ML20151W244

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Notice of Violation from Insp on 880217-0331.Violation Noted:Flow Elements 924,926 & 927 of High Head Safety Injection Sys Installed Backwards
ML20151W244
Person / Time
Site: Vogtle Southern Nuclear icon.png
Issue date: 04/26/1988
From: Brownlee V
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20151W233 List:
References
50-425-88-12, NUDOCS 8805030334
Download: ML20151W244 (2)


Text

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ENCLOSURE 1 NOTICE OF VIOLATION Georgia Power Company Docket No. 50-425 Vogtle 2 License No. CPPR-109 During the Nuclear Regulatory Commission (NRC) inspection conducted on February 17 - March 31,1988, a violation of NRC requirements was identified.

In accordance with the "General Statement of policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix C, the violation is listed below.

10 CFR 50, Apper; dix B, Criterion V, and the accepted Quality Assurance (QA) Program (FSAR 17.1.5) collectively require that activities affecting quality be prescribed by drawings and be accomplished in accordance with these drawings.

P & ID 2X40B119 details the high head safety injection flow path to be from the Safety Injection (SI) discharge valves through Flow Elements (FEs) - 924, 925, 926, and 927 into the reactor coolant system (RCS cold legs for loops 1, 2, 3, and 4 respectfully.

Contrary to the above, activities affecting quality were not adequately implemented in that an NRC walkdown conducted on March 3, 1988, of portions of the High Head Safety Injection System evealed that FEs -

924, 926, 927 were installed backwards.

This is a Severity Level IV violation (Supplement II).

Pursuant to the provisions of 10 CFR 2.201, Georgia Power Company is hereby required to submit a written statement or explanation to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555, with a copy to the Regional Administrator, Region II, and a copy to the NRC Resident Inspector, Vogtle, within 30 days of the date of the letter transmitting this Notice. ,his reply should be clearly marked as a "Reply to a Notice of Violation" and should include: (1) admission or denial of the violation, (2) the reason for the violation if admitted, (3) the corrective steps which have been taken and the results achieved (4) the corrective steps which will be taken to avoid further violations, and (5) the date when full compliance will be achieved. Where good cause is shown, consideration will be given to extending the response time. If an adequate reply is not received within the 8805030334 880426 i PDR ADOCK 05000425 iG O DCD

Georgia Power Company 2 Docket No. 50-425 Vogtle 1 License No. CPPR-109 time specified in this Notice, an order may be istuId to show cause why the license should not be modified, suspended, or revoked or why such other action as may be proper should not be taken.

FOR THE NUCLEAR REGULATORY COMMISSION op CNALstGNED BL g;CU.A.,15R.OWNl.EE Virgil L. Brownlee, Chief .

Reactor Projects Branch 3 Division of Reactor Projects DatedagAtlanta, Georgia this24 day of April 1938

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