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{{#Wiki_filter:to Ol'EltAlING DATA Ill.PoltT DOCKl.T NO.      5 0 '' h 6 DAll          8/3/79 COM11Eil D !!y          C,  conne11 TELLPilONE (914 ) 7i"-0200 OPI:lt ATING STAT US Notes
: 1. Unit Name: 3" H m Po i n+-
Mo. 3 Mucim Power Plant
: 2. !!cporting I'eriod:      Julv 1979
: 3. Licensed 1 hennal Power (MWt): _ 3025
: 4. Nameplate Itatin;;(Gross MWe): _ 1013
: 5. Design ElectricalItatin;; tNet MWel:
: 6. Maximum Dependable Capaci.y (Gross MWe): - ICOO
                                                            "< 5
: 7. blasimum Dependable Capacity (Net MWeJ:
: 8. If Changs Occur in Capacity Ratin;;s (Items Number 3 Throu;;h 7) Since Last Iteport. Gise Reasons:
None
: 9. Power Lese! To Which Restricted. lf Any (Net MWel:
: 10. I!casons for !!estrictions. If Any:          N/A
                                                                  'lhis Month      Yr..t o.Da t e            Cumulatise 744            5087                    25,584
: 11. !!ours In Rcrortm3 Period                                                        4907.1                  20,568 744
: 12. Number Of Hours Reactor Was Critical                .
0 0                0
: 13. Itcactor Pesene Shutdown llours                                                  4878.5                  20,086.2 744
: 14. I!aurs Generatcr On-Line                                                            0                        0 0
: 15. Unit !!cscne Shutdown flours                                                                              53,921,647 1,601,186      13,520,678
: 16. Grow The mal l nergy Gen; : d (MWil)                                                                      17,736,181 477,460      4,353,410
: 17. Gross Electric.il Energy Generaicd (MWill 454,669      4,196,640                  17,045,450
: 18. Net Electrical Energy Generated (MWil) lon                95.9                      78.5
: 19. Unit Senice I actor                                                                                            78.5 100                95.9
: 20. Unit As.n!.ibility F.ictor 63.T              85.5                      69.0
: 21. Unit Cap.icity Factor (Using MDC Net) 61.3              85.5                      69.0
: 22. Unit Capiuty Factor (Using DER Net)                                                                                3.9 0                      .6
: 23. Unit I orecil Outage R.cre
: 24. Shutdowns S-hednicd Oscr Nest 6 Monti:s (Type. Date.and Duration of f.ich t:
Refuelinu Outage Sep teric 1979 2.>. If Shul Dow n At Fud Of !!cport Period !Niiinatcil Date of Startup:
: 26. Umts In l est St.itus (l'aior to Cunnnercr il Operationi:                    1:urceast                Achicscil INill Al. Cilll! cal tl Y                              %        __
INill \l. I'I.I'Clllit t rY                                          ,
COMMI !!CI A l. Ol'1 !! A 1 ION                                                              ,
3 I ,'
79081405m                                      63                            eml
 
AVI.IC AGE I) AILY UNil POWI 1( !.l VLL DOCKET NO.        Ch2"6 liio i an Po i n t.
UNIT        No 3 DATE COMPLETED g;y          C . Connell TELEPIl0NE 914-739-3200 MONT!!        July 1979 DAY        AVERAGE D A!LY POWER LEVEL                      DAY        AVER AGE DAILY POWER LEVEL (MWe NetJ                                            (MWe Net) y 618                          37 610 615                                                    614 2                                                          18      .
3 617                          39                        612 615                          20 603 4
5                            615                          21                        6"4 616                                                    593 615                                                    589 7                                                            3 g                            614                          2.g                      594 613                                                    586 9                                                          25 612                          26                        597 10
!!                            C ' ''
27                        All 610                                                    636 g
33 608                          29                        635 g                              593                                                    638 30 15                            604                          31                        631 16      -
Fo' INS 1 RUCTIONS On this fornut. hst the nerage daily unit power levelin MWe. Net for each day in the repostnig anonth.Coinpute to the riestest w hole niegawatt.                                                                -
(9/77)
                                                                            ,. n j n\ OL t .i
                                                                                            )\
 
50-286 UNITS!!UTDOWNS AND POWER REDUCTIONS                    DOC}:ET NO.                  .
UNil N etE        Indian Point  ,,o . 3 DATE      9 'l COMPLETED DY          o - r-nM1 REPORT MONTl! July 1979 TELEril0NE        914 73o a2''O
                                                          -      E                            E No.          Date g
                                        .5 ?      3      4 Yl        Licensee    ,Eg,      {%                  Cause & Corrective 3g        g    ,g g 5        Esent      gg        o-3                      Action to
                                        $E        cf    Igg
                                                          <      g Report #    to O        [U O
Present Recurrentt C
29      790729          P        .7      A        1            N/A        IIII  VALVEX F  Load reduction caused by decreasing condenser vacuum due to low level in boiler feed pump seal collecting tack.
Corrective Action:
Serviced level control valve T'* g
    %      l
-eg i
s1    1                    2                                                  3
-      F: Forced                                                                                              4 Ressen:                                            Method:
ya    S: Schedu!ed          A Equ:pment Faiture(Explain)                                                        Exhibit F Instructions 1 Manual                          for Preparation of Data B-Maintenance ci Test                              2 Manual Scram.                  Entry Sheets for Licensee C Refueling                                        3 Automatic Scram D-Regulatory Restriction                                                            Esent Report ILER) File (NUREG-4-Ot her (E xplain )              0161) 1 -Operator Training 1 License Examination F AJnanistr:tbe                                                                  5 G-Operational Error (Explain)
(9/77)                  Il 04her (Explain)                                                                  Exhibi.B Same Sourec
 
                                          'MO!;THLY MAINTE!!A!!CE REPCRT July 1979 Month DATE  W.R. 4          EQUIPME!;T                        MALFUNCTION          CORRECTIVE ACTIO!J 7-5-79      I-569-1B  Charging Pump Press. Gauge      Weld leak            Removed pipe to tubing adapter, stop Valve #229                                        welded in new one.
7-13-79      I-576-2    #31 Charging Pump                Seals leak            Replaced seals in all 5 cylinders 7-15-79      I-578-1A  #32 Boric Acid Transfer          Mechanical seal leaks Replaced nochanical seal
    'N
,    2 "W.
 
MO:THLY I & C CATEGORY I REPORT July 1979 Month Date I    W.R. #        Equ ipr.c nt
* Malfunction                  Corrective Action 7/23/79    IC-1-432-2 R-ll Containment APD        Filter paper does not advanca Corrected misalignment between gear housing and paper drive motor.
T =g Qjd
    .a a
 
SU.UARY OF CP3RATII;G EXPERIEt;CE July, 1979 Indian Point Unit 3 vas synchronized to the bus for a total of 744 hours, producing a gross gencration of 477,46] mwh for this re-porting period.
The unit operated at 70% power for the major part of the month and experienced one scheduled power ascension and one load reduction.
Until July 27, 1979, the urit  was operating at 70% power in order to extend the operating cycle. At  14:32 that date, the  unit load was increased to 75% power in order to  meet with sche duling for a September 15, 1979 Refueling Outage start date. The unit rema; ed at  75% power for the rest of the month.
The load reduction occurred on July 29, 1979 at approximately 19:30.
At that time, the unit experienced a condenser vacuum transient due tc a failure in level control of Boiler Fced Pump seal collecting tank. Gen-erator output was reduced to 460 mw for approximately one hour.
                                                                                - ,-  , j /
t  j i 0
      ..}}

Latest revision as of 02:32, 2 February 2020

Monthly Operating Rept for Jul 1979
ML19242D115
Person / Time
Site: Indian Point Entergy icon.png
Issue date: 08/03/1979
From: Connell C
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
Shared Package
ML19242D109 List:
References
NUDOCS 7908140516
Download: ML19242D115 (6)


Text

to Ol'EltAlING DATA Ill.PoltT DOCKl.T NO. 5 0 h 6 DAll 8/3/79 COM11Eil D !!y C, conne11 TELLPilONE (914 ) 7i"-0200 OPI:lt ATING STAT US Notes

1. Unit Name: 3" H m Po i n+-

Mo. 3 Mucim Power Plant

2. !!cporting I'eriod: Julv 1979
3. Licensed 1 hennal Power (MWt): _ 3025
4. Nameplate Itatin;;(Gross MWe): _ 1013
5. Design ElectricalItatin;; tNet MWel:
6. Maximum Dependable Capaci.y (Gross MWe): - ICOO

"< 5

7. blasimum Dependable Capacity (Net MWeJ:
8. If Changs Occur in Capacity Ratin;;s (Items Number 3 Throu;;h 7) Since Last Iteport. Gise Reasons:

None

9. Power Lese! To Which Restricted. lf Any (Net MWel:
10. I!casons for !!estrictions. If Any: N/A

'lhis Month Yr..t o.Da t e Cumulatise 744 5087 25,584

11. !!ours In Rcrortm3 Period 4907.1 20,568 744
12. Number Of Hours Reactor Was Critical .

0 0 0

13. Itcactor Pesene Shutdown llours 4878.5 20,086.2 744
14. I!aurs Generatcr On-Line 0 0 0
15. Unit !!cscne Shutdown flours 53,921,647 1,601,186 13,520,678
16. Grow The mal l nergy Gen; : d (MWil) 17,736,181 477,460 4,353,410
17. Gross Electric.il Energy Generaicd (MWill 454,669 4,196,640 17,045,450
18. Net Electrical Energy Generated (MWil) lon 95.9 78.5
19. Unit Senice I actor 78.5 100 95.9
20. Unit As.n!.ibility F.ictor 63.T 85.5 69.0
21. Unit Cap.icity Factor (Using MDC Net) 61.3 85.5 69.0
22. Unit Capiuty Factor (Using DER Net) 3.9 0 .6
23. Unit I orecil Outage R.cre
24. Shutdowns S-hednicd Oscr Nest 6 Monti:s (Type. Date.and Duration of f.ich t:

Refuelinu Outage Sep teric 1979 2.>. If Shul Dow n At Fud Of !!cport Period !Niiinatcil Date of Startup:

26. Umts In l est St.itus (l'aior to Cunnnercr il Operationi: 1:urceast Achicscil INill Al. Cilll! cal tl Y  % __

INill \l. I'I.I'Clllit t rY ,

COMMI !!CI A l. Ol'1 !! A 1 ION ,

3 I ,'

79081405m 63 eml

AVI.IC AGE I) AILY UNil POWI 1( !.l VLL DOCKET NO. Ch2"6 liio i an Po i n t.

UNIT No 3 DATE COMPLETED g;y C . Connell TELEPIl0NE 914-739-3200 MONT!! July 1979 DAY AVERAGE D A!LY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL (MWe NetJ (MWe Net) y 618 37 610 615 614 2 18 .

3 617 39 612 615 20 603 4

5 615 21 6"4 616 593 615 589 7 3 g 614 2.g 594 613 586 9 25 612 26 597 10

!! C '

27 All 610 636 g

33 608 29 635 g 593 638 30 15 604 31 631 16 -

Fo' INS 1 RUCTIONS On this fornut. hst the nerage daily unit power levelin MWe. Net for each day in the repostnig anonth.Coinpute to the riestest w hole niegawatt. -

(9/77)

,. n j n\ OL t .i

)\

50-286 UNITS!!UTDOWNS AND POWER REDUCTIONS DOC}:ET NO. .

UNil N etE Indian Point ,,o . 3 DATE 9 'l COMPLETED DY o - r-nM1 REPORT MONTl! July 1979 TELEril0NE 914 73o a2O

- E E No. Date g

.5 ? 3 4 Yl Licensee ,Eg, {% Cause & Corrective 3g g ,g g 5 Esent gg o-3 Action to

$E cf Igg

< g Report # to O [U O

Present Recurrentt C

29 790729 P .7 A 1 N/A IIII VALVEX F Load reduction caused by decreasing condenser vacuum due to low level in boiler feed pump seal collecting tack.

Corrective Action:

Serviced level control valve T'* g

% l

-eg i

s1 1 2 3

- F: Forced 4 Ressen: Method:

ya S: Schedu!ed A Equ:pment Faiture(Explain) Exhibit F Instructions 1 Manual for Preparation of Data B-Maintenance ci Test 2 Manual Scram. Entry Sheets for Licensee C Refueling 3 Automatic Scram D-Regulatory Restriction Esent Report ILER) File (NUREG-4-Ot her (E xplain ) 0161) 1 -Operator Training 1 License Examination F AJnanistr:tbe 5 G-Operational Error (Explain)

(9/77) Il 04her (Explain) Exhibi.B Same Sourec

'MO!;THLY MAINTE!!A!!CE REPCRT July 1979 Month DATE W.R. 4 EQUIPME!;T MALFUNCTION CORRECTIVE ACTIO!J 7-5-79 I-569-1B Charging Pump Press. Gauge Weld leak Removed pipe to tubing adapter, stop Valve #229 welded in new one.

7-13-79 I-576-2 #31 Charging Pump Seals leak Replaced seals in all 5 cylinders 7-15-79 I-578-1A #32 Boric Acid Transfer Mechanical seal leaks Replaced nochanical seal

'N

, 2 "W.

MO:THLY I & C CATEGORY I REPORT July 1979 Month Date I W.R. # Equ ipr.c nt

  • Malfunction Corrective Action 7/23/79 IC-1-432-2 R-ll Containment APD Filter paper does not advanca Corrected misalignment between gear housing and paper drive motor.

T =g Qjd

.a a

SU.UARY OF CP3RATII;G EXPERIEt;CE July, 1979 Indian Point Unit 3 vas synchronized to the bus for a total of 744 hours0.00861 days <br />0.207 hours <br />0.00123 weeks <br />2.83092e-4 months <br />, producing a gross gencration of 477,46] mwh for this re-porting period.

The unit operated at 70% power for the major part of the month and experienced one scheduled power ascension and one load reduction.

Until July 27, 1979, the urit was operating at 70% power in order to extend the operating cycle. At 14:32 that date, the unit load was increased to 75% power in order to meet with sche duling for a September 15, 1979 Refueling Outage start date. The unit rema; ed at 75% power for the rest of the month.

The load reduction occurred on July 29, 1979 at approximately 19:30.

At that time, the unit experienced a condenser vacuum transient due tc a failure in level control of Boiler Fced Pump seal collecting tank. Gen-erator output was reduced to 460 mw for approximately one hour.

- ,- , j /

t j i 0

..