LR-N02-0210, May 2002 Monthly Operating Report for Hope Creek
| ML021720566 | |
| Person / Time | |
|---|---|
| Site: | Hope Creek |
| Issue date: | 06/12/2002 |
| From: | Garchow D Public Service Enterprise Group |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| LR-N02-0210 | |
| Download: ML021720566 (3) | |
Text
PSEG Nuclear LLC P.O. Box 236, Hancocks Bridge, New Jersey 08038-0236 JUN 1 2 2002 LR-N02-021 0 o PSEG Nu clear LLC U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
MONTHLY OPERATING REPORT HOPE CREEK GENERATING STATION DOCKET NO. 50-354 In compliance with Section 6.9, Reporting Requirements for the Hope Creek Technical Specifications, the operating statistics for May 2002 are being forwarded.
Sincerely, D. F. Gatchow Vice President - Operations RAR Attachments C Distribution 95-2168 REV. 7/99 0 F
DOCKET NO.:
UNIT:
DATE:
COMPLETED BY:
TELEPHONE:
50-354 Hope Creek 06/10/02 F. Todd (856) 339-1316 Reporting Period May 2002 OPERATING DATA REPORT Design Electrical Rating (MWe-Net)
Maximum Dependable Capacity (MWe-Net)
No. of hours reactor was critical No. of hours generator was on line (service hours)
Unit reserve shutdown hours Net Electrical Energy (MWH) 1083 1049 Month Year-to-date (umulative 744 3623 116045 654 3533 113797 0
0 0
631917 3657579 115293187 UNIT SHUTDOWNS NO.
DATE TYPE DURATION REASON METHOD OF CORRECTIVE ACTION/
F=FORCED (HOURS)
(1)
SHUTTING COMMENT S=SCHEDULED DOWN THE REACTOR (2) 1 5/18/02 F
90 hrs B
5 - Reactor Repairs to EHC System, remained Lightning Arrestor &
5/21/02 critical.
Feedwater Heaters (1) Reason (2) Method A - Equipment Failure (Explain)
B - Maintenance or Test C - Refueling D - Regulatory Restriction E - Operator Training/License Examination F -Administrative G - Operational Error (Explain)
H - Other I - Manual 2 - Manual Trip/Scram 3 - Automatic Trip/Scram 4 - Continuation 5 - Other (Explain)
DOCKET NO.: 50-354 UNIT: Hope Creek DATE: 06/10/02 COMPLETED BY: R. Ritzman TELEPHONE: (856) 339-1445 Summary Of Monthly Operating Experience
"* Hope Creek began the month at 100% power.
" On May 13, power was reduced due to a lightning strike, which caused the 6A, 6B, and 6C feedwater heaters to trip. Power was returned to 100% on May 14.
" On May 17, there was a planned power reduction to approximately 18% power to perform Turbine Valve Testing, to repair the EHC System and Lightning Arrestor, and to replace Motor Generator Set brushes. The unit came back on line on May 21.
" At the end of the month, the plant completed 10 days of continuous on line operation.