ML20246B651

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Insp Repts 50-327/89-15 & 50-328/89-15 on 890506-0605. Violations Noted.Major Areas Inspected:Operational Safety Verification,Operations Performance,Sys Lineups,Radiation Protection,Safeguards & Housekeeping Insps
ML20246B651
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 06/26/1989
From: Brady J, Jenison K
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20246B630 List:
References
50-327-89-15, 50-328-89-15, NUDOCS 8907100046
Download: ML20246B651 (29)


See also: IR 05000327/1989015

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Re' port Nos.:

50-327/89-151 50-328/89-15"

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Licensee: " Ten'nessee Valley Authority

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6N.38A Lookout Place

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1101 Market Square

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Chattanooga, TN. 37402-2801'

Docket'Nos.:

50-327'and 50-328-

License Nos.:

DPR-77 and.DPR-79

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Facility Name:

Sequoyah Units'I and 2

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LInspection_-Conducted:

May 6, 1989 thru June-5, 1989

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Inspector:

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K. Jepfrson, Senior Resid,ent Inspector

Date Signed

Accompanying, Personnel:

P. Harmon, Senior. Resident Inspector

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D. Loveless, Resident Inspector

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Approved by: [ [ [ M

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9. Brady, Actpfg Chief, Project Section 1

Date Signed

TVA Projects Division

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SUMMARY

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Scope:

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lhis routine monthly. inspection invo'lved inspection effort by the. Resident-

Inspectors in the area of operational safety verification including control

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room observations, operations performance, system lineups, radiation protec-

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tic.n, safeguards, and housekeeping inspections.

Other areas finspected included

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twaintenan'ce observations, surveillance testing observations, review of previous

inspection ~ findings,- follow-ep of events, review of licensee identified items,

and review of inspector follow-up items.

.Results:

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The areas lof Operations, Maintenance, and Surveillance were adequate and fully:

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capable to support current plant operations. The observed _ activities'of theJ

control rsom operators were professional and well executed., <Significant

w'eaknesses were identified in the licensee's implementation of the 10 CFR 50.59

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safety" evaluation processes, the licensee's TS interpretation process, and the

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independent qualified review process.

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The licensee had failed to follow procedures 'as .they relate to the configura-

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tion' of a Radiation . Monitor with respect to the detector cable.

This is

identified as VIO 327,328/89-15-02 (paragraph 4).

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The licensee had failed to establish, implement, and maintain written proce-

dures for controlling thermal power within license limits at steady state

operations.

This is identified as VIO 327,328/89-15-03 (paragraph 7).

The licensee had on three occasions failed to perform adequate reviews pursuant

to 10 CFR 50.59.

These examples, described below, were identified as VIO

50-327,328/89-15-04.

a.

Changing the surveillance instruction for the RHR system , without

performing an adequate review pursuant to requirements of 10 CFR 50.59

(paragraph 9.a).

b.

Changing the mode of operation of the BIT from continuous recirculation to

occasional recirculation without performing a review pursuant to the

requirements of 10 CFR 50.59 (paragraph 9.b).

c.

Changing the positions of the source range and intermediate range detector

locations which affected the intermediate range high neutron flux trip

without performing an adequate review pursuant to the requirements of

'10 CFR 50.59 (paragraph 9.c).

The licensee had on three occasions described below failed to establish,

implement and maintain adequate written procedures.

These examples were

identified as VIO 50-327.328/89-15-05.

a.

The licensee allowed a procedure that was known to be inadequate for RHR

pump and pipin0 venting to be performed (paragraph 9.a).

b.

The licensee failed to have an adequate procedure before changing the mode

of operation and the associated system lineup of the BIT (paragraph 9.b).

c.

The licensee failed to ensure that a safety evaluation accompanied the

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screening review form for tne IR and SR detector relocation as required by

SQA-119 (paragraph 9.c).

The licensee put two safety systems in an inoperable condition and failed to

comply with TS LCO action statements.

These examples, described below, were

identified as VIO 50-327,328/89-15-06.

a.

The BIT vas made inoperable during the period when recirculation flow was

stopped (paragraph 9.b).

b.

The IR high flux bistables were made inoperable when IR detectors were

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withdrawn to a new location (paragraph 9.c).

One non-cited violation was identified:

Violation of RWP procedure resulting in the contamination of two workers

(paragraph 2.e).

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One unresolved ' item was identified:

Apparent weakness in the safety evaluation program (paragraph 9).

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REPORT DETAILS

1.

Persons Contacted

Licensee Employees

J. Bynum, Vice President, riur. lear Power Production

  1. J. LaPoint, Site Directar
    1. S. Smith, Plant Manager

T. Arney, Quality Assurance Manager

    1. R. Beecken, Maintenance Superintendent
  • M. Cooper, Compliance Licensing Manager

D. Craven, Plant Support Superintendent

  • S. Crowe, Site Quality Manager
  1. R. Fortenberry, Technical Support Supervicor

J. Holland, Corrective Action Program Manager

J. Patrick, Operations Superintendent

R. Pierce, Mechanical Maintenance Supervisor

    1. M. Burzynski, Site Licensing Staff Manager

A. Ritter, Engineering Assurance Engineer

  1. R. Rogers, Plant Support Superintendent
  1. M. Sullivan, Radiological Controls Superintendent
  1. S. Spencer, Licensing Engineer

C. Whittemore, Licensing Engineer

  1. E. Whitaker, ISEG Manager
  1. G. Gault, Reactor Engineering Supervisor
  1. H. Hellums, Licensing Manager
  1. T. Flippo, QA Manager
  1. S. Crowe, Site Quality Manager
  1. C. Mason, 0&M Support Manager
  1. K. Yeller, PORC Oversight Supervisor
  1. F. kashburn, ISEG Manager
  1. V Blanco, Lead Nuclear Enginee*
  1. L. Cooco, Attorney

NRC Employees

  • J. Brady, Acting Sectien Chie'
  • Attended exit interview June 5, 1989
  1. Attended exit interview on June 9, 1989

Acronyms and initialisms used in this report are listed in the last

paragraph.

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2.

Operational Safety Verification (71707)

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a.

Control Room Observations

The inspectors conducted discussions with control room operators and

verified that proper control room staffing was maintained.

The

inspector also verified that access to the control room was properly

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controlled, and that operator behavior was commensurate with plant

configuration end plant activities in progress and with on going

control room operations.

The operators were observed adhering to

appropriate and approved procedures.

Additionally, the frequency of

visits to the control room by upper menagement was observed for

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adequacy and found to be acceptable.

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The inspector also verified that the licensee was operating the plant

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in a normal plant configuistion as required by TS.

When abnormal

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conditions existed, operatore were found to be . complying with the

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appropriate LC0 action statements.

The inspector verified that leak

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rate calculations were performd and that leakage rates were within

the TS limits,

The inspectors sampled instrumentation and recorder traces for

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indication of abnormalities and verified the status of selected

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control room annunciators to ensure that control room operators

understood the status of the plant.

Panel indications were reviewed

for the nuclear instruments, emergency power sources, the safety

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parameter display system, and the radiation monitors to ensure

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operability and operation within TS limits.

With the exception of

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VIO 327,323/89-15-03 and VIO 327, 328/89-15-04, example 3, operator

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actions with respect to control room indications were adequate,

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Control rod insertion limits were observed as specified in the TS,

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t!o viclations or deviations were observed.

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b.

Control Room Logs

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The inspectors observed control room operations and reviewed

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applicable logs including the shift logs, operating orders, night

order book, clearance hold order book, and configuration log to

obtain information concerning operating trends and activities.

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TACF log was reviewed to verify that the use of jumpers and lifted

leads causing equipment to be inoperable was clearly noted and

understood.

The licensee is actively pursuing corrections to

conditions requiring TACFs.

No issues were identified with these

specific logs.

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Plant chemistry reports were reviewed to confirm steam generator tube

integrity in the secondary side and to verify that primary plant

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chemistry was within TS limits.

A specific problem with dose

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equivalent Iodine occurred on Unit I during an approximately eight

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day period within this inspection period.

Dose equivalent Iodine

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increased by a factor of approximately five with no identifiable

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cause.

This condition was recorded, tracked, and trended by the

plant Chemistry section, but a concerted effort to identify the root

cause ' was not exerted until after the involvement of the Plant

Manager.

The resident staff will continue to monitor the licensee's

resolution of this problem.

In addition, the implementation of the licensee's sampling program

was observed.

Plant specific monitoring systems including seismic,

meteorological, and fire detection indications were reviewed for

operability.

A review of surveillance records and tagout logs was

performed to confirm the operability of the reactor protection

system.

No violations or deviations were observed.

c.

ECCS System Alignment

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The inspectors walked down accessible portions of the following

safety-related systems on Units 1 and 2 to verify operability, flow

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path, heat sink, water supply, power supply, and proper valve and

breaker alignment:

Component Cooling Water System (Unit 1)

Secondary Radiation Monitors (Units 1 and 2)

Feedwater System (Unit 2)

RHR System (Unit 1)

In I,ddition, the inspectors terified that a selected portion of the

containment isolation lineup was correct,

ho deviations or violations were identified.

d.

Plant Tours

Tours of the diesel , generator, auxiliary, conrol, turbine buildings,

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and exterior areas were conducted to observe plant equipmec

conditions, potential fire hazards, control of ignition sources,

fluid leaks, excessive vibrations, missile hazards and plant

houseke. iing and cleanliness conditions.

The plant was observed to

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be clean and in adequate condition.

The inspectors verified that

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maintenanc.e work orders had been submitted as required and that

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followup activities and prioritization of work was accomplished by

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the licensee.

The prioritization of work was discussed with the

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Maintenance Superintendent and Operations Management with respect to

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the increase of maintenance activities that are outstanding in the

control room.

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The inspector visually inspected major components for leakage, proper

lubrication, cooling water supply, and any general condition that

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could prevent fulfilling its functional requirements. The number of

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minor housekeeping and maintenance items such as small leaks,

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tagging, chipped paint, etc. is increasing.

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The inspector observed shift turnovers and determined that all

necessary information concerning the status of plant systems was

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addressed.

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No violations or deviations were observed.

e.

Radiation Protection

The inspectors observed HP practices and verified the implementation

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of radiation protection controls.

On a regular basis, RWPs were

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reviewed and specific work activities were monitored to ensure that

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activities were being conducted in accordance with the applicable

RWPs.

Workers were observed for proper frisking upon exiting

contaminated areas and the radiologically controlled area.

Selected

radiation protection instruments were verified operable and

calibration frequencies were reviewed. The following RWP was reviewed

in detail:

RWP 89-00012, CVCS Hold-up Tank Room B.

The activities that took place under this RWP involved the

contamination of two workers.

This particular RWP prohibited

entry into areas with contamination levels greater tha: 50,000

c'pm/100 square centimeters.

Contamination in the general area

where the two workers were performing activities was approxi-

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mately 9 mrad / hour /100 square centimeters.

When the two subject

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workers were discovered by a TVA Health Physics representative,

they were directed to leave the area.

Each worker was showered

several times and given a whole body count. One worker indicated

a 0.1% Maxiraum Permissible Organ Burden, Co-60.

Two Radiolo-

gical Incident Reports (RIR) were written by the licensee

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(89-67, 89-68).

No legal limits were exceeded and nb over-

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exposures took place.

Because the licensee identified this

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violation of RWP procedures, took prompt corrective actions, and

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is evaluating long term corrective actions under the referenced

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RIR, this issue will be categorized as Non-cited Violation

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327,328/89-15-01.

This violation is not being cited because the

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criteria specified in Section V.G. of the Enforcement Policy

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were satisfied.

NCV 327, 328/89-15-01 is closed.

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Safeguards Inspection

In the course of .the. monthly activities, the inspectors incl'uded a

review of the licensee's physical security program.

The performance-

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of.various shifts of the 4 security force was observed in the. conduct

of daily . activities including: protected and vital area access

- controls; searching of personnel and packages; escorting of. visitors;

badge issuance and, retrieval;.and, patrols and compensatory posts.

In . addition, - the. inspectors observed protected area lighting, and

protected and vital area barrier integrity.

The inspectors verified

interfaces between the security organization and both operations and

' maintenance.

Specifically, the Resident Inspectors:

(1) witnessed firearms training and qualification

(2). interviewed individuals with security concerns

(3) ' visited central and secondary alarm stations

(4) verified protection of_ Safeguards Information

(5) . verified onsite/offsite communication capabilities

No violations or deviations were identified,

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Conditions Adverse to Quality

The inspectors reviewed selected items to determine that the

licensee's problem identification system as defined in AI-12,

Corrective Action, was functioning.

CAQR's were routinely reviewed

for adequacy in addressing a problem. or event.

Additionally, a

sample of the following documents were reviewed for adequate handing:

.(1) Work Requests

(2) Potential Reportable Occurrences'

(3) ' Radiological Incident Reports

(4) Problem Reporting Documents

(5) Ccrrect-on-the-Spot Docuraeats

(6) Licensee Event Reports

Of the items reviewed, each was founc' to have been ident.ified by the

licensee with immediate corrective action in place.

For those issues

that required long term corrective action, the licensee was making

adequ6te progress.

No violations or deviations were observed.

Positive trends were identified in the operational safety verification

area.

Operations management changes were put in place to strengthen the

Operations Superintendent position. Personnel in the positions that

directly support the Operations Superintendent position appeared to be

taking a more active role in the operation of the units.

General

conditions in the plant were adequate.

The number of control room

maintenance and modification items increased during this inspection period

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as a result of an increased effort in the Operations Section to remove

unnecessary indications and difficulties for the operators.

Radiation

protection and security are adequate to continue two unit operations.

3.

Surveillance Observations and Review (61726)

Licensee activities were directly observed / reviewed to ascertain that

surveillance of safety-related systems and components was being conducted

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in accordance with TS requirements.

The inspectors verified that: testing was performed in accordance with

adequate , procedures; test instrumentation was calibrated; LCOs were met;

test results met acceptance criteria requirements and were reviewed by

personnel other than the individual directing the test; deficiencies were

identified, as appropriate, and any deficiencies identified during the

testing were properly reviewed and resolved by management personnel; and

system restoration was adequate.

For completed tests, the inspector

verified that testing frequencies were met and tests were performed by

qualified individuals.

The following activities were observed / reviewed with no deficiencies

identified except as noted:

SI-276, Auxiliary Feedwater Control Valves Operability.

SI-137.2, Reactor Coolant System Water Inventory.

SI-38, Shutdown Margin.

No trends were identified in the area of surveillance performance during

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this inspection period.

The area of surveillance scheduling and manage-

ment was observed to be adequate and improving.

The management of the TS

SI prcgram socears to have progressed from a reactive type process to a

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reutirely scheduled, adequately managed plant operation support activity.

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This is a significant improvement in the licensee's ability to control

plant activity schedules.

TS surveillance requirements were discussed at

the highest levels of the TVA onsite Nuclear Power organization.

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4.

Monthly Maintenance Observations and Review (62703)

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Station maintenance activities on safety-related systems and components

were observed / reviewed to ascertain that they were conducted in accordance

with approved procedures, regulatory guides, industry codes and standards,

and in conformance with TS.

The following items were considered during this review:

LCOs were met

while components or systems were removed from service; redundant

components were operable; approvals were obtained prior to initiating the

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work; activities were accomplished using approved procedures and were

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inspected as applicable; procedures used were adequate to control the

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activity; troubleshooting activities were controlled and the repair

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records accurately reflected the activities; functional testing and/or

calibrations were performed prior to returning components or systems to

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service; QC records :were maintained; activities ~ were accomplished by

qualified personnel; parts and materials used were properly certified;

. radiological controls were implemented; QC hold points were established -

where required and were observed; . fire prevention controls were

implemented; outside contractor force activities were controlled in

accordance with .the' approved QA program; and housekeeping was actively.

pursued.

The following work requests were reviewed:

WR B772426, RM 90-404.

This work activity involved the trouble shooting and repair of a post

accident monitor located in the turbine building.

The function of

the monitor is to measure the condenser exhaust' for potential .

activity which could result from a steam generator tube leak.

When inspected in the field, the RM detector cable was installed

(pressed in and - unsoldered) into the ' detector.

The inspector-

reviewed the configuration control sheet and determined that the

configuration control document did not agree with the arrangement =in

the plant.

IMI-134, Configuration Control of Instrument Maintenance

Activities,. states that the technician performing a work activity

shall list and initial any configuration changes in order on the

IMI-134 data sheet.

These changes include jumpers, wire lifts,

inhibits, temporary instrument settings,

unbolting flanges,

disconnecting tubing and pipe fittings, temporary connections, etc.

The technician 'is to list these items in sufficient detail to

uniquely identify each item.

Centrary to the above, the configura-

tion of the RM with respect to the detector. cable was not correctly

controlled.

This is VIO 327, 323/89-15-02 tor failure to follow

procedure.

In addition to the violatior3 cited, several other

weakness were identified.

Adequate corrective action for the

violation'will include correction of these weaknesses:

Work was completed over several days with no one person in

charge.

There was no indication of what trouble shooting activities ^iere

performed by the several shifts and crews that worked on the

components.

No post maintenance test was identified and an

adequate post maintenance test will be difficult in considera-

tion of the loss of control of trouble shooting activities.

Configuration control with respect to the processor portion of

the RM was not adequate in the cases of the CPU III 10889-01,

and I/O boards.

These boards were placed into and out of the

equipment without record or control of the work activities.

Several components were stored within the electrical cabinet

portion of the RM.

These included tools, spare connecting pins,

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and spare cables.

In addition, cigarettes were also stored

within the electrical cabinet portion of the RM.

One of the tools stored in the electrical cabinet portion of the

RM' was a Winchester crimper.

This tool belonged to the vendor

and was not controlled. or calibrated under the licensee's

crimper program.

In addition, several spare connecting pins

were identified in the cabinet .that did not have corresponding

-documentation in the work package.

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WR 8265544, Containment High Temperature Alarm.

During post maintenance.-testing of this repair the operator noted

that the annunciator test' circuit did not function like the other

panels.

This discrepancy, although partly by design, allowed for

some alarms to stay' in when they were not, in fact, in alarm.

The.

review. determined that the alarms would still perform their intended-

function.

The licensee is still trying to determine the source of

the problem.

WR B265525, RPI-13 Failure.

This work activity involved the extensive testing to the Rod Position

Indication System and the modification of a circuit connection.

The inspectors reviewed the outstanding maintenance activities which

directly affect the control room and control room activities.

The number

of outstanding maintenance activities is increasing and is very visible by

the tags and out-of-calibration stickers placed within the control room

horseshoa operating. area.

Both the Maintenance and Operations

Superintendents are aware that the number of outstanding maintenance items

is increasing. 16th' managers maintain that the large number of items is

an . indication of strong support by maintenance of the operators and an

attempt to maximize maintenance efforts.

The inspector determined that

the number and nature of outstanding maintenance items is presently not

affecting the safe operation of the plant.

One VID 327,328/89-15-02, and no deviations were identified in the area of

Maintenance.

5.

Management Activities in Support of Plant Operations

TVA management activities were reviewed on a daily basis by the NRC

inspectors.

Resident Inspectors observed that planning, scheduling, work

control and other management meetings were effective in controlling plant

activities.

First line supervisors appear to be knowledgeable and

involved in the day-to-day activities of the plant.

First line supervisor

involvement in the field has been observed and with the exception of the

RM activity described above appeared to be adequate.

Management response

to those plant activities and events that occurred during this inspection

period appeared timely and effective.

Examples of this management action

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were the responses - to the two personne1' contaminations, and a failed

RPI-E-13 on Unit 1.

One weakness appeared to.be the first and middle line

management being unable to explain the increase in Unit 1 dose equivalent

Iodine over a period of approximately eight days.

This issue is still

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under. consideration;with Plant Management involved in the resolution of.

the. problem.

The management activities which are discussed'in paragraph 9

and cited as VIO 327, 328/89-15-04 occurred during' previous inspection

periods.

6.

Site Quality Assurance Activities in Support of Operations-

During the7first part of this inspection period, the inspector discussed

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several recent issues involving the implementation of. SQEP-65, External

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Interface Control, with - the Site QA Manager.

The inspector expressed

concern that the SQEP-65 process could be used to bypass established

review programs.

.This process is used by DNE to transmit technical

information to the plant as a response to plant initiated questions.

The

site QA Manager established three audits of the SQEP-65, P-QIR' process.

The QA monitoring, documented in the reports listed below, determined that

. the P-QIRs were being - used as design' output. documents.

This allowed

calculations to be performed and utilized by the plant without a USQD as

required by 10 CFR 50.59 and without a 'PORC review.

A 100% review was

conducted and the problems that were identified were all associated with

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.non CSSC equipment.

The resolution of the problem was an agreement

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between site QA and the site Manager of DNE to discontinue'the implementa-

tion of.the SQEP-65 process and affects corrective actions through one PRD

and two CAQRs.

Monitoring Performed

QSQ-M-89-558, SQEP 65 Nuclear Sample

Q5Q-M-89-556, SOEP-55 Mechanical Sample

Q5Q-M-89-557, SQEP-65 Electrical Sample

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Corrective Actions

PRD SQQ 890299P

CAQR SQQ 890297

CAQR SQQ 890303

The licensee's corrective actions appear to be adequate..

The inspector discussed QA involvement in plant activities with the site

QA Manager.

The site QA Manager stated that he is continuing to operate

under the previously established written agreement between the previous

site QA Manager and the Plant Manager.

This agreement established QA

being notified of plant events and participation in the line investigation

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of plant issues.

7.

NRC Inspector Follow-up Items, Unresolved Items, Violations (92701, 92702)

(Closed) URI 327,328/89-12-02, BIT Recirculation.

This item is resolved

and is1 now being tracked under VI0s 327,328/89-15-04,05,06 which is

discussed in paragraph 9.b. of this report.

This item is closed.

(0 pen) URI 50-327,328/89-12-01, Licensed Power Indication.

Inspection Report 327,328/89-12 identified several questions concerning

the control of licensed thermal power.

Sequoyah operating licenses for

both units limit reactor thermal power to 3411 MWth.

The following four

evaluations were suggested:

a.

An evaluation to determine which of the two power indications should

be used to comply with the license condition which limits thermal

power to 3411 MWth.

b.

An evaluation of a specific eight hour period where thermal power, as

indicated by the U0908 computer point, indicated an eight hour

average in excess of 3411 MWth.

c.

An evaluation of the same eight hour period for compliance with axial

flux difference TS requirements stated in TS 3.2.1.

d.

An evaluation of a specific period of 52 minutes where thermal power

exceeded 100.75%.

1

This discussion addressed items a, b, and d above.

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On April 19, 1989, at approximately 9:50 a.m. , the inspector noted that

{

the Unit 1 power range nuclear instruments were reading approximately 101%

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reactor thermal power.

The Unit Operator informed the inspector that they

had an increase in the grid power factor that had caused an increase in

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turbine power.

The governor valve limiters installed on the Sequoyan

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turbine generators are not used by the utility to mitigate these power

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swings.

)

At this time the reactor power as indicated en the plant computer (P-250)

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data point U1118 (instantaneous reactor thermal power) was 3415.6 MWth.

l

The operator explained that he had been reducing power over several

'

minutes to reduce the average power over his 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> shift (i.e. , by

I

approximately 3:00 p.m.) to less than licensed power of 3411 MWth.

The

j

inspector discussed with the operator that both his instantaneous and his

i

8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> average power were above the licensed limit.

The inspector

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questioned whether correcting the condition over a 5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> period was

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adequate. At 10:00 a.m. the P-250 point U0908, showing the 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> average

of U1118, was reading 341t 0 MWth.

Tte operator took action to reduce

power, and by 10:00 a.m. the one hour aserage reactor power shown on P-250

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point U0018 was indicating less than licensed power, and by 12:01 p.m. the

8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> average power was down to 3408.6 MWth.

The operators explained that they were operating under TS interpretation

.119 which referenced guidance NRC has issued in this area.

The licensee

inferred from the ' guidance that the- average ;,ower level over any

eight hour shift- should not exceed the full steady-state licensed power

level and that it was acceptable to briefly exceed the licensed power

level by as much as 2% for as long as 15 minutes', but in no case should

that 102% power level be exceeded.

The 11cea:d s TS interpretation

referenced an August 22, 1980 internal NRC memorandum titled Discussion of

" Licensed Power Level", which was written to give inspectors. guidance and

address a uniform basis for enforcement.

The menorandum clearly states

that this guidance is not an NRC-wide agreement. Oiscussion with the NRR

technical staff indicates that the memo assumed trat the licensee was

controlling their power excursion and taking an active approach to

reducing the power back below 100% should they exceed that valce.

The inspector noted a period, beginning at 6:33 a.m. on April 19, 1989,

during which reactor power went above 3411 MWth, proceeded to 3436.1 MWth .

(approximately -100.75%), and returned to 3411 MWth at 7:37 a.m.

During

this time there was no apparent operator action to reduce reactor power.

Op..rators apparently waited for the grid power factors to drive thermal

power back down.

The inspector discussed this issue with the plant manager.

He committed

to maintain the plant below 100% reactor power as indicated on the nuclear

instruments until these issues can be reviewed and an acceptable

!

alternative operating method can be determined, reviewed and implemented.

The NRC recognizes that the licensee desires to operate at rated thermal

!

power on a continuous basis.

The NRC also recognizes that power tran-

sients will occur which cause thermal power to change without operator

actions.

The NRC expects that the licensee will take prompt corrective

action to reduce thermal power to the license limit when it is discovered

)

to be above the license limit.

Issuance of a TS interpretation to

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operators which infers the acceptability of operating above the licensed

!

power limit in other than a transient condition is of concern to the NRC.

]

In addition, once thermal power is discovered above the license limit, the

failure by the TS interpretation to require immediate operator action to

reduce power to the license limit is also of concern.

The inspectors were

unable to find any procedures or other guidance provided to operators

which address the proper actions to take for power transients during

steady state operation at Rated Thermal Power.

This is considered a

violation of TS 6.81 for failure to establish, implement, and maintain

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written procedures and is identified as VIO 327, 328/89-15-03.

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During the review of this issue the inspector also reviewed the following

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documents and found them to be acceptable:

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RTI-8

Statepoint- (sic)- Data Collection and Thermal Power

Measurement

51-78-

. Power. ' Range Neutron Flux Channel Calibration by Heat

Balance Comparison.

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TI-2

Calorimetric Calculation,

The review of these procedures also showed that the _ calibration of the

nuclear instruments and the P-250 data point U1118 was acceptable and

shows adequate. reliability of these indications.

Items a, b, and 'd are administratively closed and will be -addressed

further under the review of the violation.

Item c above will. remain open

and continue to be tracked as unresolved item URI 327,328/89-12-01.

8.

Licensee Event Report Followup (92700)

UNIT 2

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(Closed) LER.327/88-043, Revision 1, Inadequate Fire Watch Patrol Resulted

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In A Noncompliance With Technical Specification 3.7.12.

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On September 30, 1988, the inspector brought to the attention of TVA

management a concern involving the adequacy of the SQN fire watch patrols

which was-later cited as VIO 327,328/88-46-01, Failure to Perform Adequate

Fire Watches.

The fire watch patrols are required by action statement (a) to Limiting

Condition for Operation (LCO) 3.7.12 as a compensatory measure for several

non-functional fire barriers in the Auxiliary and Control buildings. This

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action statement requires verification of the operability of area fire

detectors on at least one side of the breached penetration and the

establishment of an hourly fire watch patrol whenever a fire barrier

penetration has been determined to be non-functional.

TVA management

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initiated an investigation which concluded that the individual who was

assigned to the fire watch route "A" had not made one of the required

hourly patrols because he was not in the protected area for the 10:00 a.n.

EDT to 11:00 a.m.

EDT hourly fire watch on September 28.

The other

individual who was assigned to fire watch route "B" had made all required

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hourly patrols, but his route durations appeared inadequate to survey his

assigned fire watch route properly.

No malicious intent was found and

this event is considered to be an isolated occurrence.

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TVA admitted that the reason for these occurrences was that management had

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failed to provide clear and concise guidance on how fire watch individuals

must perform their duties.

Further, management did not provide for

periodic checks of fire watch patrols to ensure adequate implementation of

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the fire watch program.

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To correct the situation TVA developed and implemented the following

steps:

a.

QA personnel will continue periodic monitoring activities.

b.

Fire Protection Section supervisor has designated specific

individuals to perform periodic monitoring activities.

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c.

Red hardhats were provided to fire watch personnel for unique

identification.

d.

Fire Operations Section Instruction Letter (FDSIL)-10 has been

revised to enhance the fire watch program.

The new revision includes

the following:

Added door numbers to the fire watch checkoff sheets.

Fire watch personnel can not swap routes without prior approval

from the Fire Operations shift supervisor.

Fire watch personnel are required to wear the uniquely

identified hardhats.

Fire watch personnel are required to carry the section

instruction letter and route sheets with them while walking

their routes.

Fire watch personnel are required to follow the route identified

on the route sheet unless not allowed by plant conditions.

Fire watch ruutes were revised to ensure more effective use of

fire watch personnel and reduce confusion of the routes,

e.

Formal training to fire watch personnel has been provided on the

revised section instruction letter which emphasized the importance of

accurate logs and adherence to hourly fire watch routes to fulfill TS

requirements.

!

f.

A veroal warning has been issued to all fire watch personnel stating

that if fire watch personnel fail to perform their duties,

appropriate disciplinary actions will be taken up tu and including

termination.

g.

Follow up training for fire personnel througn observation of

performance will be provided by fire protection engineers to ensure

continued compliance with fire waten requirements as outlined in the

FDSIL-10.

This action will be completed by December 31, 1988.

h.

TVA will evaluate the feasibility of watchman stations for monitoring

fire watch activities by December 31, 1988.

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The inspector verified that above corrective actions had been implemented

and performed a review of additional fire watch activities.

This review

included monitoring of fire watch routes, reviewing and observing watchman

station logs and reviewing VAACS printouts of the fire watches' progress

through the plant.

Fire watch coverage now appears to be adequate.

LER 327/8P-043 is closed.

9.

Event Follow-up (93702)

a.

Sequoyah Unit I and Unit 2 were placed in an unanalyzed condition

during several performances of RHR systelr surveillance.

This

condition was caused when improperly prepared revisions to 51-128.1,

RHR Pump and Piping Venting,51-128.2, Residual Heat Removal Pump

1A-A,51-128.3, Residual Heat Removal Pump 1B-B, SI-128.4, Residual

Heat Removal Pump 2A-A, and SI-128.5, Residual Heat Removal Pump

2B-B, were used to perform system surveillance

on twenty-six

separate occasions from March 22, 1988 through April 20, 1989. The

revised procedures caused RHR system lineups to be changed to

configurations which effectively rendered both trains of RHR

inoperable for short periods of time.

This condition is described in

LER 89-011; Root Cause Investigation Report, SQA 186, Root Cause

Assessment Adverse Action / Condition, dated May 2,1989; and CAQR

SQP89039. Placing both trains outside the design basis and in an

unanalyzed condition should have been identified in the licensee's

procedure change reviews as an Unreviewed Safety Question.

None of

the licensee's investigation reports concluded that an Unreviewed

Safety Question existed as defined by 10 CFR 50.59.

Thr: changes to the surveillance instructions were made in May 1987

frr SI 128.1 and December 1988 for 51-128.2, 128.3, 128.4, and 128.5.

s

Une review process for 51-128.1 included complction of an Unreviewed

Safety Question Determination worksheet, SQA 119, Evaluation of

Changes, Tests, or Experiments, and a qualified informal PORC review

documentation.

These independent reviews concluded that no unre-

viewed safety question, reduction of safety margin, or possibility of

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increasing the chances for an accident or malfunction of a different

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type than those previously analyzed would result from the issuance or

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use of the instruction.

During accident conditions, the RHR pumps provide automatic low-head

safety injection flow to the RCS following a safety injection signal

(SIS) and also provide suction flow to the centrifugal charging pumps

(CCPs), and the safety injection pumps after swapover to the con-

tainment sump from the refueling water storage tank (RWST).

Specif-

ically, at least one train of low-head safety injection flow is

assumed to be delivered to all four RCS cold legs.

During a LOCA,

three of these flow paths deliver water to the RCS while the fourth

is assumed to be spilling from the faulted leg.

Any configuration

which would result in less than three cold leg injection paths is

currently outside the design basis of Sequoyah Nuclear Plant.

Also,

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the' design basis of the plant does not include having the hot leg

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injection path open via FCV-63-172 while the cold leg paths are also

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open. . This condition would reduce the estimated flow to the cold

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legs to less than that 7.isumed in the accident analysis.51-128.1, originally issued in May 1967, has a step which momentarily

opens FCV-63-172 to facilitate RHR system venting. Opening the 63-172

valve places the RHR system in a configuration that is outside the

design basis if perforried during Modes 1, 2 or 3, when the RHR system

is required to be operaDie.

The licensee's investigations revealed

l

24 separate instances when the 63-172 v.31ve had been opered while the

l

cold legs ' were also aligned during modes when the RHR system was

required to be operable.

SI-128.2,128.3,128.4, and 128.5 were revised in December 1988 to

include steps to momentarily shut FCV-63-93, FCV-63-94, (cold leg

isolation valves), and to shut FCV-74-33 and FCV-74-35, (P.MR

cross-connect isolation valves) to facilitate RHR pump ve: sting.

Shutting either the 63-93 or the 63-94 valve will isolkte two

separate cold legs, putting the plant into an unanalyzed condition.

Closing either 74-33 or 73-35 isolates the cross-connect, which,

considering the single failure of either pump, would invalidate the

assumption that either pump could supply all four cold legs during an

accident.

TVA investigation revealed. that the instruction had been

used on two separate occasions, since the incorporation of the change

in December 1988, while the plant was in Modes 1, 2, or 3.

The

instances occurred on Unit 1 on February 24, 1989, and March 1, 1989.

Of the 26 performances with these surveillance since their modifi-

cation, none placed the RHR systems in an inoperable condition for

periods of time in excess of the time limitations contained in the

action statements of TS 3.b.2 or of TS 3.0.3.

However, operators

were unaware that thest: action statements were applicable because of

the inadequate surveillance.

The SQA-119 screening review form completed to document the

December 1988 revisions to the SI-128.2 through 128.5 instructions

determined that the change consisted only of a format change and the

testing methods remained the same.

As such, the licensee determined

that no further evaluation was necessary and a safety evaluation of

the change was not performed.

This conclusion was concurred in by

the independent qualified reviewers as documented on the change

control document attached to the instruction change package.

The

processes used to evaluate the safety, adequacy, deportability, and

applicability of the 10 CFR 50.59 rule in general failed to

determine, for SI-128.1 through 128.5, that an unreviewed safety

question existed.

This is considered to be a violation 10 CFR 50.59

for processing a change that involved an unreviewed safety question

and is identified as VIO 327,328/89-15-04, example a.

The licensee discovered the problems with the procedures when the

responsible supervisor was informed by the SOS on duty that he

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believed the surveillance instructions were unacceptable. based on his

determination that the hot leg isolation valve could not be open at

?

the same time as the cold leg' isolation valves, and that shutting the

cross-connect isolation valves and/or the pump discharge isolations

could cause both trains to be inoperable.

A scheduled performance of

SI-128.1 was stopped by the Operations staff on April 10.

The

responsible section, Mechanical Test, reviewed the procedure and the

file for that procedure and discovered that NRC IE Information Notice 87-01, described a condition that could render both trains of RHR

inoperable.

The described situation involved the shutting of the RHR

~

cross-connect valves and/or the pump discharge isolation valves.

The

notice warned recipients that this configuration would cause both

trains to be inoperable.

When the responsible mechanical test

engineer realized that the procedures involving pump venting,

SI-128.2 through 51-128.5, isolated two of the four cold legs,

Condition Adverse to Quality (CAQR) report SQP890239 was initiated.

The C.AQR concluded that TS LCO 3.0.3 should have been entered during

the performances of RHR venting procedures.

The NRC was notified on

April 13 that the past performances of the procedures had placed the

plant in TS 3.0.3, and in a configuration outside the design' basis.

The responsible Mechanical Test engineer believed that he was able to

control all performance

of SI-128.1 through SI-128.5 because he was

responsible for issuing the performance packages.

He did not,

therefore, make immediate corrections to the procedures.

On April

17, a performance package of SI-128.1 war prepared by the Planning

and Scheduling Section and sent to the ec' trol room.

SI-128.1 was

performed on April 20, with the attendant errors still in the

procedure.

This instance was discovered when the Mechanical Test

engineer was attempting to locate the last controlled copy of the

performance package and called the control room.

He was then told

that SI-128.1 had been performed that morning.

The performance of

SI-128.1 after it was known to be inadequate constitutes a failure to

maintain adequate written procedures as required by TS 6.8.1 and is

identified as VIO 327,328/89-15-05, example a.

b.

Unit 2 entered Mode 3 at 4:30 p.m. on April 6,1989.

At 4:55 p.m.,

the BIT to BAT recirculation was stapped and the BIT recirculation

valves .ere shut to stop back leakage from the RCS to the BIT.

This

backleakage was causing dilution of the BIT and the BAT.

The inspector questioned this procedue b9cause the recirculation

path provides the only method of ensuring tcat the proper BIT volume

is maintained.

Assurance that the EIT is full, (900 gallons), is

provided by the absence of a low flow alarm ra the recirculation path

out of the BIT.

TS 3.5.4.1 require!, the BIl to be nperable in Mode 3

with a minimum volume of 900 gallons.

TN action statement for this

requirement is to restore the BIT to ac sperable condition within one

hour or be in Hot Standby and borated to the appropriate shutdown

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margin within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.

,

The licensee's position was that even though no on-line verification

..

of BIT volume exists when the BIT is off recirculation, there is no

reason to suspect that the volume is being reduced.

Further, the

surveillance requirement = is to verify that proper volume is present

every 7 ' days.

The licensee therefore concluded that taking the BIT

off recirculation is allowed ,as long as the surveillance to verify

volume is - performed within 7 days.

This position was based.on an

existing licensee TS interpretation.

After the Resident Inspector

,

notified the plant staf f of their concern regarding this issue, the

BIT was placed back on recirculation at 10:02 a.m. on' April'10,1989.

Plant Management agreed that recirculation will be maintained until

the issue would be resolved.

The question of whether the BIT was inoperable was reviewed by the

NRC technical staff at the request of the Resident . Inspector and the

NRC Project Manager.

The FSAR states in part that to prevent cold

spots and stratification within the tank during normal operation,_the

contents of the boron injection tank are continuously recirculated.

A sparger is provided on the . inlet to the tank which, coupled with'

recirculation, will prevent channeling and ensures homogeneity of the

. boric acid solution.

Any large scale leakage is detected by a flow

indicator and alarm located on the discharge line.

The staff

concluded that the BIT must remain on recirculation .to ensure that

proper volume is maintained and to prevent possible boron crystal 11-

zation inside the BIT.

The staff concluded that the BIT was inoper-

able during the time the BIT. was off recirculation and that this

change in mode of operation of the BIT involved an unreviewed safety

question.

Processing a change to the facility or procedures which

are described in the FSAR without performing a review pursuant to

10 CFR 50.59 is considered to be a violation and is identified as

VIO 327, 328/89-15-04, example b.

The inspector questioned the licensee's determination that taking the

BIT off recirculation did not require entry into the LCO.

In

addition, the inspector questioned whether a proper review pursuant

to 10 CFR 50.59 had been completed.

The normal recirculation lineup

'

is specified in 501 62.1, Chemical and Volume Control System.

AI-4,

Preparation, Review, Approval and use of Site Procedures /Instruc-

tions, establishes the method and controls required by TS for

revision and use of site procedures.

AI-58, Maintaining Cognizance

I

of Operation Status Control, implements the review and approval

I

requirements of TS when handwritten instructions are used where an

approved procedure does not exist.

The change in the BIT system

lineup was required to be controlled by approved procedures.

Neither

of these methods were used.

Changing the BIT lineup without an

approved procedure is considered to be a violation of TS 6.8.1 for

failure to follow procedures and is identified as VIO 327, 328/

89-15-05, example b.

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AI-58, Maintaining Cognizance of Operation Status Control, Appendix

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governs the production of handwritten instructions when an

approved S0I procedure does not exist. It requires only that the SOS

review and approve the procedure, and that an Independent Qualified

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Reviewer, whict may include the STA or other shift personnel who are

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certified as Qualified Reviewers, also review and sign the change

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form.

This process was not performed until April 8,1989, two days

I

after the configuration change had been made and challenged by the

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inspector.

The AI-58, Appendix E worksheet determined that there was

)

no unreviewed safety question, and that no safety issues were

'

involved.

l

During the period.that the BIT was not on recirculation with the BAT,

the licensee attempted to meet Surveillance Requirement 4.5.4.1 by

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performing Surveillance Instruction 3, Daily, Weekly and Monthly

Logs.

51-3 verifies that the BIT has an adequate borated water

volume while the BIT is in recirculation with the BAT.

SI-3

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accomplishes this in step 3.1.4, by verifying that greater than 900

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gallons volume exists in the BIT by the absence of the low recir-

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culation flow alarm FIS-63-43.

The validity of using the absence of

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the alarm to- determine BIT volume as required by surveillance

requirement 4.5.4.1 is based on the BIT being in recirculation.

The

FSAR states that the purpose of this alarm is to detect any large

scale leakage within the BIT.

The alarm will only perform this

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function if the BIT is in recirculation.

During the period that the

BIT was not in recirculation, approximately 100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br />, the low

!

recirculation flow alarm was actuated.

Also, because of the

previously identified problems with valve leakage, performing SI-3

after the reestablishment of recirculation only ensures that the

volume was present during the period of recirculation and does not

ensure that the volume was or will be correct during the period in

i

which recirculation was or will be stopped.

Therefore SI-3 did not

adequately implement surveillance requirement 4.5.4.1 to determine

the operability of the BIT during periods when recirculation was

stopped, and as such did not prove operability of the BIT during the

absence of recirculation.

This is a violation of TS 3.5.4.1, BIT

Operability, and is identified as VIO 327,328/89-15-06, example a.

c.

At 6:00 a.m. May 5,1989, the SOS on duty noticed that the Unit 2

Intermediate Range (IR) High Flux trip bistables were not indicating

!

tripped while the reactor plant power was at 73%.

The setpoint of

the bistables is approximately 25% reactor power as indicated on the

power range monitors.

Further observation indicated that the IR

channels were low compared to the same instrument readings on Unit 1.

The IR channels, N-35 and N-36 were declared inoperable and the LC0

for TS 3.2.1 was entered.

LCO 3.2.1 allows continued operation with

both IR channels inoperable if power is above 10%.

Licensee review

of this event revealed that during the recent outage, the storage

baskets for the Source and Intermediate Range detectors had been

pulled back from their normal position against the reactor vessel

wall to a maintenance position approximately 21 inches from the

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normal position.

This configuration changed the amount.of leakage

neutron flux at the detectors and caused them to indicate lower than

actual power levels.

This event is described in LER 50-328/89-006.

The detector arrangement has Source Range (SR) channel N-31 and IR

channel N-35 in one basket and SR N-32 and IR N-36 in the other-

basket.

The storage baskets are located 180 degrees apart outside

the vessel wall.

The baskets and detectors had been retracted on

March 19 and March 20 for N-31/N-35 and N-32/N-36 respectively, while

Unit 2 was shutdown for refueling.

This change was performed ir. ar.

attempt to reduce noise spiking that had occurred intermittently on

,

the SR channels.

Moving the detectors back allowed the detector

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cables to straigSten out slightly and reduce crimping and chafing

that was postulated to be causing the spiking.

In addition to the

position change, plant personnel removed ground straps which

connected the SR and IR detectors in each basket.

This work was done

under WP 1192-01 and controlled by IMI-92-SRPC.

IMI-92-SRPC, which

controls detector positioning, was revised by ICF 98-0314 after the

detectors had been withdrawn to the maintenance position.

The major

change incorporated by the ICF was to delete the steps returning the

baskets to the normal position.

This position change was recommended

by Westinghouse in a letter dated February 28, 1989 to optimize

detector output (reduce noise on the channel).

The ICF and the accompanying screening review did not identify that

the detector movement would require readjustment or recalibration of

the source range channels.

Further, the ICF and the screening review

did not mention that the IR channels would also be affected.

A

screening review is required by SQA 119, Evaluation of Changes,

Tests, or Experiments,. to evaluate changes and insure that safety

evaluations are performed when the changes could have an affect on

,

nuclear safety or create an unreviewed safety question.

The

!

instrument technician who prepared the ICF and the accompanying

screening review concluded that changing the position of the

l

detectors did not involve a change in the facility as described in

the FSAR.

The screening review form question for this item, Question

i

l

  1. 1, is marked "NA".

Question #2 is stated as: "Does the proposed

!

i

change involve new procedures or instructions or revisions to

!

l

instructions or procedures that would make descriptions in the SAR or

l

plant TS invalid and which could impact nuclear safety ?".

The

i

preparer marked this answer box "Yes".

The screening review form

states that marking "Yes" requires a safety evaluation to be

performed.

Despite this requirement to initiate and perform a safety

evaluation, neither the preparer nor reviewers of the ICF and its

accompanying screening review recognized the requirement when

reviewing the screening review form and therefore did not perform a

safety evaluation.

SQA 119, Revision 13, controls the screening

review and independent review process.

AI-43 controls the Indepen-

dent Qualified Reviewer process that requires independent review of

the ICF and the accompanying screening review.

Failure to follow the

requirements of SQA-119 and AI-43 by not ensuring that a safety

- _ - _ _

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.

20

s

evaluation accompanied the screening review form as required is

considered a violation of the requirements of TS 6.8.1 for failure to-

follow written procedures and is identified as VIO 327,328/89-15-05,

example c.

In the space for " Justification" on the screening review form, the

preparer concluded that "... Rep;sitioning the detectors will not -

adversely affect operation of the detectors in any way...".

The

change to the position of the intermediate range detectors was

sufficient to cause the IR High Flux trip bistables to be inoperdie

which was discovered after the unit was restarted.

The screening

review form was reviewed and approved by an Instrument Engineer.

This review was inadequate because three separate errors made by the

preparer were not identified and corrected.

The' question marked

"Yes" which required a cafety evaluation was not complied with, the

effect of moving the baskets did not address the impact on the IR

channels, and the ' conclusion that the detectors would not be

adversely affected was not correct.

In addition, the completed ICF

and the accompanying screening review form were reviewed and

concurred with by three separate independent qualified reviewers

including personnel from Systems Engineering and QA.

None of these

independent reviews recognized any of the three errors associated

with the ICF and the screening review.

None of these separate

reviews questioned the operability of the source range detectors and

associated reactor trips, the involvement of the IR detectors and

their associated reactor trips, the missing safety evaluation, or the

impact of moving detectors away from their source.

The change in the

position of the detectors resulted in both IR high' flux bistables

being inoperable.

The review performed pursuant to 10 CFR 50.59 was

not adequate in that it did not identify the effect the procedure

change would have on the nuclear instrumentation or reactor trip

system and is identified as VIO 327,328/89-15-04, example c.

The maintenance and modifications performed on the instruments were

performed while the plant was in Mode 5, Cold Shddown.

Operations

personnel (the duty Shift Operating Supervisor, 503). are notified of

work in progress under the requirements of the Vo.k Package (WP)

program.

Operations was therefore aware that the detectors were to

be withdrawn, but assumed that following the ground strap removal the

detectors would be returned to their original position.

The decision

to leave the detector baskets withdrawn was made as a modification to

the original WP.

The change to the original scope of the WP was not

processed as a major change, and the ICF was not marked as requiring

notification of the SOS for a configuration change even though the SR

I

detectors, which the operators were using to monitor the core, were

)

directly affected.

The fact that this change could be processed

without the notification or the knowledge of the licensed control

room operating staff is of concern.

In addition, NRC inspectors had

suggested during the closecut of Unit 2 containment during the early

'

1988 restart that the required position of the detector baskets be

added to the containment closecut checklist.

Had that been done, an

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21

additional check on proper detector location may have helped keep the

operators informed of what was happening with the equipment they were

using to monitor the core.

Subsequent to the maintenance and modifications performed on the

detectors, Unit 2 was taken from Cold Shutdown (Mode 5) to Power

Operation (Mode 1).

Surveillance

performed on the SR channels

effectively adjusted them which eliminated any effects of the

location change.

The SR channels were, therefore, operable during

the UnN 2 Mode changes associated with the startup.

Comparable

surveillance do not adjust the IR channels until after the plant

reaches 100% power, at which time the IR High Flux Trip setpoint is

checked and adjusted to coincide with a setpoint equivalent to 25% as

determined by the Power Range excore detectors.

The trip setpoint

for the bistable was set prior to plant startup at a current value

calculated to correspond with 25% power.

As a result, mode changes

were made with both IR high flux bistables inoperable. This situ-

ation wa; the direct result of a failure to control configuration

of systems and equipment during the maintenance and modification

process.

Due to three trips which occurred while low in power, a

total of 4 separate startups and the attendant mode changes were made

with the IR channels inoperable.

TS 3.3.1.1 requires the IR channels

to be OPFDABLE in Modes 1, 2, and when the reactor trip breakers are

closed with tuc1 in the reactor vessel.

TS 3.0.4 prohibits entry

into an operational mode unless the conditions for the LC0 are met

without reliance on provisions contained in the ACTION requirements.

Contrary to this requirement, mode changes were made on four separate

occasions during the time period from April 13, 1989 to April 25,

1989 with both IR high flux bistables inoperable.

This is a viola-

tion of TS 3.3.1.1 and TS 3.0.4 and is designated VIO 327,328/

89-15-06, example b.

After the licensee staff realized that the IR channels were

inoperable, the appropriate LCOs were entered, the IR High Flux

reactor tt ip was adjusted to a setpoint of 25% power range equiva-

lent, and safety evaluations were performed for three areas.

The

first SE was completed on May 6, 1989, and provided justification for

continued operation with the SR and IR detectors in their withdrawn

position.

The second safety evaluation was completed on May 7, and

provided assurances that the IR channels could be adjusted to reflect

the change in relative position.

The third safety evaluation was

complete on May 8, and determined the impact or contribution of the

!

condition on the previously discussed startups.

The safety evalua-

tion determined that the plant was safe in its present configuration,

that the intended adjustment could be made to restore the IR channels

to Operable status, and that having the IR channels inoperable did

not cause unsafe conditions to exist during the plant startups.

{

1

Instances of improper changes to plant systems and components and/or

control processes have occurred recently at Sequoyah without accompanying

,

safety evaluations.

These include the BIT / BAT recirculation issue

described in IR 327,328/89-12-02 and this report, the RHR system lineup

change that resulted in the plant being in an unanalyzed condition as

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22

described in LER 50-327/89-011 and this report, the IR and the SR

relocation issue which affected the high neutron flux trip as described

in

this

report,

isolation

of

a

pressurizer

PORV with reliance on a TS interpretation rather than a safety evaluation

as described in URI 327,328/89-12-02, and operation with continued high

voltage on the 6.9 kv shutdown boards described in IR 327,328/89-14.

g

Apparent weaknesses in the safety evaluation program, will be addressed as

l

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URI 327, 328/89-15-07, and will include:

(1) the licensee method of implementing 10 CFR 50.59

(2) independent qualified reviewer program

(3) the experience review program feedback to the safety evaluation

process

10.

Exit Interview (30703)

The inspection scope and findings were summarized on June 5 and on June 9,

1989, with those persons indicated in paragraph 1.

The Senior Resident

Inspector described the areas inspected and discussed in detail the

inspection findings listed below.

The licensee acknowledged the

inspection findings and did not identify as proprietary any of the'

material reviewed by the inspectors during the inspection.

Inspection Findings:

This routine monthly inspection involved inspection effort by the Resident

Inspectors in the area of operational safety verification including

control room observations, operations performance, system lineups,

radiation protection, safeguards, and housekeeping inspections.

Other

areas inspected included maintenance observations, surveillance testing

observations, review of previous inspection findings, follow-up of events,

review of licensee identified items, and review of inspector follow-up

items.

Results:

The areas of Operations, Maintenance, and Surveillance were adequate and

fully capable to support current plant operations.

The

observed

activities of the control room operators were professional and well

i

executed.

Significant weaknesses were identified in the licensee's

implementation of the 10 CFR 50.59 safety evaluation processes, the

licensee's TS interpretation process and the independent qualified review

process.

(Closed) NCV 327, 328/89-15-01, " Licensee Identified Minor Contamination

of Two Individuals under RWP 89-00012"

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>

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1

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23

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(0 pen)

VIO 327, 328/89-15-02, " Configuration of RM 90-404 Detector

Cable was not controlled"

(Closed) URI 327, 328/89-12-02, " Recirculation of BIT"

(0 pen)

VIO 327, 328/89-15-03, " Reactor Operation above 3411 MWth"

(Closed) LER 327/88-043, Revision 1, " Inadequate Fire Watch Patrol

Resulted in a Non-compliance with TS 3.7 12"

(0 pen)

VIO 327, 328/89-15-04, "Three Examples of Inadequate Unreviewed

Safety Question Determinations per 10 CFR 50.59"

l

(0 pen)

VIO 327, 328/89-15-05, "Three examples of Failure to Establish

and Implement Procedures per TS 6.8.1"

(0 pen)

VIO 327, 328/89-15-06, "Two Examples of Failure to Comply with

TS LC0 Requirements"

(0 pen)

URI 327, 328/89-15-07, " Apparent Weakness in the Safety

Evaluation Program"

11.

List of Acronyms and Initialisms

ABGTS-

Auxiliary Building Gas Treatment System

ABI -

Auxiliary Building Isolation

ABSCE-

Auxiliary Building Secondary Containment Enclosure

AFW -

Auxiliary Feedwater

Aardnistrative Instruction

AI

-

A01 -

Abnormal Operating Instruction

AVO

Auxiliary Unit Operator

-

AS05 -

Assistant Shif t Operating Supervisor

ASTM -

American Society of Testing and Materials

,

'

BIT -

Boron Injection Tank

BFN -

Browns Ferry Nuclear Plant

C&A

Control and Auxiliary Buildings

-

CAQR -

Conditions Adverse to Quality Report

CCS

Component Cooling Water System

-

CCP

Centrifugal Charging Pump

-

CCTS -

Corporate Commitment Tracking System

CFR -

Code of ' Federal Regulations

COPS -

Cold Overpressure Protection System

CPU -

Central Processing Unit

CS

-

Containment Spray

CSSC -

Critical Structures, Systems and Components

CVCS -

Chemical and Volume Control System

CVI

Containment Ventilation Isolation

-

DC

Direct Current

-

DCN

Design Change Notice

-

1

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Diesel Generator

j

.DG

-

DNE -

Division of Nuclear Engineering

i

Engineering Change Notice

f

ECN

-

ECCS -

Emergency Core Cooling System

'

EDG

Emergency Diesel Generator

1

-

Emergency Instructions

)

EI

-

ENS

Emergency Notification System

-

<

E0P

Emergency Operating Procedure

-

EO

Emergency Operating Instruction

-

ERCW -

Essential Raw Cooling Water

l

ESF

Engineered Safety Feature

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FCV -

Flow Control Valve

l

FSAR -

Final Safety Analysis Report

GDC

General Design Criteria

-

GOI -

General Operating Instruction

GL

Generic Letter

-

HVAC -

Heating Ventilation and Air Conditioning

l-

HIC

Hand-operated Indicating Controller

-

' H0

Hold Order

-

HP

-

Health Physics

ICF

Instruction Change Form

-

IDI

Independent Design Inspection

IFI

Inspector Followup Item

-

IM

Instrument Maintenance

-

IMI

Instrument Maintenance Instruction

-

IN

NRC Information Notice

-

I/O -

Input Output

IR

Inspection Report

-

KVA

Kilovolt-Amp

-

KW

Kilowatt

-

KV

-

Kilovolt

LER

Licensee Event Report

-

LCO

Limiting Condition for Operation

-

Licensee Identified Violation

LIV

-

LOCA -

Loss of Coolant Accident

MCR

Main Contrni Room

-

MI

Maintenance Instruction

-

MR

-

Maintenance Report

MSIV -

Main Steam Isolation Valve

NB

NRC Bulletin

-

NOV -

Notice of Violation

NQAM -

Nuclear Quality Assurance Manual

NRC

Nuclear Regulatory Commission

-

OSLA -

Operations Section Letter - Administrative

OSLT -

Operations Section Letter - Training

OSP

Office of Special Projects

-

PLS

Precautions, Limitations, and Setpoints

PM

-

Preventive Maintenance

NCV -

Non-cited Violation

PPM

Parts Per Million

-

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-

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25

l

[

PMT

Post Modification Test

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PORC -

Plant Operations Review Committee

l

P0RS -

Plant Operation Review Staff

P-QIR

Plant Quality Information Requested / Released

-

PRO

Potentially Reportable Occurrence

l

,

-

QA

Quality Assurance

t

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l

QC

Quality Control

-

i

RCDT -

Reactor Coolant Drain Tank

RCP

Reactor Coolant Pump

-

RCS -

Reactor Coolant System

,

l

RG

-

Regulatory Guide

RHR -

Residual Heat Removal

RM

-

Radiation Monitor

R0

-

Reactor Operator

RPI

Rod Position Indication

-

RPM -

Revolutions Per Minute

RTD -

Resistivity Temperature Device Detector

RWP

Radiation Work Permit

-

RWST -

Refueling Water Storage Tank

SER

Safety Evaluation Report

-

SG

Steam Generator

-

SI

Surveillance Instruction

-

SMI

Special Maintenance Instruction

-

50I -

System Operating Instructions

SOS

Shift Operating Supervisor

-

SQM -

Sequoyah Standard Practice Maintenance

SQEP -

Sequoyah Engineering Projects

SQRT -

Seismic Qualification Review Team

SR

-

Surveillance Requirements

SR0

Senior Reactor Operator

-

550MI-

Safety Systems Outage Modification Inspection

SSQE -

Safety System Quality Evaluation

i

SSPS -

Solid State Protection System

'

STA

Shift Technical Advisor

-

STI -

Special Test Instruction

TACF -

Temporary Alteration Control Form

TAVE -

Average Reactor Coolant Temperature

TDAFW-

Turbine Driven Auxiliary Feedwater

TI

-

Technical Instruction

TREF -

Reference Temperature

TROI -

Tracking Open Items

TS

-

Technical Specifications

TVA -

Tennessee Valley Authority

UHI -

Upper Head Injection

U0

Unit Operator

-

URI -

Unresolved Item

USQD -

Unreviewed Safety Question Determination

VDC -

Volts Direct Current

VAC -

Volts Alternating Current

VAACS-

Vital Area Acess Control System

1

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26

WCG

Work Control Group

-

,

WP

Work Plan

-

.

WR

Work Request

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