LR-N02-0187, April 2002 Monthly Operating Report for Hope Creek

From kanterella
Jump to navigation Jump to search
April 2002 Monthly Operating Report for Hope Creek
ML021650319
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 05/15/2002
From: Garchow D
Public Service Enterprise Group
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LR-N02-0187
Download: ML021650319 (3)


Text

PSEG Nuclear LLC P.O. Box 236, Hancocks Bridge, New Jersey 08038-0236 MAY 1 5 2002 LR-N02-0187 o PSEG Nuclear LLC U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:

MONTHLY OPERATING REPORT HOPE CREEK GENERATING STATION DOCKET NO. 50-354 In compliance with Section 6.9, Reporting Requirements for the Hope Creek Technical Specifications, the operating statistics for April 2002 are being forwarded.

Sincerely, D. F. Garchow Vice President - Operations RAR Attachments C Distribution 95-2168 REV. 7/99

DOCKET NO.:

UNIT:

DATE:

COMPLETED BY:

TELEPHONE:

50-354 Hope Creek 05/10/02 F. Todd (856) 339-1316 Reporting Period April 2002 OPERATING DATA REPORT Design Electrical Rating (MWe-Net)

Maximum Dependable Capacity (MWe-Net)

No. of hours reactor was critical No. of hours generator was on line (service hours)

Unit reserve shutdown hours Net Electrical Energy (MWH) 1083 1049 Month Year-to-date Cumulative 719 2879 115301 719 2879 113143 0

0 0

773353 3025662 114661270 UNIT SHUTDOWNS NO.

DATE TYPE DURATION REASON METHOD OF CORRECTIVE ACTION/

F=FORCED (HOURS)

(1)

SHUTTING COMMENT S=SCHEDULED DOWN THE REACTOR (2)

(1) Reason (2) Method A - Equipment Failure (Explain)

B - Maintenance or Test C - Refueling D - Regulatory Restriction E - Operator Training/License Examination F - Administrative G - Operational Error (Explain)

H - Other 1 - Manual 2 - Manual Trip/Scram 3 - Automatic Trip/Scram 4 - Continuation 5 - Other (Explain)

DOCKET NO.: 50-354 UNIT: Hope Creek DATE: 05/10/02 COMPLETED BY: R. Ritzman TELEPHONE: (856) 339-1445 Summary Of Monthly Operating Experience Hope Creek began the month at 100% power.

On April 14, there was a planned power reduction to approximately 84% to conduct control valve testing. Power was returned to 100% later that day.

At the end of the month, the plant completed 140 days of continuous operation.