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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217L0421999-10-21021 October 1999 Forwards Insp Rept 50-382/99-20 on 990815-0925 & Notice of Violation.Two Severity Level IV Violations of NRC Requirements Identified & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20217N2111999-10-19019 October 1999 Forwards Insp Rept 50-382/99-14 on 990913-17 & 1004-08.No Violations Noted.Licensed Operator Requalification Program, Effective,Utilized Systems Approach to Training & Showed Continued Improvements Over Previous Insp Findings ML20217L0101999-10-18018 October 1999 Provides Update of Waterford 3 Effort for Review of Ufsar. Info Listed Includes Background Mgt Expectations,Review Status & Results,Clarifications Re Review & Conclusions ML20217L0141999-10-18018 October 1999 Submits Update to NRC Staff Re Circumstances & Plans for Submitting Certification Rept on Waterford 3 Plant Specific Simulator ML20217G7051999-10-14014 October 1999 Forwards Comments on Four of NRC RO Examination Questions for Exam Administered During Week of 991004 05000382/LER-1999-014, Forwards LER 99-014-00,providing Details of Reactor Shutdown Due to Loss of RCP Controlled bleed-off Flow.Attached Commitment Identification/Voluntary Enhancement Form Identifies All Commitments Contained in Submittal1999-10-12012 October 1999 Forwards LER 99-014-00,providing Details of Reactor Shutdown Due to Loss of RCP Controlled bleed-off Flow.Attached Commitment Identification/Voluntary Enhancement Form Identifies All Commitments Contained in Submittal ML20217D5151999-10-0707 October 1999 Forwards Application for Renewal of SRO License for C Fugate License SOP-43039-3,IAW 10CFR55.57.Without Encls ML20217C6251999-10-0505 October 1999 Informs That NRC Reviewed Util Ltr & Encl Exercise Scenario Package for Waterford 3 Emergency Plan Exercise Scheduled for 991013.Based on Review,Nrc Determined That Exercise Appropriate to Meet Objectives ML20212J6921999-09-29029 September 1999 Forwards Insp Rept 50-382/99-18 on 990830-0902.One Noncited Violation Identified Re Failure to Follow Procedural Instructions to Ensure That Members on Fire Brigade Shift Were Qualified ML20216G2441999-09-27027 September 1999 Forwards Insp Rept 50-382/99-19 on 990830-0903.No Violations Noted 05000382/LER-1999-013, Forwards LER 99-013-00,providing Details of Exceeding TS Limits for RCS Cooldown Rates.All Commitments Contained in Submittal Are Identified on Encl Commitment Identification/ Voluntary Enhancement Form1999-09-23023 September 1999 Forwards LER 99-013-00,providing Details of Exceeding TS Limits for RCS Cooldown Rates.All Commitments Contained in Submittal Are Identified on Encl Commitment Identification/ Voluntary Enhancement Form IR 05000382/19993011999-09-21021 September 1999 Informs That NRC License Exam Previously Associated with NRC Insp Rept 50-382/99-301 Will Be Incorporated Into NRC Insp Rept 50-382/99-14 ML20212D8761999-09-16016 September 1999 Informs That on 990818,NRC Staff Completed Midcycle PPR of Waterford 3.During Assessment Period,Number of Personnel Errors Occurred,Which Demonstrated Lack of Attention to Detail by Plant Personnel.Historical Listing of Issues,Encl ML20212C2471999-09-16016 September 1999 Forwards Five Final Applications for RO Licenses for G Esquival,Jm Hearn,Md Lawson,Re Simpson & PI Wood.Written Exam & Operating Test to Be Administered,Is Requested. Encls Withheld ML20212C2391999-09-16016 September 1999 Requests Cancellation of SRO Licenses for Bn Coble,License SOP-43835,due to Job Assignment Location & CA Rodgers, License SOP-43537-1,due to Resignation from Company, Effective 990901 ML20212C5881999-09-14014 September 1999 Forwards Insp Rept 50-382/99-15 on 990719-23 with Continuing in Ofc Insp Until 0819.No Violations Noted ML20211Q4421999-09-0909 September 1999 Forwards Insp Rept 50-382/99-07 on 990601-11.Three Violations Being Treated as Noncited Violations ML20211P4121999-09-0707 September 1999 Requests NRC Staff Review & Approval of Integrated Nuclear Security Plan (Insp) & Integrated Security Training & Qualification Plan (Ist&Q), for Use by All Entergy Operations,Inc.Encl Withheld,Per 10CFR2.790(d) ML20211M8391999-09-0303 September 1999 Forwards Revised Epips,Including Rev 25 to EP-001-020,rev 24 to EP-001-030,rev 25 to EP-001-040,rev 30 to EP-002-100,rev 22 to EP-001-010,rev 27 to EP-002-010,rev 26 to EP-002-102 & Rev 16 to EP-002-190.Listed Proprietary Revs to Epips,Encl ML20211L3681999-09-0202 September 1999 Forwards Five Preliminary Applications for Reactor Operator Licenses for Individuals Listed,Iaw 10CFR55.31.Encls Withheld ML20211K9741999-09-0101 September 1999 Forwards Insp Rept 50-382/99-16 on 990704-0814.Two Severity Level IV Violations Identified & Being Treated as Noncited Violations,Consistent with App C of Enforcement Policy 05000382/LER-1999-011, Forwards LER 99-011-00,providing Details of Reactor Shutdown Due to Loss of Controlled bleed-off Flow.All Commitments Contained in Submittal Identified on Attached Commitment Identification/Voluntary Enhancement Form1999-08-31031 August 1999 Forwards LER 99-011-00,providing Details of Reactor Shutdown Due to Loss of Controlled bleed-off Flow.All Commitments Contained in Submittal Identified on Attached Commitment Identification/Voluntary Enhancement Form ML20211M3641999-08-30030 August 1999 Forwards Written Examination,Operating Tests & Supporting Ref Matl Identified in Attachment 2 of ES-210,in Response to NRC .Encl Withheld ML20211G5751999-08-27027 August 1999 Forwards RAI Re IPEEE Submittal.Please Provide RAI within 60 Days of Receipt of Ltr,Per Util Response to GL 88-20,suppl 4 ML20211E3281999-08-26026 August 1999 Forwards fitness-for-duty Performance Data for Period of 990101-0630,IAW 10CFR26.71(d).Ltr Does Not Contain Commitments 05000382/LER-1999-009, Forwards LER 99-009-00 Re Discovery of Condition of Noncompliance with App R Involving Inadequate Separation of Essential Cables Routed in Fire Area RAB-30 in Rab. Compensatory Measures Were Established Immediately1999-08-26026 August 1999 Forwards LER 99-009-00 Re Discovery of Condition of Noncompliance with App R Involving Inadequate Separation of Essential Cables Routed in Fire Area RAB-30 in Rab. Compensatory Measures Were Established Immediately 05000382/LER-1999-010, Forwards LER 99-010-00,providing Details of Inadequate Pumping Capacity in Dry Cooling Tower Area.All Commitments Contained in Submittal Are Identified on Attached Commitment Identification Voluntary Enhancement Form1999-08-26026 August 1999 Forwards LER 99-010-00,providing Details of Inadequate Pumping Capacity in Dry Cooling Tower Area.All Commitments Contained in Submittal Are Identified on Attached Commitment Identification Voluntary Enhancement Form ML20211F5421999-08-24024 August 1999 Forwards Proposed marked-up TS Page Xviii, Index Administrative Controls, Correcting Page Number Re TS Change Request NPF-38-220.Editorial Changes for TS Change NPF-38-221 Discussed ML20211F3561999-08-24024 August 1999 Forwards CTS Pages & TS Proposed marked-up Pages for Insertion Into TS Change Request NPF-38-207 Re Efas, Originally Submitted on 980702.Original NSHC Determination Continues to Be Applicable ML20211F4611999-08-24024 August 1999 Informs That NRC Reviewed Ltr & Encl Objectives for Waterford 3 Emergency Plan Exercise Scheduled for 991013.Exercise Objectives Appropriate to Meet Emergency Plan Requirements ML20211G1731999-08-23023 August 1999 Informs That Info Submitted in ,B&W Rept 51-1234900-00,will Be Withheld from Public Disclosure,Per 10CFR2.790 ML20211C5101999-08-19019 August 1999 Forwards Certified Copies of Liability Insurance Policy Endorsements Issued in First Half of 1999 for Each Entergy Operations,Inc Nuclear Unit,Per 10CFR140.15 ML20210T9791999-08-18018 August 1999 Discusses Which Responded to Reconsideration of Violation Denial (EA 98-022) Enforcement Action Detailed in .Concludes That Violation Occurred as Stated ML20211A9501999-08-12012 August 1999 Discusses 990720-21 Workshop Conducted in Region IV Ofc,Re Exchange of Info in Area of Use of Risk Insights in Regulatory Activities.List of Attendees,Summary of Topic & Issues,Agenda & Copies of Handouts Encl ML20210S0561999-08-12012 August 1999 Submits Voluntary Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for NRC Fys 2000 & 2001 for Waterford 3 ML20210Q6161999-08-12012 August 1999 Forwards Corrected Copy of Monthly Operating Rept for July 1999 for Waterford 3.Original Rept,Submitted with ,Contained Typos ML20217F2661999-08-12012 August 1999 Forwards Copy of 1999 Waterford 3 Biennial Exercise Package to Be Performed Using Waterford 3 CR Simulator ML20210R9231999-08-11011 August 1999 Forwards Insp Rept 50-382/99-10 on 990719-23.Violations Noted.Nrc Has Determined That One Severity Level IV Violation of NRC Requirements Occurred ML20210L1461999-08-0303 August 1999 Informs That NRC Plans to Administer Gfes of Written Operator Licensing Exam on 991006.Requests Submittal of Ltr Identifying Individuals Taking Exam,Personnel Allowed Access to Exams & Mailing Address for Exams 05000382/LER-1999-008, Forwards LER 99-008-00,re Failure to Perform Testing of ESF Filtration Units Per TS Srs.Commitments Made by Util Also Encl1999-07-29029 July 1999 Forwards LER 99-008-00,re Failure to Perform Testing of ESF Filtration Units Per TS Srs.Commitments Made by Util Also Encl ML20210H4291999-07-29029 July 1999 Forwards Response to NRC Rai,Associated with TS Change Request NPF-38-208,proposing to Replace Ref to Supplement 1 with Ref to Supplement 2 of Calculative Methods for CE Small Break LOCA Evaluation Model, in ACs Section of TSs ML20210F9451999-07-27027 July 1999 Forwards Proprietary & non-proprietary Version of Rev 29 to EPIP EP-002-100, Technical Support Ctr Activation,Operation & Deactivation. Proprietary Info Withheld,Per 10CFR2.790 ML20210D3171999-07-23023 July 1999 Submits Proposal for Final Resolution of Reracking Spent Fuel Pool at Plant,Per License Amend 144,issued by NRC in .No New Commitments Are Contained in Ltr 05000382/LER-1999-007, Forwards LER 99-007-00,providing Details of Operation Outside Tornado Missile Protection Licensing Basis for turbine-driven Emergency Feedwater Pump Exhaust Stack & Steam Supply Piping.All Commitments Identified on Attached1999-07-23023 July 1999 Forwards LER 99-007-00,providing Details of Operation Outside Tornado Missile Protection Licensing Basis for turbine-driven Emergency Feedwater Pump Exhaust Stack & Steam Supply Piping.All Commitments Identified on Attached ML20210D8701999-07-23023 July 1999 Forwards Safety Evaluation Re First 10-yr Interval Inservice Insp Plan Requests for Relief ISI-018 Through ISI-020 for Entergy Operations,Inc,Unit 3 ML20210B1521999-07-15015 July 1999 Forwards Insp Rept 50-382/99-13 on 990523-0703.Three Violations Being Treated as Noncited Violations ML20209G9771999-07-13013 July 1999 Forwards Objectives & Guidelines for Waterford 3 Emergency Preparedness Exercise Scheduled for 991013.List of Objectives cross-referenced Where Applicable to Relevant Sections of NUREG-0654 IR 05000382/19990081999-07-12012 July 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-382/99-08 Issued on 990503 ML20209E5231999-07-0909 July 1999 Informs That as Result of NRC Review of Util Responses to GL-92-01,rev 1 & Suppl 1,staff Revised Info in Reactor Vessel Integrity Database & Releasing Database as Rvid Version 2.This Closes Staff Efforts Re TAC MA0583 ML20209D4051999-07-0707 July 1999 Forwards Revised TS Pages to Replace Attachment C,Entirely in Original TS Change Request NPF-38-207,per 990519 Discussion with C Patel of Nrc.Changes to Action 20 Delete Word Requirement & Revise Word Modes to Mode 1999-09-09
[Table view] Category:OUTGOING CORRESPONDENCE
MONTHYEARML20217L0421999-10-21021 October 1999 Forwards Insp Rept 50-382/99-20 on 990815-0925 & Notice of Violation.Two Severity Level IV Violations of NRC Requirements Identified & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20217N2111999-10-19019 October 1999 Forwards Insp Rept 50-382/99-14 on 990913-17 & 1004-08.No Violations Noted.Licensed Operator Requalification Program, Effective,Utilized Systems Approach to Training & Showed Continued Improvements Over Previous Insp Findings ML20217C6251999-10-0505 October 1999 Informs That NRC Reviewed Util Ltr & Encl Exercise Scenario Package for Waterford 3 Emergency Plan Exercise Scheduled for 991013.Based on Review,Nrc Determined That Exercise Appropriate to Meet Objectives ML20212J6921999-09-29029 September 1999 Forwards Insp Rept 50-382/99-18 on 990830-0902.One Noncited Violation Identified Re Failure to Follow Procedural Instructions to Ensure That Members on Fire Brigade Shift Were Qualified ML20216G2441999-09-27027 September 1999 Forwards Insp Rept 50-382/99-19 on 990830-0903.No Violations Noted IR 05000382/19993011999-09-21021 September 1999 Informs That NRC License Exam Previously Associated with NRC Insp Rept 50-382/99-301 Will Be Incorporated Into NRC Insp Rept 50-382/99-14 ML20212D8761999-09-16016 September 1999 Informs That on 990818,NRC Staff Completed Midcycle PPR of Waterford 3.During Assessment Period,Number of Personnel Errors Occurred,Which Demonstrated Lack of Attention to Detail by Plant Personnel.Historical Listing of Issues,Encl ML20212C5881999-09-14014 September 1999 Forwards Insp Rept 50-382/99-15 on 990719-23 with Continuing in Ofc Insp Until 0819.No Violations Noted ML20211Q4421999-09-0909 September 1999 Forwards Insp Rept 50-382/99-07 on 990601-11.Three Violations Being Treated as Noncited Violations ML20211K9741999-09-0101 September 1999 Forwards Insp Rept 50-382/99-16 on 990704-0814.Two Severity Level IV Violations Identified & Being Treated as Noncited Violations,Consistent with App C of Enforcement Policy ML20211G5751999-08-27027 August 1999 Forwards RAI Re IPEEE Submittal.Please Provide RAI within 60 Days of Receipt of Ltr,Per Util Response to GL 88-20,suppl 4 ML20211F4611999-08-24024 August 1999 Informs That NRC Reviewed Ltr & Encl Objectives for Waterford 3 Emergency Plan Exercise Scheduled for 991013.Exercise Objectives Appropriate to Meet Emergency Plan Requirements ML20211G1731999-08-23023 August 1999 Informs That Info Submitted in ,B&W Rept 51-1234900-00,will Be Withheld from Public Disclosure,Per 10CFR2.790 ML20210T9791999-08-18018 August 1999 Discusses Which Responded to Reconsideration of Violation Denial (EA 98-022) Enforcement Action Detailed in .Concludes That Violation Occurred as Stated ML20211A9501999-08-12012 August 1999 Discusses 990720-21 Workshop Conducted in Region IV Ofc,Re Exchange of Info in Area of Use of Risk Insights in Regulatory Activities.List of Attendees,Summary of Topic & Issues,Agenda & Copies of Handouts Encl ML20210R9231999-08-11011 August 1999 Forwards Insp Rept 50-382/99-10 on 990719-23.Violations Noted.Nrc Has Determined That One Severity Level IV Violation of NRC Requirements Occurred ML20210L1461999-08-0303 August 1999 Informs That NRC Plans to Administer Gfes of Written Operator Licensing Exam on 991006.Requests Submittal of Ltr Identifying Individuals Taking Exam,Personnel Allowed Access to Exams & Mailing Address for Exams ML20210D8701999-07-23023 July 1999 Forwards Safety Evaluation Re First 10-yr Interval Inservice Insp Plan Requests for Relief ISI-018 Through ISI-020 for Entergy Operations,Inc,Unit 3 ML20210B1521999-07-15015 July 1999 Forwards Insp Rept 50-382/99-13 on 990523-0703.Three Violations Being Treated as Noncited Violations IR 05000382/19990081999-07-12012 July 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-382/99-08 Issued on 990503 ML20209E5231999-07-0909 July 1999 Informs That as Result of NRC Review of Util Responses to GL-92-01,rev 1 & Suppl 1,staff Revised Info in Reactor Vessel Integrity Database & Releasing Database as Rvid Version 2.This Closes Staff Efforts Re TAC MA0583 ML20196E6931999-06-22022 June 1999 Forwards Corrected Ltr Re Changes to Rev 19 to Emergency Plan.Original Ltr Had Error in Subject Line ML20196E0831999-06-21021 June 1999 Forwards Insp Rept 50-382/99-12 on 990524-27.No Violations Noted.Purpose of Insp Was to Conduct Assessment of Emergency Preparedness Program ML20196D9941999-06-18018 June 1999 Forwards Insp Rept 50-382/99-11 on 990524-28.No Violations Noted ML20195J8091999-06-17017 June 1999 Forwards Safety Evaulation Re First 10-yr Interval Inservice Insp Relief Request for Plant,Unit 3 ML20196C8711999-06-15015 June 1999 Discusses Insp Rept 50-382/99-08 & Forwards Notice of Violation Re Unescorted Access Which Was Mistakenly Granted to Individual Whose Background Investigation Indicated That He Had Failed Prior Drug Screening with Another Employer ML20196F3721999-06-0909 June 1999 Corrected Ltr Forwarding Rev 19 to Emergency Plan ML20195G3711999-06-0909 June 1999 Ack Receipt of Ltr Dtd 981223,which Transmitted Waterford 3 Steam Electric Station Emergency Plan,Rev 24,under Provisions of 10CFR50,App E,Section V.No Violations of 10CFR50.54(q) Identified During Review ML20207E8541999-06-0303 June 1999 Forwards SE Accepting Licensee 990114 Submittal of one-time Request for Relief from ASME B&PV Code IST Requirements for Pressurizer Safety Valves at Plant,Unit 3 ML20207G3441999-06-0303 June 1999 Forwards Insp Rept 50-382/99-09 on 990411-0522 & Notice of Violation.One Violation Identified & Being Treated as Noncited Violation C ML20207D3771999-05-27027 May 1999 Ack Receipt of 990401 & 0504 Ltrs Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-382/99-01 on 990303 ML20207A5121999-05-24024 May 1999 Refers to Which Responded to NOV & Proposed Imposition of Civil Penalty Sent by .Violations A,B & E Withdrawn & Violations C & D Changed to Severity Level IV ML20206U7851999-05-18018 May 1999 Forwards Insp Rept 50-382/99-06 on 990405-09.Three Violations of NRC Requirements Occurred & Being Treated as non-cited Violations ML20206N6961999-05-11011 May 1999 Informs That NRC Office of Nuclear Reactor Regulation Reorganized Effective 990328.As Part of Reorganization, Division of Licensing Project Management Created ML20206S4411999-05-10010 May 1999 Forwards Insp Rept 50-382/99-05 on 990228-0410.Three Violations of NRC Requirements Identified & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20206H3841999-05-0707 May 1999 Informs That on 990407,NRC Administered Generic Fundamental Exam Section of Written Operator Licensing Exam.Licensee Facility Did Not Participate in Exam,However Copy of Master Exam,With Answer Key,Encl for Info.Without Encl ML20206K0951999-05-0606 May 1999 Discusses Insp Rept 50-382/99-08 Issued 990503 Without Cover Ltr Documenting EA Number & Subject Line Indicated NOV Which Was Incorrect.Corrected Cover Ltr Encl ML20206F4701999-05-0303 May 1999 Forwards Insp Rept 50-382/99-08 on 990405-07.One Apparent Violation Re Failure to Review & Consider Derogatory Access Authorization Background Info as Required by PSP Identified & Being Considered for Escalated Enforcement Action ML20206K1211999-05-0303 May 1999 Corrected Cover Ltr Forwarding Insp Rept 50-382/99-08 on 990405-07.One Violations Noted & Being Considered for Escalated EA ML20205N7251999-04-13013 April 1999 Forwards Summary of 990408 Meeting with EOI in Jackson, Mississippi Re EOI Annual Performance Assessment of Facilities & Other Issues of Mutual Interest.List of Meeting Attendees & Licensee Presentation Slides Encl ML20205M0561999-04-0909 April 1999 Forwards Insp Rept 50-382/99-04 on 990301-19.One Violation of NRC Requirements Occurred & Being Treated as Noncited Violation,Consistent with App C of Enforcement Policy ML20205J8781999-04-0505 April 1999 Forwards Insp Rept 50-382/99-02 on 990117-0227.No Violations Noted.Inspectors Determined That Six Violations Occurred & Being Treated as Noncited Violations Consistent with App C of Enforcement Policy ML20205J0901999-04-0202 April 1999 Informs That Info Submitted by & 970313 Affidavit Will Be Withheld from Public Disclosure,Per 10CFR2.790(b) (5) ML20205A4681999-03-26026 March 1999 Forwards Insp Rept 50-382/99-03 on 990308-12.Two Violations of Radiation Protection Requirements Occurred & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20205A6141999-03-25025 March 1999 Forwards SE Accepting Request to Use Mechanical Nozzle Seal Assemblies (Mnsas) as an Alternative Repair Method,Per 10CFR50.55a(a)(3)(i) for Reactor Coolant Sys Application at Plant,Unit 3 ML20205F3311999-03-19019 March 1999 Advises of Planned Insp Effort Resulting from Plant,Unit 3 PPR Review,Which Was Completed on 990211.Performance at Plant,Unit 3 Was Acceptable ML20204E4941999-03-17017 March 1999 Discusses TSs Bases Change Re 3/4.4.1,3/4.6.1.7,3/4.6.3, 3/4.7.12 & 3/4.8.4.Forwards Affected Bases Pp B 3/4 4-1, B 3/4 6-3,B 3/4 6-4,B 3/4 7-7 & B 3/4 8-3 ML20207F1251999-03-0303 March 1999 Forwards Insp Rept 50-382/99-01 on 990125-29 & 0208-12 & Notice of Violations ML20203H8501999-02-17017 February 1999 Forwards SE Accepting Licensee 970701 Submittal of Second Ten Year ISI Program & Associated Relief Request for Plant, Unit 3.Nine Relief Requests Had Been Authorized Previously & Proposed Alternatives Remain Authorized ML20203D7211999-02-11011 February 1999 Forwards Request for Addl Info Re Licensee 970317 & 990111 Responses to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves. Response Should Be Provided within 60 Days 1999-09-09
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UNIT ED STATES
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L i 2 !O93 Docket: 50-382 License: NPF-38 Entergy Operations, In .
ATTN: Ross P. Barkhurst, Vice President Operations, Waterford i P.O. Box B Killona, Louisiana 70066 SUBJECT: NRC INSPECTION REPORT 50-382/93-25 ,
Thank you for your letter of October 27, 1993, in response to our letter and Notice of Violation dated September 28, 1993. We have reviewed your reply
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and find it responsive to the concerns raised in our Notice of Violation. We will review the implementation of your corrective actions during a future ,
inspection to determine that full compliance has been achieved and will be
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Sincerely,
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a,e .dollins, Director Division of Reactor Safety cc:
Entergy Operations, In ATTN: Harry W. Keiser, Executive Vice President & Chief Operating Officer P.O. Box 31995 Jackson, Mississippi 39286-1995
Entergy Operations, In ATTN: Jerrold G. Dewease, Vice President Operations Support P.O. Box 31995 Jackson, Mississippi 39286 '
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ATTN: Robert B. McGehee, Es ;
P.O. Box 651 .
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Jackson, Mississippi 39205
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Entergy Operations, In '
ATTN: D. F. Packer, General :l Hanager Plant Operations -i i
P.O. Box B Killona, Louisiana 70066 Entergy Operations, In i ATTN: L. W.-Laughlin t Licensing Manager ,
P.O. Box B l Killona, Louisiana 70066 j Chairman Louisiana Public Service Commission !
One American Place, Suite 1630 - ;
Baton Rouge, Louisiana 70825-1697 i Entergy Operations, In j ATTN: R. F. Burski, Director :
Nuclear Safety -j o
P.O. Box B -
Killona, Louisiana 70066 Hall Bohlinger, Administrator j Radiation Protection Division .
P.O. Box 82135 l Bato.: Rouge, Louisiana 70884-2135 Parish President St. Charles Parish P.O. Box 302 ;
Hahnville, Louisiana 70057 ;
Mr. William A. Cross ;
Bethesda Licensing Office 3 Metro Center
i Suite 610 Bethesda, Maryland 20814 Winston & Strawn i ATTN: Nicholas S. Reynolds, Es ,
1400 L Street, Washington, D.C. 20005-3502 j
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Section Chief (DRP/TSS) Section Chief (DRS/ES)
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October 27, 1993 f _ REG!OfGr U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555 Subject: Waterford 3 SES Docket No. 50-382 License No. NPF-38 NRC Inspection Report 93-25 Reply to Notice of Violation Gentlemen:
In accordance with IOCFR2.201, Entergy Operations, Inc. hereby submits in Attachment I the response to the violation identified in Appendix A of the subject Inspection Repor If you have any questions concerning this response, please contact T.S. Becker at (504) 739-669 Very truly yours,
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R.F. Burski Director Nuclear Safety ( ,37449 3 s ' i.:J J,cn RFB/TSB/ssf Attachment cc: .J.L. Milhoan (NRC Region IV), D.L. Wigginton (NRC-NRR),
R.B. McGehee, N.S. Reynolds, NRC Resident Inspectors Office f
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Page 1 of 3 ATTACHMENT 1 ENTERGY OPERATIONS. INC. RESPONSE TO THE VIOLATION IDENTIFIED IN APPENDIX A 0F INSPECTION REPORT 93-25 VIOLATION NO. 9325-01 Criterion V of Appendix B, 10CFR Part 50, states, in part, that activities affecting quality shall be prescribed by documented procedures and shall be accomplished in accordance with these procedure Waterford 2 Procedure UNT-005-002, " Administrative Procedure Condition Identifications," Revision 10, states, in Section 4.1.1, that Waterford-3 employees are responsible for " reporting and identifying abnormal conditions upon observation and initiating a condition identification to obtain resolution. Conditions adverse to quality shall also be further identified as a Nonconformance Condition Identification (NCI)."
Contrary to the above, the licensee failed to identify and initiate Nonconformance Condition Identifications for the ASME Section III pressurizer safety valves exceeding the 1 percent tolerance specified in the Technical Specifications in December 1986, April 1988, January 1991, and June 1992. The licensee also failed to identify and initiate Nonconformance Condition Identifications for the main steam safety valves when their as-found set pressures exceeded the 1 percent tolerance specified in the Technical Specifications in November 1986, April 1988, September 1989, and March 199 RESPONSE (1) Reason for the Violation Entergy Operations, Inc. admits this violation and believes that the root cause is personnel error in that the required procedure was not followe Administrative Proceduro UNT-005-002, " Condition Identification," requires that a Condition Identification (CI) be generated for any test that fails because of an equipment deficiency or a nonconforming anomalous condition. Further, the procedure requires that a Nonconformance Condition Identification (NCI) be generated if a deficiency exists which represents a condition adverse to quality. When the pressurizer safety and main steam safety valves were discovered to have lift setpoints outside of the Technical Specification required tolerance, a NCI should have been generated in accordance with the guidance of UNT-005-002.
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Deficiencies in two other procedures were a contributing cause of this event. Maintenance Procedures MM-007-004, " Pressurizer Safety Valve Test," and MM-007-015, "Trevitest of Main Steam Safety Valves," ,
both provide guidance regarding actions to be taken if any acceptance criterion is exceeded, if any condition is identified that could q prevent fulfillment of safety valve functional requirements, or if *
any valve parameter is found to be out of tolerance based on test results. Contrary to the upper-tier requirements of Site Directive W2.501, " Corrective Action," and UNT-005-002, neither maintenance l procedure requires that these problems be documented 'on a Corrective .
Action Program document (Condition Report or NCI). In both cases, ,
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the procedures direct that corrective actions and explanations be documented in the " remarks" section of the test performance recor The net effect of this procedure guidance was to allow corrective action to be taken for a cond" ;n adverse to quality without i documenting the adverse condit.an in the Corrective Action Progra (2) Corrective Steos That Have Been Taken and the Results Achieved Condition Reports 93-52 and 93-53 were generated in order to formally document the pressurizer safety and main steam safety valve as-found test failures in the Corrective Action program. Although the as-found test failures were not properly documented, Waterford 3, in concert with the industry, has been proactive in resolving identified 1 concerns with main steam and pressurizer safety valve setpoints, ,
especihlly in the area of setpoint drift. Waterford 3 will continue to pursue the resolution of and implement necessary corrective actions for identified industry concerns associated with main steam '
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and pressurizer safety valve setpoint In addition, the failure data for the pressurizer safety valves was ,
entered into NPRDS to enhance the industry data base regarding these valve (3) Corrective Steps Which Will Be Taken to Avoid Further Violations This violation was a result of a failure to enter an adverse ;
condition into the Corrective Action Program. As such, a review of ;
the Corrective Action Program will be performed and enhancements made i as necessar MM-007-004 and MM-007-015 will be revised to reflect those enhancements. In addition, other procedures which are used to perform surveillance type testing will be reviewed for possible ,
inclusion of the Corrective Action Program enhancement ,
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$ Page 3 of 3 Failure data for the. main steam safety valves will be entered into )
the NPRDS component databas !
l, Finally, this event and any program changes made as a result of the Corrective Action Program review will be discussed with Waterford 3 personnel. The discussion will stress the importance of documenting conditions adverse to quality in the Corrective Action Program so that root causes may be identified and appropriate corrective action take .
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(4) Date When Full Comoliance Will Be Achieved P All corrective action for this event will be complete January 26, ,
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