IR 05000382/2020001

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Integrated Inspection Report 05000382/2020001 and Independent Spent Fuel Storage Inspection 07200075/2020001
ML20118C992
Person / Time
Site: Waterford  Entergy icon.png
Issue date: 04/24/2020
From: John Dixon
NRC/RGN-IV/DRP/RPB-D
To: Vasquez S
Entergy Operations
References
IR2020001
Download: ML20118C992 (24)


Text

April 24, 2020

SUBJECT:

WATERFORD STEAM ELECTRIC STATION, UNIT 3 - INTEGRATED INSPECTION REPORT 05000382/2020001 AND INDEPENDENT SPENT FUEL STORAGE INSPECTION 07200075/2020001

Dear Mr. Vazquez:

On March 31, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Waterford Steam Electric Station, Unit 3. On April 9, 2020, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC Resident Inspector at Waterford Steam Electric Station, Unit 3.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC Resident Inspector at Waterford Steam Electric Station, Unit 3. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, John L. Dixon, Jr., Chief Reactor Projects Branch D Division of Reactor Projects

Docket Nos. 05000382 and 0720075 License No. NPF-38

Enclosure:

As stated

Inspection Report

Docket Number:

05000382 and 0720075

License Number:

NPF-38

Report Number:

05000382/2020001 and 0720075/2020001

Enterprise Identifier: I-2020-001-0002 and 1-2020-001-0091

Licensee:

Entergy Operations, Inc.

Facility:

Waterford Steam Electric Station, Unit 3

Location:

Killona, LA 70057

Inspection Dates:

January 1, 2020 to March 31, 2020

Inspectors:

R. Alexander, Senior Emergency Preparedness Inspector

S. Makor, Reactor Inspector

J. ODonnell, Senior Health Physicist

F. Ramirez Munoz, Senior Resident Inspector

C. Speer, Resident Inspector

L. Brookhart, Senior Spent Fuel Storage Inspector

E. Simpson, Health Physicist

Approved By:

John L. Dixon, Jr., Chief

Reactor Projects Branch D

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Waterford Steam Electric Station, Unit 3, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Follow Work Instructions When Performing Maintenance on the Safety-Related Essential Chilled Water System Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000382/2020001-01 Open/Closed

[H.11] -

Challenge the Unknown 71152 The inspectors reviewed a self-revealed Green, non-cited violation of Technical Specification 6.8.1.a for the licensees failure to follow work instructions for replacing the damaged section of wiring for a temperature element in essential chilled water system loop A.

Specifically, maintenance technicians elected to remove and repair the temperature element conduit box, actions beyond the scope of the work order instructions, which created a breach in the system, a loss of level of the swing AB expansion tank, and a trip of the swing AB essential chiller. The actions resulted in having only one operable loop in the essential chilled water system and the unexpected entry into a 72-hour shutdown limiting condition of operation.

Additional Tracking Items

Type Issue Number Title Report Section Status NOV 05000382/2017009-01 Failure to Establish Appropriate Electrical-Related FLEX Strategies for Mitigating a Beyond-Design-Basis External Event 92702 Closed

PLANT STATUS

The unit operated at or near rated thermal power for the entire inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/readingrm/doc-collections/insp-manual/inspection-procedure/index.html.

Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. From January 1 - March 19, 2020, the inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the coronavirus (COVID-19), resident inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time the resident inspectors performed periodic site visits each week and during that time conducted plant status activities as described in IMC 2515, Appendix D; and observed risk-significant activities when warranted. In addition, resident and regional baseline inspections were evaluated to determine if all or portions of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In the cases where it was determined the objectives and requirements could not be performed remotely, management elected to postpone and reschedule the inspection to a later date.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

External Flooding Sample (IP Section 03.03) (1 Sample)

(1) The inspectors evaluated readiness to cope with external flooding for the following areas on March 15, 2020:
  • Reactor auxiliary building
  • Turbine building

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Auxiliary component cooling water train B following system maintenance on January 24, 2020
(2) Temporary emergency diesel generators aligned to replace emergency diesel generator B on January 27, 2020
(3) Emergency feedwater train B with train A out of service for maintenance on March 3, 2020
(4) Essential chilled water train AB following re-alignment to replace essential chiller A on March 11, 2020

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Fire area RAB 33, shutdown cooling heat exchanger rooms A and B on February 10, 2020
(2) Fire area RAB 34, safeguards valve gallery rooms A and B on February 10, 2020
(3) Fire area RAB 8B, switchgear room B on February 26, 2020
(4) Fire area RAB 32, auxiliary component cooling water room and pipe penetration area on January 26, 2020

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the control room during a period of heightened activity for the turbine inlet valve stroke testing on January 30, 2020.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the simulator during an emergency preparedness drill on March 4, 2020.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (2 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components remain capable of performing their intended function:

(1) Nitrogen gas system on February 3, 2020
(2) Emergency feedwater system on February 7, 2020

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Planned auxiliary component cooling water train B maintenance on January 23, 2020
(2) Planned yellow risk due to emergency diesel generator B being out of service for maintenance on January 27, 2020
(3) Planned static uninterruptible power supply re-alignment on March 2, 2020

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (4 Samples)

The inspectors evaluated the licensees justifications and actions associated with the following operability determinations and functionality assessments:

(1) Operability assessment of low pressure safety injection train A when the low pressure safety injection pump A discharge flow control valve failed stroke time testing on February 6, 2020
(2) Operability assessment of control element assembly calculators and core protection calculators following a control card failure on March 2, 2020
(3) Operability assessment of the control room envelope when the train B control room outside air intake valve and air handling unit inlet isolation valves opened unexpectedly during maintenance on March 21, 2020
(4) Operability assessment of emergency diesel generator B when an unexpected locked-in local annunciator horn was discovered on March 30, 2020

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1) Permanent modification to replace the pneumatic transducer for auxiliary component cooling water header train A component cooling water heat exchanger outlet temperature control valve on February 11, 2020

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the following post maintenance test activities to verify system operability and functionality:

(1) Emergency feedwater pump A following maintenance on January 14, 2020
(2) Chemical and volume control pump AB following maintenance on March 12, 2020
(3) Component cooling water pump A following troubleshooting on March 26, 2020
(4) Main steam isolation valve 1 upstream drip pot startup drain valve following maintenance on March 27, 2020

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01)

(1) Emergency feedwater header A to steam generator 1 backup flow control valve on March 9, 2020
(2) Essential chilled water pump AB on March 11, 2020

Inservice Testing (IP Section 03.01) (2 Samples)

(1) High pressure safety injection pump B on January 29, 2020
(2) Emergency feedwater pump AB on March 12, 2020

71114.04 - Emergency Action Level and Emergency Plan Changes

Inspection Review (IP Section 02.01-02.03) (1 Sample)

(1) The inspectors evaluated the Waterford Steam Electric Station, Unit 3 Emergency Plan, Revision 51, on March 22, 2020. The licensee implemented Revision 51 on January 30, 2020, and submitted the revised emergency plan to the NRC on February 6, 2020. This evaluation does not constitute NRC approval.

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated:

(1) Site Emergency Preparedness Drill on March 4,

RADIATION SAFETY

71124.02 - Occupational ALARA Planning and Controls

Verification of Dose Estimates and Exposure Tracking Systems (IP Section 03.02) (1 Partial)

The inspectors evaluated dose estimates and exposure tracking.

(1)

(Partial)

WF3 RF21 and WF3 RF22 Post Outage ALARA Reports, each of which included an analysis of the top five dose jobs for each outage.

71124.04 - Occupational Dose Assessment

Source Term Characterization (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated licensee performance as it pertains to radioactive source term characterization.

External Dosimetry (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated licensee performance as it pertains to external dosimetry that is used to assign occupational dose.

Internal Dosimetry (IP Section 03.03) (2 Samples)

The inspectors evaluated the following internal dose assessments for actual internal exposures:

(1) Dose assessment for facial contamination event on refuel bridge during movement of In-core Instrumentation on January 14, 2019, CR-WF3-2019-00737
(2) Dose assessment for facial contamination event during transfer cart repairs in the lower cavity on February 17, 2019, CR-WF3-2019-02942

Special Dosimetric Situations (IP Section 03.04) (1 Sample)

The inspectors evaluated the following special dosimetric situations:

(1) Dose assessment for three declared pregnant workers.

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01)===

(1) January 1, 2019, through December 31, 2019

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02) (1 Sample)

(1) January 1, 2019, through December 31, 2019

IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (1 Sample)

(1) January 1, 2019, through December 31, 2019

71152 - Problem Identification and Resolution

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed the licensees corrective action program for potential adverse trends in maintenance rule functional failure evaluations that might be indicative of a more significant safety issue. The inspectors identified an observation related to a programmatic weakness and an associated minor violation that are documented in the Inspections Results section below.

Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) CR-WF3-2018-00998, impact of potential external toxic gas event on Waterford Steam Electric Station, Unit 3, FLEX Mitigation Strategies (Order EA-12-049) on January 23, 2020
(2) CR-WF3-2019-08826, unauthorized maintenance on essential chiller A resulting in an unplanned 72-hour limiting condition for operation entry on February 17,

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL

60855 - Operation of An ISFSI Operation of An ISFSI

(1) The Waterford independent spent fuel storage installation (ISFSI) is located approximately 900 feet southwest of the reactor building within the plant protected area. The pad is roughly 120 feet wide and 154 feet long with the capacity to hold 72 HI-STORM 100S spent fuel storage casks configured in an 8 by 9 array. At the time of the routine inspection, the Waterford ISFSI pad contained a total of 26 HI-STORM 100S overpacks. The licensee was in the process of loading and processing canister 27. The licensee was loading canisters to the Holtec Certificate of Compliance No. 1014, Amendment 13, and HI-STORM 100 Updated Final Safety Analysis Report, Revision 18.

The inspectors evaluated the licensees ISFSI cask loading from March 16 through 19, 2020. Specifically, the inspectors observed the following activities:

  • Fuel assembly selection and placement into the dry fuel storage canister
  • Processing of the spent nuclear fuel for storage, including forced helium dehydration, and helium backfill operations
  • Heavy load lifts by the cask handling crane of the transfer cask and the spent fuel storage canister
  • Stack-up operations for transferring the storage canister from the transfer cask to the HI-STORM overpack
  • Walk-down of the ISFSI haul path
  • Partial transport of the loaded HI-STORM overpack from the auxiliary building to the vertical cask transporter (VCT) for movement to the ISFSI pad The inspectors performed a walk-down of the ISFSI radioactive materials area and completed an independent radiation survey. The inspectors also performed a walk-down of the spent fuel floor and reactor auxiliary building. The inspectors observed the movement of the loaded HI-STORM cask on the low-profile-transporter as it was moved from the fuel building, transferred to the VCT, and part of its travel along the haul path to the ISFSI pad for final storage.

The inspectors evaluated the following:

  • Spent fuel selection for the current dry cask loading campaign for Waterford (casks 26 and 27)
  • Compliance with the requirements of Title 10 of the Code of Federal Regulations (10 CFR) 72.104 for calendar years 2017, 2018, 2019, and 2020
  • Fire hazards analyses and control of combustibles for ISFSI operations
  • Selected radiological surveys of the ISFSI and dry fuel storage casks
  • Selected ISFSI-related condition reports
  • Quality assurance (QA) program implementation, including recent QA audits, surveillances, and quality control activities related to ISFSI operations
  • Documentation of required annual maintenance and inspection activities for heavy lifting components, including special lifting devices, the sites cask handling crane, and the VCT

60857 - Review of 10 CFR 72.48 Evaluations Review of 10 CFR 72.48 Evaluations

(1) The inspectors reviewed a list of 10 CFR 72.48 screenings performed by the licensee since November 2016. During this time period the licensee did not perform any 10 CFR 72.48 evaluations. The inspectors evaluated the following:
  • Selected licensee 10 CFR 72.48 screenings for associated changes, tests, and experiments associated with ISFSI operations
  • The process by which the licensee evaluates 10 CFR 72.48 screenings and evaluations performed by the Certificate of Compliance holder
  • Changes made to the licensees 10 CFR 72.212 Report since November 2016 (moving from Revision 5 to Revision 8)

92702 - Follow-up on Traditional Enforcement Actions Including Violations, Deviations, Confirmatory Action Letters, Confirmatory Orders, And Alternative Dispute Resolution Confirmatory Orders

(1) VIO 05000382/2017009-01, Failure to Establish Appropriate Electrical-Related FLEX Strategies for Mitigating a Beyond-Design-Basis External Event (EA-18-020), on January 23,

INSPECTION RESULTS

Failure to Follow Work Instructions When Performing Maintenance on the Safety-Related Essential Chilled Water System Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems

Green NCV 05000382/2020001-01 Open/Closed

[H.11] -

Challenge the Unknown 71152 The inspectors reviewed a self-revealed Green, non-cited violation of Technical Specification 6.8.1.a for the licensees failure to follow work instructions for replacing the damaged section of wiring for a temperature element in essential services chilled water system loop A. Specifically, maintenance technicians elected to remove and repair the temperature element conduit box, actions beyond the scope of the work order (WO)instructions, which created a breach in the system, a loss of level of the swing AB expansion tank, and a trip of the swing AB essential chiller. These actions resulted in having only one operable loop in the essential chilled water system and the unexpected entry into a 72-hour shutdown limiting condition for operation.

Description:

On December 5, 2019, instrumentation and controls (I&C) technicians were performing maintenance on temperature element RFRITE3017A in essential chilled water system loop A. The purpose of the essential chilled water system is to provide air conditioning to the essential equipment rooms and main control room during normal operations and operation following a design basis accident. Work Order 536240 contained written instructions to repair a damaged wire associated with the temperature element.

During this maintenance window, essential chiller AB was being used in place of essential chiller A; therefore, two loops of the essential chilled water system were operable.

While performing the maintenance work, the instrumentation and controls technicians noticed that the conduit box that housed the temperature element was degraded. With the approval of the maintenance supervisor, the instrumentation and controls technicians decided to remove the degraded conduit box to replace it. They did not consider it a change in the scope of the work and felt confident based on previous work with similar applications of conduit boxes. However, WO 536240 did not contain instructions to remove the conduit box.

When the instrumentation and controls technicians removed the conduit box, it caused a breach of the essential chilled water system due to removal of the temperature element well that was attached to it. This system breach caused a loss of level in the essential chiller AB expansion tank. The control room operators noticed expansion tank AB rapidly dropping, which caused the trip of essential chiller AB and resulted in operations manually securing essential chiller pump AB. The loss of essential chiller AB resulted in an unexpected entry into TS 3.7.12, Essential Services Chilled Water System, which is a 72-hour shutdown limiting condition for operation.

Corrective Actions: The licensees immediate corrective action was to repair the system breach by installing a new conduit box and realigning and restoring the level in the essential chiller AB expansion tank. Following the system restoration, essential chiller AB was placed back in service and the limiting condition for operation was exited within the allowed time frame.

Corrective Action References: Condition Report CR-WF3-2019-08826

Performance Assessment:

Performance Deficiency: The failure to follow work instructions as specified in WO 536240 was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the configuration control attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, when the electricians performed unauthorized maintenance on the essential chilled water system, it resulted in a breach in the system, a loss of level in expansion tank AB, and a trip of essential chiller AB. The actions resulted in having only one operable loop in the essential chilled water system and the unexpected entry into a 72-hour shutdown limiting condition for operation.

Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors determined that the finding was of very low safety significance (Green) because

(1) the finding was not a deficiency affecting the design or qualification of a mitigating system;
(2) the degraded condition did not represent a loss of the PRA function of a single train technical specification system for greater than is technical specification allowed outage time;
(3) the degraded condition did not represent a loss of the PRA function of one train of a multi-train technical specification system for greater than its technical specification allowed outage time;
(4) the degraded condition did not represent a loss of the PRA function of two separate technical specification systems for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />;
(5) the degraded condition did not represent a loss of a PRA system and/or function as defined in the PRIB or licensees PRA for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />; and
(6) the degraded condition did not represent a loss of the PRA function of one or more non-technical specification trains of equipment designated as risk-significant in accordance with the licensees maintenance rule program for greater than 3 days.

Cross-Cutting Aspect: H.11 - Challenge the Unknown: Individuals stop when faced with uncertain conditions. Risks are evaluated and managed before proceeding. Specifically, when the instrumentation and controls technicians and their supervisor encountered a condition that was not within the scope of the work instructions, they proceeded with the maintenance without evaluating the system consequences.

Enforcement:

Violation: Technical Specification 6.8.1.a, requires, in part, that procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2. Appendix A to Regulatory Guide 1.33, Section 9.a, requires, in part, that, maintenance that can affect the performance of safety-related equipment be properly pre-planned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. The licensee established work instructions in WO 536240 to repair a damaged wire associated with a temperature element on the essential chilled water loop A.

Contrary to the above, on December 5, 2019, the licensee failed to implement the work instructions established in WO 536240 to repair a damaged wire associated with a temperature element on essential chilled water loop A, a safety-related system. Specifically, the instrumentation and controls technicians performed unauthorized maintenance that was not directed by the WO by also removing an adjacent degraded conduit box which pulled the associated temperature element well. This added work resulted in a breach in the system, a loss of level of expansion tank AB, a trip of essential chiller AB, and an unexpected entry into a 72-hour shutdown limiting condition for operation.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Minor Violation 71152 Minor Violation: The inspectors identified a minor violation of 10 CFR 50.65(b)(1) for the licensees failure to include the closed function of the emergency feedwater header B to steam generator 2 flow control valve, EFW-224B, in the scope of the maintenance rule program.

Screening: The inspectors determined the violation to be minor because it did not impact the Mitigating Systems cornerstone, consistent with Inspection Manual Chapter 0612, Appendix E, Example 8.c. The licensee generated condition report CR-WF3-2020-01183 to address the failure to include the closed function of EFW-224B in the scope of the maintenance rule program.

Enforcement:

The licensee has taken action to restore compliance. This failure to comply with 10 CFR 50.65(b)(1) constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy.

Observation: Semi-Annual Trend Review: Maintenance Rule Adverse Trend 71152 The inspectors identified an adverse trend involving the licensees implementation of their maintenance rule program. Specifically, the inspectors noted multiple instances where adverse conditions for structures, systems, and components scoped into the maintenance rule were not consistently evaluated against all applicable functional failure criteria.

  • CR-WF3-2019-03069 documented three instances where failed local leak rate testing of containment isolation valves was not evaluated against the containment building maintenance rule functions. For each of these failures, the valves were evaluated against the maintenance rule functional failure criteria for the system they were explicitly assigned to (i.e., SI-405B was evaluated against the safety injection system criteria), but they were not evaluated against the applicable containment building system criteria despite being containment isolation valves. When challenged by the inspectors, the licensee re-evaluated the three instances and determined that they represented functional failures of the containment building system criterion for failing to satisfactorily pass local leak rate testing. This deficiency was previously communicated to the licensee and documented in NRC Inspection Report 05000382/2019001 as a semiannual trend review for weaknesses in the licensees maintenance rule program.
  • CR-WF3-2019-07024 documented the failure of the auxiliary component cooling water header train A component cooling water heat exchanger outlet temperature control valve, ACC-126A, such that the associated nitrogen accumulator would not be able to supply adequate nitrogen on the loss of instrument air to meet the required 10-hour mission time to operate automatically. This failure was evaluated against the auxiliary component cooling water maintenance rule functions, but it was not evaluated against the nitrogen gas system maintenance rule criteria. When challenged by the inspectors, the licensee re-evaluated the condition and determined that it represented a functional failure of the nitrogen gas system criterion to provide enough nitrogen gas to the valve to perform for the required 10-hour mission time.

This condition is associated with a finding documented in NRC Inspection Report 05000382/2019004.

  • CR-WF3-2019-02901 documented a failure of the emergency feedwater header B to steam generator 2 flow control valve, EFW-224B, in which the associated controller would not close the valve due to an air leak. The failure was evaluated against the emergency feedwater system maintenance rule criteria, but the inspectors noted that only the open functions were captured in the scope of the maintenance rule. The actual failure of the valve involved a failure to close, which is a required safety function for the valve evaluated in the licensees Updated Final Safety Analysis Report to combat a ruptured steam generator. When challenged by the inspectors, the licensee determined that the closed function of the valve was inappropriately not scoped into the maintenance rule program. In addition to the failure to properly scope EFW-224B into the maintenance rule program, the inspectors noted that the air leak on EFW-224B was not evaluated against the nitrogen gas maintenance rule functions.

When challenged by the inspectors, the licensee determined that a functional failure evaluation should have been performed but that the condition ultimately was not a maintenance rule functional failure. This issue was documented as a minor violation in the Inspection Results section of this report.

The inspectors concluded that the repeated failure to consistently consider all applicable functions when performing maintenance rule functional failure evaluations represents a weakness in the licensees maintenance rule program. However, the inspectors did not find that accounting for these functional failures would result in systems being reclassified from maintenance rule (a)(2) to (a)(1) status.

The licensee captured the inspectors observation in condition reports CR-WF3-2020-01190 and CR-WF3-2019-08187. The licensees immediate corrective action was to perform functional failure evaluations for the identified condition reports. The licensee is planning action to assess the extent of condition for potentially missed functional failure evaluations and to address the weakness in their maintenance rule program. Included in the planned actions is the development of an enhanced maintenance rule database that would explicitly tie each plant component scoped into the maintenance rule to all the applicable system functions and functional failure criteria.

Assessment 92702 Background On July 20, 2018, the U.S. Nuclear Regulatory Commission (NRC) issued a Notice of Violation (NOV) to Entergy Operations, Inc. (Entergy), Waterford Steam Electric Station, Unit 3 (Inspection Report 05000382/2017009 (Agencywide Documents Access and Management System Accession (ADAMS) No. ML18201A492). The Green finding and NOV (EA-18-020)were associated with the failure to establish appropriate design and procedures associated with providing electrical power using the N+1 FLEX diesel generator to support transition phase (Phase 2) strategies. These strategies, required by Post-Fukushima Lessons Learned Order EA-12-049, are intended to maintain or restore the core cooling and spent fuel pool cooling capabilities in mitigating a beyond-design-basis external event.

Entergy (the licensee) provided their initial response to the NOV on August 8, 2018 (ADAMS Accession No. ML18221A639), and provided supplements on September 12, 2018 (ADAMS Accession No. ML18255A321) and May 17, 2019 (ADAMS Accession No. ML19137A341).

Inspection and Assessment The inspectors reviewed the licensees responses to the NOV to confirm the stated corrective actions would be timely and appropriate to address the nature of the violation. Further, the inspectors reviewed the cause evaluation completed by the licensee to address the Green finding and NOV, and determined that the licensee:

(1) appropriately evaluated the problem, at a level commensurate with the significance of the problem (Level B Adverse Cause Analysis), using a systematic methodology in accordance with licensee procedures;
(2) appropriately considered the extent of condition;
(3) appropriately identified the direct cause and causal factors; and
(4) appropriately established and prioritized corrective action plans to address the direct cause, causal factors, and extent of condition.

The inspectors conducted an onsite inspection of the completed corrective actions the week of January 21, 2020, by way of procedure walk-throughs, reviewing engineering changes and related documentation, and conducting physical walkdowns of new equipment and modifications made to the plant. Specifically, the inspectors reviewed:

(1) the design change to allow for the staging and operation of the N+1 FLEX diesel generator from within the Nuclear Plant Island Structure (on the Q-Deck);
(2) revisions to the licensees Technical Requirements Manual relative to the functionality and allowed outage time criteria for the N and N+1 FLEX diesel generators;
(3) revisions to the FLEX Support Guidelines, Abnormal Procedure for Severe Weather and Flooding, and other work orders necessary to stage and operate the N+1 FLEX diesel generator on the Q-Deck; and
(4) additional enhancements to licensee organizational and programmatic review processes identified which may have precluded the problem from occurring during the initial design of the FLEX strategies.

The inspectors concluded that the corrective actions were completed in a timely manner, commensurate with the safety significance of the problem, and were appropriate to establish the strategy to utilize the N+1 FLEX diesel generator in response to an extended loss of all AC power for all of the beyond-design-bases external events applicable to Waterford Steam Electric Station, Unit 3. No issues of more than minor safety significance were identified.

Therefore, the inspectors determined that the causes, corrective actions taken to address recurrence, and full compliance NRC Order EA-12-049 has been achieved, such that the violation (VIO 05000382/2017009-01) is adequately addressed and may be closed.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On January 23, 2020, the inspectors presented the N+1 FLEX diesel generator-related NOV follow-up inspection results to M. Lewis, Plant Manager and other members of the licensee staff.
  • On February 18, 2020, the inspectors presented the Radiation Safety Exit Meeting inspection results to Mr. S. Vazquez, Site Vice President, and other members of the licensee staff.
  • On March 19, 2020, the inspectors presented the Independent Spent Fuel Storage Installation inspection results to Mr. S. Vazquez, Site Vice President, and other members of the licensee staff.
  • On March 31, 2020, the inspectors presented the EP exit briefing for Emergency Plan revision in-office inspection results to Mr. J. Overly, Manager, Emergency Preparedness and other members of the licensee staff.
  • On April 9, 2020, the inspectors presented the integrated inspection results to Mr. S. Vazquez, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.04

Procedures

OP-002-001

Auxiliary Component Cooling Water

315

71111.04

Procedures

OP-002-004

Chilled Water System

318

71111.04

Procedures

OP-009-003

Emergency Feedwater

309

71111.04

Procedures

OP-901-521

Severe Weather and Flooding

334

71111.04

Procedures

OP-TEM-008

Emergency Diesel Generator A(B) Backup Temporary

Diesel Generator(s)

71111.05

Procedures

RAB 33-001

Shutdown Cooling Heat Exchanger A and B

71111.05

Procedures

RAB 34-001

Safeguards Valve Gallery Rooms A and B

71111.05

Procedures

RAB 8B, E, F-001

Switchgear Room B

71111.11Q Procedures

OP-903-007

Turbine Inlet Valve Cycling Test

71111.12

Corrective Action

Documents

CR-WF3-YYYY-

NNNN

2019-02889, 2019-00941, 2019-02901, 2019-04868,

2019-06698, 2019-06162, 2019-07024, 2019-08184,

2019-02123, 2019-02067, 2019-02066, 2019-01955,

2019-01955, 2019-02066, 2018-03165, 2018-03164,

20-01225, 2020-01190, 2020-01183, 2020-01178,

20-01175

71111.12

Drawings

G-166 Sheet 2

Flow Diagram N2, H2, CO2 Systems

71111.12

Procedures

EN-DC-203

Maintenance Rule Program

71111.12

Procedures

EN-DC-204

Maintenance Rule Scope and Basis

71111.12

Procedures

EN-DC-205

Maintenance Rule Monitoring

71111.13

Calculations

EC 43924

Vital and Measurement SUPS Upgrade Project

71111.13

Calculations

EC 72768

Update SUPS EC-43927 with NFPA-805 Requirements

71111.13

Corrective Action

Documents

CR-WF3-YYYY-

NNNN

20-00756, 2020-01079, 2020-01091, 2020-01092

71111.13

Miscellaneous

Tagout 2020-0014 EDG B Outage - List of Protected

Equipment

January 27,

20

71111.13

Procedures

EN-WM-104

On Line Risk Assessment

71111.13

Procedures

OI-037-000

Operations Risk Assessment Guideline

314

71111.13

Procedures

OP-006-005

Inverters and Distribution

339

71111.13

Procedures

OP-006-005

Inverters and Distribution

340

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.13

Work Orders

2783599

71111.15

Calculations

ECM11-003

W3 Decay Heat Removal with Reduced Flow Through the

Shutdown Cooling Heat Exchanger

71111.15

Calculations

ECM97-069

Design Basis Review for Safety Injection System Valves SI-

29A and SI-129B

71111.15

Calculations

MNQ6-48

Safety Injection System Split Flow Calculation

71111.15

Corrective Action

Documents

CR-WF3-YYYY-

NNNN

20-00618, 2018-00628, 2020-00998, 2020-01019

20-01020, 2020-01021, 2020-01042, 2019-06693

20-01391. 2020-01326, 2020-01487, 2020-01495

71111.15

Procedures

EN-OP-104

Operability Determination Process

71111.15

Procedures

MI-003-500

Chlorine Detection system channel functional Test and

Calibration HVCIA5400 A or B

71111.18

Miscellaneous

EC 84264

Parent EC - Replace/Relocate the Masoneilan 8005N I/P

Transducers with Conoflow GT25CD1826 I/P Transducers

71111.18

Miscellaneous

EC 84294

Child EC (ACC-126A) - Replace/Relocate the Masoneilan

8005N I/P Transducer with Conoflow GT25CD1826 I/P

Transducer

71111.19

Corrective Action

Documents

CR-WF3-YYYY-

NNNN

20-01383

71111.19

Procedures

EN-MA-101

Conduct of Maintenance

71111.19

Procedures

EN-MA-107

Post-Maintenance Testing

71111.19

Work Orders

541434

71111.22

Corrective Action

Documents

CR-WF3-YYYY-

NNNN

20-01251, 2020-01256

71111.22

Miscellaneous

OP-903-063

Chilled Water Pump Operability Verification

311

71111.22

Procedures

OP-903-030

Safety Injection Pump Operability Verification

71111.22

Procedures

OP-903-046

Emergency Feedwater Pump Operability Check

23

71111.22

Procedures

OP-903-121

Safety Systems Quarterly IST Valve Tests

71114.04

Miscellaneous

CFR 50.54(Q)(3) Screening and Evaluation for Waterford

Emergency Plan Revision 51

2/11/2019

71124.02

Self-Assessments

WF3 RF21 Post Outage ALARA Report

05/31/2018

71124.02

Self-Assessments

WF3 RF22 Post Outage ALARA Report

01/14/2020

71124.04

Corrective Action

Documents

CR-HQN-

2019-2210, 2019-2840, 2020-0037

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71124.04

Corrective Action

Documents

CR-WF3-YYYY-

NNNN

2018-4963, 2018-5061, 2018-5216, 2018-6182,

2019-0054, 2019-1022, 2019-4407, 2019-6179,

2019-7004, 2019-7240, 2019-7522, 2019-7683,

20-0134

71124.04

Miscellaneous

Dosimeter of Legal Record Expectations

2/10/2020

71124.04

Miscellaneous

2019

NVLAP Accreditation for 100518-0

2/17/2018

71124.04

Miscellaneous

20

NVLAP Accreditation for 100518-0

01/01/2020

71124.04

Miscellaneous

DLR# 190021

DLR/SRD Discrepancy Investigation (CR-WF3-2019-5555)

06/06/2019

71124.04

Miscellaneous

DLR# 191638

DLR/SRD Discrepancy Investigation (CR-WF3-2019-5555)

06/06/2019

71124.04

Miscellaneous

DLR# 194028

DLR/SRD Discrepancy Investigation (CR-WF3-2019-5555)

06/06/2019

71124.04

Miscellaneous

DLR# 194175

DLR/SRD Discrepancy Investigation (CR-WF3-2019-5555)

06/06/2019

71124.04

Miscellaneous

DLR# 194199

DLR/SRD Discrepancy Investigation (CR-WF3-2019-5555)

06/06/2019

71124.04

Miscellaneous

EN-RP-204

Neutron Dose Tracking Form (3 workers)

03/31/2018

71124.04

Miscellaneous

EN-RP-204

Neutron Dose Tracking Form (2 workers)

03/31/2018

71124.04

Miscellaneous

EN-RP-204

Neutron Dose Tracking Form (4 workers)

04/18/2018

71124.04

Miscellaneous

EN-RP-204

Neutron Dose Tracking Form (2 workers)

04/18/2018

71124.04

Miscellaneous

EN-RP-204

Neutron Dose Tracking Form (3 workers)

05/02/2018

71124.04

Miscellaneous

EN-RPT-19-003

Standardization of a Bias Between DLRs and SRDs in the

Entergy Fleet

Update Based on 2018 Results

10/31/2019

71124.04

Miscellaneous

LWM 2019

Part 61 Waste Stream Analysis for LWM and DAW

01/01/2019

71124.04

Miscellaneous

NAIPKLCT.NLB

Nal Peak Locate Library

2/11/2020

71124.04

Miscellaneous

STDNPPNA.NLB

Basic NaI NPP Library

2/11/2020

71124.04

Miscellaneous

WF3-RPT-16-001

Waterford 3 Containment Neutron Study

06/07/2016

71124.04

Miscellaneous

WF3-RPT-16-002

Waterford 3 Dry Fuel Storage Neutron Study

06/07/2016

71124.04

Miscellaneous

WF3-RPT-85-001

Neutron Dose and Energy Spectral Measurements Inside

Reactor Containment at Waterford 3 SES

05/01/1985

71124.04

Procedures

EN-RP-131

Air Sampling

71124.04

Procedures

EN-RP-151

Radiological Diving

71124.04

Procedures

EN-RP-152

Conduct of Radiation Protection

71124.04

Procedures

EN-RP-201

Dosimetry Administration

71124.04

Procedures

EN-RP-203

Dose Assessment

71124.04

Procedures

EN-RP-204

Special Monitoring Requirements

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71124.04

Procedures

EN-RP-205

Prenatal Monitoring

71124.04

Procedures

EN-RP-208

Whole Body Counting / In-Vitro Bioassay

71124.04

Procedures

EN-RP-311

Electronic Alarming Dosimeters

71124.04

Self-Assessments LO-WLO-2019-

00041

Self-Assessment: Occupational Dose Assessment

10/07/2019

71124.04

Self-Assessments QA-14/15-2019-

W3-1

Quality Assurance Audit Report:

Radiation Protection and Radwaste

10/28/2019

71151

Miscellaneous

W3F1-2019-0030

NRC Performance Indicator (PI) Data - 1st Quarter ROP

Data

04/11/2019

71151

Miscellaneous

W3F1-2019-0075

NRC Performance Indicator (PI) Data - 3rd Quarter ROP

Data

10/17/2019

71151

Miscellaneous

W3F1-2020-0004

NRC Performance Indicator (PI) Data - 4th Quarter ROP

2019 Data

01/16/2020

71151

Procedures

W3F1-2019-0053

NRC Performance Indicator (PI) Data - 2nd Quarter ROP

Data

07/15/2019

71152

Corrective Action

Documents

CR-WF3-YYYY-

NNNN

20-01183, 2020-01190, 2020-01175, 2020-01178,

20-01225, 2019-02901, 2019-02821, 2019-08187

2019-07204, 2019-03069, 2020-00472, 2019-08184,

2019-08185, 2019-02066, 2019-02067, 2019-03144,

2019-03957

71152

Miscellaneous

White Paper: Impacts of External Toxic Gas Event on

Waterford 3 FLEX Mitigating Strategies

01/21/2020

71152

Procedures

EN-DC-203

Maintenance Rule Program

71152

Procedures

EN-DC-205

Maintenance Rule Monitoring

71152

Procedures

EN-DC-206

Maintenance Rule (A)(1) Process

71152

Procedures

FIG-001

Extended Loss of AC Power

71152

Procedures

STA-001-005

Leakage Testing of Air and Nitrogen Accumulators for

Safety Related Valves

21

2702

Calculations

ECC19-013

FLEX N+1 Diesel Generator Seismic Restraint

000

2702

Corrective Action

Documents

CR-WF3-YYYY-

NNNN

2018-04443

2702

Corrective Action

Documents

CR-WF3-2018-

04443

Adverse Condition Analysis: Failure to implement

appropriate strategy for N+1 FLEX diesel generator

08/07/2018

2702

Corrective Action

CR-WF3-YYYY-

20-00331

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Documents

Resulting from

Inspection

NNNN

2702

Drawings

SK-EC80346-CS-

001

Restraint for FLEX N+1 DG

10/11/2019

2702

Engineering

Evaluations

EC 80346

FLEX N+1 Diesel Strategy Revision (including P2E

Attachments)

000

2702

Engineering

Evaluations

WF3-ME-15-

00003

Wind-Generated Missile Evaluation of Exposed Piping for

FLEX

2702

Engineering

Evaluations

WF3-SA-14-

00002

Waterford 3 FLEX Strategy Development

2702

Fire Plans

CT1-001

Pre-Fire Strategy: Dry Cooling Tower A

007

2702

Fire Plans

CT3-001

Pre-Fire Strategy: Wet Cooling Tower A

009

2702

Miscellaneous

EOS Checklists

19-0231, 19-0373, 19-0523 (TRM action statement entries

for N or N+1 FLEX DG non-functional)

05/14/2019,

07/30/2019,

10/12/2019

2702

Procedures

EN-FAP-LI-015

Response to New Regulatory Requirements

2702

Procedures

EN-HU-104

Technical Task Risk & Rigor

2702

Procedures

FIG-001

Extended Loss of AC Power

007

2702

Procedures

FSG-005

Initial Assessment and FLEX Equipment Staging

011

2702

Procedures

OP-901-521

Off Normal Procedure: Severe Weather and Flooding

333

2702

Procedures

OP-902-005

Emergency Operating Procedure: Station Blackout

Recovery Procedure

2702

Procedures

UNT-007-060

Control of Loose Items

306

2702

Work Orders

00532845

Stage FLEXMDSG0002 and Support Equip to RAB+21 Q-

Deck

60855

Corrective Action

Documents

CR-WF3-YYYY-

NNNN

2016-02536, 2016-05342, 2016-05409, 2019-06119

Miscellaneous

CFR 72.212 Evaluation Report for the Waterford Unit 3

ISFSI

CFR 72.212 Evaluation Report for the Waterford Unit 3

ISFSI

CFR 72.212 Evaluation Report for the Waterford Unit 3

ISFSI

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Procedures

DFS-003-002

Transport of Loaded and Unloaded HI-STORM

DFS-003-003

MPC Preparation for Loading

DFS-003-004

Handling and Loading of MPC

DFS-003-005

MPC Backfill and Sealing Operation

DFS-003-006

Stack-Up and Transfer of Loaded MPC

DFS-003-008

Heavy Haul Path Preparation for Cask

DFS-007-003

Radiation Monitoring Requirements for Loading and Storage

HI-STORM

EN-FAP-OU-108

Fuel Handling Process

EN-LI-102

Corrective Action Program

RF-005-001

Fuel Movement

23

RF-005-004

Transfer of Spent Fuel Assemblies to the Multi-Purpose

Canister

Radiation

Surveys

WF3-2001-00100

ISFSI Pad Survey Map

03/02/2020

Self-Assessments O2C-W3-2016-

0533

O2C Report

2/02/2016

QA-20-2018-W3-

Quality Assurance Audit Report

08/15/2017

60857

Engineering

Changes

EC #66989

Revised Seismic Stack-up Analysis

10/31/2016

Procedures

EN-LI-100

Process Applicability Determination

EN-LI-100,

8.1

Process Applicability Determination Form

09/26/2018

EN-LI-100,

8.1

Process Applicability Determination Form

2/10/2020

EN-LI-101

CFR 50.59 Evaluations

EN-LI-112

CFR 72.48 Evaluations

14