ML20236J663

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Insp Repts 50-327/98-06 & 50-328/98-06 on 980426-0606. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support
ML20236J663
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 06/26/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20236J656 List:
References
50-327-98-06, 50-327-98-6, 50-328-98-06, 50-328-98-6, NUDOCS 9807080301
Download: ML20236J663 (42)


See also: IR 05000327/1998006

Text

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U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-327. 50-328

License Nos:

DPR-77. DPR-79

Report ~No:

50-327/98-06. 50-328/98-06

Licensee:

Tennessee Valley Authority (TVA)

Facility:

Sequoyah Nuclear Plant. Units 1 & 2

Location:

Sequoyah Access Road

Hamilton County. TN 37379

Dates:

April 26 through June 6, 1998

Inspectors:

M. Shannon. Senior Resident Inspector

R. Starkey. Resident Inspector

R. Telson, Resident Inspector

D. Thompson, Safeguards Inspector (Sections S1. S2 and

S4)

W. Kleinsorge. Reactor Inspector (Section M1.3)

H. Whitener. Reactor Inspector (Section E2.5 and E2.6)

C. Smith. Reactor Inspector (Sections E8.3 through

E8.7)

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J. Colaccino. Reactor Engineer. NRR. (Section E2.5 and

E2.6)

J. Blake. Reactor Inspector (Section M3.1)

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Approved by:

Harold O. Christensen. Chief

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Reactor Projects Branch 6

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Division of Reactor Projects

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9807080301 980626

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Enclosure 2

PDR

ADOCK 05000327

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PDR

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EXECUTIVE SUMMARY

Sequoyah Nuclear Plant. Units 1 & 2

NRC Inspection Report 50-327/98-06. 50-328/98-06

This integrated inspection included aspects of licensee operations,

maintenance, engineering, plant support, and effectiveness of licensee

controls in identifying, resolving, and preventing problems: in addition. it

included the results of regional security, steam generator inservice

inspection (ISI), pump and valve ASME Section XI testing, post maintenance

testing, and engineering corrective action inspections.

Ooerations

A positive finding was identified in that the operators performed well

.

in addressing the degrading plant conditions prior to the automatic

reactor tri) and performing the subsequent recovery actions.

In

addition. t7e plant startup was well performed.

In both evolutions,

communications was considered to be good (Section 01.2).

A negative finding was identified in that the assistant unit operator's

.

(AUO) actions of tapping on the valve / valve limit switch, without

guidance from the control room caused the loss of the as-found

condition of a valve that had failed to fully stroke (Section 01.3).

The inspector identified a negative finding when operators failed to

.

locally monitor the Unit 2 turbine driven auxiliary feedwater (TDAFW)

pump during a maintenance run of the pump (Section 01.4).

The inspector concluded that the licensee has implemented compensatory

.

actions to address the issue of part length control rod drive mechanism

(CRDM) potential cracking (Section 02.1).

A positive finding was identified in that the licensee responded

.

promptly and appropriately to an essential raw cooling water (ERCW) leak

inside the Unit 1 annulus which had rendered a radiation monitor

containment isolation valve inoperable (Section 02.2).

Maintenance

A positive finding was identified in that the licensee executed a well

.

planned forced outage schedule following the May 19. 1998. Unit 1

reactor trip (Section M1.1).

A negative finding was identified for the licensee's failure to

.

establish a preventative maintenance (PM) activity (18 years) for

sampling or changing emergency diesel generator (EDG) generator bearing

oil (Section M1.2).

A positive finding was identified in that post maintenance testing was

conducted appropriately and in a manner consistent with procedural and

regulatory requirements (Section M1.3).

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A weakness was identified in the Work Order process relating to

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documentation deficiencies (Section M1.3).

A concern was identified with the potential deficiencies in maintenance

and inspection procedures which resulted in ice condenser ice basket

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dam'ge and also did not promatly identify the damage, for at least ten

Uni. 1 ice baskets (Section 12.1).

A weakness was identified for a less than effective program for the

identification and correction of water intrusion into electrical

components (Section M2.2).

A concern was identified for the potential improper compression setting

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and the potential inadequate post maintenance testing of the shutdown

bus alternate supply breaker (Section M2.3).

A strength was identified in that eddy current data evaluation and

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management tools were strong components of the licensee's program for

steam generator degradation management (Section M3.1).

Enaineerino

A violation was identified for failure to perform an adequate safety

e

evaluation prior to making modifications to the waste gas analyzer

system (Section E2.1).

A positive finding was identified based on System Engineering

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successfully developing and implementing an action alan to remove boron

from the Unit 1 lower compartment coolers (Section E2.2).

A weakness was identified due to continuing steam dump system problems

which resulted in the May 19. 1998. water hammer event and piping

sapport damage (Section E2.3).

A positive finding was identified based on engineering support of

.

facilities and equipment when a licensee identified steam generator

hydraulic snubber leak was properly assessed for operability and a

thorough corrective action plan was promptly implemented (Section E2.4).

Observation of pump tests. review of pump test procedures, and review of

.

pump parameter trend data indicate that the licensee has established and

implemented an adequate pump IST program.

The insSectors noted that the

limiting values for pum) acceptance criteria were Jased on the most

conservative of the tec1nical specification. design basis, or code

calculated values (Section E2.5).

The acquisition of a new software program for analysis, tracking and

trending IST data was considered a positive addition to the IST program

(Section E2.5).

The inspectors concluded that the licensee had developed and implemented

.

an IST program which, in general, was consistent with the regulations

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and the ASME Boiler and Pressure Vessel,Section XI code.

However. one

violation, with three examples for failure to adequately implement

Section XI code testing requirements, was identified during the

inspection (Section E2.6).

Plant Sucoort

A positive finding was identified based on the licensee conducting its

security and safeguards activities in a manner that protected public

health and safety.

This portion of the program. as implemented, met the

licensee's commitments and NRC requirements (Section S1).

A violation was identified for a failure to properly control access at

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the sally port (Section 51).

A positive finding was identified in that the licensee's security

.

facilities and equi) ment were determined to be very well maintained and

reliable even thoug1 a test procedure for standardized testing of the

intrusion detection equipment had not been developed (Section S2).

The excellent Engineering and instrumentation and controls (I&C) support

was the major contributing factor to continued operability of the

detection and assessment equipment (Section S2).

A positive finding was identified in that the security force members

.

(SFMs) adequately demonstrated that they have the requisite knowledge

necessary to effectively implement the duties and responsibilities

associated with their day-to-day and contingency response duties

(Section S4).

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Report Details

Summary of Plant Status

Unit 1 automatically trip]ed from 100% power on May 19. 1998, due a low-low

steam generator level.

T1e sequence of events was initiated by a

malfunctioning 480 Vac shutdown board breaker and the subsequent failure of a

vital 120 Vac inverter.

Repairs were made to affected electrical equi) ment

and the unit was restarted and achieved criticality on May 20; the tur]ine

generator was returned to service at 8:54 a.m.. on May 21: and Unit I reached

100% power on May 22. 1998.

Unit 2 operated at full power for the entire inspection period.

Review of Uodated Final Safety Analysis Report (UFSAR) Commitments

While performing inspections discussed in this report, the inspectors reviewed

the applicable portions of the UFSAR that were related to the areas inspected.

The inspectors verified that the UFSAR wording was consistent with the

observed plant practices, procedures, and/or parameters.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707. the inspectors conducted frequent

reviews of ongoing plant operations.

In general, the conduct of

o)erations was considered to be good based on operator actions following

t1e reactor trip on May 19 and the subsequent plant startup on May 20.

Instances of weak operations performance were noted based on an

assistant unit o)erator tapping on a valve limit switch and lack of

operator oversigit during post maintenance testing of the turbine driven

,

auxiliary feedwater pump.

01.2 Automatic Reactor Trio Due to loss of Vital Inverter

a.

Insoection Scooe (71707)

The ins)ectors reviewed the events and observed the activities related

to the Jnit 1 automatic reactor trip on May 19, 1998, and the subsequent

startup on May 20, 1998.

b.

Observations and Findinas

AT 10:43 a.m., on May 19.1998. Unit 1 experienced an automatic reactor trip from 100% power.

The inspectors observed the various control room

activities just prior to the trip and the recovery actions following the

trip.

Surveillance activities were in progress on the 1Al-A vital 480 volt

alternating current (Vac) shutdown board and the shutdown board was

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being transferred to its alternate supply breaker.

The system is

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designed such that the normal supply breaker is opened and then the

alternate supply breaker is manually closed.

Following closure of the

alternate sup)ly breaker, the operators noted an arcing sound and smoke

coming from t1e alternate supply breaker cubicle.

The alternate breaker

was reopened and the normal supply breaker was re-closed. The total

evolution took approximately 45 seconds.

During the time period that the alternate breaker was closed onto the

vital bus, the vital 120 Vac inverter experienced voltage spikes of

sufficient magnitude that the output fuses for the silicon control

rectifiers failed and deenergized the 120 Vac vital Bus 1.

Loss of

vital 120 Vac Bus 1 caused a loss of channel 1 of the steam flow

instrumentation for all four steam generators which led to a closure of

all four main feedwater regulating valves.

The loss of Steam Flow

Signal also caused the main feedwater pumps' master control circuitry to

run tha feedwater pump speed to minimum.

The operators made an attempt

to recover the feedwater regulating valves and feedwater pump speed

control; however, the plant tripped on low-low steam generator level

approximately 35 seconds after total loss of the vital inverter.

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The. operators experienced other abnormal plant conditions that further

complicated recovery actions.

Due to the loss of vital 120 Vac Bus 1.

feedwater isolation valves to steam generators #1 and #3 did not

automatically close when the feedwater isolation signal was generated.

The operators had to manually close the valves.

In addition, the loss

of the vital 120 Vac bus caused a loss of essential and nonessential

control air to containment and caused letdown to isolate. As a result.

the pressurizer level increased and pressurizer pressure increased

until the pressurizer power operated relief valves (PORVs) opened.

The inspector was in the control room area at the start of the event and

observed control room operator activities just 3rior to the trip and

following the trip.

The inspector noted that tie control room operators

followed the applicable procedures and clearly communicated plant

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conditions during the recovery.

Pending actions were fully discussed

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prior to implementation and interim shift status briefings were

detailed.

The inspectors also observed the Unit 1 startup on May 20. 1998.

Pulling of the shutdown bank rods was started at 3:30 p.m. and Unit 1

entered Mode 2 at 5:28 p.m.

At 6:27 p.m.. on May 20. 1998, the reactor

went critical. The inspectors observed good communications and

procedure adherence during the startup.

The root cause for the automatic reactor trip was a faulted 480 Vac

supply breaker. This issue is discussed in more detail in Section M2.3

of this report.

c.

[gnclusions

The inspectors concluded that the operators performed well in addressing

the initial plant conditions prior to the automatic reactor trip and in

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performing the subsequent recovery actions.

In addition, the plant

startup was well coordinated.

In.both cases communications were

considered to be good. -This is considered to be a positive finding.

01.3 Inaoorooriate Tacoina of Valve Limit Switch

a.

Insoection Scooe (71707)

The inspectors reviewed the licensee's actions in response to

ina)propriate status light . indication for the 2A residual heat removal

(RHR) system temperature control valve.

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'b.

Observations and Findinos

On June 1.1998, during routine control room observations, the

' ins)ectors noted that the licensee was experiencing problems with the-

lig1t indication for the 2A RHR system temperature control valve 2-FCV-

74-16.

Status light panel 2-XX-55-6C indicated that the valve was not

fully open. The licensee had previously successfully completed the

stroke time testing of this valve and after completion of the post

maintenance testing of the 2A RHR pump the valve did not indicate fully-

open as required.

The control room operators dispatched an. AUO to verify the valve

)osition. The AU0 informed the control room that the valve appeared to

)e fully open. The control room operators called the system engineer to

discuss the valve problem and initiated a work request (WR C-397112) to

check on the limit switch.

~Several minutes later the inspectors and the control room operators

observed.that the 2-FCV-74-16 status light indication went'out. The

control. room operators contacted the AUO again'to verify valve status.

The AVO. stated that he had tapped on the valve with his flashlight. .The

-licensee subsequently identified that the ' collar on the valve, stem for

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operation of the fully open limit switch was loose. .It was retightened

and the valve was successfully stroke time tested.

.c.

Conclusions

The AUO's actions of tapping.on the valve / valve limit switch, without

guidance from the control room, caused the loss of the as-found

condition of the valve. .This item is identified as a negative finding.

01-.4 Ooerators Fail ~ to Locally Monitor TDAFW Pumo Durina Maintenance Run'

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~ Insoection Scooe'(71707)

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The inspector followed u) on the failure of Operations to station an

operator at' the Unit 2 T)AFW pump during a maintenance run of the pump.

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b.

Observations ^and Findinas

On. June 5,1998,- the inspector entered the Unit 2 TDAFW pump room during

a' maintenance run of the pump and observed the inboard pum) shaft

packing failure. The ins)ector observed black smoke, sparcs and heard a

)opping noise during' the 3rief interval prior to the pump being stopped

Jy the main control room. At the time of the packing failure, a

mechanical maintenance technician'was in the pump room.

However, there

. were no o)erations personnel. in the area.

Prior to the packing failure,

the pump lad been run twice that day, once for an' ASME Section XI test

and a second-time to perform the check valve test. The packing failure

occurred during a third pump run following a change out of the bearing-

-oil.

Once the pump was stopped, the inspector remained in the area for

approximately 30 minutes during which time no one from operations

, arrived in the area to inspect the pump for damage

The inspector informed the Unit Supervisor and Shift Manager of the

absence of an AVO or other Operation's personnel in the area during the

. maintenance run of the TDAFW. The ins)ector was informed later in the

day by the Operations Superintendent t1at it was management's

. expectation that an operator be in the area during running of safety

related~ equipment. However, miscommunication occurred between a

licensed operator in the control room and the responsible AUO. which

resulted 'in no operator being present in the. area during the TDAFW pump

run.

The licensee initiated PER No. SQ980695PER to document the failure of

the Unit 2 TDAFW inboard packing. The pump was subsequently inspected,

the packing replaced, and an ASME Section XI test was run prior to-

' operations declaring the pump operable.

On June 6. 1998, Operations management issued Standing Order 98-032.

entitled Equipment Monitoring, which stated that whenever safety related

or any other large piece of equipment is started, stopped, or tested, an

o)erator. is expected to be present to monitor equipment performance for

t1e duration of the equipmcot test.

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c.

Conclusions

The inspector . identified'a negative finding when operators failed to

locally monitor the Unit 2 TDAFW pump during a maintenance run of the

pump.

02.

Operational Status of Facilities and Equipment

02.1 Plan -for Addressina Part Lenath Control Rod Drive Mechanisms (CRDM)

Potential Crackina

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a.

Insoection Scoce (71707).

The inspector reviewed the licensee's compensatory actions which were

put~in place;until TVA and the Westinghouse Owner's Group (WOG) resolve

the issue of part length CRDM potential cracking.

bs Observations and Findinas

In a letter to the NRC, dated April 9,1998. TVA provided its plan

to address the industry issue of part length CRDM cracking, a problem

which was first identified at the Prairie Island. Nuclear Plant. The

' letter stated that TVA believes that the data and evaluation to date

suggests that the finding on the one part length CRDM at Prairie Island

is- related to a unique set of circumstances at that facility a id

configurations at Sequoyah and Watts Bar are less susceptible to this

phenomenon.

TVA stated that it will continue to follow industry

initiatives addressing this issue and may further revise the outlined

comprehensive approach based on the results of these initiatives.

Until the TVA and WOG evaluation is completed. TVA has issued guidance

to the Operations staff to heighten awareness and implement compensatory

.RCS leakage monitoring actions. The inspector verified that on April 7.

1998. Standing Order 98-020.. Interim Increased RCS Leakage Monitoring,

was issued to Operations personnel.

Specifically, each shift was

directed to monitor the following parameters: containment moisture.

' containment pressure, containment radiation levels, containment

temperature, and containment sump levels.

A more in-depth technical

rev4ew will be performed to identify the source of leakage identified

above a pre-established threshold.

c.

Conclusions-

The inspector. concluded that the licensee has impl'mented compensatory

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actions to address the issue of part length CRDM potential cracking.

02.2 ERCW Leak Inside Unit 1 Annulus

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a.

Insoection Scooe (71707)-

The inspector reviewed the circumstances involving an ERCW pin hole leak

inside the Unit 1 annulus which resulted in the inoperability of the

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1ower compartment radiation monitor containment isolation valve.

b. Observations and Findinas-

On June 3. 1998, at 12:08 a.m., while troubleshooting a ground on vital

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battery board;I. . electricians identified 1-FCV-90-107. the Unit 1 lower

compartment radiation monitor containment outboard isolation valve, a

normally open. valve, as being the source of the ground. At 3:37 a.m..

operators. observed from' control room indications that 1-FCV-90-107 was

. indicating mid-position, declared the valve inoperable and entered the

action statement.of TS 3.6.3. Containment Isolation Valves. At 4:10

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a.mi. during an inspection of 1-FCV-90-107 in the Unit 1 annulus.

. electricians and radiation control technicians identified a water leak

in the general area of 1-FCV-90.-107, but were unable to identify the

source of the-leak. Operators subsequently isolated ERCW cooling water

to upper com)artment cooler 1B. which stopped the leak.

The inspector

arrived in t1e control room at 4:15 a.m. and observed the licensee's

response.and resolution to the problem of the inoperable containment

isolation valve.

The licensee; believing that the problem with 1-FCV-90-107 was a

grounded limit switch, attempted to clean and dry out the limit switch

which had apparently been exposed to spray from the ERCW leak. After

the cleaning efforts proved to be unsuccessful, the decision was made to

replace the limit switch.

Prior to replacing the limit switch the

containment penetration was isolated'at 7:12 a.m. to comply with the

action statement of TS 3.6.3.

The limit switch was then replaced. 1-

FCV-90-107 was stroke time tested and declared operable and at 9:50 a.m.

TS 3.6.3 was exited.

Isolation of the containment penetration also

rendered the lower compartment radiation monitor (1-RM-90-106)

ino)erable which required entry into TS 3.4.6.1. Reactor Coolant System

Leacage. At 10:30 a.m., following repairs to 1-FCV-90-107, radiation

monitoring of lower containment was reestablished and TS 3.4.6.1 was

exited. At no time were any TS action statements exceeded.

This event

was documented in PER No. SQ980671PER.

Later on June 3. the licensee inspected the Unit 1 annulus and

discovered a pin hole leak in a section of 2-inch diameter ERCW piping

to the;18 upper compartment cooler. The licensee stated that this

section of piping was verified not to have been leaking during the week

of May 24. 1998. when the piping had been ultrasonically tested (UT) for

pipe wall' thinning.

During the UT of the pipe no abnormalities were

identified. The pipe will remain isolated until the next refueling

outage at which time repairs will be made,

c.

Conclusions-

The inspector concluded that the licensee responded promptly and

appropriately to an ERCW pipe leak inside Unit 1 annulus which had

rendered a radiation monitor containment isolation valve inoperable.

This is considered a positive finding.

08'

Miscellaneous Operations Issues (92901)

08.1

(Closed) URI 50-327. 328/98-03-03. Potential Failure to Meet UFSAR

Requirements. Failure to Revise the UFSAR. Inaoorooriately Closina a

10c ification Packaae. and not Establishing a Periodic Samolina Proaram

for the Waste Gas-Collection System.

This issue was discussed in

Section E2.1 of this report and resulted in a violation for failure to

perform an adequate safety evaluation prior to making modifications to

the waste gas analyzer system.

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08.2 (Closed) URI 50-327/98-03-01. Potential Failure to Enter TS 3.11.2.5 LC0

Action Statement When Samoles Indicated High Concentrations of Oxygen in

the PRT.

The inspectors completed a review of the licensee's design

basis docurrents and discussed this issue with regional management.

It

was concluded that the PRT would not be applicable te TS 3.11.2.5.

However, the licensee did revise their waste gas sampling procedures to

limit explosive gas concentrations in the pressurizer relief tanks

(PRT). volume control tanks, spent resin stor6ge tank 6 rid waste holdup

tanks to be consistent with the TS explosive gas limits of less than 2%

oxygen with great'.. than 4% hydrogen.

The inspectors concluded that no

violation of TS occurred.

II. Maintenance

M1

Conduct of Maintenance

M1.1 General _ Comments

a.

Insoection Scooe (61726 & 62707)

Using inspection procedures 61726 and 62707 the inspectors conductea

frequent reviews of ongoing maintenance and surveillance activities.

The inspectors observed and/or reviewed all or portions of the following

work ac wities and/or surveillance:

1-MI-TFT-201-051.A

Relay Functional Test For 480V Shutdown

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Board 1Al-A. Rev. 2

WO 98-004981-000

Repair of Water Intrusion Into Control

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Station For ERCW Pump Traveling Screens

2-SI-IFT-092-N41.1

Functional Test Of Power Range Nuclear

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Instrumentation System. Channel 41. Rev. 9

WO 97-013195-000

Repair Oil Leak On Main Feedwater Pump Oil

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Filter

0-PI-IXX-092-N45.0

Calibration Of Power Range Nuclear

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Inc.trumentation System Following

Incore/Excore Detector Calibration. Rev. 6

0-PI-SFT-032-001A

Auxiliary Control Air Compressor "A"

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Operability Test. Rev. 4

b.

Observations and Findinos

On May 19. 1998. Unit 1 entered a forced maintenance outage following an

automatic reactor trip.

The inspectors noted that the licensee had a

well planned forced outage schedule and completed approximately 50 work

orders prior to restarting the unit.

Some of the major activities

included repairing an air leak on a main feedwater regulating valve.

repsiring an electro-hydraulic control oil leak on the 1A main feedwater

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(MFW) pump, and sparing out a main bank transformer which haa been

indicating higher than normal combustion gas concentrations.

C.

Conclusions

3

The licensee executed a well planned forced cutage schedule following

the May 19, 1998. Unit I reactor trip. This is a positive finding.

M1.2 Eneraency Diesel Generator Bearino Oil Samol g

a.

Inspection Scoce (62707)

The inspector reviewed the issue regarding periodic oil samples not

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being taken on emergency diesel generator (EDG) generator bearing oil

and the fact that the generator bearing oil had never been changed

during the inservice life of the EDGs.

b.

Observations and Findinas

During a predictive maintenance (PM) lobe oil PM optimization review.

the licensee discovered that oil in all four EDG generator bearing

housings had never been sampled or changed during the approximate 18

years of EDG service.

Following this identification, samples were taken

from each of the EDGs. The sample analysis indicated elevated levels of

iron. lead, tin. silicon. copper and zinc. as well as elevated viscosity

and neutralization number, indicative of the acidity of the oil.

PER

No. S0980378PER dated April 10. 1998, documented the discovery of the

lack of generator bearing oil sampling or change-out and discussed root

causes, extent of condition, vendor recommendations, and corrective

actions.

On May 5. 1998, the licensee com)leted a Technical Support Investigation

Request (TSIR) which concluded tlat there was no technical basis

requiring immediate oil replacement and no operability concern with any

diesel generator in performing its intended safety function.

The TSIR

recommended that oil replacement be scheduled during upcoming EDG

outages unless opportune times occur earlier.

Work Requests were

written to change the generator bearing oil in each EDG.

The inspector discussed with the licensee the vendor and owners group

recommendations regarding generator bearing oil change-out.

The

generator portion of vendor manual E130-0010 recommended that the oil be

drained and flushed at least once a year. The bearing manufacturer

recommended oil change-out based on run time hours.

(None o' the

Sequoyah EDGs have exceeded the bearing manufacturer's run time hour

limits.) Finally, the owners group recommended maintenance program did

not specifically state any requirements for generator bearing oil.

Although it appears that there were no specific vendor recommendations

which applied to the ty)e service to which the EDGs are exposed, the

licensee had never esta)11shed a PM activity to either sample or change

the generator bearing oil on EDGs.

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The inspector reviewed Surveillance Instruction (SI)-102 M/M. Diesel

Generator Monthly Mechanical Inspections, and concluded that maintenance

personnel have been visually checking the generator bearing oil level

sight gauge on each EDG once each month, during the EDG monthly

surveillance o)erability run.

Following identification that the bearing

oil had never Jeen sampled the licensee revised SI-102 M/M to include a

quarterly samaling frequency. The frequency of oil change out will be

conditional. Jased on results of the quarterly oil sample analysis.

Inspector discussions with Operations management indicated that

generator bearing oil levels have not been monitored by operations.

The licensee performed an extent of condition review on safety related

rotating equipment and determined that all lubricated equipment reviewed

had a preventative maintenance task to perform lube oil change-out or

sampling.

The licensee's review of EDG attendant equipment revealed

that the EDG air compressors, which are non-safety related did not have

a PM for oil change-out, although the oil filters had been changed every

three months. All the EDG air compressors had been replaced, on an as

needed basis, within the last five years. The licensee has revised the

PM procedure to change the EDG air compressor oil filters and oil every

six rionths.

c.

Conclusions

A negative finding was identified for the licensee's failure to

establish a PM activity for sampling or changing EDG generator bearing

oil.

M1.3 Post Maintenance Testina (PMT)

a.

Insoection Scoce (62700)

To evaluate the licensee's program for PMT, the inspectors reviewed:

the licensee's written practice for PMT. three recent assessments

addressing PMT. the corrective action documents associated with those

assessments, and com)leted work order (WO) packages.

The inspectors

also conducted a walc down inspection of the equipment associated with

several completed WO packages.

From January 1. 1998 to A)ril 27, 1998,

the licensee completed approximately 2000 WO packages.

T1e inspectors

selected for review a sample of 30 WO packages, from that period,

representing 21 systems and all three maintenance disciplines

(mechanical, electrical and instrumentation).

The WO packages were

reviewed for adequacy of PMT and observations were compared to the

licensee's written practice and the UFSAR.

The 30 WO packages were

reviewed for proper capture of unavailability times, as required by the

maintenance rule. 10 CFR 50.65.

l

l

b.

Observations and Findinas

PMT was implemented at the Sequoyah Nuclear Plant by SSP-6.31.

" MAINTENANCE MANAGEMENT SYSTEM PRE- OR POST-MAINTENANCE TESTING".

[

Revision 10. effective April 22, 1998.

As a result of their review, the

1

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- __ ___ _ __ - _ - - ___ _ - _ -

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. _ _ - _ _

_ --__-__

10

'. inspectors. identified to the licensee some inconsistencies and a number

of enhancements.

The licensee indicated that they would address those

items in the next revision of-SSP-6.31.

'

Self-Assessment SA-MTN-98-003. ." Post-Maintenance Testing". was conducted

  1. -

u

February 9-27, 1998. Assessment SA-MTN-98-003 identified three findings

L

which were addressed in three problem evaluation reports (PERs).

These

L

findings included: documentation deficiencies in some W0s: WO scope

l-

changes made without re-review by the Operations Department: and some

i

personnel ap3 roving WO activities which were not on the PMT approval

l'

list. The t1ree PERs addressed the specific examples identified and

!

took or planned a) pro')riate actions to prevent reoccurrences of similar

l

circumstances. .T1e PER's' corrective action plans did not address

similar problems in the remainder of the licensee's completed WO

'

packages.' Assessment NA-S0-98-28. " WORK ORDER (WO) CLOSURE BACKLOG".

com)leted April 7.-1998, indicated that over 50 3ercent of the WO

paccages reviewed were submitted for closure wit 1 deficiencies, the

l

majority of which .were the result of inattention to detail. (human

performance).

A PER was issued to address this issue and remains open.

Assessment SA-MTN-98-05. " Maintenance & Modification Quarterly Self -

'

Assessment". conducted March 16-A)ril 4.1998, identified problems using

not applicable (N/A) in W0s.

A PER was issued to address this issue and

remains open. .Of the 30 completed WO packages reviewed by the

inspectors. 12 were electronic records, for which the licensee provided

computer screen prints for review, no discrepancies were identified.

The. remaining 18 completed WO packages reviewed were hard copy records

L

reproduced from microfilm in some cases, completed by handwriting.

No

deficiencies were identified in 6.

The remaining 12 contained

I

documentation deficiencies, which included: missing signatures: missing

'

data; missing documents: vague PMT acce)tance criteria: and PMT

g

accomplished. but'not documented as sucl. _Several WO packages

a)parently had their pages out of order, making it' difficult to follow

t1e course of work.

Page numbering would have alleviated this

difficultly. A space is provided for page numbering on most pages in WO

packages but that option was infrequently used. The inspectors did not

identify any examples of inadequate or inappropriate PMT.

The inspectors consider the documentation deficiencies, identified by

both the licensee and.the NRC, the result of inattention to detail and a

'

l

_ eakness in the licensee's Post Maintenance Test Program.

w

Equipment' unavailability time as it relates to 10 CFR 50.65 was properly

L

captured for the 30 WO packages reviewed by the inspectors.

l

c.

Conclusions

Post maintenance testing wasl conducted appropriately and consistent with

procedural and regulatory requirements.

A weakness in the licensee's Post Maintenance Test Program relating to

documentation deficiencies was identified.

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11

M2

Maintenance and Material Condition of Facilities and Equipment

M2.1. Damaae to Multiole Ice Condenser Ice Baskets.

a.

Insoection Scooe (61726)

Inspectors reviewed Problem Evaluation Report No. SO980597PER. Technical-

Operability Evaluation (TOE) 1098-061-0597 and applicable maintenance

and surveillance procedures in connection with a recent licensee finding

{

of ten damaged Unit 1 Ice Condenser Ice Baskets.

1

b.

Observations and Findinas

On May 19. 1998, during a Unit 1 forced outage the licensee conducted

an inspection of the ice condenser. The inspection identified lateral

deformations in the vicinity of the bottom su) port rings of nine baskets

and torn ligaments in the same area of a tenti basket.

T0E~1098-061-0597.. performed to assess ice condenser operability,

concluded that, due to the limited number of baskets involved, the

damage to the ice baskets did not degrade the ability of the ice

condenser to limit peak pressure in the containment following a LOCA or

high energy line break.

Discussions with the . system engineer indicated

!

that the baskets had probably been damaged by jacking from below while

l

attempting to free them during previous outages.

L

The inspectors' evaluated the ice condenser ice basket maintenance and

l

surveillance procedures for adequacy with' regard to maintaining ice

basket mechanical integrity durina and following efforts to break loose

frozen-in-place ice baskets from Tattice framework. .The licensee's

procedure for breaking ice baskets free allows up to 4.000'lbs, of

upward thrust to be applied to the bottom of the ice basket while

simultaneously applying twisting and lifting forces.

The procedure

cautions against excessive force that would cause basket damage, yet

contains no guidance to inspect for damage before during or after

.

basket-freeing activities.

Surveillance procedure 0-SI-MIN-061-003.0 " Ice Condenser - Ice Baskets"

describes ice condenser. ice basket visual inspection requirements in

- accordance with Technical Specification Surveillance Requirement 4.6.5.1.C.

Reliance ~on this surveillance procedure alone to identify

the type of damage addressed in PER S0980597PER appeared to be

inadequate.in that-(1) The procedure only. required sampling six of the

1944 baskets once every 40 months and (2) the procedure required that

the baskets be unpinned and lifted ten feet before the ins)ection.

Because of these. requirements, the surveillance could not 3e performed

on damaged frozen-in-place baskets and could fail to identify damage in

the vicinity of basket bottoms due to the baskets having been lifted

before. inspection.

_ _

_ _ - _ _ _ _ _ _ _ _ _ _ - .

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_

_ _ _ _ _ _ _ _ _

_

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--_

12

The licensee in res)onse to heightened regulatory interest and ongoing

concerns regarding tieir ice condensers, formed a self-assessment team

to evaluate this and other issues.

To date the licensee's self

assessment process has identified approximately fifteen additional PERs

that were being generated in connection with the licensee's assessment

team's findings.

c.

Conclusions

The )otential deficiencies in maintenance and inspection procedures

whici resulted in ice condenser ice basket damage and the failure to

identify the damage, for at least ten Unit 1 ice baskets is considered

to be an Unresolved Item (URI 50-327/98-06-01).

M2.2 Water Intrusion Into Essential Raw Coolina Water (ERCW) Buildina

Electrical Boxes

a.

Insoection Scooe (62707)

The inspectors reviewed the licensee's corrective actions related to

3revious events where water was found inside various electrical junction

aoxes.

b.

Observations and Findinas

On April 20, 1998, the inspectors identified water intrusion into the

ERCW building vital motor control center (MCC) b-B ERCW MCC.

The

licensee subsequently discovered that rain water was entering the screen

wash control switch junction box and draining down the cable into the

MCC. Discussions with the licensee indicated that other susceptible

junction boxes in the ERCW building had been inspected for water

intrusion.

This issue was discussed in Inspection Report 98-04 and a

negative finding was identified at that time.

On May 18, 1998, the inspectors were conducting a walkdown of the ERCW

building and noted several electrical boxes that appeared to have been

subjected to water intrusion.

This issue was discussed with the

licensee and the licensee subsequently opened the suspect electrical

boxes. The licensee found that six fire protection electrical

Jull

boxes had internal evidence of water intrusion.

In addition t1e

licensee found five additional electrical boxes with deteriorated cover

gaskets which needed to be replaced.

In October 1996. Unit 2 experienced a turbine run back that led to a

reactor trip due to water intrusion into the turbine impulse switches.

,

The licensee noted that electrical box sealing requirements were

!

proceduralized for the safety related buildings, but were not specified

for the turbine building.

The appro)riate procedures were revised to

include sealing requirements for tur)ine building electrical boxes.

In

addition, the licensee stated that im] roved inspection methodology for

inspection for water intrusion would )e developed.

Based on the two

recent inspector findings of water intrusion into ERCW electrical boxes.

i

I

. _ _ . _ - _ - _

.

..

. _ -

l

13

the licensee's corrective actions for the previous 1996 violation have

not been fully effective in the identification and correction of water

intrusion issues.

c.

Conclusions

i.

A weakness was identified for a less than effective program for the

i

identification and correction of water intrusion into electrical

L

compon'ents.

M2.3- . Failure of the Alternate Sucoly Breaker to Shutdown Bus 1Al-A

a.

Insoection Sccue (62707)

,,

The inspectors reviewed the work history and observed the

troubleshooting: efforts for the alternate supply. breaker for shutdown

Bus 1Al-A following the reactor trip on May 19,

b.

Observations and Findinos

On May 19. 1998, while placing the alternate supply breaker in service

for shutdown Bus 1Al-A. the breaker started to make an arching noise and

began smoking.. The' operators immediately removed the breaker from

_

service. When the breaker was subsequently. inspected. the licensee

identified that .the main line contacts were severely pitted and burned.

The manufacturer's technical representative assisted the licensee in

disassembly and troubleshooting of the faulted breaker. The inspectors

observed portions of.the' disassembly and observed that the licensee

identified that the breaker did not have the pro)er contact alignment or

compression. This preliminary cause explained way the breaker began

arcing with much less than design loading when it was placed in service.

Further review of the licensee's work history and discussions with the

licensee revealed that-this breaker had previously. failed to close on

demand and had been extensively overhauled (January 1998).

Following

the corrective maintenance. the breaker was reinstalled as the alternate

supply breaker.

The breaker remained in standby from January until the

failed transfer on May 19.

-Inspector review of work documents indicated that the contact

compression was-set in accordance with the maintenance 3rocedure during

)

the corrective maintenance activity. However, the breater failed

following its first closure onto a loaded bus. The inspectors

~ determined that this maintenance activity would be considered to be

l

online maintenance and would carry the associated risk for online

maintenance.

In this case. )erformance of the post maintenance

1

testing / load testing of the areaker carried the risk of deenergizing the

shutdown bus

The apparent improper compression setting of the breaker

i

[

main contacts and the potential inadequate post maintenance testing for

breaker loading is considered to be an unresolved item pending further

. review (URI 50-327/98-06-02).

>

l

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.. .

_ - _ - _ _ _ _ _ _ _ _ _ _ _ _ _ .

14

c.

Conclusions

An unresolved item was identified for the apparent improper compression

setting and the potential inadequate post maintenance testing of the-

shutdown bus alternate supply breaker.

M3

Maintenance Procedures and Documentation

-M3.1 Steam Generator-(SG) Degradation Manaaement'

a.

Insoection Scooe (50002)

-The inspectors reviewed.the licensee's programs for steam generator

' degradation management and eddy current data evaluation.

b.

Observations and Findinos

Steam Generator Degradation Management: The inspectors reviewed the

degradation history-for all of the Sequoyah steam generators. The

records showed that the major contributor to tube plugging in' Unit I has

been 'an increase in the number of 3rimary water stress corrosion

cracking (PWSCC) indications at tu)e support plate (TSP) locations.

In

Unit 2 the major contributors to tube plugging were PWSCC at the top of

the tubesheet (TTS) and PWSCC in the small radius U-bends. The total

number of tubes plugged at the end of fuel cycle eight for each SG was

1

as follows:

-Unit 1 SG 1: 77 p gged

2.273%

Unit 2 SG 1:-31 p ugged

0.915%

SG 2:-104

ugged 3.070%

SG 2: 91 p ugged

2.686%.

-SG 3: 205

ugged '6.051%

SG 3: 58 p ugged

1.712%

SG 4: 239

ugged 7.054%

SG 4: 22 p ugged

0.649%

,

The inspectors reviewed the licensee's plans for degradation management

which included alternate plugging criteria-(APC) for PWSCC at TSP

locations.

(The licensee had already received approval for an APC for

ODSCC (secondary side SCC) at TSP locations.

The licensee was also

- actively involved in development of an inspectable electro-sleeving

process to mitigate'PWSCC problems.

Eddy Current (EC) Evaluations: Thslicensee'sEC'dataevaluation

methodology:for using Bobbin Coil data to screen dented TSP

intersections for PWSCC was reviewed by reviewing selected EC data from

i

the last Unit.1 outage.

The Bobbin Coil lissajous signals provided the

)

analysts with a conservative screening process for indicating which

!

~ dented TSP intersections should be inspected with EC RPC Coils.

-The licensee's Access-based EC data sorting and evaluation program

provided an orderly. auditable record of the decision process for-

. plugging / repair lists. The use of the program ensured that all data

were considered in the selection of in-situ pressure test candidates.

!

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_ _ - _

_ _ _ _ _ _ - _ _ _

15

.c.

Conclusions

Eddy current data evaluation and management tools were strong components

of.the licensee'c program for steam generator degradation management.

M8

Miscellaneous Maintenance Issues (92902)

M8.1

(Closed) LER 50-327/97013. Revision 1. Missed Surveillance as a Result

,

of an Inadeauate Procedure.

Revision 0 to this LER was discussed and-

closed in IR 50-327, 328/98-04. .The issue of the missed breaker

surveillance in revision 0 resulted in the identification of a non-cited

violation, 50-327. 328/98-04-03.

During the licensee's extent of -

-condition review, an additional breaker was identified which had been

mistakenly omitted from the surveillance program during a surveillance

procedure revision.

The additional breaker, identified in revision 1.

was the isolation device protecting a safety-related bus from a

nonqualified load, the onsite paging system.

Other that the additional

breaker, identified during the licensee's extent of condition review, no

new issues were revealed by ~ revision 1 of the LER.

M8.2 (Closed) IFI 50-327/98-03-04. Follow Licensee's Review of the Section XI

Valve Testina Procedure to Determine if a Better Method Would Be

Available to Test the CCS Pumo Discharge Check Valves.

The inspectors

reviewed the mainten6nce history for the five CCS pump discharge valves

and for the essential raw cooling water pump discharge valves and did

not identify any instances that would indicate check valve damage due to

- slamming shut during testing.

Engineering indicated that the valves

were designed to operate with the as observed differential pressure

conditions. Based on the review, the inspectors concluded that the

present CCS pump testing method did not appear to be causing any check

valve problems and therefore would be considered to be acceptable.

III. Enaineerina

i

E2

Engineering Support of Facilities and Equipment

E2.1 Modifications to the Waste Gas Analyzer System

a.

Insoection Scooe (37551)

The inspectors reviewed the modification to the waste gas analyzer

system which the licensee implemented during the U2C8 refueling outage.

= b.

Observations and Findinas

-In May 1997. the licensee' prepared Design Change Notice (DCN) M-11549-A

to re) lace the Waste Gas Analyzer (common to both units) with a more

relia)le, state-of-the-art analyzer.

Prior to the modification, the

Waste. Gas Analyzer monitored various tanks in the Waste Disposal System

and' Chemical and Volume Control System (CVCS) for hydrogen and oxygen

= concentrations. The concentrations were. indicated, recorded, and

c

alarmed at the analyzer. The modification, which was completed on

_ . _ _ _ - _ . .______ _ ___________ _-____ ____-_____

____-_ - _ __ - _-__ __- _____

16

October 6.1997, converted the sampling system from an electrically

actuated tank selection, which aligned various tanks to the gas analyzer

for sampling, to an automatic and grab sample operation.

The new

analyzer automatically sampled the in-service Waste Gas Decay Tank only.

The modification eliminated the automatic sampling the pressurizer

relief tank (PRT). Volume Control Tank (VCT). Holdup Tank (HUT). and the

Spent Resin Storage Tank (SRST) and )rovided for only grab sampling

capability for these tanks.

Unc'er t1e new design configuration, these

tanks are sampled from a separate sample header which is physically

separated from the waste gas analyzer.

In March / April 1998, the inspectors, while following up on a related PRT

gas sampling issue (IR 50-327. 328/98-03), reviewed the licensee's 10 CFR 50.59 safety evaluation for the modification to the waste gas

analyzer system.

The inspectors determined that the safety evaluation

did not adequately address the elimination of the automatic sampling

system and replacing it with grab sample capability for the PRT. VCT.

HUT. and SRST. The safety evaluation referred to taking grab samples.

but did not evaluate the adequacy of grab samples as compared to an

automatic system nor did it recommend sampling frequencies or procedure

changes to ensure that grab samples would be taken.

By not ensuring

that grab samales would be obtained, the licensee created a situation

where the tan (s went unsampled for an extended period of time with the

)otential to develop explosive / combustible concentrations of oxygen and

lydrogen.

The inspectors concluded that the licensee failed to perform an adequate

safety evaluation prior to modifying the waste gas analyzer system.

'

This is identified as a violation of 10 CFR 50.59 (b)(1) which requires

that the licensee shall maintain records of changes to the facility and

that these records include a written safety evaluation which provides

the bases for the determination that the change does not involve an

unreviewed safety question (VIO 50-327, 328/98-06-03).

In March 1998 the licensee reopened the closed DCN package and revised

the safety evaluation.

The ins)ectors concluded that the revision

corrected the deficiencies in t1e evaluation and adequately addressed

the elimination of the automatic sampling capabilities of the waste gas

,

analyzer. The revision also added an attachment to the DCN modification

criteria which specified the sampling frequency of the PRT. HUT. VCT,

and SRST.

Procedure 0-PI-CEM-000-080.1. Chemistry Sampling Requirements

NRC Inspection and Enforcement (IE)Bulletin 80-10. was revisec

on May

l

11. 1998, to include quarterly sampling of the PRT. VCT. HUT and SRST.

The inspectors reviewed Amendment 13 to the UFSAR which stated that "The

online gas analyzer determines the quantity of oxygen and hydrogen in

'

the volume control tank, pressurizer relief tank, holdup tanks. gas

decay tanks, and spent resin storage tank by monitoring the waste gas

header, or by selecting the individual sample Joint.

The waste gas

analyzer provides an alarm on high oxygen and lydrogen concentration."

Amendment 13 was the "living" UFSAR when the waste gas analyzer

f.

t

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17

modification was planned and implemented. Amendment 13 was formally

issued in March 1998.

In March 1998 the licensee revised the "living" UFSAR. Amendment 14. to

correctly state the present as built design of the waste gas analyzer

system. That amendment stated that. "The online gas analyzer determines

the quantity of oxygen and hydrogen in the waste gas decay tank that is

in service. The Volume Control Tank. Pressurizer Relief Tank. Holdup

Tanks, and Spent Resin Storage Tank may be analyzed by grab sample as

plant conditions require.'

'

By the end of this inspection period, the licensee had recommended

)

several corrective actions as part of a root cause investigation for PER

S0980240PER. However, the licensee had not yet demonstrated the ability

to consistently take reliable gas samples from the PRT. A DCN has been

drafted to modify the sampling system piping to allow unobstructed grab

samples to be taken.

c.

Conclusions

One violation was identified for failure to perform an adequate safety

evaluation prior to making modifications to the waste gas analyzer

system.

E2.2 Hgron Accumulation on Containment Coolers

a.

Insoection Scooe (37551)

The inspectors reviewed the licensee's Technical Operability Evaluation

(T0E) and corrective actions regarding the boron accumulation on the

Unit 1 lower compartment coolers (LCC).

o.

ObsWVations and Findinas

The licensee identified in PER No. SO980347PER that a Unit 1

unidentified reactor coolant system (RCS) leak was causing boron to be

dispersed in the air in lower containment.

(IR 50-327, 328/97-18

discussed the increase in Unit 1 unidentified RCS leakage.) The

airborne boron then plated out on any wet surface. As air was drawn

into the LCCs the boron accumulated on the wetted portions of the

cooler coils. On April 1. 1998, system engineers performed a

walkdown/ visual inspection of all Unit 1 LCC coils.

LCC B-B was

observed to have the most accumulation of boron on its cooling coils as

com)ared to the other LCCs. The ins)ection also showed that the amount

of Joron in the fan rooms was more tlan had been seen previously during

j

a similar inspection in February 1998.

On April 8.1998, the licensee made an entry into Unit 1 lower

containment fan room 1 to measure airflow of the B-B LCC.

The data

obtained was used for TOE 1-98-030-0347-00 and TVAN calculation MDQ1030-

980016 to determine how the heat removal capacity of the coolers was

affected by the boron buildup.

The analysis concluded that boron

'

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, _

L

L

18

accumulation on the B-B LCC cooler would not reduce the heat removal

capacity of the cooler to below design heat load arovided that the ERCW

temperature heat sink remained equal to or less t1an 72 F.

During the

time the TOE was in effect. ERCW temperatures were less than 72 F.

On April .16.1998, operators changed the inservice LCC fan combination

and removed LCC B-B from service.

ERCW still flowed though the-cooling

coils and thus, with the fan stopped, condensation on the coils

increased as did the accumulation of boron on the coils (washing).

Later on April'23. 1998, operators isolated ERCW to the B-B LCC. but the

fan remained inservice. With no ERCW cooling to the cooler the

l

condensation on.the cooler coils stopped and the boron dust was blown

away by the cooler fan (baking). The air flow was significantly

l

improved following the. evolution. On April 29. 1998, system engineers

{

l

measured the air flow of LCC B-B and noted an improvement of about 60%

l

-in the air flow. After this successful evolution, the licensee took new

L

air flow measurements and recalculated t5ct a maximum allowed ERCW

temperature of 84.5 F would allow the LCC to perform within their design

i

basis. Based on the reevaluation, the TOE was closed on May 15, 1998.

The inspectors reviewed the licensee's calculations and field data and

concluded that the TOE closure was appropriate.

c.

Conclusions

System Engineering successfully developed and implemented an action plan-

to remove boron from the Unit I lower compartment coolers. This is a

positive finding.

_

E2.3 Steam Dumo Water Hammer Event Followino Plant Shutdown

a.

Insoection Scooe (37551)

The inspectors reviewed the Unit 1 steam dump water hammer event which

occurred several hours ~after the May 19. 1998, automatic reactor trip.

b.

Observations and Findinos

Following the Unit 1 reactor trip on May 19, the inspectors walked down

. the steam dump system to verify 3 roper operation._

Immediately following

the trip. the inspectors noted tlat the steam dump system was operating

as' designed.. Previous improper steam dump o)eration at the Sequoyah

~ ite had resulted in significant piping and langer damage and, as a

s

result, the. licensee had implemented several design changes to improve

operation'of the system.

On May 20, during the reactor startup, the inspectors noted a deficiency

tag on steam dump valve 1-FCV-1-111

When questioned about the

deficiency the control room operators noted that 1-FCV-1-111 was

isolated and would remain isolated due to damage from a water hammer

!

event. --The ins)ectors walked down the . steam dump system again and

'

observed that tie'line from steam dump valve 1-FCV-1-111 to the

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- _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _

_.

..

19

condenser was being supported with a chain fall.

One of the three

spring can supports had been broken.

Subsequent discussions with the licensee indicated that after the one

steam dump isolation discharge valve had been isolated for corrective

maintenance. the downstream discharge line filled with condensation from

the condenser. The licensee reported that due to a long horizontal run

of the line, as the line filled with condensation, steam trapped in the

line collapsed and caused a water hammer event.

In addition,

j

discussions with engineering indicated that the discharge of the

condensate booster pump recirculation line into the condenser

would/could cause rapid filling of this steam dump line and that this

was a known problem that had not yet been resolved.

'

In October 1996, water in the steam dump line on Unit 2 caused a

significant water hammer event that resulted in cracking of the main

steam supply piping from the main steam header to the steam Jump system.

Since the event, the licensee had implemented several modifications to

improve the operation of the steam dump system. However, based on the

water hammer event on May 19, 1998, the continuing problems with the

steam dump system are being identified as a weakness.

Following the water hammer event, the licensee inspected the steam dump

piping welds and did not identify any indications of pipe cracking based

on visual and magnetic particle inspections.

However. licensee

management decided that this steam dump line would remain manually

isolated until the next refueling outage. Although the licensee

conducted surface inspections of the piping welds, ultrasonic testing of

the welds could not be performed due to the high temperature of the

piping.

c.

Conclusions

A weakness was identified due to continuing steam dump system problems

,

which resulted in the May 19. 1998, water hammer event and piping

support damage.

E2.4 Unit 2 Steam Generator Looo Four (2-SG-4) Hydraulic Snubber Fluid Leak.

a.

Insoection Scoce (37551)

The inspectors observed onsite engineering response to the discovery of

a loss of SG snubber hydraulic fluid.

b.

Observations and Findinos

On April 29, 1997, during a weekly Unit 2 containment inspection, an AUO

observed that fluid could not be seen in the sight glass of the

reservoir servicing five Paul Munroe Snubbers for the Unit 2 number 4

steam generator.

Hydraulic fluid was immediately added to restore fluid

to normal and level was monitored to assess leak rate. A potential

_ _ _ _ _ - _ _ _ _ - _ _

_ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _

,

20

snubber operability concern, under TS 3/4.7.9 was recognized and

addressed on April 30, in TOE 2-98-068-0489.

The T0E concluded the snubbers would remain operable as long as fluid

level could be maintained in the reservoir and, based on the volume

required to refill the reservoir, sufficient fluid had been continuously

available to maintain uninterrupted snubber o)erability.

PER No.

SO980489PER was generated on May 4 to track t1e issue.

The licensee used a flexible neck fiber optics camera to identify the

L

'

leaking flexible hoses connecting the reservoir to the snubbers. Direct

personnel access to the area was not attempted due to high at-power

radiation levels.

' The licensee's ins)ections indicated that the leaking fluid had not come

into contact with lot piping which could have been a concern due to the

'

potential for production of hazardous decom)osition gases. The Material

. Safety Data Sheet and licensee-conducted la3 oratory tests confirmed that

lost lubricant posed a negligible fire loading risk.

The licensee

reported a long term corrective action plan to replace the present

clamp-type flex fittings with more reliable threaded fittings at the

next scheduled outage. subsequently installed a temporary drip

collection apparatus until permanent repairs can be effected.

'

c.

Conclusions

A positive finding was identified concerning engineering support of

' facilities and equipment when a licensee-identified steam generator

hydraulic snubber leak was properly assessed for operability and a

thorough corrective action plan was promptly implemented.

LE2.5 Inservice Testina Proaram Activities

a.

Insoection Scooe (37551 and 73756)

The. inspectors observed all or portions and reviewed documentation of

the following pump testing as required by the ASME Section XI IST

program as implemented through the technical specifications and 10 CFR 50.55a(f).

. -

1-SI-SXP-063-201.B." Safety Injection Pump B-B Performance Test".

-

2-SI-SXP-072-201.A," Containment Spray Pump 2A-A Performance Test".

,

,

b.

Observations and Findinas

Tests

The inspectors observed the quarterly test on Containment Spray Pump 2A-

A and Safety Injection Pump B-B and reviewed the test procedures for

these pumps. Calibrated test instrumentation for flow and pressure

,

-measurements met code requirements for accuracy and range.

Vibration

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21

data were collected from pre-identified points on the equipment.

These

data were verified to be in the acceptance range and stored for later

analysis by engineering. The test parameters of flow, pressure and

vibration data met the ASME code acceptance criteria.

The tests were

successful and performed in accordance with the test procedure.

Trendina

The inspectors reviewed the trending plots for certain pumps in the

auxiliary feedwater, safety injection. containment spray anc emergency

raw cooling water systems.

Data indicated that the pumps met the

frequency requirements and acceptance criteria for differential pressure

and vibration over the last 12 months.

Sequoyah is in the early stages of improving their ability to analyze,

track and trend IST data with the acquisition of a new software system.

The new software program has the capability of retrieving for each

component in the IST program specific test, design and maintenance

information.

The inspectors considered the new analysis tracking and trending

capabilities a positive addition to the IST program.

c.

Conclusions

Observation of pump tests, review of pump test procedures, and review of

pump parameter trend data indicated that the licensee has established

and implemented an adequate pump IST program.

The ins)ectors noted that

the limiting values for pump acceptance criteria were Jased on the most

conservative of the technical specification, design basis, or code

calculated values. Additionally, the acquisition of a new software

program for analysis, tracking and trending IST data was considered a

positive addition to the IST program.

E2.6 Maintenance Procedures and Documentation

a.

Insoection Scone (73756)

The inspectors e iewed various aspects of the ASME Section XI IST

program as implemc ted through the technical specifications and 10 CFR 50.55a(f).

b.

Observations and Findinas

Scooe of the IST oroa am

The inspectors reviewed the Program Basis Document. Revision 5. plant

system drawings, and the design criteria documents for the auxiliary

feedwater safety injection, and component cooling water systems.

This

review was performed to verify that the appropriate components had been

included in the test program.

The inspectors did not identify any

components omitted from the test program in this review.

.

-___ _ _

- _ - . .

,

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_ _ _ _ _ - _ _ _ _ - - _

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22

Valves

The inspectors did not witness any valve testing but did review test

procedures frequency of testing and implementation of the test

schedule.

The following procedures were reviewed:

0-SI-SXV-003-266.0. ASME Section XI Valve Testing. Revision 3

I

2-SI-SXV-00-201.0. Full Stroking of Category "A" and "B" Valves During

Operation. Revision 0

2-SI-SXV-000-203.0. Full Stroking of Category "A" and "B" Valves During

Cold Shutdown. Revision 0

The test procedures were well written and easy to follow. Acceptance

criteria were included in each procedure. The procedures documented the

test results and were reviewed for any change in schedule by the IST

Lead Engineer.

For a selected set of valves the inspectors reviewed the

performance tracking records for two cycles and specific valve tests for

the last two quarterly tests.

The inspectors found that the licensee

had implemented.and controlled test frequency.

Sfroke Time Testina of CCS Outlet Isolation Valves on RHR Heat

Exchanaers

- Inspection Report 50-327, 328/98-03 documented inspector concerns

regarding the licensee's ASME Section XI testing of CCS valves.

URI 50-

327, 328/98-03-06 was o)ened to identify potentially inadequate valve

testing, specifically tie CCS outlet isolation valves on the RHR heat

exchangers. FCV-70-153 and FCV-70-156 for both units. The ASME

Inservice Valve Testing Program Basis Document. ) age 15. Stroke Time

Test.. states that: " power operated valves shall lave their stroke time

measured while traveling to the position (s) denoted in Appendix A.

Appendix A-ASME Inservice Valve Testing Tables, requires that Valves

- FCV-70-153 and FCV-70-156 only be stroke timed tested in the open

direction. This position is the automatic response direction or initial

response direction for MOVs.

MOVs are not stroke timed in both

directions of travel." The licensee does exercise valves FCV-70-153 and

FCV-70-156 in both directions, but only times them in the open

'

direction.

Subsequent to the initial inspection. the ins)ectors, after further

- review, concluded that Valves FCV-70-153 and ~CV-70-156 have functions

which could require them to be stroked in either direction during

accident conditions. As an example, following an accident, only one

train of RHR could be required to be inservice due to the alignment or

failures ~of CCS pumps.

Emergency Abnormal Procedure. EA-74-1. Placing

RHR Shutdown Cooling in Service, specifically refers to placing one

train of RHR in cooldown mode, which indicates that Valves FCV-70-153

and FCV-70-156 would have to be opened or closed to achieve the desired

-lineup.

Based on this review, the inspector determined that these

,

valves have both an open and closed function.

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23

Technical Specification 4.0.5. Inservice Testing Program, requires that

inservice testing of ASME code Class 1. 2. and 3 pumps and valves shall

be in accordance with Section XI of the ASME Boiler and Pressure Vessel

code and applicable Addenda as required by 10 CFR 50.55a. Codes and

Standards. Section (f). Inservice Testing Requirements.

10 CFR 50.55a

identifies ASME/ ANSI OM-1987 edition of the code and Oma-1988 addenda as

the required codes. ASME/ ANSI OMa-1988 Addenda to ASME/ ANSI OM-1987.

Operation and Maintenance of Nuclear Power Plants. Part 10. Section

4.2.1.2. Exercising Requirements. Part (a) requires that valves shall be

.

tested to the position (s) required to fulfill its functions (s). The

failure to strole time test Valves FCV-70-153 and FCV-70-156 in both the

open and closed directions is identified as the first example of

,

'

violation. VIO 50-327, 328/98-06-04. Although this problem was

initially identified by the licensee, specific and comprehensive

corrective action to prevent recurrence had not been determined by the

licensee at the time the unresolved item (50-327, 328/98-03-06) was

identified ~ by the NRC.

Timeliness of Relief Reauests

The licensee's second 120 month IST Program interval started on December

15. 1995.

Prior to the interval start date, the licensee submitted

!

'

relief requests associated with the second 120 month program interval.

.Many of these requests for approval to perform alternative tests in

place of the code specified testing had been previously approved.in the

first 120 month IST 3rogram interval. .The NRC issued a Safety

Evaluation Report (SER) for-the second 120 month IST. program interval on

March 20. 1996.

In the SER relief requests RP-03. RV-05 and RV-06 to

perform alternative-tests were denied.

However, a 180-day delay was

granted on RP-03 for the licensee to. resubmit additional information.

Through an oversight, the licensee did not provide additional

'information for NRC review on RP-03 by September 20, 1996. The licensee

continued to conduct the alternate tests in RV-05 and RV-06 after. March

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20, 1996, and RP-03 after September 20, 1996, without NRC approval. The

L

licensee subsequently resubmitted requests for relief for RP-03. RV-05

'

and RV-06 in letters dated December 22, 1997 and April 16. 1998.

The

staff is in the process of evaluating these submittals.

Technical Specification 4.0.5 requires that inservice testing of ASME.

,

Code Class 1, 2 and 3 pumas and valves shall be performed in accordance

i

'

with Section XI of the ASiE Boiler and Pressure Vessel Code and

-

a)plicable addenda as required by 10 CFR 50. Section 50.55a. except

L

w1ere . specific written relief has been granted by the Commission.

10 CFR 50.55a. (a)(3) provides for alternative tests but requires NRC

approval prior to implementation.

Performing alternative tests without

. prior NRC approval is identified as the second example of violation. VIO

50-327.328/98-06-04.

,

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24

Relief Valve Procedure

During the review of Procedure 0-ST-SXV-000-264.0. Testing Setpoints of

Safety and Relief Valves (ASME Section XI Category C Valves). Revision

0. the test procedure for Class 2 and Class 3 pressure relief valves,

the inspector noted that the procedure did not contain a direction to

conduct a 10-minute hold time between valve openings. Technical specification 4.0.5 specifies that testing of ASME Code Class 1, 2. and

3 pumps and valves shall be performed in accordance with Section XI of

the ASME Boller and Pressure Vessel Code and applicable addenda as

required by 10 CFR 50.55a. Codes and Standards. Section (f). Inservice

Testing Requirements.

10 CFR 50.55a identifies ASME/ ANSI OM-1987

edition of the code and Oma-1988 addenda as the required codes.

ASME/ ANSI OM-1987 edition. Part 10 references Part 1 for relief valve

requirements.

Part 1. Paragra)hs 8.1.1.8. 8.1.2.8. and 8.1.3.7 require

a minimum 10 minute hold time 3etween valve openings.

Additionally

Paragraph 8.3.3(e) requires that the hold time be specified in a written

procedure.

Failure to s)ecify the minimum 10 minute' hold time in the test procedure

as required ]y the ASME code is identified as the third example of

violation. VIO 50-327.328/98-06-04.

c.

Conclusions

The inspectors concluded that the licensee has developed and implemented

an IST program which. in general. is consistent with the regulations and

the ASME Boiler and Pressure Vessel.Section XI code.

However, one

violation, with three examples, for failure to adecuately-im]lement

Section XI code testing requirements was identifiec during t1e

inspection.

E8

Miscellaneous Engineering Issues (92903)

E8.1

(Closed) URI 50-327. 328/98-03-06. Potential Inadeauate Section XI Valve

Stroke Testina. Section E2.6 of this report identified violation 50-327,

328/98-06-03 for inadequate Section XI valve stroke testing.

Based on

this violation, the unresolved item is considered to be closed.

E8.2 (Closed) IFI 50-327/97-18-06. Followuo on Concern with Two Year

Surveillance on Remote Position Indication Verification.

The issue of

performing the two-year remote position verification was reviewed during

the region based inspection of the ASME Section XI pump and valve

testing program.

Based on a review of the licensee's program and

discussions with regional and NRR inspectors. the inspector concluded

that the licensee was adequately implementing the Section XI requirement

for valve remote position indication verification.

E8.3 (Closed) VIO 50-328/98-01-01. Failure to Perform a 10 CFR 50.59

Evaluation for Chanaes Made to the 2A-A Motor Driven AFW Pumo.

The

j

licensee's response dated April 29. 1998. was considered acce] table.

The inspector reviewed procedure SPP-3.1. Corrective Action,

Revision 0.

{

)

_

_ _ _ _ - _ _ _ _ _ _ _ _ - .

__- __ _ _ _ .

_

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_ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

!

25

and verified that the corrective action program had been revised to

include the guidance of Generic Letter 91-18. Revision 1. concerning the

disposition of degraded and non-conforming items.

The inspector also

reviewed the following documents prepared and used in connection with

the replacement of Unit 2 MDAFW pump with a pump from Watts Bar:

Design Change Notice (DCN) T-12799A. Replacement of motor driven

.

AFW pump 2A-A. Revision 0.

Work Order (WO) No. 97-001409-000. Implement DCN T-12799A.

.

Replace 2-PMP-003-0118/2A MDAFWP with WBN MDAFWP. dated January

15. 1997.

Work Controlling Document No. 2-PI-SFT-003-727A. Motor driven AFW

.

pump 2A-A full flow test, dated November 2. 1997

Work Controlling Document No. 2-SI-SXP-003-201A. Motor driven AFW

.

pump 2A-A performance test. Revision 2.

Based on review of the above documents the inspector verified that MDAFW

pump 2A-A was replaced with a pump from Watts Bar Nuclear Facility.

The

replacement pump had both performance and full flow tests performed and

satisfactorily met all acceptance criteria.

The replacement pump was

declared operable and returned to the operations staff on October 30,

1997.

This item is closed based on objective evidence reviewed.

E8.4

(Closed) VIO 50-327.328/97-03-08. Untimely Corrective Action for Non-

conformina Pl?nt 'ondi ti ons .

The licensee's response dated June ll.

1997, was considered acceptable.

The ins)ector reviewed the corrective

actions completed in connection with PER

10.

SO940040II. TROI Sequence

item 36.

Based on this review the inspector verified that 14

essentially mild calculations had been revised by design change notices

(DCNs) M-08779 and M-08780 to specify accident radiation doses based on

i

a source term of 1000 effective full power day (EFPD) average core

i

exposure.

The calculations were also revised to delete references to

environmental drawings and added references to Design Criteria Document

No. SON-DC-V-21.0.

One hundred and fourteen E0 binders were also

revised to address the environmental parameters in design criteria SON-

DC-V-21.0.

The inspector reviewed the revision log of 12 randomly

selected E0 binders and verified that they had been revised to delete

references to environmental drawings and to include accident radiation

doses based on 1000 EFPD average core exposure.

This item is closed

based on objective evidence reviewed.

E8.5 (Closed) VIO 50-327.328/97-03-09. Inadeouate J)esian Control for Non-

conformina Plant Conditions.

The licensee's response dated August 20,

1997, was considered acceptable.

The inspector reviewed design basis

!

calculation TI-RPS-48. Integrated Accident Doses Inside of Primary

Containment. Revision 6. and verified that the maximum 100-day

integrated doses inside the containment and annulus were based on an

average core exposure of 1000 EFPD with 5% U-235 enrichment.

The

maximum 100-day integrated doses inside containment and the annulus were

_ _ _ - _ - - _ _

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26

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calculated to be 3.157 E+7 rads beta and 6.83 E+6 rads gamma.

l

Additionally, the 100-day free field beta dose doses were determined to

be 6.311 E+8 rads and 1.009 E+6 rads for the containment and annulus

respectively. The inspector reviewed design criteria SON-DC-V-21.0.

Environmental Design, and verified that 'it had been revised to

incorporate thel 100 day integrated accident doses delineated in

,

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calculation TI-RPS-48. Revision 6.

L

UFSAR Section 15.1.7.1. Activities in the Core, states that the design

l

basis LOCA' source terms are based on an average core exposure of 1000

EFPD with an enrichment of 5% U-235.

The UFSAR also requires each

l

reload fuel evaluation to verify that the consequences of an accident

previously evaluated has not changed. The inspector concluded that with

issuance of the above design output documents and changes to the UFSAR

incorporated by Amendment 13 the licensee has established consistency

i

between the plants licensing basis and the design criteria used for 10

l

- CFR 50.49 environmental qualification of electrical equipment. This

L

item is closed based on objective evidence reviewed.

E8.6 (Closed) IFT 50-327.328/98-01-05. Turbine Driven AFW Pumo Room Exhaust

'

l

Fan E0. .The result of the SSEI concluded that flow rate of the DC

l

exhaust fan for the turbine ~ driven AFW pump' room was reduced without a

'

formal revision to the calculation. The SSEI also determined that the

calculation did not address events such as station blackout (SB0) and

that the upper temperature of 120 degrees Fahrenheit was not used for

environmental qualification of the DC exhaust fan.

The inspector. reviewed design output documents and verified the

technical adequacy-of the calculated air flow rates for the following

conditions:

Air flow rate required to maintain normal maximum temperature of

104 degrees Fahrenheit.in the room with all three fans in

operation.

. .

Air flow required to maintain the LOCA maximum temperature of 110

degrees Fahrenheit in the room with the emergency A.C. and D.C.

exhaust fans in operation.

Air flow required to maintain the LOCA maximum temperature of 110

degrees Fahrenheit in the room with only the D.C. emergency

exhaust fan in operation during a loss of off-site power.

The following design output documents were reviewed:

Design Criteria SON-DC-V-21.0 Environmental Design. Table 1.

' Auxiliary Building. Elevation 669. TD Aux. feedwater pump room

U-1.

Calculation No. EPM-DLM01-030887. SON HVAC Verification Program :

  • -

HVAC Cooling Load calculations: Aux. Bldg. TDAFW Pump Room, dated

June 2. 1987.

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27

Calculation No. SON-31C-D053-EPM-RG-060987 HVAC Equipment

a

Requirements Evaluation: TDAFW Pump Room, dated May 19. 1998.

Drawing CCD No. 1, 2-47W920-2. Mechanical Heating and Ventilating

.

and Air Conditioning. Revision 2.

The inspector verified that the heat loads documented in calculation

EPM-DLM01-030887 and which were used as design inputs for calculation

SON-31C-0053-EPM-RG-060987 were correct.

The total heat load at the

maximum temperature during a loss of off-site ]ower was documented in

calculation EPM-DLM01-030887 as 37636 BTUH.

T1e heat load used for

calculating the air flow required under this condition was 35.516 BTUH.

The reason given for this difference was that the D.C. fan motor heat

load of 2120 BTUH was subtracted from 37636 BTUH because the fan motor

was installed outside the room.

The installation details for the 0.5 HP

D.C. emergency exhaust fan was verified from drawing number 1,2-47W920-

2.

The inspector determined that the heat load of 35516 BTUH used in

the calculation for determining flow rates with only the D.C. fan in

o]eration was justified.

Based on this review the inspector concluded

tlat the required flow rate of 1077 CFM determined by analysis was

correct.

The supplied flow rate of 1200 CFM provided a 10% margin which

ensured that the LOCA maximum temperature of 110 degrees Fahrenheit will

not be exceeded with only the D.C. emergency fan in operation during a

loss of offsite power. This item is closed based on objective evidence

reviewed.

E8.7 (Closed)IFI 50-327.328/98-01-06. Terry Turbine Governor Minimum Voltaae

Requirements.

During the SSEI TVA 3rovided documentation which

supported the licensee's position tlat the required minimum terminal

voltage of 100 Volts D.C. at the terminals of the Woodward governor was

acce] table. WA had no documentation, however, from the governor vendor

whic1 corroborated the minimum voltage requirements identified by the

turbine vendor.

The inspector reviewed the following documents in

connection with resolution of this item:

Calculation No. SON-VD-VDC-001. 125 Volts D.C. Instrument Power

.

System. Appendix 11. dated January 1. 1998.

Drawing CCD No.1-45W646- 6. Wiring Diagrams Feedwater Pump

.

Turbines Schematic Diagrams. Revision 2.

Facsimile from Woodward Governor Co. to TVA dated May 12. 1998.

.

Subject: EGM Power Supply.

The governor vendor in the referenced facsimile stated that test data

demonstrated that a 20% variation in input voltage to the power resistor

assembly, i.e.

120 VDC to 95 VDC. resulted in a 6% variation of input

voltage to the EG-M control box.

The vendor verified that the

controlling minimum voltage requirement was the input to the EG-M

control box. The vendor also stated that at minimum voltage to the

power resistor assembly, the minimum voltage to the EG-M control box.

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terminals 1 and 2. must be 42 VDC in order to conservatively assure

reliable operation.

Based on review of design-basis calculation SON-VD-VDC-001. Appendix M.

the inspector determined that the worst case calculated voltage to the

EG-M control. box was 102.96 Volts with a minimum voltage of 103 Volts to

o

the power resistor assembly. .This value of-103 Volts was calculated at

the end of the.125 VDC battery 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> duty cycle when the battery

terminal. voltage was 104.4 Volts. The inspector concluded that a

minimum voltage of 100 Volts to the EG-M control box was acceptable

based on the vendors test data which. bounded the worst case calculated

voltage of 102.96 volts. This item is closed based on review of

objective' evidence.

IV. Plant Sucoort

R8

. Miscellaneous RP&C Issues (92904)

R8.1- (Closed) VIO 50-328/97-18-07: Personnel Monitorina Discrepancies: Two

examples of not pro)erly frisking out of a posted radiologically

controlled area. T1e inspector reviewed the corrective actions

described in the licensee's response letter. dated March 13. 1998, to be

reasonable and complete.

No similar problems were identified.

S1

Conduct of Security and Safeguards Activities

..

a.

'Insoection Scooe (81700. 92904)

The purpose of the inspection was to determine whether the conduct of

. security and safeguards activities met the licensee's commitments in the

NRC-approved security plan (the Plan) and NRC regulatory requirements.

The security program was inspected during the period of April 27 to May

1. 1998.

Areas inspected. included the access authorization program,

alarm stations and communications, and protected area access control of

personnel and hand-carried packages

b .-

Observations and Findinas

Access Authorization (AA) Proaram-

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The inspector reviewed implementation of the AA program to verify

implementation was in accordance with applicable regulatory requirements

,

.and Plan commitments. The review included an evaluation of the

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' effectiveness of the AA procedures, as implemented.'and an examination

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of AA records for 46 individuals.

Records reviewed included both

persons who had been granted and had been denied access. The AA

program, as, implemented, provided assurance that Jersons granted

unescorted access did not constitute an unreasonable risk to the health

and safety of the'public. Additionally, the inspector verified by

reviewing access denial records that appropriate actions to remove

individuals' access were taken when individuals were denied access or

access was terminated.

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Alarm Stations-

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The inspectL caserved operations of the Central Alarm Station and the

Secondary Alarm Station and verified that the alarm stations were

equi) ped with appropriate alarms, surveillance and communications

capa)ilities.

Interviews with the alarm station operators found them

knowledgeable of their duties and responsibilities. The inspector also

verified, through observations and interviews, that the alarm stations

were continuously manned, independent, and diverse so that no single act

could remove the plant's capability for detecting a threat and calling

L

for assistance, and the alarm stations did not contain any operational

'

activities that could interfere with the execution of the detection,

assessment, and response functions. . The inspector closed violation

97-07-01, concerning failure to take required compensatory ~ action during

a security system failure. The NRC did not require a response to the

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violation because the' corrective actions taken and )lanned to correct

.the violation and prevent recurrence and the date w1en full compliance

i.

was achieved was already adequately addressed on the' docket in IR 50-

i

327. 328/97-07, dated July 24. 1997.

L

Communications

The inspector verified. by document reviews and discussions with alarm

station operators, that the alarm . stations were ca)able of. maintaining

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continuous intercommunications. communications wit1 each security force

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member (SFM) on duty, and were exercising communication methods with the

'

local law enforcement agencies as committed to in the Plan.

Protected Area (PA) Access Control of' Personnel and Hand-Carried

Packaaes

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L On April 29 and 30,1998, the inspector observed personnel and package

'

search activities at the personnel _ access portal. The inspector

determined.:by. observations. -that positive controls were in place to

ensure only authorized individuals were granted access to the PA and

that all personnel and hand-carried items entering the PA were )roperly

searched. ~However, the' inspector determined during review of tie

l

Security Event Logs (SELs) that on May 8. October 22.. December 11, 1997.

and March 27. 1998. individuals had gained access to the PA without

,

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utilizing the badge and hand-geometry system at the vehicle sally port.

The four individuals were licensee employees-who were authorized

unescorted access.

Based on the SEL dated May. 8.1997. the officer at

the ' sally port failed to ensure that the individual entering the PA used

the card reader and hand-geometry.

The-licensee determined that'the

i

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event was caused by personal error and a warning letter was placed in

the individual's file. - On October 22. 1997, another officer at the

sally. port failed to ensure that the individual entering the PA used the

card reader and hand-geometry. The licensee stated that as corrective

L.

action. "the card reader was relocated to_ provide the officers with a '

better view of.the card reader and hand geometry to ensure that this

type event did not reoccur." Additionally, they stated that they

retrained the officers and took disciplinary action against the

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individual.

However, the licensee was unable to provide the inspector

with any documentation to validate these statements.

On December 11.

1997, a third event occurred at the sally port when a security officer

failed to assure that an individual entering the PA used the card and

hand-geometry reader to gain access.

The officer was counseled and no

further action was taken.

On March 27. 1998, the fourth event of an

officer failing to control access via the card reader and hand-geometry

reader at the sally port occurred. The corrective action for the event

was closed with the statement that "the officer no longer was employed

by the Tennessee Valley Authority (TVA)."

The inspector identified that the initial corrective actions had failed

to be effective in that the same type events were continuing to occur.

Based on the inspectors findings the events do not meet the criteria of

NUREG-1600. VII B.1 to be classified as a Non-Cited Violation. Security

management stated that they had viewed the events as single occurrences

over a year period and had not noted that there was a continuing trend

of failing to control access at the sally port. After senior management

became aware of the events. immediate and thorough corrective action was

implemented. The corrective action as of May 1. 1998 was:

.

I

-

To write a problem evaluation report (PER) (S0980501)

-

To require the security officer at the sally port to physically

take the badge and swi)e it through the card reader and then

watch the person use tie hand-geometry

-

To issue temporary orders to the sally port officers limiting

the number of vehicles in the sally port to one

-

To dispatch supervision to the sally port to verify that the new

post orders and officer actions were acceptable and to discuss

the new requirements with the officer on post

-

To ensure that all TVA and contractor supervision understand the

problem, and the immediate corrective action

-

To brief the event at the plan of the day meeting

-

To issue a site bulletin on changes that were made at the sally

port

,

-

To require senior management to review all security event

reports for trending and analysis

-

To present selected security PERs to the Management Review

Committee for their consideration

,

Additionally, the licensee is continuing to review the event and are

.

considering additional corrective actions.

l

_ _ _ _ _ _ _ - _ - _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _

__

31

Paragraph 5.2.4. Revision 4. dated September 10. 1996, states.

" Verification of each individual will be with the hand geometry system

which provides a nontransferable means of identifying individuals,

coupled with the badgecard reader.

Both the badgecard and hand geometry

shall be necessary for normal access to the PA.

Hand geometry shall

provide assurance that only authorized personnel are allowed access to

the PA."

Physical Security Instruction - 32. Revision 16. Appendix N. Post 12.

and 13 - Vehicle Search / Access Control, paragraph 3.6. states. " Ensure

individuals with PA badges utilize the hand geometry readers."

On May 8. October 22. December 11. 1997, and March 27. 1998, an

individual did not utilize the badge and hand-geometry system prior to

entering the PA at the vehicle sally port.

The four individuals were

licensee employees who were authorized unescorted access.

The failure to

properly control access at a sally port constitutes a violation (50-327,

328/98-06-05).

c. Conclusions

The licensee was conducting its security and safeguards activities in a

{

manner that protected public health and safety and this portion of the

'

program, as implemented. met the licensee's commitments and NRC

requirements.

i

A violation was identified for failure to properly control access at the

sally port on four different occasions.

S2

Status of Security Facilities and Equipment

a.

Insoection Scooe (81700)

Areas inspected were:

Testing, maintenance and compensatory measures. PA

detection aids, and PA assessment aids.

b. Observations and Findinas

Testina. Maintenance and Compensatory Measures

The inspector reviewed testing and maintenance records for security-

related equipment and found that documentation was on file to demonstrate

that the licensee was maintaining. and with the exception of the PA

intrusion detection system,

testing systems and equipment as committed

to in the Plan. A priority status was being assigned to each work

request and repairs were normally being completed within the same day a

work request necessitating compensatory measures was generated.

The

inspector reviewed SEls and maintenance work recuests which were

generated over the last year.

These records incicated that the need for

compensatory measures was minimal.

When necessary, the licensee

,

1mplemented compensatory measures that did not reduce the effectiveness

!

E_________

_ _ _ _ _ _

_ __

_ - . . . _ _ _

_

_j

_- _

-___ __ __ - ___ _ _ _ _ _ _ - _ _ _ __

i

32

of the security; system as it existed prior to the need for the

I

compensatory measure.

Assessment Aids

'On April 29, 1998.~ the inspector evaluated the effectiveness of the

assessment aids. by observing on closed circuit television.'a SFM

conducting a walkdown of the PA. The assessment aids had good picture

quality and excellent zone overlap. Additionally, to ensure Plan-

-commitments were satisfied, the licensee had procedures in place

requiring the implementation of compensatory measures in the event'the

alarm station operator was unable to properly assess the cause. of an

alarm.

PA Detection Aids

'On April 29. 1998, the inspector observed testing of five of the

~ intrusion detection systems in the plant PA. The zones tested were

capable of. detecting. attempts to pass'a sphere under (to simulate

crawling) and over (to simulate-jumping) the intrusion detection system

1(microwave).

The inspector' observed four. attempts by an-individual to

l

pass through the E-Field. The inspector..while reviewing the seven day

)eriodic instruction (PI) PI-SS0S-000-630.W. "Seven Day Functional Test

or Non-Card readers: Alarms and Closed Circuit Televisions'.' Revision 4.

'

. dated November ~7. 1996, and the annual testing procedure (" Post

Maintenance Testing No. 92.~ Revision 0). determined that the licensee

l

had established procedures to test the security equipment.

However. as

part.of the testing procedure, the licensee had not established a

consistent testing method and the number of. tests.to be conducted for

each system.

Therefore, the security equipment may not function to the

licensee's expectations. During discussion with-the licensee concerning

their testing measure they also had concluded that a method and standard

needed to be established to ensure the security detection equipment

operated to the ex)ectations. The licensee had scheduled a meeting on

May 6. 1998, for.tle three TVA nuclear facilities to develop an equipment

testing-method.

Upon detection of equipment failures, the licensee

implements immediate corrective actions which included the establishment

of compensatory measures and submission of a work order to the I&C

3

Department. The inspector determined, by observations and by reviewing

'

the testing documentation associated with the equipment repairs. that the

repairs were made in a timely manner and that the equipment was

. functional and-effective, and. met the requirements of the Plan,

c. Conclusions

j

-The -licensee *s security- facilities and equipment were determined to be

very well-maintained and reliable even though a test procedure for-

L

standardized testing of the intrusion detection equipment had not been

9

. developed.

4

'

Y

._ -

_

_.

. _ - -

_ _ - _ _ _ _ _ _ _

_ _ _ - _ _ _ - _ _ - _ _ _ _ _ _ _ _ _ _____

33

The excellent Engineering and I&C su) port was the major contributing

factor to continued operability.of t1e detection and assessment

equipment.

- S4_ Security and Safeguards Staff Knowledge and Performance

a.

Insoection Scooe (81700)

. Areas inspected were security staff requisite knowledge and response

capabilities.

b. Observations and Findinas

Security Force Recuisite Knowledae

The inspector observed a number of SFMs in the performance of their

routine duties

These. observations included alarm station operations,

i

personnel and package. searches. and visitor processing. Additionally.

the ' inspector interviewed SFMs and security management.

Based on all of

the above activities. it was determined that the SFMs were knowledgeable

of their responsibilities and duties, and could effectively carry out

their. assignments.

Resoonse' Capabilities

l

On April 29, 1998, the inspector conducted a review of the documentation

i

of: drills for May 20. June 1. July 29-30. August 6. 7 & 9. Se)tember 23- ,

October 1 & 2. 1997, and April'8 & 10. 1998.

Additionally, tie lnspector

reviewed the table-top time line drills conducted September 12 & 28.

November 1, 2 & 24, December 7 & 10. 1997, and January 3. 11 &.17, 1998.

The drills were developed by using the target sets developed and refined

by the licensee and the Operational Safeguards Response Evaluation.

The

benchmark _for the drills was the NRC design basis threat. The criteria

used by the licensee to determine response capability were:

(1) can the

isecurity force provide a sufficient number of. responders, (2) are they

. appropriately armed, (3) are they in protected fighting positions. and-

(4) will they be.in time to interdict armed intruders. The inspector, by

)

review of the licensee's drills and discussions with security personnel,

1

determined that the licensee's ability to defend against the design basis

threat is adequate.

c. Conclusions

The SFMs adequately demonstrated that they have the requisite knowledge

necessary to effectively implement the duties and responsibilities

-associated with their day-to-day and contingency response positions.

!

-

__ _ _ __

_ - - _ - _ _ _ - - _ - _ _ _ _ _ - _ _ - - - - _ _ _

_ - _ _ _

34

V. Manaaement Meetinas

X1- Exit Meeting Summary

The inspectors ] resented the inspection results to members of licensee

management at tie conclusion of the inspection on June 12. 1998, and on

May 1. May 15. June 4 and June 5.1998 (for regional based inspections).

The' licensee acknowledged the findings presented.

An inspectors' exit was held on May 22. 1998, and was not held with the

Residents closure exit. The licensee stated that they believed the

failure to test MOVs in both d;rectirs was licensee identified and met

the criteria;for a non-cited-7 olaticn. The inspectors stated that this

would be considered lit the Regics Management review.- A re-exit was held

by conference call on. June 4. 1998. At which time the examples failure

to test valve a in both directions when the valve had a safety function

' n both directions was discussed, the failure to meet 10 CFR 50.55a in

i

the timeliness of relief request submittal.s. and the failure to meet the

code requirements to include the hold. time between valve openings in test

procedures were identified as a violation. The-licensee restated his

position regarding the licensee-identified failure to test in both

directions when valve functions required both directions.

i

During the inspection period, the inspectors asked the licensee whether

..I

any materials would be considered proprietary.

No proprietary

information was > identified.

PARTIAL LIST OF PERSONS CONTACTED

Licensee

!

  • Bajestani. M., Site Vice President

Burton. .C. . Engineering and Support -Systems Manager

Butterworth. H., Operations-Manager

  • Gates. J.. Site Support Manager
  • Freeman. E., Maintenance and Modifications Manager

L

-*Herron. J.. Plant Manager

.

i

Kent. C.. Radcon/ Chemistry Manager

!

Koehl. D. , Assistant Plant Manager

O'Brien. B., Maintenance Manager

.

Salas. P.... Manager of Licensing and Industry Affairs

L

Valente. J., Engineering & Materials Manager

l

  • Attended exit interview

INSPECTION PROCEDURES USED

IP 37551

Onsite Engineering

IP 50002:

Steam Generators

-IP< 61726':

Surveillance Observations

IP 62700:

Maintenance

IP 62707:

Maintenance Observations

_ _ ___ _ _ __ _ _ _

35

IP 71707:

Plant Operations

IP 73756:

Inservice Testing

IP 81700:

Physical Security Program for Power Reactors

IP 92901:

Followup - Operations

i

IP 92902:

Followup - Maintenance

IP 92903:

Followup - Engineering

IP 92904:

Followup - Plant Support

ITEMS OPENED. CLOSED. AND DISCUSSED

Opened

Tvoe

,11pm Number

Status

Description and Reference

URI

50-327/98-06-01

Cpen

Potential Deficiencies: in

Maintenance and Inspection

Procedures Which Resulted In

Ice Condenser Ice Basket

Damage and Did Not Promptly

Identify the Damage (Section

M2.1).

URI

50-327/98-06-02

Open

Potential Improper Corrective

Maintenance Activities Related

to Improper Breaker Contact

Compression Setting and

Inadequate Post Maintenance

Testing (Section M2.3).

VIO

50-327, 328/98-06-03

Open

Failure to Perform an Adequate

Safety Evaluation Prior to

Making Modifications to the

Waste Gas Analyzer System

(Section E2.1).

VIO

50-327. 328/98-06-04

Open

Failure to Adequately

Implement Section XI Code

Testing Requirements (Three

Examples) (Section E2.6).

VIO

50-327. 328/98-06-05

Open

Failure to Implement Adequate

Access Controls at the Vehicle

Sally Port (Section S1).

Closed

11D.g

Item Number

Status

Description an(! Reference

URI

50-327. 328/98-03-03

Closed

Potential Failure to Meet

UFSAR Requirements. Failure to

Revise UFSAR. Inappropriately

Closing a Modification

_ _ _ - - _ _ _ _ _ _ _ .

,

36

Package and Not Establishing

i

a Periodic Sampling Program

for the Waste Gas Collection

System (Section 08.1).

URI

50-327/98-03-01

Closed

Potential Failure to Enter TS 3.11.2.5 LCO Action Statement

When Samples Indicated High

Concentrations of Oxygen in

the PRT (Section 08.2).

LER

50-327/97013. Rev. 1

Closed

Missed Surveillance as a

Result of an Inadequate

Procedure (Section M8.1).

IFI

50-327/98-03-04

Closed

Follow Licensee's Review of

the Section XI Valve Testing

Procedure to Determine if a

Better Method Would Be

Available to lest the CCS Pump

Discharge Check Valves

(Section M8.2).

URI

50-327. 328/98-03-06

Closed

Potential Inadequate Section

XI Valve Stroke Testing

(Section E8.1).

IFI

50-327/97-18-06

Closed

Followup on Concern with Two

Year Surveillance on Remote

Position Indication

Verification (Section E8.2).

VIO

50-328/98-01-01

Closed

failure to Perform a 10 CFR 50.59 Evaluation for Changes

Made to the 2A-a Motor Driven

AFW Pump (Section E8.3).

VIO

50-327, 328/97-03-08

Closed

Untimely Corrective Action for

Non-conforming Plant

Conditions (Section E8.4).

VIO

50-327. 328/97-03-09

Closed

Inadequate Design Control for

Non-conforming Plant

Conditions (Section E8.5).

IFI

50-327, 328/98-01-05

Closed

Turbine Driven AFW Pump Room

Exhaust Fan E0 (Section E8.6).

IFI

50-327. 328/98-01-06

Closed

Terry Turbine Governor Minimum

Voltage Requirements (Section

E8.7).

- _ _ _ _

_ - _ - _ _ _ _ _ _

. _ _ -

37

VIO

50-328/97-18-07

Closed

Personnel Monitoring

Discrepancies (Section R8.1).

VIO

50-327, 328/97-07-01

Closed

Failure to take required

compensatory action during a

security system failure

(Section S1).

LIST OF ACRONYMS USED

AA

Access Authorization

-

AFW -

Auxiliary Feedwater

APC -

Alternate Plugging Criteria

ASME -

American Society of Mechanical Engineers

AUD -

Assistant Unit Operator

CCS -

Component Cooling System

CFR -

Code of Federal Regulations

CRCM -

Control Rod Drive Mechanism

CVCS -

Chemistry and Volume Control System

DCN -

Design Change Notice

EC

-

Eddy Current

EDG -

Emergency Diesel Generator

EFPD -

Effective Full Power Days

EQ

-

Environmentally Qualified

ERCW -

Essential Raw Cooling Water

FCV -

Flow Control Valve

GL

-

Generic Letter

HUT -

Holdup Tank

HVAC -

Heating Ventilation and Air Conditioning

I&C -

Instrumentation and Control

IFI -

Inspector Followup Item

IR . -

Inspection Report

ISI -

In-Service Inspection

)

l

LCC -

Lower Compartment Cooler

l

LER

-

Licensee Event Report

.

LOCA -

Loss of Cooling Accident

MCC -

Motor Control Center

i

i

MDAFW . Motor Driven Auxiliary Feedwater

!

' MFW -

Main Feedwater

'

NRC -

Nuclear Regulatory Commission

NRR -

Nuclear Reactor Regulation

PA

-

Protected Area

PER -

Problem Evaluation Report

PI

Periodic Instruction

)

-

PM

-

Predictive Maintenance

PM

-

Preventative Maintenance

PMT -

Post Maintenance Test

PORV -

Power Operated Relief Valve

PRT -

Pressurizer Relief Tank

PWSCC-

Primary Water Stress Corrosion Cracking

RCS -

Reactor Coolant System

_ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _

_ -

_

_

~

, - _- _ - __ _

38

RHR -

Residual Heat Removal System

SEL -

Security Event Log

SFM -

Security Force Member

SG

-

Steam Generator

SI

-

Surveillance Instruction

SRST -

Spent Resin Storage Tank

SSEI -

Safety System Engineering Inspection

TDAFW-

Turbine Driven Auxiliary Feedwater Pump

TOE -

Technical Operability Evaluation

TROI -

Tracking and Reporting of Open Items

TS

-

Technical Specifications

TSIR -

Technical Sup) ort Investigation Request

TSP -

Tube Support ) late

TTS -

Top of tubesheet

TVA -

Tennessee Valley Authority

TVAN -

Tennessee Valley Authority Nuclear

UFSAR - Updated Final Safety Analysis Report

URI -

Unresolved Item

UT

-

Ultrasonic Testing

i

Vac -

Voltage Alternating Current

VCT -

Volume Control Tank

Vdc -

Voltage Direct Current

!

VIO -

Violation

WO

-

Work Order

WOG -

Westinghouse Dwners Group

,

WR

-

Work Request

l

)

l

l

!

l

_ _ _ _ _ _ _ _ _ _ _ _ _ _ .

_ _ _ _ _ _

,