LR-N05-0262, April 2005 Monthly Operating Report for Hope Creek Generating Station

From kanterella
Jump to navigation Jump to search
April 2005 Monthly Operating Report for Hope Creek Generating Station
ML051440289
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 05/13/2005
From: Massaro M
Public Service Enterprise Group
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LR-N05-0262
Download: ML051440289 (3)


Text

PSEG Nuclear LLC P.O. Box 236, Hancocks Bridge, New Jersey 08038-0236 MAY 130 2005 o PSEG Nuclear LLC LR-N05-0262 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 MONTHLY OPERATING REPORT HOPE CREEK GENERATING STATION DOCKET NO. 50-354 In compliance with Section 6.9, Reporting Requirements for the Hope Creek Technical Specifications, the operating statistics for April 2005 are being forwarded.

Sincerely, Michael J. Massaro Hope Creek Plant Manager Attachments C Distribution 95-2168 REV. 7/99

DOCKET NO.: 50-354 UNIT: Hone Creek DATE: 5/5/05 COMPLETED BY: K. Hight TELEPHONE: (856) 339-3887 Reporting Period April 2005 OPERATING DATA REPORT Design Electrical Rating (MWe-Net) 1083 Maximum Dependable Capacity (MWe-Net) 1049 Month No. of hours reactor was critical 535 No. of hours generator was on line (service 503 1918 133997 hours)

Unit reserve shutdown hours 0 0 O Net Electrical Energy (MWH) 519590 1903174 135691312 UNIT SHUTDOWNS NO. DATE TYPE DURATION REASON METHOD OF CORRECTIVE ACTION/

F=FORCED (HOURS) (1) SHUTTING COMMENT S=SCHEDULED DOWN THE REACTOR (2) 4 4/1/05 S 216 B 4 Drywell Leakage Due to Recirculation Piping 4/10/05 Leak (1) Reason (2) Method A - Equipment Failure (Explain) 1 - Manual B - Maintenance or Test 2 - Manual Trip/Scram C - Refueling 3 - Automatic Trip/Scram D - Regulatory Restriction 4 - Continuation E - Operator Training/License Examination 5 - Other (Explain)

F - Administrative G - Operational Error (Explain)

H - Other

- t DOCKET NO.: 50-354 UNIT: Hope Creek DATE: 5/5/05 COMPLETED BY: R. Ritzman TELEPHONE: (856) 339-1445 Summary Of Monthly Operating Experience

  • Hope Creek began the month in planned outage to identify and repair drywell leakage.
  • The unit was placed back on-line on April 10, reaching 100% power on April 13.
  • On April 14, power was reduced to approximately 78.5% in response to grass buildup at the Service Water intake structure. The unit returned to 100% power on April 15 and operated for the remainder of the month without experiencing another power change that exceeded 20% of reactor power.
  • At the end of the month, Hope Creek completed 20 days of continuous on-line operation.