Discharge Check Valves

(Section M1.1).

IFI 50-327/98-03-05

Open

Follow Licensee's Review of EDG

Degraded Winding Insulation (Section

M1.1).

URI 50-327,328/98-03-06

Open

Potential Inadequate Section XI

Valve Stroke Testing (Section E1.1).

IFI 50-327,328/98-03-07

Open

Review an Action Plan to Track and

Reduce the Number of Contaminated

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Catch Basins (Section R1.1).

IFI

50-327,328/98-03-08

Open

Review the Resolution of the Survey

Map Generation Data Loss (Section

R1.1).

URI

50-327.328/98-03-09

Open

Determine the Acceptability of Using

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an Alternate Method of Analyzing

Post Accident Hydrogen Samples

(Section R1.3).

URI

50-327.328/98-03-10

Open

Revise procedures to include

precautions & load limit

requirements of DCN 012261B (Section

E2.1).

Closed

Tvoe Item Number

Status

Descriotion and Reference

VIO

50-327/EA 97-232

01013

Closed

Failure to Identify and Take

Corrective Actions for Loss of RCS

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Inventory Control While Draining

Pressurizer (Section 08.1).

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VIO

50-327/EA 97-232

01023

Closed

Failure to Properly Log a Unit 1 RCS

Drain Down Evolution (Section 08.1).

-VIO

50-327, 328/EA 97-409

Closed

Failure to Maintain Operable DC

01013

Vital Battery Channels (Section

08.2).

VIO

50-327, 328/EA 97-409

Closed

Failure to Follow Procedures

01023

While Aligning a Spare Vital Battery

(Section 08.2).

VIO

50-327, 328/EA 97-409

Closed

Failure to Include Independent

01033

Verification Per Procedure While

Aligning Vital Batteries (Section

08.2).

LER

50-327. 328/97011/Rev 0 Closed

Operation of Vital Battery Board # 4

Without a Battery Source (Section

08.3).

LER

50-327, 328/97011/Rev 1 Closed

Operation of Vital Battery Board # 4

Without a Battery Source (Section

08.3).

IFI

50-327. 328/96-04-13

Closed

Weak Freeze Protection Program

(Section M8.1).

VIO

50-327. 328/97-06-11

Closed

Failure to Identify and Promptly

Correct an Adverse Condition

Resulting in the Auxiliary Building

Railroad Bay not Being at a Slight

Negative Pressure and Railroad Track

Seals n01. Being Installeo

(Section R8.1).

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