ML20129A214
ML20129A214 | |
Person / Time | |
---|---|
Site: | Sequoyah |
Issue date: | 10/10/1996 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
To: | |
Shared Package | |
ML20129A195 | List: |
References | |
50-327-96-09, 50-327-96-9, 50-328-96-09, 50-328-96-9, NUDOCS 9610220067 | |
Download: ML20129A214 (31) | |
See also: IR 05000327/1996009
Text
- _-
. .
'
.
U.S. NUCLEAR REGULATORY C0l#11SSION
REGION II
Docket Nos: 50 327, 50 328
Report Nos: 50 327/96 09, 50 328/96 09
Licensee: Tennessee Valley Authority (TVA)
.
Facility: Sequoyah Nuclear Plant, Units 1 & 2
i
Location: Sequoyah Access Road
Hamilton County, TN 37379
Dates: July 28 through September 14, 1996
Inspectors: M. Shannon, Senior Resident Inspector
W. Holland, Senior Resident Inspector
R. Starkey, Resident Inspector
J. Blake, Reactor Inspector, (Sections H3.1, M6.1,
M8.1, E2.1)
G. MacDonald, Reactor Inspector,(Sections M1.2,M1.3,
& H2.4)
K. VanDoorn, Senior Resident Inspector Watts Bar,
(Section 03.1)
Approved by: M. Lesser, Chief
Reactor Projects Branch 6
Division of Reactor Projects
.
Enclosure 2
- eA 88e?oes8s827
G PDR ,
_ .. _._ __ _ _ ___ - ._ _ _ . _ . . _.. _ .. _ _ .._ _ . . . _
, o
>
. .
.
'
l
i
, 2
i
.
.
EXEClTlIVE SUMMARY
i
j Sequoyah Nuclear Plant, Units 1 & 2
- NRC Inspection Report 50 327/96 09, 50 328/96 09
-
This integrated inspection included aspects of licensee operations,
- maintenance, engineering, riant support, and effectiveness of licensee
1 controls in identifying, resolving, and preventing problems. In addition, itL
! includes the results of announced inspections by engineering and maintenance
j inspectors.
Ooerations
! e' Negative observations were noted in the areas of operation's log keeping
detail, emergency diesel generator starting air system operation,
4
operation's log keeping status control, and guidance in operator rounds
j (Sectioas 01.2 and M1.1).
!
i e Back filling of pressurizer level transmitters presented a potential
safety hazard to personnel and could result in a breach of the reactor
coolant system (RCS) (Section 02.2).
4
i e A weakness was identified in the control of certain engineering
- documents provided to control room operators (Section 03.1).
e A non cited violation (NCV) was identified for the placing of an
i Emergency Gas Treatment System (EGTS) dam mr control switch in the wrong
i position which rendered the "A" train of iGTS inoperable for 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and
,
43 minutes (Section 03.2).
1
e Technical Specification (TS) wording does not accurately reflect the
, current shift hours worked by operations personnel. However, the
i licensee has been in compliance with the TS guidelines regarding use of
j
'
overtime and has initiated a proposed ct,ange to TS to clarify normal
shift hours (Section 08.1).
!
l Maintenance
J
'
e Maintenance and surveillance activities observed were satisfactorily
wrformed in accordance with licensee procedures. A weakness in
4
Emergency Diesel Generator (EDG) maintenance trending was noted
regarding not performing any compensatory measures for failed EDG
j cylinder exhaust gas temperature parameters (Section M1.2).
i e Several completed work orders were reviewed and the level of detail of
work documentation was adequate but not thorough. A minor documentation
4
weakness was noted in a mechanical maintenance work order which was
corrected by the licensee (Section M1.3).
I,
i
i
_ _ _ _ _ _J
. _
'. .
'
.
3
e An ERCW pump discharge check valve stuck open due to wear and resulted
in a system backflow of approximately 3000 gallons per minute.
Subsequently, engineering determined that the stuck open ERCW pump
discharge check valve had been installed incorrectly (Section M1.4).
e Repetitive equipment problems caused added operator burden and impacted
maintenance resources, operation's switching and tagging resources, and
day to day operations (Section M2.3).
e Corrective action for the Emergency Diesel Generator (EDG) Governor
Booster Servomotor was satisfactory (Section M2.4).
e Steam Generator records indicated that the licensee has implemented a
comprehensive program to minimize stress related degradation of Steam
Generator tubes (Section M3.1).
e The licensee *s Steam Generator organization has done a very good job of
reviewing their inspection and repair options, and then soliciting plant
and corporate management support for the options selected (Section
M6.1).
Enaineerina
e After identification of initial concerns based on the engineering
evaluation for a Part 21 potential problem associated with material, the
licensee took appropriate positive actions to determine the issue did
not affect Sequoyah (Section E2.1).
i
e A weakness in the licensee *s process for design control of system
operational status wa: identified. Sample valves located in the Unit i
hot sample room for the Safety Injection system were in poor material '
condition and presented potential housekeeping problems. In addition,
this portion of the sample system was not formally dispositioned as to
its operational status in the plant (Section E2.2).
e The practice of venting the residual heat removal (RHR) system prinr to
calculating the volume of gas in the system did not provide an accurate
representation of the total amount of gas in the RHR system (Section
E2.3). -
e A violation was identified for untimely and inadequate corrective
actions associated with the failures of the EDG starting air compressor
control switches (Section E4.1).
i
e A weakness was identified for the inadequate root cause evaluations
associated with the initial EDG starting air compressor control switch
failures (Section E4.1). '
o Weak engineering sup mrt and maintenance was indicated by repetetive
equipment problems w1ich added operator burden and impacted maintenance
resources (Section M2.3).
. . .. . _ . . _ _ _ . _ _ _ . _ . _ . _ _ -_ . ._, ___ _ ._ _
- . o
.
- .
!
i 1
'
- 4
Plant Supoort
e The licensee did not take adequate immediate corrective actions for a !
i transient fire load issue identified during the week of July 8 - 12, i
- 1996. Appropriate corrective action was only taken after the Nuclear !
,
Regulatory Comission (NRC) comenced additional review of the issue on
j July 30,1996 (Section F1.1).
!
!
t
i
i
i
i l
r :
- l
- 1
!
1
i
j
,I
I
t
I
d
1
!
!
$
!
i
i
i
I
a
9
i
!
.
1
,
._.
--- -
= . - .- . . .
4
, .
. .
.
'
Report Details ,
'
.
Summary of Plant Status
Unit 1 began the inspection period in power operation. The unit operated at
power for the duration of the inspection period.
Unit 2 began the inspection period in power operation. The unit operated at
power for the duration of the inspection period.
- I. Operations l
l
01 Conduct of Operations
l
'
- 01.1 General Comments (71707)
Using Inspection Procedure 71707, the inspectors conducted frequent
i reviews of ongoing plant o In general, the conduct of
operations was acceptable.perations.Smcific events and notesorthy observatio'
- are detailed in the sections slow.
01.2 Emeraency Diesel Generator Startina ,^1r System Ooeration
,
a. Insoection Scope (71707)
The control room logs were reviewed in order to determine the frequency
at which the EDG starting air system relief valves were lifting and to
'
determine what operational problems were being experienced as a result
of the various starting air compressor malfunctions. The supporting
documentation for the EDG starting air compressor control switch
problems is detailed in Section E4.1.
b. Observations and Findinas
While reviewing documentation and actions associated with the EDG
starting air compressor control switch failures, various observations
related to the conduct of operations were made. The following items
were identified during the review:
e The control room logs and the associated PERs did not always
identify which relief valve was lifting or identify the affected
compressor unit. The lack of engineering's and management's
knowledge that the receiver tank / system reliefs were lifting
appeared to contribute to the licensee's slow implementation of
corrective actions,
e Operation's actions, in responding to deficient conditions, were
considered to be weak in that on August 23 the 2A2 EDG starting
air system was found relieving and the compressor control was not
. -- - - - -
, *
. .
. ,
1
2 l
placed in "off" and approximately 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> later the relief valve i
was found relieving again. In addition, on August 4 and again on j
September 10, after the 2A2 EDG stating air compressor was placed
in "off", the startia air system alarmed on low pressure.
e The September 8, control room logs documented that at 03:07 p.m.,
" fire operations" reported that the 1A A EDG air relief valve was
actuated. The logs for 03:34 p.m., documented that the
compressors were found in "off" and the relief valves were seated.
The logs did not document control room directions to alace the ,
compiessors in "off", did not document that the switcles had been I
placed in "off" following the 03:07 p.m., entry, and did not
document who placed the switches in "off".
e The logs noted that the operator increased receiver tank pressure
to 305 psig on two occasions. The normal operating band for
receiver pressure control was 250 300 psig and the low pressure i
alarm actuates at approximately 250 psig. The logs only consider '
an abnormal condition when pressure drops to less than 240 psig
and does not give the operator a limit for a high pressure
abnormal condition. Routinely, log reading limits are based on
the automatic operational setpoints for a system to ensure
abnormal operation is identified prior to the development of more i
serious deficiencies. j
a
c. Conclusions
The failure to identify the specific relief valves that were lifting in
the control room logs was considered to be' a negative observation.
The failure to maintain the starting air system within the normal
operational band when operational problems are known was considered to I
be poor implementation of compensatory measures.
The lack of status control in the control room logs was considered to be
a negative observation. .
!
The lack of clear guidance in operator rounds was considered to be a !
negative observation. j
i
02 Operational Status of Facilities and Equipment !
!
02.1 Main Control Room Alarms. Indications. and Control Deficiencies l
l
a. Insoection Scope (71707)
During the period of August 23 28, 1996, the inspectors walked down the l
main control room boards and the common boards of each unit. This l
walkdown, cccomplished over several days, had as its purpose to identify t
all the deficiencies, (Work Requests (WR), disabled annunciators, !
l
- -- -. . - . - . - - - - - . ~ - - . . -- - _. - .- ~ .-
. .
,
c . .
'
.
i caution orders), on each unit and to determine Operator's awareness of
the deficiencies,
- b. Observations and Findinas
'The inspectors noted 54 WR stickers in the Unit I horseshoe area, four
,
WRs on the nuclear instrumentation back panel and 39 WRs on the common
i control board (panels 1 M 15 through 0 M 15). These panels contained a
j
'
total.of 12 disabled or partially disabled annunciators and 12 posted
caution orders. When questioned about specific deficiencies, operators
did not always have a ready explanation for the deficiency, but
generally knew where to look to find the requested information.
4
.
c. Conclusions
1
- The ins)ectors concluded that the number of deficiencies, as noted by
the num)er of WRs, disabled annunciators, and caution orders, made it
difficult for an operator to be cognizant of the nature of each
deficiency, thus placing an unnecessary work load on licensed operators.
,
02.2 Backfill of Pressurizer Level Transmitter
i a. Inspection Scope (71707)
4
'
,
The inspectors reviewed a recent Unit 1 evolution involving the
backfilling of a pressurizer (PZR) level transmitter reference leg and
the licensee's practice of bypassing and tripping related
instrumentation to accomplish the evolution.
b. Observations and Findinos
On August 28, 1996, the licensee documented in Problem Evaluation Report
4
(PER) No. SQ962300PER a level deviation between the three Unit 1 Main
- The maximum observed level deviation between the instruments was 4%
,
while the maximum allowed deviation was St. On August 29, the licensee
initiated action to backfill the reference leg of 1-LT 68 320 to correct
l the problem.
The design of the PZR level / pressure instrumentation is such that 1 LT-
68 320 shares a common reference leg with two PZR pressure transmitters,
'
1 PT 68 322 and 1-PT 68 323. In order to fill the reference leg of 1-
LT 68 320, the two pressure transmitters had to be bypassed / tripped. TS 3.3.1, Reactor Tri) System Instrumentation, Table 3.31, requires that
three out of four )ZR pressure channels be operable in Modes 1 & 2, with
<
two channels required to initiate a unit trip. The licensee determined
that a recent change to the TS Bases allows one channel to be bypassed,
1 which would make that channel inoperable, and allows the second channel
! to be tripped. The TS Bases states that the placing of a channel in the
i tripped condition provides the safety function of the channel and if the
'
channel is tripped for testing and no other condition would have
- indicated inoperability, the channel should not be declared inoperable.
.
!
.. .- - . - - .-- - -
, .
. .
.
.
~
4
Based upon the licensee's TS interpretation, operators bypassed 1 PT 68-
322 and tripped 1 PT 68 323 for the backfilling evolution. The licensee
successfully completed the backfillirg in less than two hours and
returned the protection system to a normal alignment.
The inspectors questioned the licensee on the necessity of backfilling
the level transmitter since the reference leg is designed with a
condensing pot would should ensure that the reference leg remains
filled. The licensee is evaluating the root cause as to why the
reference leg is not being maintained filled by tb condensing pot.
7 c. Conclusions
i
The inspectors discussed with the licensee the licensee's interpretation
of TS 3.3.1.1 which allows bypassing / tripping of two of four instruments
- ' in the same protection set. The inspectors are continuing to determine
'
if the licensee was correctly interpreting TS 3.3.1.1. This issue is
identified as Unresolved Item (URI) 50 327. 328/96 09 01. Determine
2
Whether TS 3.3.1.1 Allows One Pressurizer Pressure Channel to Be
'
. Bypassed at the Same Time that a Second Pressurizer Pressure Channel is
Tripped.
The inspectors noted that during the backfilling evolution that a
portable high 3ressure pump was used to backfill the reference leg. At
times during tie evolution the pump was exposed to RCS pressure. The
inspectors considered that this evolution presented a potential safety
hazard to personnel and could result in a breach of the RCS.
03 Operations Procedures and Documentation
03.1 Uncontrolled Guidance Found in Main Control Room (MCR) (71707)
i
'
a. Insoection Scope (71707)
On August 15. 1996, the inspector conducted a review of engineering
documents availab'.e for operator use/ reference in the MCR.
b. Observations and Findinas
The inspector noted that two binders containing miscellaneous
information from the engineering group were in the MCR. A binder in the
Unit 1 area was marked " Assistant Shift Operations Supervisor (AS0S)
Letters of Interest." It contained 38 different documents providing
information and guidance to operators. These included memoranda, single
pages of information with an engineering signature Technical Su) port
Investigation Requests (TSIRs), and portions of PERs. Some had land
written notes. One Unit 1 Senior Reactor Operator (SRO) indicated that
they might operate in accordance with this guidance, however, they would
not operate outside of procedures. In the Unit 2 area the binder was
marked "TSIR, Action Plans". The licensee somet.imes develops Action
Plans to direct activities to be performed to address problems noted in
_
__ _- _ _ ._
, .
. .
-
,
,
5
3
'
TSIRs. The Unit 2 binder contained various documents similar to the
'
Unit 1 binder although, no Action Plans were in the book. Information
was organized by system in this binder.
4 c. Conclusions
The inspector noted that these documents appeared to have no attendant
- controls by operation's management to evaluate whether the guidance was
to be followed, whether the information was current, whether a Shift l
Order or Standing Order was appropriate, and to assure consistent
information was given to operators. The inspector considered this to be
a weakness in control of information to operators. This observation was I
.
discussed with licensee management.
.
03.2 Lnoggroole Emeraency Gas Treatment System Train (EGTS)
a. Insoection ScoDe (71707)
Inspection Report 50 327,328/96 08 identified an unresolved item (URI)
50 327/96 08 01, which discussed a mispositioned switch in the EGTS on
July 24,1996. The mispositioned switch rendered the EGTS train
inoperable for 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and 43 minutes. Further review of the post
4
maintenance and operational procedures, in addition to a review of the
corrective actions in the associated PER, were conducted.
<
b. Observations and Findinas
Initial reports indicated that both trains of EGTS were inowrable
during this event. However, further review noted that, altlough the "B"
,
'
train was administratively inoperable because management review of the
testing had not been completed, the system was aligned and capable of
performing its safety function. This precluded the system from being
inoperable according to TS and eliminated the potential TS 3.0.3 entry.
'
The inspectors noted that the operators had placed control switch 1 HS-
65-10 in the wrong position and also had improperly and independently
verified the switch in the wrong position. Following a detailed review
of the procedure, the inspectors concluded that the operator actions
were the result of an inadequate procedure. While the procedure
specified the final damper position, it did not specify the final switch
, position.
The inspectors also noted that the majority of safety related control
4
room control switches, spring return to their safety po itions, however,
i not all of the switches associated with the EGTS spring return to their
safety positions. For these switches additional procedural guidance
would be warranted to ensure proper positioning.
.
. _ . __ _ _
, -
. .
-
.
6
c. Conclusions
The placing of the EGTS control switch in the wrong position, which
rendered the "A" train of EGTS inoperable for 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and 43 minutes, is
a violation of NRC requirements. The operator, who mispositioned the
control switch, identified the error during shift turnover and promptly
reported the error to shift management. Subsequently, the licensee has
identified 5 procedures which do not adequately control hand switch
configuration. The deficient procedures have been or will be revised
prior to future use. Based on the operator's )rompt reporting of this
error and the corrective actions detailed in PER SQ962041PER, this
licensee identified and corrected violation is being treated as a Non-
-
Cited Violation, consistent with Section VII.B.1 of the NRC Enforcement
'
Policy (NCV 327/96 09 02).
08 Miscellaneous Operations Issues
08.1 Proposed Technical Soecification Chanae Reaardina Normal Work Day
a. Insoection Scope (71707)
During this ins ction period the inspectors reviewed the licensee's
established wor,,ing hours, as described in TS 6.2.2, Facility Staff.
- b. Observations and Findinas
TS 6.2.2.g (working hours of unit staff who perform safety related
- functions) states, in part, that the objective shall be to have
'
operating personnel work a normal 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> day, 40 hour4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> week while the
unit is operating. Since the last refueling outage (U2C7) which ended
in the Spring of 1996, SR0s have worked a 12-hour rotating shift while
Reactor Operators (RO) and Assistant Unit Operators (AU0) have worked an
8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> shift.
The licensee agreed with the inspector that the current TS wording
.
'
does not accurately reflect the current, or possible future, shift hours
worked by operations personnel. As a result, on August 19, 1996, the
licensee initiated a TS amendment which will be worded to more clearly
reflect the normal work shift hours for operations personnel,
c. Conclusions
The inspector concluded that this proposed TS change was administrative
in nature and that the licensee has been in compliance with the
guidelines of TS 6.2.2.g regarding use of overtime,
e
. _ _ _ _
, .
,
.
7
II. Maintenance
M1 Conduct of Maintenance
M1.1 General Comments (62703)
a. Inspection Scoce (61726 & 62703)
The inspectors observed and/or reviewed all or portions of the following
work activities and/or surveillances:
e 2 SI-SXV 003 219.0 Auxiliary Feedwater Check Valve Test
During Operation
e 2-SI 0PS 030 286.0 Cumulative Time That Containment Purge
Supply and Exhaust Isolation Valves Are
Open
e 2 SI SXP 003 201.B Motor Driven Auxiliary Feedwater Pump 2B B
Performance Test
e WO9632986 Lube & Inspect Charging Pump and Charging
Pump Speed Increaser
e WO9636019 Install Refurbished Reactor Trip Breaker
in Unit 2.
b. Observatior.s and Findinas
The inspectors noted that the work activities and the performance of
surveillance activities were adequately performed.
c. Conclusions
The inspectors noted that the control room logs, associated with
surveillance 2 SI 0PS 030 286.0, were incomplete. The logs did not
always document the initiation and completion of the various containment
purge evolutions and this was considered to be a negative observation.
M1.2 Observation of Maintenance and Surveillance Activities
a. Insoection Scope (62703)
Maintenance activities were observed to determine if the activities were
performed in accordance with licensee procedural requirements. The
-
-.- . . - . _- - - - . - _ _ . - _- ,- - . - .
o o
.
.
.
.
!
' inspection scope included observation of portions of the following
maintenance activities by a NRC Region II maintenance inspector:
i e WO963502000 Electrical maintenance implementation of relay
4
protection design change of 1C Condenser Cooling
Water (CCW) Pump Motor.
. e WO963548400 Hechanical corrective maintenance on auxiliary
building fire door
i
e WO963534500 Customer Group corrective maintenance to disable
gas operated relay protection and install sudden
. pressure relay protection for Main Bank
'
,
Transformer 1C
[ e WRC336606 Troubleshooting corrective maintenance by the
Fix It-Now team to locate a ground on electrical
panel LC104
e MI 4.2.3/SI 102 Mechanical preventive maintenance monthly
mechanical inspection of EDG 2A A
b. Observations and Findinas
The maintenance activities observed were required to meet the applicable
requirements of Site Standard Practice (SSP) 6.1, Conduct of
Maintenance, SSP 6.2, Maintenance Management System, and SSP 6.25,
Maintenance Management System Performance of Work Orders.
The maintenance activities observed were satisfactorily >erformed. Work
was accomplished per the work documents and the work paccage
instructions were actively in use. Drawing and procedure revisions were
verified prior to use. Personnel qualifications were checked for the
Maintenance Instruction (MI) 4.2.3/ Surveillance Instruction (SI) 102
monthly Preventive Maintenance (PM) inspection of EDG 2A A and the
3ersonnel >erforming the work were task qualified. Personnel were
(nowledgea)1e on the equi) ment and the procedures. Measuring and Test
Equipment (M&TE) was checced and verified to be in calibration. The
pre job briefir9 for WO963502000 was considered good.
During review of the work package for the 2A A EDG monthly mechanical
inspection work activity, the inspector noted a weakness in EDG
trending. Procedure MI 4.2.3 obtains cylinder exhaust temperature data
for trending purposes. The procedure requires that adjacent cylinder
exhaust temperature differential be s 100 degrees F. Turbocharger inlet
temperature differential was required to be s 200 degrees F. If the
cylinder exhaust temperature differential exceeds 100 degrees F or
turbocharger inlet temperature differential exceeds 200 degrees F then a
work request is required to be initiated for resolution. If a WR
already exists, then the procedure requires that the WR number be
recorded in the procedure.
.- - --- . . . . .
. - , - .. - .- -- - - -
, .
.
.
..
,
9
The inspector determined that cylinder No. 7 was reading 660 degrees F
' and the remaining cylinder temperatures ranged from 940 1000 degrees F.
Existing WR 201222 written in June, 1995, documented this condition on
engine 2A1 cylinder No. 7 and a condition of high turbocharger inlet
temperature differential. Licensee WO 950658600 performed in February
1996, to implement WR C201222 determined that engine 2A1 turbocharger
and cylinder M. 7 temperature parameters had open thermocouples or
thermocouple wiring.
The cylinder exhaust temperatures were recorded for trending purposes to
monitor engine performance. Low cylinder exhaust temperature readings
or high cylinder exhaust temperature differential values could be due to
failed indication circuitry or could be an indication of performance
problems with the cylinder. High turbocharger inlet temperature
differential could be due to failed indication circuitry or governor
performance problems. The exhaust gas and turbocharger inlet
temperature values were not utilized as part of EDG operability
verification.
Discussions with licensee technical support and maintenance personnel
indicated that while the temperature measurement conditions existed
since June 1995, no attempt was made during the monthly inspections to
utilize compensatory measures to obtain the data on these two
temperature parameters.
The licensee operated EDG 2A A from June 1995, until February 1996,
without identifying that the problem was open thermocouples or
thermocouple wiring. The licensee operatea EDG 2A A since June 1995,
without utilizing any compensatory measures to obtain the 2A1 EDG engine
turbocharger inlet and cylinder No. 7 exhaust temperature values for
trending. This is considered a weakness in trending and performance
monitoring of the EDG.
c. Conclusions
The maintenance and surveillance activities observed were satisfactorily-
performed in accordance with licensee procedures. A weakness was noted
in EDG temperature parameter trending.
M1.3 Review of Comoleted Work Orders
a. Inspection Scooe (62703)
Selected work orders for completed work activities were reviewed to
determine if the completed work met ap)11 cable procedural requirements
and to determine the degree to which t1e activity was documented in the
work order (W0). The following work orders were reviewed by a NRC
Region II maintenance inspector.
"I
, *
. .
'
.
10
e WO963548400 Hechanical corrective maintenance on auxiliary
building fire door
e MI 4.2.3/SI 102 Mechanical preventive maintenance monthly
mechanical inspection of EDG 2A A
e WO963001700 Chemical and Volume Control System (CVCS) valve
2VLV 62 659 machining
e WO962806000 Non-return valve 2 FCV-005 0037 counter weight
modification
b. Observations and Findinas
A minor documentation error was noted in the work package for the 2A A
EDG monthly mechanical inspection. Procedure MI-4.2.3 requires that a
work request be written if adjacent cylinder exhaust temperature
differential exceeds 100 degrees F. EDG 2A A cylinder No. 7 read 660*F
while the rest of the cylinders read from 940 1000 degrees F. If an
existing work request existed for the condition then the existing WR
number was to be recorded. No work request was recorded and the
inspector considered this an example of lack of attention to detail.
The licensee corrected the work package. The documentation reviewed
showed that except for the item mentioned the work was done according to
the procedural requirements.
c. Conclusions
The level of detail of work documentation was adequate but not thorough.
A minor documentation error was noted in one work order which was
corrected by the licensee.
M1.4 ERCW Discharae Check Valve Stuck Open
a. Insoection Scope (62703)
The insxctors reviewed the licensee's actions related to repair of ERCW
pump L 3 discharge check valve.
b. Observations and Findinas
On August 23, 1996, the licensee identified that the discharge check
valve on ERCW pump L B was leaking by, when the pump was stopped, at the
rate of approximately 3000 gallons per minute (gpm). The licensee
subsequently determined that the swing arm of the valve exhibited
excessive wear which resulted in the valve not properly seating. The
licensee also discovered that the valve had been incorrectly installed
approximately two years ago. The inspector determined from the valve
vendor's manual that the valve had in fact been installed incorrectly.
Further discussions with the system engineer revealed that it could not
be concluded that the incorrect installation resulted in the valve
- _ _ _
. .
,
.
11
failure. The valve was repaired and returned to service. The licensee
initiated Problem Evaluation Report (PER) No. SQ962283PER to document
the valve failure,
c. Conclusions
The inspectors concluded that the ERCW check valve had been installed
incorrectly at some time in the past, but could not conclude that the
incorrect installation resulted in its subsequent failure. The licensee
plans to inspect the remaining seven ERCW discharge check valves at a
future date. The corrective actions associated with the PER will be
reviewed during a future inspection. This item is identified as
Inspector Followup Item (IFI) 50-327, 328/96-09 03, Review Corrective
Actions Related to ERCW Check Valve Failure, PER SQ962283PER.
'
M2.3 Eauioment Material Condition and Reliability Issues
a. Insoection Scope (62703)
The inspectors noted that during shift relief / turnovers, the morning
status meeting and while reviewing operator logs that a variety of
systems and components appeared to be experiencing repetitive / multiple
failures. A detailed review of the control room logs and site
'
information reports (morning status meeting) was conducted, to identify
those systems / components with multiple deficiencies. The operations
logs and status reports covered the period from July 28 through
September 14.
. b. Observations and Findinas
- The operations logs, although not always detailed, provided the majority
J of the examples documented in the following section. The individual
descriptions were taken from the unit operations logs or the site
information re) orts and a detailed review of each item has not been
performed by t1e NRC. The operations logs indicated that many of the
- items were corrected in = ti..aly manner. While this list was intended
4
'
to document the quantity and types of problems being experienced, it
also was intended to focus on systems with recurring failures / problems.
The following are examples of equipment failures / problems noted during
the period, however, note that this list is not all inclusive.
e Various EDG starting air system relief valves were found relieving
eight times (Section E4.1),
o At one point, only one of four primary water pumps was available
to supply both units due to excessive seal leakage and vibration
problems.
s
e Only one of four shutdown board room cooling fans was available
due to a loss of freon from one chiller unit (two fans inoperable)
. and high vibration on one of the other fan units.
.__ __ _ _ . _ . _ . _ _ _ _ __ .. .- _ . __ _ _ _ _ _ _ _ _ . .. _
.- .
.
.
! ,
i 12
) e Various reactor coolant pump (RCP) seal leakoff detectors (3 of 8)
- - became stuck; twice during the inspection period, with a third
j occurrence just following the completion of this inspection
- period.
? e The glycol chillers experienced multiple problems: on July 31, the
l- "E" chiller had excessive vibration; on August 8, the "A" chiller
was found tripped, on August 15, the "A' chiller tripped due to
air in the system which could not be removed: on August 20, after
l filling and venting the "I" chiller, the operators could not keep
- it running; on August 20, maintenance replaced the "I" chiller
i control module due to shorting; on August 21 all of the chillers
i and pumps tripped due to low ex
o)erators could not get the "D"pansion tank level; on August 21, chiller t
i t1e "H" chiller tripped for no appartnt reason and could not be
i restarted, in addition, "there were no spare chillers available";
! and on September 11, the "E" chiller was taken out of service for
i troubleshooting.
L
! e The boric acid system experienced problems with flow oscillations,
j tripping thermal overloads, and slow controller operation.
i
e The main turbine oil systems ex)erienced problems with low turbine
i Auto Stop 011 pressure and low 91C pressure.
l. -e There were multiple leaks from the ERCW hypochlorite system: the
i 2A header on August 2, the 1A header on August 3, the IB header on
! August 17, the 2A header on August 20, the 1A header on August 25,
. the 1A relief valve was found lifting on August 27 and the "A"
i skid discharge piping had a leak on September 9. 'In addition, on
- September 1, the supply breaker for the injection pumps kept
j tripping,
e .The Control Rod Drive Motor (CRDM) automatic temperature control
l cooling valves were drifting closed and sometimes caused the fan
- cooling supply air to exceed the administrative limits of 110
i degrees F.
1
! e There were various computer problems during the period such as:
- the Integrated Control System (ICS) computer system had not been
l able to calculate core burnup since the system was installed; a
i digital link to the ICS computer for point U1118 failed causing an
4 indicated increase of 10 Megawatts Thermal (MWT) to the total
- power calculation; and the ICS com> uter calorimetric readings have
failed due to a failed input from ) lowdown flow.
l
L e The station air compressors had multiple problems: on August 9,
l the "D" compressor had a blown gasket on the top of the
intercooler; on August 20, the "D" compressor inner cooler relief
~
i lifted too much to stay in service: on August 20, the operators
- noted that the "A" compressor was in lead but only half loads, the
"C" compressor trips on high discharge pressure and the "D"
'
l
l
> _. . -.
. _ _ - _ - - _ . _ _ ___
. .
.
.
'
.
13
compressor had a stuck ERCW rotometer/or flow blockage to the
t
compressor; when released from clearance on August 22, there was
no ERCW flow to the "D" compressor: on August 23, the "D"
compressor was removed from service because its intercooler relief
valve was lifting; on August 23, when "D" comaressor was placed
back in service, the post maintenance test (pit) was unsuccessful
t,ecause air was blowing out the side plate on the compressor; on
August 24, a work request was written on the "C" control air
,
prefilter due to high filter differential pressure (DP): and on
August 24, operaters tagged out the "D" compressor.
e On August 13, Unit 2 roc'3 auto stepped "out" with no signal (8:00,
8:05, 11:04, and 11:09 a.m., and 12:11 p.m.). On August 16. Unit
I rods stepped "in" for no apparent reason. On August 17, Unit 2
rods stepped "in" for no apparent reason at 2:03 p.m., and
3:07 p.m. On August 18, Unit 1 rods stepped "in" for no apparent
reason.
,
- e On August 23, Unit 2 loop calculation processor (LCP) card failed.
Shortly after the card failure, a steam dump failed open when the
a steam dumas were placed in the " pressure mode". On September 10,
a Unit 1 _CP card failed. A replacement card was not available
and the unit had to remain in a degraded condition until a
replacement card could be found.
! e The 161 and 500 kv switchyard cable tunnels were flooded with
several inches of water. The permanent
and the temporary pump had been removed, pumps were not operable
e On Unit 2, 3 of 4 steam generator blowdown sample valves will not
,
open.
l Several of the problem areas listed above were also included in
i IR 50 327,328/96 08, Section M2.3, Equipment Material Condition and
Reliability Issues, and included the EDG air starting system, the
-
station air compressors, a protection set card and the containment
chillers.
i c. Conclusions
- The listed examples indicate weaknesses in plant material condition.
The repetitive problems caused added operator burden (work arounds).
Such as: increased monitoring of the EDG starting air receivers; manual
o>eration of the EDG starting air compressors; and special monitoring of
t1e CRDM cooling supply valves. The multiple failures impacted
maintenance resources in correcting the problems and operations
resources for switching and tagging and equipment status control.
Examples such as the stuck RCP seal leakoff detectors, automatic rod
1 stepping, and failed LCP cards impacted day to day operations. These
are indicative of weaknesses in maintenance and engineering support.
a
. . . _ _ _
, a
.
.
'
.
14
,
M2.4 Review of EDG Governor Booster Cylinder Corrective Actions
a. Insoection Scope (40500)
The inspector reviewed the corrective actions for a previous EDG
governor booster cylinder failure to determine if corrective actions
were adequate,
b. Qbservations and Findinas
NRC Inspection Report 50 327,328/96 02 described the circumstances of a
, failure of the EDG 1A1 governor booster servomotor. The booster
servomotor was replaced and the failed unit was sent to the vendor for
failure analysis. The licensee also evaluated the failure at their own
independent laboratory.
The licensee determined that no PM existed for replacing governor
booster servomotors. The governor booster servomotor which failed had
been in service for approximately 20 years. A 12 year PH was submitted
by the technical support engineer to establish a governor booster
servomotor replacement interval.
The inspector reviewed the failure analyses wrformed by the vendor and
the TVA lab. The vendor concluded that the moster had exceeded its end
of bfe and the booster piston seals were worn due to normal aging.
Greasy debris and rust particles were also observed to be restricting
the cylinder air ports. The inspector discussed the failure analyses
with technical support personnel and determined that the rust particles
were probably due to system piping corrosion which occurred prior to the
use of system air dryers. Oil side leakage past the cylinder seals
could have contributed to the air port fouling. The inspector verified
by plant walkdowns that the air lines to the governor servomotors were
upstream of the air line lubricators. The inspector determined that the
licensee had evaluated the findings of the two fadlure analyses reports
and was taking action to address these findings.
c. Conclusions
The licensee's corrective actions for the EDG governor booster
- servomotor failure was satisfactory.
M3 Maintenance Procedures and Documentation
M3.1 Review of Steam Generator Documentation
a. Inspection Scope (73753)
The inspector reviewed procedures, programs, and records associated with
the condition of the Sequoyah Steam Generators (SGs) to determine if the
licensee met FSAR commitments. (This review was the ccmpletion of an
inspection initiated July 8 12, 1996, and documented in Inspection
Report 50 327,328/96-08. Paragraphs M2.2 and M6.1)
.. .- .- . _ . . .. .-
,
,
,
.
15
,.
b. Observations and Findinas
Two SG areas which have historically contained tubing materials with
high residual tensile stresses, and therefore susceptible to stress-
'
related cracking
i the tube bunfle, problems, are the
and the inside tight radius
surface bends where
of the tubing in rowsit 1was and 2 of
explosively expanded against the tube sheet. The licensee has attempted
<
to reduce, or eliminate, the tensile stresses in these areas of the SGs
- 3
by: heat treating (stress relieving) the tubing in the tight radius
bends; and by peening the inside surface of the tubing in the tube
sheet, to change the surface condition of the material from residual
tensile stresses to residual compressive stresses.
,
The inspector selected the heat treatment of the Unit 2 SGs as a sample
of this >rogram to review. The review included the Westinghouse Field
Service )rocedure STD FP 1993 6558. Rev 1, dated 4/28/94, "Se
i Unit 2 (TEN) Model 51 U bend Heat Treatment Field Procedure"and quoyah
individual tube heat treatment records for the work done.
The inspector also reviewed material heat numbers and subsequently the
chemistry and physical properties of the Unit 2 SGs tubes which have
been plugged.
c. Conclusions
Steam Generator records indicated that the licensee had implemented a
<
comprehensive program to minimize stress related degradation of SG
tubes.
M6 Maintenance Organization and Administration
! M6.1 Manaaement Involvement in the Steam Generator Proaram
'
a. Insoection Scooe (73753)
- The inspector reviewed documentation and held discussions with licensee
personnel concerning management involvement with the SG program.
. b. Observations and Findinas
'
The inspector reviewed the current five year plan for SG inspection and
maintenance. During this review the licensee discussed their )lans for
'
requesting licensing approval for the repair of degraded SG tu>es by the
use of laser welded sleeving. This repair method will also be used as a
contingency method for recovery of previously plugged tubes.
- A discussion was held with licensee engineering aersonnel concerning the
, fact that SG management is currently working wit 1 a 5% plugging limit on
the SGs. The explanation offered .was that in the past, TVA had not
contracted for a more rigorous accident analysis to justify a higher
plugging limit. The licensee went on to explain that TVA had recently
changed nuclear fuel vendors, and as a part of the analysis of the new
_
. -
_ _ _ _ . _ . . . _ . _ _ _ _ _ . . _ . _ .-_____- - -._. --
,
'
, .
.
.
m
i
l 16
fuel, TVA had requested an accident analysis which would support a 15%
plugging limit on the SGs.
The inspector, and licensee SG management personnel, also discussed the
licensee's rationale for not lowering T to protect the SGs. The major
reason for not reducing Tu appearsto$t the significant revenue loss
from the resulting power reduction.
c. Conclusions
The licensee's SG organization has done a very good job of reviewing
their inspection and repair options, and soliciting plant and corporate
management support for the options selected.
MB Miscellaneous Maintenance Issues
M8.1 (Closed) Licensee Event Report (LER) 50 327/95014, " Failure to Properly
Identify and Plug a Steam Generator (SG) Tube that was Determined to
Exceed the Technical Specification Plugging Limit."
(Closed) Licensee Event Report (LER) 50 328/96002, " Failure to Properly
Identify a Steam Generator (SG) Tube that may have Exceeded the
Technical Specification Plugging Criteria."
The similarities between these two events is that the defects in
question were caused by degradation mechanisms expected in these SGs,
and that in each case, two independent analyses missed the defects.
The licensee's corrective action for LER 50 327/95014 included the
addition of dented intersections with flaws to the )erformance data base
used to train and qualify eddy current analysis. T1e corrective action
for LER 50 328/96002 included the addition of Rows 1 and 2 U bends with
severe permeability variations in the performance data base, and an
update to the Steam Generator Analysis Guidelines, to enhance
permeability variation effects in the U bend regions.
The inspector reviewed the August 1996, revision of the Steam Generator
Analysis Guidelines and verified that permeability variation effects had
been enhanced. The inspector also reviewed a demonstration of the
licensee's performance data base, which included the Row 1 U bend with
severe permeability which had been the subject of LER 50 328/96002.
The problems identified in the LERs constituted two examples of licensee
identified violations of the 31 ant technical specification definitions
for SG operability. The two .ERs are considered to be two examples of
one violation because the violation reported in LER 50 328/96002 had
already occurred when the violation reported in LER 50 327/95014 was
discovered, and the increased sensitivity to that type of problem led to
the second discovery.
The TS violations descrioed in the LERs meet the criteria for a licensee
identified, non cited violation, as described in Section VII.B.1 of the
,
- - -. - -.
a. ,no,. .s u aa uu,..m.m.a- m ..na. a ~n , . , . . , w. .p w.s . a - , . ..,~..an... aus-..as.--ws-~..ae .w
. se, -~a a-,s...n-u n.a s - .r a , ,s.u. a .ss--s a s a. s w x
.
.
- ,
.
'
4
17
i NRC Enforcement Policy. This will be reported as NCV 50 327,328/96 09-
04, " Failure to Identify Steam Generator Tube Defects Which Were u
!
Excess of TS Plugging Limits."
i
'
III. Enaineerina
El Conduct of Engineering
E1.1 General Comments (37551)
During the inspection period, TVA finalized the reorganization of sita
staffing. Discussions with engineering indicated that the system
engineering department /section was significantly affected. Seventeen of
forty nine )ositions were left unfilled / vacant. In additien, some
engineers clanged positions and responsibilities. Engineering plans to
fill the positions as soon as appropriate personnel are identified.
E2 Engineering Support of Facilities and Equireent
E2.1 Review of Licensee Evaluation of Potential for Incorrect Material
Received From Vendor
a. Insoection Scooe (37551)
On June 21, 1996, the licensee received a request for assistance letter
relating to a 10 Code of Federal Regulations (CFR) Part 21 Evaluation
for material received from Consolidated Power Supply. The material
included 3/4" schedule 80 pipe which may not have been the ty)e
specified on the purchase order. The inspector reviewed the ' art 21
informaticn, PER SQ961874PER, which was written to evaluate the
condition.-and the corrective actions associated with the issue,
b. Observations and Findinas
The initial licensee engineering evaluation for PER No. SQ961874PER was
reviewed by Region II specialists during the week of July 8 12, 1996.
The licensee stated they received a shipment of the sus.nect material
under Contract Number P 95N2J 148011 000. The licen a determined that
the material was used in different plant applications; however, the only
technical concern for material received was associated with weld
processes used if the material was not as specified in the contract.
The licensee initially determined that no safety related applications
were involved in the use of the supplied material which involved
welding. The Region II inspectors noted that the weld process used by
the licensee may have been ina)propriate for materials supplied and
could result in cracking, breating, or failure.
During this period, the inspector conducted additional review of the
issue. The inspector met with licensee engineering personnel and
discussed the concerns associated with potential welding applications.
i
- _ . - - -. - - . . - . - . - - - . - _ - - . - - _ _ - - . _ - -
-
- . :
- l
.
.
l 18
i l
Over the next two weeks, the licensee conducted additional testing of
the materials received from the vendor. Testing of samples of piping
from the five pieces received from the vendor under Contract Number P-
,
95N2J 148011-000 determined the piping was as specified in the contract.
,
c. Conclusions
! The inspector concluded that after identification of initial concerns
- based on the engineering evaluation for the Part 21 potential problem,
j the licensee took appropriate positive actions to determine the issue
l did not affect Sequoyah.
i
E2.2 Review of Status of Unit 1 Samole System
!
- a. Insoection Scope (37551)
i
- On August 2,1996, the inspector conducted a walkdown of a temporary
! system installed on Unit 2 for drainage from steam generator blowdown
- sample drains in accordance with Temporary Alteration Control Form
(TACF) 2-95 0012 043. The inspector revicwed the associated
-
. documentation supporting the TACF, and also conducted a walkdown of the
l Unit 1 hot sample room to evaluate the condition of the Sample System in
l this area.
f
j b. Observations and Findinas
i
j The inspector verified the proper installation of the temporary
4 alteration. During the review, the inspector noted that several sample
'
valves on c panel associated with sampling of boron injection tanks .
4
(BIT), appeared to be in poor material condition. Past leakage was ;
! obvious on several of the valves based on coatings of boric acid. !
9
'
Further review of this issue determined that this portion of the sample '
system was not being used. The inspector noted that there was no l
.'
documentation that abandoned this mrtion of the sample system. The '
system engineer wrote PER SQ962182)ER for determination of whether these
- sampling lines need to be formally abandoned. The ins wctor noted that
4
proper valve status control was being maintained for t11s portion of the
- sample system.
i c. Conclusions
i The inspector concluded that the temporary alteration in the Unit 2 hot
< sample sink room was installed in a satisfactory manner and the safety
assessment justified the installation. However, the inspector noted
that sample valves located in the Unit I hot sample room for the Safety
Injection system were in poor material ccndition and presented potential
housekeeping problems. In addition, this portion of the sample system
was not formally abandoned. The poor material condition of the valves
and the informal control of abandoned equipment were considered to be
negative observations.
-- . ._ . .- -. -- _.
. .
.
.
.
19
E2.3 Unit 1 Residual Heat Removal System (RHR) Gas Accumulation
a. Inspection Scoce (37551)
'
The inspectors reviewed the results of the Unit 1 RHR gas accumulation
data which the licensee calculated during the American Society of
Mechanical Engineers (ASME)Section XI tests on August 29, 1996 (A-
Train) and September 5, 1996 (B-Train). The inspectors compared the
data with previous gas accumulation data and reviewed the licensee's
corrective actions for the gas accumulation problem. Previous reviews
of the RHR gas accumulation issue were discussed in IPs 50 327,328/95-
04, 95-06, 95 12, 96-01, and 96 08 and in Licensee Event Report (LER)
50 327/95001.
.
b. Observations and Findinas
In November 1995, the licensee added Tracking and Reporting of Open
Items (TROI) Action Item Number 29 to PER No. SQ950029PER. That PER was
the original PER, initiated in January 1995, which dealt with the RHR
gas accumulation. Action Item 29 required the licensee to " Develop
. methodology for evaluating the gas void momentum effect on RHR injection
'
piping loads. Determine relationship of the piping void size to pipe
loading and establish maximum allowable void size based upon piping
, structural margins."
"
In January 1996, an independent contractor com)leted a study of the
Sequoyah RHR gas accumulation issue. One of t1e long term actions from
that study stated that if too much gas was present, it could interfere
with or delay delivery of low pressure injection in accident conditions
and that the limit (maximum gas accumulation volume) should be
determined by TVA and Westinghouse Accident Analysis.
In March 1996, the licensee established 8 cubic feet as the maximum
, allowable void size in the RHR system. The decision to use 8 cubic feet
'
as the limit was based upon the known gas volume in the RHR system at
the time and not upon a formal engineering analysis of the structural
limits of the RHR system. The licensee concluded that since 8 cubic
feet was known not to cause water hammer damage to the RHR system that
it was reasonable to use 8 cubic feet as the maximum allowed limit and
thus close the TROI action 29 based upon that assumption. However, the
closure of action item 29 stated that the void size of 8 cubic feet
could not be relaxed.
On August 29, during an ASME Section XI test on the RHR 1A-A pump, the
licensee calculated the gas volume to be 11.6 cubic feet. On August 30,
1
1996, in response to the identification of 11.6 cubic feet of gas, the
licensee completed another engineering evaluation to determine the
maximum allowable gas accumulation. The new evaluation referred to the
previous 8 cubic feet limit as an administrative limit and revised the
gas accumulation limit to 15 cubic feet. Again, the evaluation was
'
based upon the known history of gas build up rate and not upon a formal
engineering evaluation. The evaluation stated that the average gas
. - - . . - .. . . . _ . - _
,
, 1
.
- .
.
20
-
accumulation rate since January 1996, has been approximately 4 cubic
feet per quarter. The evaluation assumed that 4 cubic feet was
indicative of the accumulation rate in the past and that as much as 24
cubic feet of gas (4 cubic feet per quarter x 6 quarters per operating
cycle) had been present, prior to the current practice of quarterly
venting, during previous quarterly Section XI pump testing and had not I
resulted in water hammer damage. The licensee concluded that since 15
cubic feet of total gas accumulation was significantly less than the
total volume of gas expected to accumulate for a full fuel cycle (24
cubic feet), the associated pipe movements would not be sufficient to
cause pipe support failures or challenge the integrity of the piping
pressure boundary.
2
On September 5, 1996, during a Section XI test on the RHR 1B B pump, the
gas volume was determined to be 13.8 cubic feet. Following the
identification of 13.8 cubic feet of gas, the licensee reevaluated the
limit of 15 cubic feet which had been established on August 30. On
- September 6, using the same methodology as was used on August 30, the
licensee reestablished the maximum. gas void limit at 22 cubic feet.
It should be noted that the gas accumulation calculations on August 29
.
and Seatember 5, were performed after the RHR system had been vented and
that t1e licensee did not measure the volume of the vented gas.
Therefore, the calculated gas accumulation of 11.6 and 13.8 cubic feet
represented the "as left" gas accumulation in the system.
.
As discussed in Inspection Report 50 327, 328/96 08, the licensee plans
to install a continuous venting modification during the next two
refueling outages,
c. Conclusions
The inspectors were unable to conclude whether the licensee's method of
determining the maximum allowable RHR gas accumulation, to preclude
i water hammer damage, was acceptable. Pending the resolution of this
issue, this item is identified as URI 50 327, 328/96 09 05, Determine
l Whether the Licensee's Method of Determining the Maximum Permissible RHR
Gas Void Size is Acceptable.
The inspectors concluded that licensee's practice of venting the RHR
system prior to calculating the volume of gas in the system did not
provide an accurate representation of the total amount of gas in the RHR
system.
E2.4 Unit 2 Core Flux Tilt
a. Insoection Scoce (37551)
During the inspection period the inspectors were informed of a Unit 2
,
'
core flux tilt and of potential plans to reduce axial flux difference
(AFD) limits if subsequent flux maps identified additional reductions in
margins.
_.
.- - . . .- - - .
, , .
.
.
-
.
21
b. Observations and Findinag
i
After noting the flux tilt problem in Unit 2, the inspectors discussed ,
the condition with site reactor engineering personnel. Engineering '
noted that the unit 2 core tilt had developed following the refueling
outage in May 1996 and that the tilt had increased to almost 3%. A
,
specific reason for the tilt could not be identified. At the completion
of the inspection period the tilt had decreased to approximately 1.7%.
The inspectors discussed the tilt condition with NRC Region II and
headquarters personnel.
Subsequent discussions with control room operators noted that some of
the operators had not been aware of the tilt condition until the AFD
limits had been reduced. The inspectors noted that the control room
indications such as delta T and Tave did not identify a tilt condition.
In addition, the inspectors noted that the computer printout for tilt,
did not indicate a tilt condition. Discussions with engineering
indicated that following a flux map, the nuclear instrument inputs are
normalized which eliminates the actual tilt indication. Discussions
with the region and with other utilities noted that this was a standard
practice.
c. Conclusions
It was determined that while the tilt condition was somewhat unusual,
the licensee was properly monitoring the condition and had taken
appropriate actions. However, engineering did not clearly communicate,
to operations personnel or to the resident inspectors, the fact that a
tilt condition existed in the Unit 2 core for an extended period of time
following discovery. Although not reportable or safety significant, the
lack of prompt communication is being noted as a negative observation.
E4 Engineering Staff Knowledge and Performance
E4.1 Imorocer Emeraency Diesel Generator Startina Air System Operation
a. Insoection Scooe (37551)
The inspectors reviewed various documents and historical records to
determine why the EDG starting air compressors were causing their relief
valves to lift and causing the low pressure alarms to alarm. The
documents included the control room logs, EDG starting air system
corrective maintenance history, EDG design basis document FSAR section
containing the EDG starting air system, and the operator rounds logs.
In addition, the inspectors interviewed the system engineers, auxiliary
operators, and control room operators and observed system operation in
manual and in automatic.
l
- -- -- -,--- _-- - . - . - . - . _ , . - - - . - - ,
. =
-
.
,
'
.
i
22
l
j b. Observations and Findinas
During the inspection period, the inspectors noted that the control room
j
logs were documenting instances when the EDG starting air compressors
2
were found with their relief valvas lifting or when the low pressure
alarms were in alarm. In addition, while observing outside AVO duties,
the inspe W r observed the 2-B 2 EDG staring air receiver relief valve
' ne receiver tank pressure was at approximately 343 psig and
'
lifting. ,
, the compressor was still running although the normal system operating
- pressure band is 250-300 psig.
The inspectors discussed the improper operation of the EDG starting air
. compressor control circuitry with the system engineering technical
l support staff. The engineers stated that the root cause of the
i
compressor misoperation was two fold: (1) o)erations was cycling the I
. control switches when routinely (per shift) alowing down the air lines,
j and (2) due to the compressor dryer timer which could cause the
i
compressor to run for up to 5 minutes after reaching shutoff pressure.
Corrective actions were already in place for eliminating the air line
blowdown requirement and the dryer timer issue was under review.
The ins)ectors observed actual operation of the air compressors and
noted tlat it took approximately 20 minutes to increase system pressure
from 270 psig to 300 psig and concluded that an additional 5 minutes '
would not have caused the pressure to increase to the relief valve
setpoints. The inspectors then interviewed approximately 10 AU0s and a
few control room operators and concluded that blowing down the air lines
almost never caused the compressors to start unless already at the low
pressure automatic start setpoint.
A detailed review of the control room logs noted that various relief
valves had been found lifting on July 23, August 1 and 3, twice on
August 23, and September 8, 9 and 10. In addition, the low pressure
alarm was noted on August 4 and September 10. The inspector noted that
the control room logs did not identify which specific valve was lifting
and it appeared that system engineering was not aware that the receiver
tank / system relief valves were lifting on occasion. It appeared that
the engineers had assumed that only the compressor reliefs had been
lifting.
The inspectors reviewed the corrective maintenance history for the
compressor control switches. All of the switches had been replaced
(modification) in late 1993 due to previous failures. Following
replacement there were five recalibrations due to setpoint drift and
eight replacements. In two cases, switches replaced in 1995, failed
again in 1996 and in one case, a switch replaced on August 1, failed on
August 3 and again on September 9. It was also noted that the switch
problems were being encountered only during summer months.
After additional relief valve lift problems in September and open
discussions with operations during the Plan of the Day meeting,
engineering determined that the control switches were sticking due to
_ _ _ _ _. ._.
. .
.
.
.
23
being temperature sensitive and plans were under development to replace
the faulty switches.
c. Conclusions
,
The ins)ectors concluded that the licensee's efforts to resolve the
faulty EDG starting air comaressor control switch problem to be l
, inadequate and untimely. T1e failure to promptly identify and correct
conditions adverse to quality, is a violation of the licensee's
corrective action program as required by 10 CFR 50, A)pendix B,
- Criterion XVI, Corrective Action, and as implemented )y SSP-3.4
'
(VIO 50 327, 328/96 09 06).
In addition, the root cause determination for the initial failures was
1 also considered to be inadequate and is considered to be a weakness.
This ultimately led to multiple challenges to starting air system
integrity (reliefs lifting).
,
E.7 Quality Assurance in Engineering Activities I
~i
E7.1 Updated Final Safety Analysis Report (UFSAR) Review
i
- A recent discovery of a licensee o>erating their facility in a manner
contrary to the UFSAR description lighlighted the need for a special
.
focused review that compares plant practices, procedures and/or
4
parameters to the UFSAR descriptions. While performirg the inspections
-
discussed in this re) ort the inspectors reviewed the applicable
portions of the UFSAR that related to the areas inspected. The
, inspectors verified that the UFSAR wording was consistent with the
4
observed plant practices, procedures and/or parameters.
1
IV. Plant Support
1
! F1.1 Review of Transient Fire Loadina (TFL) Conditions
a. Insoection Scooe (71750)
During the week of July 8 12, 1996, an NRC inspector questioned a
- condition associated with a TFL Permit TFL 95 0254 which was issued for
i the storage of 1500 pounds of cloth / rubber / plastic radiation arotection
clothing on Elevation 690 between column lines A4 and A6 in t1e
Auxiliary Building. After the issue 4 .dentified, the licensee wrote
. PER SQ961962PER on July 12, 1996. DL< y this period, the inspector
reviewed the licensee's interim actions associated with the issue.
1
b. Observations and Findinas
.
'
On July 30, 1996, the inspector reviewed the status of the licensee's
interim actions. He conducted a tour of the area in the Auxiliary
Building and noted that radiation protection clothing was still being
1
7 *
1
j
-
.
.
24
stored in this location. He also noted Permit TFL 95 0254 dated i
November 14, 1995, was still posted in the area. After the tour, the
'
inspector questioned the licensee about the observed conditions, and
requested appropriate justification for the transient fire loading
condition. On July 31, 1996, after additional review by licensee
engineering personnel, the licensee determined that the location being
used to store the radiation protection clothing had been included under
a deviation for compliance with 10 CFR 50, Appendix R as a low l
combustible area. Although a portion of the clothing had been removed
after July 12, the licensee had not initiated a new transient fire load
permit to justify the observed condition on July 30. The licensee took
immediate action to remove the remaining radiatico protective clothing.
The inspector verified that remaining pre Oive clothing was removed I
from the Auxiliary Building area.
c. Conclusions
The inspector concluded the licensee did not take adequate
im m diate corrective actions for this transient fire load issue
identified during the week of July 8 - 12, 1996. Appropriate
corrective action was only taken after the NRC commenced
additional review of the issue on July 30, 1996. This issue will
be further dispositioned as part of a special inspection
documented in Inspection Report 50 327, 328/96-10.
V. Manaoement Meetinas
X1 Exit Meeting Summary
The resident inspectors 3 resented the inspection results to members of
licensee management at tie conclusion of the inspection on September 17,
1996. The licensee acknowledged the findings presented.
The inspectors asked the licensee whether any materials would be
considered proprietary. No proprietary information was identified.
PARTIAL LIST OF PERSONS CONTACTED
Licensee
- Adney, R., Site Vice President
Brock, D., Maintenance Manager
Bryant L., Outage Manager
- Burzynski, M., Engineering & Materials Manager
Clift, D., Planning and Technical Manager
Driscoll, D., Training Manager
- Fecht, M., Nuclear Assurance & Licensing Manager
Fink, F., Business and Work Performance Manager
- Flippo, T., Site Support Manager
P.-
.
.
.
25 ,
- Kent, C., Radcon/ Chemistry Manager
- Lagergren, B., Acting Operations Manager
- Meade, K., Compliance Manager
Poage, L., Site Quality Assurance Manager
- Rausch, R. . Maintenance and Modifications Manager
Reynolds, J., Acting Operations Superintendent
Robertson, J., Independent Analysis Manager
- Rupert, J., Er gineering and Support Services Manager
- Shell, R., Site Licensing Manager
- Skarzinski, M., Technical Support Manager
Smith, J., Regulatory Licensing Manager
- Summy, J., Assistant Plant Manager
Symonds, J. Modifications Manager
- Attended exit interview ,
INSPECTION PROCEDURES USED
IP 37551: Onsite Engineering
Effectiveness of Licensee Controls In Identifying, Resolving, &
.
IP 40500:
'
Preventing Problems
IP 61726: Surveillance Observations
IP 62703: Maintenance Observations
IP 71707: Plant Operations
IP 71750: Plant Support Activities
IP 73753: Inservice Inspection
ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
T.yge Ites Number
_ St_atus Description and References
URI 50 327,328/96 09 01 Open Determine Whether TS 3.3.1.1 Allows
One Pressurizer Pressure Channel to
Be Bypassed at the Same Time that a
Second Pressurizer Channel is
Tripped (Section 02.2). i
NCV 50 327/96 09-02 Open/ Inoperable "A" Train of EGTS for 2
Closed Hours and 43 Minutes D* to Operator
Error (Section 03.2).
IFI 50-327, 328/96-09 03 Open Review Corrective Actions Related to
ERCW Check Valve Failure, PER
SQ962283PER (Section M1.4).
NCV 50-327, 328/96 09 04 Open/ Failure to Identify Steam Generator
Closed Tube Defects Which Were in Excess of
TS Plugging Limits (Section M8.2).
I .
l
..
.
.
26
URI 50 327, 328/96 09 05 Open Determine Whether the Licensee's
Method of Determining the Maximum )
Permissible RHR Gas Void Size is
Acceptable (Section E2.3). j
VIO 50 327, 328/96 09 06 Open Inadequate and Untimely Corrective
A tions Associated With the -
Resolution of the EDG Starting Air
Compressor Switch Failures (Section
E4.1).
$ Closed
'
T_.yge Item Ntaber
. Status Description and References
LER 50 327/95014 Closed Failure to Properly Identify and
- Plug a Steam Generator (SG) Tube
I
that was Determined to Exceed the 4
Technical Specification Plugging
Limit (Section M8.1). l
l
LER 50 328/96002 Closed Failure to Properly Identify a Steam I
Generator (SG) Tube that may have
Exceeded the Technical Specification
Plugging Criteria (Section 8.1).
LIST OF ACRONYMS USED
AFD -
Axial Flux Difference
ASME -
American Society of Mechanical Engineers
AS0S -
Assistant Shift Operations Supervisor
AVO -
Assistant Unit Operator
BIT -
Boron Injection Tank
CCW -
Condenser Cooling Water
CFR - Code of Federal Regulations
CRDM -
Control Rod Drive Mechanism
EDG -
EGTS -
Emergency Gas Treatment System
ERCW -
Essential Raw Cooling Water
FSAR -
Final Safety Analysis Report
ICS -
Integrated Control System
IFI -
Inspector Followup Item
IP -
Inspection Report
GPM -
Gallons Per Minute
KV -
Kilo Volt
LCP -
Loop Calculation Processor
LER -
Licensee Event Report
MCR -
Main Control Room
MI -
Maintenance Instruction
M&TE -
Measuring and Test Equipment
,,
P ., ,
'
.
27
MWT -
Megawatt Thermal
NCV -
Non Cited Violation
NRC -
Nuclear Regulatory Commission
NRR -
Nuclear Reactor Regulation
PER -
Problem Evaluation Report
PM -
Preventive Maintenance
PMT -
Post Maintenance Testing
PSIG -
Pounds Per Square Inch Gauge
PZR -
Pressurizer
RCS -
RHR -
R0 -
Reactor O p rator
RP&C -
Radiological Protection & Chemistry
SG -
SI -
Surveillance Instruction
SR0 -
Senior Reactor Operator
SSP -
Site Standard Practice
TACF -
Temporary Alteration Change Form
TFL -
Transient Fire Load
T-H0T - Temperature of the Primary Hot Leg
TROI -
Tracking and Reporting of Open Items
TS -
Technical Specifications
TSIR -
Technical Support Investigation Flequest
TVA -
Tennessee Valley Authority
UFSAR - Updated Final Safety Analysis Report
URI -
Unresolved Item
WO -
Work Order
WR -
Work Request
m